ML18102A953
| ML18102A953 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 04/03/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML18102A952 | List: |
| References | |
| 50-272-97-03, 50-272-97-3, 50-311-97-03, 50-311-97-3, NUDOCS 9704090281 | |
| Download: ML18102A953 (75) | |
See also: IR 05000272/1997003
Text
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Docket Nos:
License Nos:
R~port No.
Licensee:
Facility:
Location:
Dates:
Inspectors:
Approved by:
U. S. NUCLEAR REGULATORY COMMISSION
50-272, 50-311
REGION I
50-272/97-03, 50-311/97-03
Public Service Electric and Gas Company
Salem Nuclear Generating Station, Units 1 & 2
P;O. Box 236
Haricocks Bridge, New Jersey 08038
January 26, 1997 - March 15, 1997
C. S. Marschall, Senior Resident lnsp~ctor
J. G. Schoppy, Resident Inspector
T. H. Fish, Resident Inspector
R. K. Lorson, Resident Inspector
L. J. Prividy, Senior Reactor Engineer
E. H. Gray, Project ~: * .:nager
8. Smith, NRC Contract Engineer
J. Greene, NRC Contract Engineer
.James C. Linville, Chief, Projects Branch 3
- Division of Reactor Projects
9704090281 970403
PDR _ ADOCK 05000272
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EXECUTIVE SUMMARY
Salem Nuclear Generating Station
NRC Inspection Report 50-272/97-03, 50-311197-03
This integrated inspection included aspects of licensee operations, engineering,
maintenance, and plant support. The report covers a 7-week pe,riod of resident inspection.
In addition, it includes the results of inspections of steam generator replacement, the
Motor-operated valve program, and the commitment management system.
Operations
Operators continued to demonstrate deliberate control of plant activities and conservative
decision-making. Unit 2 operators demonstrated good awareness of technical specification
requirements in controlling pressurizer auxiliary spray even though a surveillance procedure
did not provide appropriate precautions (Section 03.2). Although the inspectors observed
good overall operator performance, the inspectors noted some weaknesses involving use
of the alarm response procedures, evaluation of an off-normal plant condition, and shift
turnovers (Section 04.2). Plant managers demonstrated leadership and commitment to
excellence in demanding that containment inspection teams implement higher standards
for containment cleanliness and material condition (Section 08.2).
The station implemented a number of programs designed to enhance procedure use and
adequacy. Recent inspection observations indicate good and improving procedure use.
Procedures were reviewed and revised in key station functional areas. The operations
staff appropriately identified operations procedures that required revision prior to restart.
Selected procedures reviewed appeared adequate and generally consistent with the
procedure writers guide. The inspector concluded that procedure use and adherence is
adequate (Section 03.1 ). Implementation of effective operability determination training for
operations and system engineering staff resulted in an effective i:>rocess for developing
operability determinations (Section 02.1 ).
The operations staff implemented extensive corrective measures resulting in significant
im.provement in operator performance since June 1995. Operators demonstrated safety-
conscious decision making, ownership for plant equipment, detailed knowledge of plant
operation, a good questioning attitude, effective communications, procedure compliance,
low tolerance for workarounds, and a tendency to identify and correct deficient conditions.
The inspectors considered the measures to improve performance effective (Section 04. 1 ) .
The operations staff also established, implemented and completed the Operations Restart
Action Plan. Inspectors considered the results of the completed actions effective in
improving: oversight of plant activities, operator training, standards for equipment
condition, communication, and control of plant .operation (Section 08.1 ).
In a letter dated March 18, 1997, NRC issued a violation for two aspects of licensed
operator requalification trainina that did not meet 10 CFR 55.59(c) based on licensee
submittals dated November 7, 1996, January 6, 1997, and February 12, 1997. The two
aspects related to compliance with requirements for an annual operating test for all
operators and for continuous requalification training programs not to exceed 2 years in
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duration. The NRC letter also noted that the operator training has been high quality and
effective, but the violation represents weak program planning (Section 05).
The inspectc1rs concluded that Salem radiation monitors and procedures adequately
addressed the requirements of 10 CFR 70.24 for criticality monitors {Section 08.3). An
independent investigation, in response to a employee concern, effectively demonstrated
that Quality Assurance {QA) management actions had not resulted in toning down QA
inspector findings. The investigation also effectively demonstrated that QA managers had
not taken action to reprimand or otherwise penalize QA inspectors as a result of the QA
inspectors' findings {Section 08.4). The licensee developed and improved their methods
for commitment management {e.g. Commitment Manager and the 30-day look ahead
report), informed responsible personnel of these methods and management expectations,
and began to 'improve commitment management procedures. The NRC Restart Item
(111.14) remains open pending completion of the procedure changes {Section 08.5).
Maintena*nce
The maintenance restart action plan effectively addressed previous performance
deficiencies. The inspectors found that management monitored emergent work and
actively participated in the assignment of priorities to safety significant work.
Maintenance personnel identified new problems and initiated corrective action. For the
activities observed, maintenance technicians used procedures and tools properly.
Management actively monitored performance using trending tools and self assessments.
Additionally, QA provided useful performance assessment. The self assessments and QA
assessments enabled management to continue to improve maintenance performance.
Although performance deficiencies continue to occur, significant reduction in the error rate
and significant improvement in equipment performance indicated that implementation of
the maintenance restart plan resulted in effective maintenance (Section M1 .2).
Inspectors noted that good quality generally characterized the performance of the Salem
Unit 1 steam generator replacement project (SGRP). When workers identified problems,
the managers and supervisors stopped or delayed work until they established an
acceptable course of action (Section M1 .3). Technicians demonstrated good procedure
adherence during repair of the 1 C EDG jacket cooling leak, and during replacement of the
11 SW pump .. Troubleshooting of the 1 C EDG frequency variations was logical. Weak
engineering controls were established prior to changing the type of packing in the 11 SW
pump (Section M 1 .4). Maintenance did not effectively repair a packing leak or adequately
use equipment malfunction identification system tag tracking. Maintenance and
engineering did not adequately support operations in resolving diesel day tank level
indication inadequacies (Section M2.1 ). Technicians properly controlled and conducted
safety-related maintenance on the no. 23 component cooling water pump (Section M3.1 ).
Salem management has improved, and continues to improve, work control effectiveness.
They improved the process, trained personnel, and increased staffing levels in the planning
- and scheduling group. PSE&G's staff addressed the work order backlog and they are
using performance indicators to monitor progress. While personnel could still improve their
performance, the work control staff's response to their self assessment indicated to the
inspector that management would ensure the organization continued to address
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deficiencies. The inspector concluded the work control program is ready to support Salem
restart (Section M8.1 ).
Engineering
Significant progress arid improvements in the MOV program were evident since the last
NRC inspection of July 19.96. The justifications for key program assumptions were
complete and the applied valve factors of Salem Unit 2 MOVs were adequate for GL 89-10
closure, demonstrating design-basis capability. These conclusions were based on the
understanding that PSE~G would pursue additional actions for certain MOVs in Families 6
_and 9 in conjunction with their periodic verification program (Sections E1 .3 and E1 .4).
PSE&G's actions to address pressure locking and thermal binding of motor-operated gate
valves were acceptable (Section E1 .5). PSE&G had developed a good tracking and
trending program and was adequately addressing MOV performance problems (Section
E1 .6). *
Inspectors observed generally good engineering performance during the period with
occasional lapses. During review of an operability determination, station operations review
committee (SORC) members questioned the basis for assurance that containment fan coil
unit (CFCU) modifications did not affect containment integrity. The plant staff did not
address the SORC question, and station management demonstrated lack of follow through
by not ensuring that the plant staff developed a satisfactory response to the containment
integrity question. In response to inspector questions, and prior to entering the affected
mode, SORC approved a 10 CFR 50.59 safety evaluation that adequately addressed the
concern regarding the UFSAR commitments for Type C leak rate testing the CFCU SW
cooling line containment isolation valves (Section E1 .9). As a result of a proposed
modification, an alert system manager discovered an incomplete surveillance of the circuit
for automatic operation of the Pressurizer Overpressure Protection System. The plant staff
immediately devised and completed an effective test. The inspectors noted that TSSIP, *
- phase 2, scheduled for completion in late 1997, would have discovered this deficiency
(Section E 1 . 1 0). The engineering staff conducted appropriate trouble-shooting to
determine the cause of control room ventilation performance problems. The Salem
managers properly elected to correct system deficiencies rather than change the licensing
basis for control room ventilation. As a result of considerable effort, the engineering staff
successfully demonstrated the ability of control room ventilation to perform its design
function (Section E8.1)
Pending satisfactory implementation of the modifications to address the effects of multiple
hot shorts on safe shutdown, the associated NRC Restart Item and Unresolved Items will .
remain open (Section E8.3):
Plant Support
Inspectors concluded that PSE&G had adequately addressed various open items relating to
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TABLE OF CONTENTS
EXECUTIVE SUMMARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
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TABLE OF CONTENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
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I. Operations .................................*..................
II. Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
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Ill. Engineering ......................... * . . . . . . . . . . . . . . . . . . . . . . . . .
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IV. Pla.nt Support . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
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Report Details
Summary of Plant Status
Unit 1 remained defueled for the duration of the inspection period.
Operators maintained Unit 2 in Mode 5, Cold Shutdown, for the duration* of the period.
I. Operations
01
Conduct of Operations
. 01 . 1 *General Comments (71 707)
Using Inspection Procedure 71707, the inspectors conducted frequent reviews of
ongoing plant operations. In general, the conduct of operations was professional
and safety-conscious; specific events and noteworthy observations are detailed in
the sections below. *
02
. * Operational Status of Facilities and Equipment
02.1
Operability Determinations. NRC Restart Item 111.6 (Closed) and Unresolved Item 50~ *
272&311/95-80-01 (Closed)
a.
Inspection Scope (71707)
b.
. Various NRC Inspection Reports, such as 50-272&311 /95-80, documented
unacceptable and poor quality operability determinations at Salem. The inability of
the Salem staff, in the past, to appropriately determine equipment operability
contributed. significantly to the cause of the shut down of Salem Units 1 and 2 in
1995. In NRC Inspection Report 50-272&311 /96-08, section 02.1, the inspectors
reviewed Salem's method for assessing the operability of degraded or
nonconforming structures, systems, and components. The inspectors concluded
that the new operability determination process provided clear guidance for
documenting and tracking the operability of degraded or nonconforming equipment ..
ThE;i inspectors noted, however, that operations and system engineering staff had
not received training on implementation of the new system. As a result, the
inspectors left NRC Restart Item 111.6 open at that time.
Observations and Findings
The inspectors verified that operations and system engineering staff had received
training on implementation of the new system. In addition, the inspectors reviewed
several recent operability determinations and observed the staff presentations of
operability determinations to SORC. The inspectors noted that the station staff
presented comprehensive operability determinations that included consideration of
design and licensing basis information pertinent io the equipment evaluated in the
operability determination. The presentations included operability determinations for
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component cooling water room coolers, containment fan coil units, and others. The
inspectors considered the operability determinations acceptable.
Conclusions
The inspectors concluded that implementation of effective operability determination
training for operations and system engineering staff resulted in an effective process
for developing operability determinations.
03
Operations Procedures and Documentation
03.1
Procedure Use And Adequacy - NRC Restart Item 111.3 (Closed)
a.
b.
Inspection Scope (92901)
The inspector reviewed the licensee's actions to address problems with the use and
adequacy of procedures.
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Observations and Findings
Procedure Adherence
Salem implemented several initiatives to improve performance in procedure
adherence including:
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Site and departmental management reinforced procedure use expectations
through memorandums and site messages.
Salem staff upgraded.procedure use instructions in several areas .
Plant staff conducted procedure use training for operations and maintenance
department personnel.
The inspector concluded that these actions improved procedure adherence. The
inspector performed several observations and reviewed the recent inspection record
to determine the effectiveness of these actions. Recent inspection reports (96-15,
96-17, 96-18) noted generally good and improving procedure adherence
performance. Inspectors also noted good procedure adherence for operations and
maintenance activities monitored this period.
Proc<:?dure Adequacy
The licensee reviewed procedures in the station operations, maintenance,
chemistry, radiological protection, and engineering areas. Plant staff revised or
validated a number of operations procedures including the abnormal, emergency,
alarm response, and integrated operating procedures. They also upgraded
maintenance troubleshooting, Hagan module configuration and calibration, and
foreign material exclusion control procedures. Plant staff targeted specific
enhancements for chemistry and radiological procedures .
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Salem staff updated the procedure writer and reviewer's guide, and developed a
program to train procedure writers on the new guide. The licensee recently
identified additional chemistry procedure enhancements to remove statements that
could lead to mis-interpretation. The licensee reviewed the procedure revision
backlog in the operations, maintenance, chemistry and radiological areas and
identified the procedures that required revision prior to restart.
The inspector reviewed a portion of the operations procedure backlog and di_d not
identify any procedures that required revision prior to restart. Additionally, the
inspector reviewed normal operating procedures and did not identify any technical
deficiencies. Maintenance procedures reviewed during plant observations appeared
adequate.
Conclusions
The station has implemented a number of programs designed to enhance procedure
use and adequacy. Recent inspection observations indicate good and improving
procedure use. Plant staff reviewed and revised procedures in key station
functional areas. They appropriately identified corrected operations procedures that
required revision prior to restart. The inspector considered sampled procedures
adequate and generally consistent with the procedure writer's guide. The inspector
considered procedure use and adherence adequate.
03.2 Control of Pressurizer Auxiliary Spray 171707)
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On March 11, Unit 2 operators stroked 2CV75 (auxiliary spray valve) in accordance
with S2.0P-ST.CVC-0007, /nservice Testing Chemical and Volume Control Valves
in Modes 5 and 6. The reactor operator ensur~d that spray differential temperature
did not exceed 320°F as specified in Technical Specification 3.4.10.2.C. The
inspector noted, however, that S2.0P-ST.CVC-0007 did not provide guidance to
prevent operators from exceeding a 320°F differential temperature and impacting
pressurizer spray nozzle fracture toughness. The reactor operator initiated a
procedure revision request to improve S2.0P-ST.CVC-0007. The inspector
concluded that operators demonstrated good awareness of technical specification
requirements and ensured plant operation within specified limits despite lack of
procedure guidance to limit the differential temperature.
Operator Knowledge and Performance
04. 1 Operator Performance, NRC Restart Item Ill. 7 (Closed)
a.
Inspection Scope (92901)
The inspector reviewed corre~tive actions to address operator performance
weaknesses. The inspector assessed operator performance relative to the restart o.f
the $alem units.
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Observations and Findings
Starting in June 1995, the operations manager acted to increase operations
staffing, improve operator training, and raise operator standards. The operations
manager strengthened shift resources through increased shift technical advisor
(ST A) staffing, hiring seven previously licensed senior reactor operators (SROs) with
significant operating experience, and balancing operating crews based on strengths,
weaknesses, and personalities .. The operations and training staff developed and
implemented a comprehensive two phase training program to improve operator
performance. The first phase involved a comprehensive assessment of licensed
operator knowledge, skills, and attitudes through written, oral, and performance
evaluations. The second phase contained training specifically targeting phase one
weaknesses and involved approximately 500 contact hours. The training focused
not only oil knowledge and skills, but on affecting the cultural shift needed for safe
plant operations.
In recent inspection reports (50-272 and 311/96-17 and 96-18), inspectors
documented good performance in the following areas:
- risk management and safety focus,
- technical specification* compliance,
- intolerance for workarounds,
- identification of degraded conditions and timely corrective action,
- procedure compliance, ..
- operator knowledge,
- questioning attitude,
Ii communication and coordination,
- plant ownership, and
- .awareness of plant equipment status.
Although operator performance continued to improve since June 1995, operators
periodically failed to meet management expectations and, on occasion, NRC
requirements. Operations mar,iagement's prompt and comprehensive corrective
actions for past errors reduced the frequency and consequences of similar
performance lapses. For example, on January 2, 1997, operators experienced a
problem with reactor coolant system (RCS) level indication as a result of an
operator-induced valve misalignment during the RCS fill and vent. Operators
immediately recognized and responded to the problem as a result of their focus on
RCS level. Operations management immediately took comprehensive corrective
action. The valve misalignment had no safety consequence.
Conclusions
Operations management implemented extensive corrective measures and affected
significant improvement in operator performance since June 1995. Operators
demonstrated safety-conscious decision making, ownership for plant equipment,
detailed knowiedge of plant operation, a good questioning attitude, effective
communications, procedure compliance, an intolerance for workarounds, and a
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propensity to identify arid correct deficient conditions. Operator performance
supports restart of the Salem units.
04.2 Routine Operator Performance Observations
a.
Inspection Scope (717071
b.
The inspectors observed the control room operators perform routine plant activities
including transfer of the operating Unit 2 residual heat removal (RHR) heat
exchanger in accordance with S2.0P-SO.RHR~0001, "Initiating RHR" and response
to a low ambient temperature condition in the Unit 1 and Unit 2 service water (SW)
pump bays.
Observations and Findings*
Transferring Residual Heat Removal Loops - Unit 2
The inspectors observed that a reactor coolant pump (RCP) bearing low cooling
flow alarm repeatedly actuated and cleared during transfer of the operating Unit 2
RHR heat exchanger. The control room operator (CRO) attributed the alarm
condition to aligning the component coolin[I water (CCW) flow into the standby
RHR system heat exchanger. The CRO did not refer to the alarm response card
(ARC) and completed transferring the RHR heat exchangers. The RCP cooling flow
alarm promptly cleared upon completion of the transfer evolution, demonstrating
that the alarm did not represent a degraded condition. The inspector considered
that not referring to the alarm response card demonstrated a poor operator practice.
The inspector did not identify any other operator deficiencies during the evolution.
The system manager and the assistant operations manager indicated that they
would review the S2.0P-SO.RHR*0001 procedure to determine if the RHR heat
exchangers could be transferred with less impact on the CCW system flow.
Low Service Water Pump Bay Ambient Temperature Readings
The inspector noted that the logged 1 and 2 SW pump bay ambient temperatures
were between 50 and 58°F during a two day period. The minimum specified log
temperature for these rooms was 60°F. The plant operators properly identified and
circled the out of specification log readings, and verified that an active action
request existed to address the cause for the low room temperature conditions.
The nuclear shift supervisor (NSS) did not know whether the low temperature
condition had been evaluated to ensure that the safety-related components in the
SW pump bays remained operable. The inspector reviewed the Updated Final
Safety Analysis Report (UFSAR), Section 9.4.7.1, and noted that the SW pump bay
room had a low ambient temperature alarm setpoint of 40°F and concluded that the
recorded SW pump bay temperatures did not exceed the room ambient temperature
design limits .
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The inspector discussed this observation with the Operations Manager and learned
that a previous shift had evaluated the impact of the low temperature condition on
the operability of components. The inspector concluded that NSS's lack of
familiarity with this evaluation demonstrated weaknesses in the evaluation of off-
normal plant conditions and the communication of information during shift
turnovers.
c.
Conclusions
The inspector concluded that although routine operator performance is generally
good; some weaknesses were noted involving use of the alarm response cards,
evaluation of an off-normal plant condition, and shift turnovers.
05
Operator Training *and Qualification
In a letter dated March 18, 1997, NRC issued a violation for two aspects of
licensed operator requalification training that did not meet 10 CFR 55.59(c) based
on licensee submittals dated November 7, 1996, January 6, 1997, and February
12, 1997: The two aspects related to compliance with requirements for an annual
operating test for all operators and for continuous requalification training programs
not to exceed 2 years in duration. The NRC letter also noted that the operator
training has been high quality and effective, but the violation represents weak
program planning. For follow-up purposes, this violation will be numbered as VIO
50-272&311/97-03-01.
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Miscellaneous Operations Issue
08. 1 Operations Restart Action Plan (Closed)
a.
Inspection Scope (92901 l
The Salem Operations Restart Action Plan established a performance based
approach to specify and control the actions required to demonstrate operations
restar:t readiness. The inspector reviewed operations implementation of their restart
- plan and assessed operations readiness for restart.
b.
Observations and Findings
The Operations Manager identified six major areas for improvement, and developed
six problem statements to describe the weaknesses and outline corrective actions.
The inspector closed problem statements nos. 1, 2, 3, and 6 in inspection report
50-272 and 311 / 96-18.
Problem statement no. 4 identified that operations procedures and policies need to
be strengthened to support long-term operational excellence and plant startup. The
inspector reviewed operations' corrective actions and concluded that the adequacy
and use of procedures supported restart of the Salem units (see section 03.1 ). The
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inspector consic!.::.ied the actions to address problem statement no. 4 adequate to
support restart.
Problem statement no. 5 identified that operations' ownership for skills, knowledge,
attitude and training of operators needed significant improvement. Inspectors
reviewed the adequacy of training, NRC Restart Item 111.16, in inspection report 50-
272 and 50-311 / 96-08. Inspectors concluded that the Salem training staff
significantly improved the training programs through implementation of the Salem
Training Restart Action Plan. The PSE&G staff made significant improvements in
training program self-assessments and line management involvement in the training
programs. The inspector considered the actions to address problem statement no.
5 adequate to support restart.
c.
Conclusions
Operations established, implemented, and completed an effective restart action plan
to demonstrate operations' readiness for restart of both Salem units.
oa.2* Containment Cleanliness (71707)
The inspector assessed the Unit 2 containment material condition and housekeeping
as plant staff prepared for mode 4, Hot Shutdown, operation. Early in the period,
five "sparkle" teams led by radiation protection identified approximately 200 minor
deficiencies. The Operations Manager and OA/NSR Director spearheaded a
management effort to upgrade standards concerning plant material condition. Plant
management set higher standards for the inspection teams and the teams identified .
60 additional containment deficiencies. Further management guidance and direct
inspection effort resulted in 40 more documented defiC:iencies. The inspection .
teams identified and removed a significant amount of small debris including paint
chips, plastic bags, loose lagging, tape, cable ties, and discrepancy tags. Plant
management planned to apply the same high level inspection effort to the remainder
of the Salem facility. The inspector noted that plant managers successfully
accomplished two goals: they significantly raised the standards for acceptable
plant cleanliness, and they successfully implemented the standards in the Salem .
Unit 2 containment.
08.3 Criticality Monitors
a.
Inspection Scope (71707)
b.
The inspectors reviewed the Salem Unit 1 and Unit 2 plant design to determine
compliance with the requirements of 10 CFR 70.24.
Observations and Findings
The Salem UFSAR, section 12.1.3.6, states: "A Geiger-Mueller, or equivalent
monitor is located on the operating deck floor (Elevation 1 30 feet) of each Fuel
Handling Building. These monitors are sensitive to gamma radiation and are
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alarmed in accordance with NRC Regulation 10 CFR 70.24; The alarm will sound
locally and in the control room." The UFSAR also states that Salem staff has
written comprehensive emergency procedures to ensure that all personnel withdraw
upon the sounding of the alarm to a designated area of safety. The inspectors
verified installation of the radiation monitors ( 1 R5 and 1 R9 for Unit 1 , _2R5 and 2R9
for Unit 2) described in the UFSAR. *The engineering staff verified that the alarm
setpoints for the radiation monitors met requirements of 10 CFR 70.24 a(1) for
both Salem units. The Salem Operating Procedures and Emergency Plan
Implementing Procedures contain procedures to evacuate the Fuel Handling Building
in the event of high .radiation conditions. The Salem staff intended to review
station procedures for opportunities to improve the procedures with respect to the
requirements of 10 CFR 70.24 a(3). *
Conclusions
The inspectors concluded that Salem radiation monitors and procedures adequately
addressed tfle requirements of 10 CFR 70.24.
08.4 Management Oversight of Quality Assurance and Nuclear Safety Review (QA/NSRl
a.
Inspection Scope (71707)
b.
The inspectors -reviewed the results of an investigation of potentiai adverse
management oversight effects on QA reports.
Observations and Findings
In January 1997, the Employees Concern Program received an anonymous concern:
that certain activities by QA/NSR managers could lead to inappropriate toning down
or alteration of QA reports, and may have resulted in reprimands. The Nuclear
Business Unit (NBU) managers concluded that the nature of the concern
necessitated investigation by an independent source. The NBU managers appointed
the Director, Nuclear Business Support as the investigation manager. The
investigation manager, in turn, chose a nuclear procurement manager and an
outside consultant to conduct the investigation.
The investigators reviewed a random sample of 1996 QA audits and surveillances
for Salem and Hope Creek. They compared the field notes and checklists with the
final reports to determine if findings had changed. The investigators also
intervievJed randomly selected personnel to determine the validity of the concern.
In addition, the investigators reviewed performance appraisals for indications of
reprimands as suggested by the concern.
The investigators found no evidence that QA staff had toned down the findings in
their audits and surveillances. All intervif:wed members of the QA staff confirmed
this conclusion. The interviewed personnel indicated that managers had not
pressured them to tone down their findings with the exception of the occasiona.1
use of abrasive language in their reports. The interviewees all stated that any such
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changes were made with their concurrence, *and if they disagreed the wording was
not changed. The investigators found no indication of reprimands or other
repercussions in the performance appraisals. Although the performance appraisals
contained critical observation of auditors' communication skills, the investigators
considered the observations constructive criticism.
Conclusions
The inspectors concluded that the independent investigation effectively
demonstrated that QA management had not taken action that resulted in toning
down QA inspector findings. The investigation also effectively demonstrated that
QA managers had not taken action to reprimand or otherwise penalize QA
"inspectors as a result of the aA inspectors' findings.
08.5 Commitment Management. NRC Restart Item 111.14 (Open)
a.
b.
Inspection Scope
The NRC Staff identified instances where the licensee failed to meet commitments,
both within the licensee's organizations and ~ith the NRC Staff. The inspector
reviewed licensee actions to insure that plant staff takes effective action to address
commitments.
Observations and Findings
On August 21, 1996, the licensee documented the completion of. a review of a
sampll;l of completed NRC commitments to ascertain whether these commitments
were properly implemented. The sample included 2653 commitments consisting of
98% of commitments made between 1990 and 1995, 58% of commitments made
between 1985 to 1989, 17% of the commitments associated with NRC's NUREG-
0737, and 99% of the commitments associated with NRC's Generic Letter 83-28.
The licensee staff obtained the commitments associated with Salem Units 1 and 2
directly from the original source documents *(e.g .. Licensee Event Reports, response
to Notices of Violations, and docketed correspondence). The results of the review
indicated that less than 2 % of the commitments (45 commitments) had not been
properly implemented due to never having been implemented (7 commitments),
implemented but inadvertently changed (7 commitments), or not properly
implemented (31 commitments). The plant staff verified that all Salem Unit 2
restart commitments had been entered in a commitment management system.
The inspector verified that the licensee had initiated measures to resolve the 45
deficient commitments. In addition, the inspector reviewed a sample of ten
additional commitments, observed the retrieval of these commitments from the
licensee's data base, and confirmed that they were properly managed.
In addition to reviewing completed commitments, the licensee evaluated the
commitment management process to resolve the deficiencies that had resulted in
the failure to properly implement the 45 commitments noted above. The
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evaluation, contained in Performance Improvement Request (PIA) No. 960111309,
resulted in the following short term corrective actions:
A.
Plant management held a meeting with licensing personnel on January 26,
1996 to discuss the issue of commitment tracking.
B.
The staff initiated a 30-day look ahead and overdue report for commitments.
c.
The support staff developed commitment Performance Indicators.
D.
Licensing planned to provide due dates for all commitments in
correspondence to the NRC.
The inspector reviewed the implementation of the licensee's short term corrective
actions and found them useful and well implemented. This is particularly true of
the 30-day look ahead and overdue report, provided periodically to Salem and Hope
Creek to alert responsible individuals to pending or late commitments.
In addition to the above, PIA 960111309 proposed the following long term
corrective actions:
A.
The licensee planned to _establish expectations and standards for
commitment management and communicate them to all licensing personnel.
The inspector observed accomplishment of this objective in meetings held on
March 27 and 29, 1996.
B.
c.
D.
Licensing staff planned to review current Nuclear Department Administrative
procedures and work standards associated with management of
commitments. The inspector could not determine the schedule for.
completion of the revised commitment management procedures. This task is
open pending inspector revi""-' and acceptance of the finalized procedures.
(IFI 50-311/97-03-02)
Licensing planned to clearly communicate commitment management
expectations to NBU managers. The inspector reviewed the statement of
expectations associated with commitment management, forwarded to NBU
management in a memo dated April .29, 1996 and found these expectations
acceptable.
Licensing planned to evaluate other commitment tracking databases and
determine if changes were necessary. The inspector noted that the licensee
utilized several tracking databases to manage commitments. Although the
licensee no longer used A TS to manage. new commitments, it contains old
commitments that still require implementation. The PIA system superseded
ATS but also stopped using it to manage new commitments as of December
31, 1996. The licensee began to use the Commitment Manager database to
manage all commitments as of January 1, 1 997.
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Plant staff planned to perform a self-assessment of the commitment
management process. This licensee has not completed the self~assessment
since it is viewed as a long term verification effort. The inspector did not
consider completion of the self-assessment necessary for NRC closure of
Restart Item 111.14.
The staff planned to evaluate the process for identifying commitments. The
licensee completed this eff_ort as documented in PIR 960111309. The
inspector noted that no list of long term commitments for Salem existed
prior to implementation of procedure NC.NA-AP.ZZ-0030(0), "Commitment
Management", on March 15, 1992. The source documents for these
commitments, however, remain available and computer searchable.
Moreo_ver, the results of the commitment verification process (an
approximately 98 % success rate for fulfillment of commitments) indicate
that plant staff effectively managed commitments although improvements in
the process remain warranted.
Con~!usior.:J
The licensee took action to improve commitment management. The licensee has
developed and improved methods for commitment management (e.g .. Commitment
Manager and the 30-day look ahead report), made the responsible management and
personnel aware of the use of these methods and commitment management
expectations, and began to improve commitment management procedures. When
the licensee completes the improvements to the commitment management
procedures, the NRC will close NRC Restart Item 111.14.
08.6 (Closed) Violations 50-272&311/93-23 (EA 94-003-01013, 01023, 01033,
01043, 01053, 01063, 01073. & 010831 and 50-272&311/96-06-01. 96-01-01 &
96-01-02: Collectively these violations documented failure to follow procedures,
and fell into two categories: Tagging work practices, and verbal and procedural
work control. The licensee conducted root cause analyses and identified the
following causal factors: 1 ) less than adequate supervisory methods (insufficient
management/supervisory oversight), 2) less than adequate verbal communications,
and 3) less than adequate work practices (failure to follow procedures), and self
checking by the individual workers. The inspector reviewed the above analysis and
did not identify any additional contributing factors to those identified by the
licensee.
Corrective actions: The licensee temporarily stopped work to communicate
- expectations with regard to safety and work standards to the workers. Meetings
were held with contractor supervisors and craft personnel to relay the licensee
expectations for safety and adherence to work standards. Operation directives
were issued to re-emphasize the proper sequence of tagging work releases.
Radiation technicians were reminded of the requirements for the release of
materials from the work controlled area. Regarding the 1993 violation, the licensee
established an on-~hift middle management review group to review and assess and
control of maintenance activities.
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The inspector reviewed documentation confirming that the corrective ac.tions stated
above were enacted to correct the immediate concerns.
Actions to prevent recurrence: The licensee took the following actions to prevent
recurrence:
1 .
Directions, from station management, were made annotating the expectation *
that supervisory/managerial. personnel increase the field time spent
2.
3.
4.
5.
monitoring and assessing work, providing direction, and taking appropriate
corrective actions when necessary.
Carefully reviewed the scope of future outages to ensure management
oversight is sufficient for the job tasks.
Decreased the number of vendors from 3 to 2 to provide better licensee
oversight.
Provided better focus on station planning and proposed the establishment of
two separate work control centers by *the end of 1996.
Established an oversight team to; review pre-outage work progress,. monitor
work control progress, and review incidents of previous outages as they
relate to the work standards, contractor control and work control process in
general for lessons learned.
The inspector reviewed the documentation of meetings held by licensee*.
management with all levels of the Salem organization* that identified reasons for the
events and emphasized management expectations for all maintenance work to be .; ..
performed in the future. The inspectors noted that the concern over control of the
scope of outages did not apply,.._ the current outage due to its duration. However,
the licensee plans to address the control of outage scope in the. new work control
process implemented after restart. Inspectors als.o noted that the licensee has
greatly reduced the use of vendors in recent months. The plant managers
implemented the "war room" concept to improve work control center effectiveness.
The oversight team was established. The inspector reviewed selected findings of
the group and determined that they were focusing on the areas that would make
failure to follow procedure problems less likely.
Inspectors will review the effectiveness of corrective actions for tagging
deficiencies as part of NRC Restart Item 111.12 prior to plant start-up.
The inspectors considered the implemented corrective actions adequate, and noted
recent improvements in procedure use and adherence. This item is closed.
08. 7
(Closed) LER 50-311 /96-009: fourteen day followup report regarding 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts
for operations personnel. This LER identified a conflict between the Operations
staff's practice of assigning operators 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> work shifts versus a license
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13
requirement for 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shifts (NRC Inspection Report 50-272&311 /96-15 has
details). Salem management requested an operating license amendment to delete
the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shift restriction and the NRC has approved this request. Salem staff
implemented ~he amendment (no. 169) on January 13, 1997. This item is closed.
08.8 (Closed) Unresolved Item 50-272&311 /96-08-06: Salem Unit 2 Operating License
does not permit 1 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> operating shifts. This issue is identical to the issue in LER *
50-311196-009. This issue was licensee identified and corrected, and predates the
shutdown of Salem Units 1 and 2. This licensee identified and corrected violation
is being treated as a Non-Cited Violation, consistent with Section Vll.B.1 of the
08. 9 (Closed) Violation E94-11 2-04013: PSE&G staff provided inadequate training,.
guidance, and procedures for operators to handle plant transients properly. On
April 7, 1994, events initiated ~y grass intrusion into the circulating water system
led to a rapid power reduction, a reactor trip and a safety injection. During the rapid
p::>wer reduction, Salem operators exceeded allowable shutdown rates and the
reactor temperature dropped below minimum allowable*temperature. The safety
injection resulted in operators filling the pressurizer to solid conditions. During the
recovery from the solid pressurizer condition, neither plant procedures nor operator
' * training was adequate in that the operators were unable to use any procedure
relating to existing plant conditions.
In response to the violation, the licensee.'s staff made numerous procedure changes
to operating and emergency procedures to provide adequate guidance for operators
in handling a future event of this type. Also, the licensee developed a new
procedure to address rapid* load reduction for turbine load reductions of equal to or
greater than 5% per minute. Salem staff trained and qualified all operating crews *
on the new and revised procedures. Operations personnel ran the event scenario at
the Salem simulator and training personnel stopped the scenario at critical points to
discuss lessons learned. The Operations manager required individuals whose
performance was less than expected to complete additional training for
qualification.
The inspector reviewed documentation specific to this i.ncident and confirmed that
Salem staff enhanced the procedures and that operators completed the training.
The generic issue of procedure adequacy and adherence is the subject of NRC
Restart Issue 111.3.1. Salem staff must complete the corrective action for that item
and NRC staff must evaluate the response prior to the restart of Salem Unit 2.
Based ori the response to this violation and the understanding that Salem
management will complete NRC Restart Issue 111.3. 1 prior to restart, this violation is
closed.
08.10 (Closed) Violation 50-27 L & 311 /95-07-03: failure to follow procedures. During
inspections in April and May 1995, inspectors noted five examples of activities in
progress that they judged not to meet Salem procedure requirements. Although
none of the examples was safety significant, the number of examples indicated a
trend of procedure non compliance. PSE&G staff responded to four of the
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examples with appropriate corrective* action and contested one example as not
being a procedure violation. The inspector reviewed the response and samples of
corrective action documentation. The review confirmed that Salem staff completed
procedure changes and training for the four non disputed examples. The inspector
reviewed the response for the disputed example and found the justification
sufficient to withdraw only the fifth example of the violation. The inspector
concluded that the activity, specifically, an attempt to correct a malfunctioning
security door latch, did not require a procedure. Also, Salem personnel later
generated a corrective action to document the replacement of worn parts. The
inspector concluded that the response to this violation was satisfactory. This item
is closed.
08.1 l (Closed) Violation 50-272 & 311 /96-15-02: failure to follow procedures. While
preparing to remove the 1 C 460/230 volt bus from service, operators performed
steps out of sequence. The procedure did not provide for this latitude. PSE&G
staff responded to this violation with several corrective action steps as follows:
Salem management counseled the personnel involved in accordance with PSE&G
site procedures.
The Operations staff revised the procedure to reflect the changed step sequence.
Salem operations management prpvided guidance to all operations personnel via
night orders, a departmental memo, and temporary standing orders.
Salem staff issued Administrative Procedure NC.NA-AP.ZZ-0001 (Q), Nuclear
Procedure System, Revision 10, effective December 6, 1996 and trained operations
personnel regarding use of procedures.
The inspector .found that the corrective action for this specific violation was
acceptable. The generic issue of procedure adequacy and adherence is the subject
of NRC Restart Issue 111.3.1. The NRC staff must evaluate the response to this
issue prior to the restart of Salem Unit 2. Based on the response to this violation
and the understanding that Salem management will resolve NRC -Restart Issue
111.3.1 prior to restart, this violation is closed.
i
08.12 (Closed) Unresolved Item 50-272&311 /93-15-04: 50-354/93-11-01. Corrective
Action Program Weaknesses
In the subject inspection, the inspector identified weaknesses in the licensee's
corrective action program (CAP). During a followup investigation concerning a
containment fan cooler unit (CFCU) regulator, the licensee identified minor
weaknesses in the incident report, engineering discrepancy control, a deficiency
report, and work control processes. In this case, the inspector found the processes
to be properly implemented, but noted weak coordination between these processes.
Currently, the licensee has made significant progress in imp~oving the CAP. The
implementation of a single point of entry (Action Requests) for the CAP has virtually
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15
eliminated the c0nrdination problem between programs and processes. A recently
completed inspection (50-272/96-18) noted marked performance improvement in
the administration and implementation of the CAP. Based on the above, this item is
closed.
08.13 (Closed) Violation 50-272 & 311 /96-08-05 : inadequate procedures. From June
30, 1996 until August 10, 1996, the NRC inspectors identified four inadequate
Salem plant procedures; three were for operating plant safety related systems and
one was for reactor vessel head reassembly. Salem management's response to the
violation stated that plant staff revised the procedures and provided details of those
changes. The response also detailed corrective steps to prevent recurrence. These
corrective actions included steps specific to the procedures identified, such as
_communication to procedure writers and to reviewers, and. more generic corrective
action such as the extensive procedure review for technical adequacy as part of the
Salem Restart effort.
The inspector reviewed the specific procedures identified in the violation and
determined that Salem staff made the required changes. From the review of the
response, the inspector also concluded that other corrective actions were
satisfactory for these specific procedure i1adequacies. Considering the corrective
action already taken and since Salem management will resolve the generic issue of
procedure adequacy prior to restart as part of NRC Restart Issue 111.3. 1, Adequacy
and Use of Procedures, the inspector considered this violation closed.
08.14 (Closed) Violation 50-272 & 311 /96-17-01: failure to perform a safety evaluation
in accordance with 10 CFR 50.59. Operators developed a temporary procedure to
control activities during a total station air outage. Personnel developing the
- procedure incorrectly concluded that the changes to the plant detailed in the
procedure did not meet the criteria of 10 CFR 50.59 to require a safety analysis.
Once questioned by the inspector, Salem staff promptly completed the safety
analysis. NRC Inspection Report 50-272&311 /96-17 documented the fact that the
inspector reviewed the safety analysis and found it acceptable. In response to the
violation, Salem management communicated the event and lessons learned to
operations staff and other department managers, and incorporated these lessons in
the 10 CFR 50.59 training program. The inspector concluded that the corrective
action for this violation was adequate. This item is closed.
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II. Maintenance
M 1
Conduct of Maintenance
M1 .1
General Comments
a.
Inspection Scope !62707)
The inspectors observed .all or portions of the following work activities:
- 950610179:
- 961031038:
.* 960927115:
RHR discharge valve weld repair
1 B EOG Elliot strainer 92 day lube
addition of overpressure device on CFCU return piping
The inspectors observed that the plant staff performed the maintenance effectively
within the requirements of the station maintenance program.
b.
Inspection Scope (61726)
The inspectors observed all or portions o*; the following surveillances:
- S2.0P-ST.DG-0003:
- S2.0P-ST.DG-0004:*
- S1 .OP-ST.DG-0001:
- S2.RE-ST.ZZ-0002:
- S2.0P-ST.DG-0001:
- 52.0P-ST.CVC-0001:
- SC.OP-ST.CAV-0001:
- SC.OP-ST.CAV-0001:
2C diesel generator surveillance test
diesel generator auxiliaries 21 fuel oil transfer system
operability test
1 A diesel generator surveillance test
shutdown margin calculation
2A diesel generator surveillance test
inservice testing - 21 boric acid transfer pump
plant systems control room ventilation
- control room emergency air conditioning system manual
operation
The inspectors observed that plant staff did the surveillar:ice safely, and effectively
demonstrates operability of the associated system.
M1 .2 Salem Maintenance Restart Action Plan (Closed)
a.
Inspection Scope
The inspector reviewed the list of corrective maintenance work orders and a sample
of work orders required for restart. The inspector also reviewed corrective action
documents related to maintenance issues that Salem personnel generated during
the previous month to determine the nature and significance of the problems
identified. In addition, the inspector monitored an ongoing Quality Assurance audit
of maintenance activities and observed maintenance work in progress to gain
additional insight regarding the maintenance program .
b.
17
Observations and Findings
Salem maintenance personnel provided the inspector a list of work orders required
for the restart of Unit 2 as of January 31, 1997. The list provided brief
descriptions of 728 work orders and provided the status and priority of these work
orders. From the review of this list, the inspector found four examples where the
priorities were incorrect when compared with the criteria of procedure NC.NA-
AP.ZZ-0009(0), Work Control Process. However, personnel had appropriately.
prioritized the vast majority. Three of the four had a lower priority assigned than
was appropriate. However, work was in progress indicating that they were in fact
getting treated as priority work. Also, for those work orders* on the list that were
of highest priority, the status was "Work In Progress". thus indicating they too were
. in fact receiving priority treatment. The inspector found that this prioritizing
method allowed emergent wor.k that was urgent to be given immediate attention
when necessary.
The Quality Assessment group provided copies of corrective action documents that
documented problems .related to maintenance. These documents, 108 in total,
represented the total related to maintenance issued during December 1996. Of
these, thirty-four were examples of completed work orders which did not resolve
- the original problem. The inspector reviewed these in_ more detail and determined
that although this number was greater than optimum, i.e., zero, the number did not
represent a significant problem in the quality of work being performed (considering
that Salem maintenance was completing more than 1000 work orders per month).
The inspector also noted from his review of the 108 dqcuments that Salem staff
had given adequate consideration regarding generic implications.
The inspector met with the manager of the Salem maintenance department to
discuss the metl-\\ods by which supervisors monitor work in the field. The inspector
learned that the primary method used is a formal Self Assessment Program. The
maintenance manager has set up a program that requires each supervisor to
conduct and document three observations of field work per week, at a minimum.
The observations are performed using an 85-point checklist as a guide.
Maintenance compiles and trends the data periodically to detect weak areas of
performance. Manage.ment can then direct attention to problem areas and apply
corrective action. In addition, the inspector learned that the Quality Assessment
group routinely performs field observations and assessments of maintenance
activities and forwards this information to maintenance.
To assess the acceptability of post maintenance testing, the inspector selected ten
completed work orders that, by the nature of work performed, would require testing
to demonstrate acceptable work completion. The inspector found that each work
order reviewed provided documentation of acceptable retesting, but noted that in
most cases, the description 'at testing requirements, as originally provided in tl:le
work order by the planners, was vague. The inspector reviewed ten more work
orders, the planning for which, had been performed within the past two months.
The inspector found that for each of these more recent work orders, the description
of the post maintenance testing was more specific. Most referenced a specific
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procedure that the technician should use to conduct a suitable test. The inspector
considered these as examples of improvement in the planning of work orders with
regard to describing required post maintenance testing.
The inspector performed field observations of mai.ntenance work iri progress to help
assess the effectiveness of improvements made to the maintenance program. The
inspector observed a calibration of a containment fan coil unit water flow controller,
installation of temporary test equipment on a turbine steam bypass valve,
assembly of a turbine auxiliary cooling pump, and .preventive maintenance for
moisture separator reheater controls. Contractors were working the first two jobs
and PSE&G personnel were working the last two jobs. The inspector found that
personnel were properly using procedures, were storing tools and* disassembled
.equipment properly, and were using measuring and test equipment (M&TE) which
had been properly calibrated. PSE&G personnel were knowledgeable regarding their
work and when in doubt, were contacting their supervisor for assistance.
In addition to the Salem plant maintenance organization, the Maintenance Services
group also performs maintenance work.- Most of the work performed by this group
is related to the site f~cilities such as buildings, traveling screens, heating boiler,
and switchyar:d. However, the group sometimes performs work on_ in-plant
systems such*as service water (a safety* related system), heater drain pumps, and
the turbine. During this inspection period, the Quality Assessment organization :
performed an audit of Maintenance Service activities; As a result of findings from .. *
- that audit regarding the M& TE calibration process and* procedure non-compliance.
within the site services activities, the manager of Maintenance Services ordered a
w.ork stoppage. During this three day stoppage, managers and supervisors *
counseled. technicians regarding procedure use and compliance, quality of work,
safety, identification of problems and use of the corrective action-program and
other applicable topics. The Salem plant management decided that Maintenance
Services would no longer be utilized for safety related work until the Maintenance
Services.management demonstrated r<>adiness for satisfactory work control and
implementation.
Conclusions
The inspector concluded from his observations that the maintenance restart action *
plan was effective. Management is aware of emergent work and actively
participates in the assignment o.f priorities to safety significant work. Overall,
maintenance personnel are willing to identify new problems and initiate corrective
action. For the activities observed, maintenance technicians were using procedures
and tools properly in the conduct of maintenance. Management actively monitors
performance and status utilizing various trending tools and through the use of self
assessments. Additionally, OA provides useful feedback regarding performance.
The inspector considers the assessment program and the QA feedback strengths in
that these feedback processes should enable manage.ment to continue the .
improvement process for the maintenance program. Through the review of
maintenance related deficiency documentation, the inspector concluded that there
are still weaknesses in the maintenance program. However, the licensee has
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significantly improved, and continues to improve the maintenance program. The
inspector concluded that the maintenance program is ready to support restart of
Salem Units 1 & 2.
M1 .3 Steam Generator Replacement Project !SGRP> Inspection Procedure 50001
a.
Inspection Scope
Inspections were performed to obtain an overview of current and planned work,
related procedures, documentation, quality inputs and progress of the .Salem Unit 1
steam generator replacement project (SGRP) .
. Specific areas inspected included observation of reactor coolant system (RCS)
welding on no. 13 replacement steam generator (RSG), feedwater (FW) pipe
welding in the fabrication shop, FW pipe welds in containment, main steam (MS)
pipe machine welding mockup practice; RSG weld planning and extent of weld
supervisory coverage; weld procedures and materials for RCS, MS, FW, steam
generator blowdown (SGBD) *piping and structural steel welding; the pre-service
inspection and inservice inspection (ISi) planning to meet the requirements of 10
CFR 50.55a(g) and .the ASME Code Section XI; adequacy of weld's for ISi, review
of Work Package 3011871086 for RSG no. 14 primary pipe welding; the as-welded
root valves; the Authorized Nuclear Inspector (ANI) involvement in SGRP activities
as documented in work packages; preparation and procedure controls for
Radiography, the quality and acceptability of interim and final Radiographs on the
RCS welds of RSGs 11, 12 & 14; original steam genere1tor (OSGI and RSG moving,
handling, rigging and lifting; observation of movement of the third OSG to and onto
the barge for transport offsite; the prejob briefing for and upending of RSG 11 in
containment; foreign material exclusion (FME) control; the basis for why the new .
insulation for RSGs and piping is acceptable; the*post RSG installation restoration
process including controls and documentation; the Polar crane remote control; Polar
Crane track clamps/seismic restraint interferences; and fire control.
The site inspection included observations of conditions and work in and outside the
containment structure.
b.
Observations and Findings
By March 1 2, 1 997, the 4 original steam generators (OSGs) had been shipped from
the site by barge for burial. The 4 replacement steam generators (RSGs) were in
place in the. Unit 1 containment building with welding of the steam generator
nozzles to the reactor coolant piping complete and accepted by radiographic
examination. Fitup and. welding of the feedwater and main steam piping was in
progress.- Restoration of other items removed as a part of the SGRP, including the
steam generator upper restraints and structural steel, was continuing.
The inspection found that work activities were generally well planned and properly
documented. The machining of the steam generator RCS nozzles and RCS piping
elbow ends to dimensions developed, using computer-based measuring techniques,
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resulted in RCS weld joint fitups that met very close tolerances. The work
packages were being tracked and closed out at a rate commensurate with work
completion. Surveillances of project conditions and specific work activities were
done by project Quality Assurance. In project areas. where problems were
identified, work was delayed or stopped until an acceptable course of action was
established. Examples of problems include the interference of the polar crane
.seismic lug with one of the track hold down lugs during positioning of the fourth
RSG, resolution of upper RSG support details, the selection of a volumetric .ISi
inspection method for the RCS elbow-to-head nozzle welds due to the difficulty of
performing an adequate UT examination of the cast stainless material, and the *
acceptability of the weld surface contour for ISi ultrasonic inspection of the FW
pipe transition pieces to RSG FW nozzles.
The engineering work packages, EWP-1 EA-1243-01 and EWP-1 EA-1243-02 and
PCI Report on Transport Analysis of Nukon Insulation (PCI ltr 90-1079-09), provide
information on the adequacy of the replacement insulation for the RSGs and piping.
These are inputs for the 10 CFR 50.59 evaluation to determine that the thermal
insulation used on the RSGs and that replaced on piping would not interfere with
the flow of water to the containment sump during assumed accident scenarios.
The engineering review of the replacement insulation was noted to be a detailed
process that, although not final, had not identified any unexpected difficulties in the
performance of the RSG arid piping insulation.
Conclusions
The inspections found a generally high level of project performance in the areas
inspected and identified no safety significant project deficiencies. For example,
controlled work packages were in use and project communication was maintained *
by prejob briefings and daily plan of the day meetings. Quality assurance, mainly
by surveillances, was continuirin. Welder qualification testing, control of weld *
materials and component welds were of high quality.
M 1 .4 Routine Maintenance Observations
a.
b.
Inspection Scope (62707)
The inspector observed routine corrective maintenance activities including the repair
of a jacket cooling water leak and restoration of the 1 C emergency diesel generator
(EOG), and the replacement of the 11 service water (SW) pump.
Observations and Findings
ii
1 C Emergency Diesel Generator
The operators identified a leak from 1 C EOG jacket cooling water system following
a post maintenance test run. Maintenance technicians pressurized .the EOG jacket
cooling system and determined that the leak was through the 7L cylinder. The
maintenance technicians removed the cylinder head and installed blind flanges to
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permit additional EOG jacket water pressure testing to ensure that there were no
other system leaks. The inspector observed the pre-evolution. brief, and a portion of
the EOG jacket cooling water pressure test and noted that the brief was thorough,
and that the testing was performed in accordance with procedure SC.MD-PT.DG-
0001, "Diesel Engine Jacket Water Pressure Test." No other leaks were identified,
and the maintenance technicians replaced the 7L cylinder head. A maintenance
supervisor indicated that the failed cylinder head would be shipped to the vendor
for a failure analysis.
During the subsequent post-maintenance testing, operators noticed variations in the
EOG output frequency. The licensee contacted the EOG vendor for technical
assistance and developed a troubleshooting plan for correcting the frequency
problem. The inspector reviewed the troubleshooting plan and determined that it
was logical. During troubleshooting, the licensee identified that the frequency
problem was caused by the electronic governor assembly. Maintena.nce technicians
replaced the assembly and successfully retested the EOG on March 6. The
inspector observed: a portion of tlie testing and noted that it appeared to be well
controlled and in accordance with the procedure.
The inspector reviewed the EOG test data taken during the post-maintenance
surveillance testing in accordance with S1 .OP-ST.DG-0003. The inspector verified
that the EOG starting response characteristics (frequency, engine speed, and
voltage) were acceptable. The inspector concluded that procedure adherence was
excellent throughout this maintenance activity, and that the licensee implemented a
. sound plan for restoring the EOG following the cylinder water leak.
11 Service Water Pump
Th~ 11 service water (SW) pump was replaced in accordance with maintenance
procedure, SC.MD-EU.SW-000, "Johnston Service Water Pump Removal .And
Installation." During the pump removal and installation activities the inspector
observed good procedure adherence, supervisory oversight, and foreign material
exclusion (FME)" controls.
During the post-maintenance testing and packing adjustment, the pump packing
assembly became overheated. The operator secured the pump, however, the heat
generation damaged. the pump shaft necessitating an additional. replacement of the
pump. Condition report (CR) 970228053 was generated to investigate the root
cause(s) for the packing problem. The investigation identified several potential root
causes for the packing problem including inadequate installation* and adjustment
instructions.
The packing was a new style packing and several inconsistencies were identified in
the vendor's guidance rega1~ing adjustment and installation of the packing. The
inspector interviewed* a design engineer and learned that the licensee intended to
replace the pump and install the original style packing. The inspector concluded
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. that this occurrence demonstrated poor engineering design control, but noted that
this condition was of minimal significance since the SW system was not required to
be operable for Unit 1 .
c.
Conclusions
Maintenance technicians demonstrated good procedure adherence during repair of
the 1 C EOG jacket cooling leak, and during replacement of the 11 SW pump.
Troubleshooting of the 1 C EOG frequency variations was logical. Weak engineering
controls were established prior to changing the type of packing in the 11 SW pump.
M2
Maintenance and Material Condition of Facilities and Equipment
M2. 1 Packing Leakage and Control of Deficiency Tags
a.
Inspection Scope 1717071
b.
The inspector routinely toured the facility to assess safety-related component
leakage, lubrication, and general conditiun.
Observations and Findings
The inspector identified that numerous safety-related valves exhibited. minor packing
leakage shortly after maintenance personnel had retorqued or repacked the glands
(22RH 18, 2RH71, 2CV54, 21SS116, 215546). Maintenance supervision initiated
a CR (970218215) to investigate the apparent cause of persistent packing leakage.
T.he inspector identified that a planner inappropriately closed a. packing adjustmenL
work request for 22RH18 (22 residtial heat removal heat exchanger outlet throttle
valve) and failed to remove the equipment malfunction identification system (EMl5)
tag. : A maintenance supervisor replaced the inactive EMl5 tag and initiated a work
order to repair the packing leak. In addition, maintenance staff .failed to remove
several other EM15 tags that listed previously corrected or rejected deficiencies
(22CC pump, 21 CC3, 21CC16, 2A EOG jacket water cooler).
The inspector observed inactive EMl5 tags in place identifying inadequate 2B and
2C diesel day tank level indication. On July 29, 1996, engineering closed out CR
960516192 for 2C day tank and on January 21, 1997, the maintenance work-it-
now (WIN) team rejected CM 970116120 on 2B day tank without resolving
operator concerns. The lack of resolution, combined with the inactive EMIS tags,
caused operators to unnecessarily abort a diesel fUel oil transfer pump surveillance
on February 16, 1997, and estimate daily diesel day tank log readings. Following
inspector identification, the operating shift*initiated CR 970218221 to address
diesel day tank level indication.
During the inspection, plant staff and managers separately identified several cases
of problems resulting from ineffective control of EMIS tags. As a result, the
management team planned to inspect the plant to identify and remove inactive
23
EMIS tags. In add:~::m, they intended to develop methods to improve EMIS tag
controls.
c.
Conclusions
The minor material condition deficiencies did not result in any safety consequence,
however, maintenance did not demonstrate effective packing leakage repair or
adequate EMIS tag control. Maintenance and engineering did not adequately
support operations in resolving diesel day tank level indication inadequacies. Plant
managers independently identified problems with EMIS tag controls. _The licensee
planned to systematically remove inactive tags and develop methods to improve
control of the tags.
M3
Maintenance Procedures and Documentation
M3.1 Component Cooling Pump Repair (62707)
The inspector observed* maintenance technicians repair no. 23 component cooling
pump mechanical seah Technicians demonstrated good maintenance practices
- involving foreign material exclusion, safP.ty-related part storage, tagging,* and work
area cleanliness. Technicians appropriately implemented procedure revisions in
accordance with station policy. Technicians properiy documented work and
maintained the procedure .up to date. The supervisor provided good oversight and
direction at the job site. The inspector concluded that technicians properly
controlled and conducted safety-related maintenance on the no. 23 component
cooling water pump.
MB
Miscellaneous Maintenance Issues
MS.1 NRC Restart Item 111.17, Work Control and Planning Program: Work Control Process
Improvement Restart Action Plan (Closed)
a.
Inspection Scope
Salem staff determined that emergent work, work package content; and process
inefficiencies limited work control effectiveness. The inspectors reviewed Salem
staff's resolution of these defic.iencies.
b.
Observations and Finding*s
The Work Control staff, comprising planners and scheduler.s, developed problem
statements to address major areas.for improvement. They' completed the actions
associated with the problem statements and on January 8, 1997, the Management
Review Committee (MRC) affirmed the work control process ready for restart. Each
problem statement is followed by the results of inspection for the area .
.I
,<
24
Problem Statement 1 : The existing work control process requires better definition,
structure, and discipline.
To resolve this problem, the Work Control Manager established new mechanisms
such as a WIN team to. screen and validate corrective maintenance tasks; a Minor
Maintenance program; a process for controlling limiting condition for operation
(LCO) maintenance; a checklist to establish consistency in work package quality; an
automated, on-line process for resolving work-in-progress problems; and a work
package 'completion *. retest, and closure process. s*alem management incorporated
these innovations in a* Work Control Program Manual, and trained the planning and
scheduling staff on the new processes contained in the Manual.
By a sample of
training records, the inspector confirmed planning management trained their staff
. on the Manual. The inspector also discussed the process improvements with work
control members to determine whether the measures were effective and, based on
the responses, concluded the initiatives adequately resolved the problem statement. *
This problem stateme~t is* closed. .
'
- *
.
'
Problem Statement 2: Low staffing levels and process inefficiencies hav.e
contributed to an accumulation of functional area backlogs which contribute to
material and performance deficiencies. The existing backlogs should be reduced to -
levels which permit the application of available resources to the resolution of real
time conditions.
Inspectors reviewed the status and content of the maintenance backlog during the
inspection for NRC Restart Item 111.4.2, Work Order Backlog Reduction Plan. From
. that inspection, the inspectors determined that Salem management was managing
the backlog and the inspectors no longer consider this. issue a restraint to the .
restart of Salem Unit 2. The inspectors documented the details of that inspe-ction in
NRC Inspection Report 50-272,311 /96-18. This problem statement is closed.
Problem Statement 3: Organizational functions interfacing with and supporting the
Work Control Process need improvement.
- *
To aSSE!SS the effectiveness of corrective actions taken by Salem management to
resolve this problem, inspectors attended daily work coordination meetings and - *
performed field observations of work in progress. Each day, representatives of the
principal organizations~ (maintenance, operations, chemistry, radiation protection,
fire protection, and engineering), meet for the sole purpose of discussing a~d * -
coordinating the work items which *maintenance plans to work that day. The
inspectors determined that the representatives were knowledgeable and they
conducted the meetings professionally. In several cases observe,d, operators
postponed or rescheduled work due to conflicts the staff identified during these *
meetings. In other cases, operations pointed out high priority items needing
maintenance to support operation of plant systems. *The inspector found that these
meetings improved coordination of work. From the field observations, the
inspectors determined that technicians were working priority tasks as required, and
were rnceiving support as needed from planning, supervision, and engineering when
problems arose. In one example, technicians could not ,install a pump seal in
- *.
25
accordance with the procedure. The technicians stopped work, and held
discussions with engineering to resolve the problem. Later, the staff revised the
procedure to reflect the field requirements.
Inspectors monitored a Quality Assessment maintenance audit that was ongoing
during the inspection period. As part of that audit, Quality Assessment personnel
interviewed maintenance technicians to help assess the effectiveness of work
control. The inspectors. found that technicians recognized a need for more
improvement in work control but all stated that the work control staff made
significant improvements to the process during the past six months. Supervisors
frequently visited the job site, and engineering and planners were readily available
to help resolve problems.
This problem statement is closed.
Problem Statement 4: The Managed Maintenance Information System (MMIS)
needs to be enhanced to support a comprehensive work. control process .
. The Planning staff implemented software changes that made the work order system
more efficient and increased 'task accountability. For example, now work initiators
can assign minor maintenance directly to the WIN team, and senior reactor
operators can electronically approve work orders.
Also, work orders now have a
- required sign-off for job supervisors that signifies they have walked down a task
and it is ready for technicians to work. The inspector confirmed that work control
management t~ained the staff on the modifications and, based on discussions with*
the staff, concluded the enhancements had improved and streamlined the work
control process;
This problem statement is closed.
Problem Statement 5: The performance indicators used to monitor and track work
control process functions do not provide sufficient visibility of process weaknesses.
During this inspection period and in past inspection periods, inspectors reviewed
and utilized Salem performance indicators. The inspectors noted that indicators are
in place to monitor backlog status, job rework rate, work holds due to engineering
and parts requirements, and. other important indicators that enable Salem
management to identify and correct work process weaknesses. This problem
statement is closed.
Problem Statement 6: A systematic, structured Self-Assessment is needed as part
of th.e Work Management Program process control function.
Procedure SC.SA-AP.ZZ-0034(Q), Self Assessment Program, governs*
implementation of self assessments. The. adequacy of AP-34 is the subject of NRC
Restart Issue 111.21, Self Assessment Capability, and ther13fore was not part of
inspecting this problem statement.
'*
- ~ l
.*.;
26
The inspector verified that the work control and planning group performed a self
assessment in accordance with AP-34. The inspector read the assessment and
reviewed QA staff's comments regarding the assessment. The inspector noted the
QA staff made several insightful comments. First, the assessors did not discuss
work control performance with key users of the work control and planning program.
For example, the assessors did not interview personnel from radiation protection,
the work control center, chemistry, or tagging. Second, the assessment team was
made of exclusively planning and work control personnel; no personnel from outside
the organization were members. The QA team provided these comments to the
assessment team leader for resolution. Subsequently, the self assessment leader
augmented his team with representatives from the work control center and
maintenance, then conducted additional interviews with personnel from radiation
.protection, the work control center, and maintenance. The inspector reviewed the*
followup assessme.nt and noted it identified additional areas for improvement. The
inspector concluded that the work control staff adequately implemented the
assessment process. This problem statement is closed.
Problem Statement 7: Ensure functions to support on-line processes are in place
prior to startup.
The inspector noted work control management has implemented the functions that
support the work management process. For example, the inspector determined the
staff has issued the WIN Team D.esk Guide, the Radiation Protection Desk Guide,
identified work week managers, named work group coordinators, and trained the
staff on the Guides and new functions.
This problem statement is closed.
c.
Conclusions
Salem management has improved, and continues to improve, work control
effectiveness. The licensee improved the process, trained personnel, and increased
staffing levels in the planning and scti~-iuling group. The Salem staff addressed the
work order backlog and are using performance indicators' to monitor progress.
While personnel could stm improve performance, work control staff's response to
their self assessment indicated to the inspector that management would ensure the
organization continued to address deficiencies. The inspector concluded the work
control program is ready to support Salem restart.
M8.2 (Closed) Unresolved Item 50-272 & 311 /95-17-03: evaluation of corrective action
regarding Salem Unit 1 steam generator tube inspection weaknesses.
Westinghouse personnel performed the eddy current tes,ting and data analysis as a
contractor to PSE&G dur_ing the 1993 and 1995 outages. The NRC inspection
determined that Westinghouse engineers misinterpreted defects that should have
required plugging of eight tubes. Consequently, Salem technicians did not plug
these tubes. Also, Westinghouse staff used probes that were not qualified for the
application, and data from different style probes did r.ot correlate. Salem
management was very prompt and aggressive in addressing these issues. The
licensee issued a stop work order, arranged for an independent organization to
perform data reanalysis, and developed site specific analysis guidelines for eddy
27
current testing probes. Subsequently, management corrected eddy current testing
weaknesses, contracted with a new vendor for steam generator inspections, and
replaced Unit 1 steam generators. The inspector also verified that, as part of the *
maintenance restart plan, Salem management implemented significant corrective
action during the past months to improve control of contractors. Based on the
information above, the inspector considers this unresolved item closed.
M8.3 (Closed) Violation 50-272&311 /94-14-02: failure to provide adequate training to
maintenance personnel. In July 1994, maintenance personnel attempted to
implement preventive maintenance on the turbine driven auxiliary feedpump. The
objective was to change the oil in the gear box. During the process, technicians
inadvertently added oil to the governor oil reservoir and also disturbed the turbine
overspeed trip device. The turbine subsequently tripped on overspeed during post
maintenance testing.
The inspector completed an inspection on the effectiveness of the maintenance
restart plan and documented the results in Section M1 .2. Maintenance
management addressed the causes of this incident, i.e. poor training, lack of a
questioning attitude, and poor pre-job briefing, in generic maintenance program
improvements described in the restart plan. Salem staff also responded to the
violation with detailed corrective actions that addressed this specific event. Salem
staff counseled the personnel involved, enhanced training modules, and stressed to
first line supervisors the importance of good pre-job briefings. r.he inspector
concluded the corrective measures adequately addressed this issue. This item is
closed.
Ill. Engineering
E1
Conduct of Engineering
E1 .1
Generic Letter 89-10 Motor-Operated Valve Program Review IT /I 2515/109)
!Closed), NRC Restart Issue 111.a.23. Adequacy of Motor Operated Valve Program
!Closed)
Introduction and Purpose
On June 28, 1989, the NRC issued Generic Letter (GL) 89-10, "Safety-Related
Motor-Operated Valve Testing and Surveillance," requested licensees to establish a
program to ensure that switch settings for safety-related motor-operated valves
(MOVs) were selected, set, and maintained properly. Seven supplements to the GL
have been issued to provide additional guidance and clarification. NRC inspections
of licensee actions implementing the provisions of the GL and its supplements have
been conducted based on the guidance provided ir1 NRC Temporary Instruction
2515/109, "Inspection Requirements for Generi~ Letter 89-10," which is divided
into three parts.
- .* .. ~***
.'
.
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28
The NRC conducted the Part 1 inspection at Salem in May 1992 as documented in
NRC Inspection Report (IR) 92-80. IR 93-24 reviewed the status of the open items
developed during the Part 1 (program) inspection. A Part 2 (implementation)
inspection, conducted in November and December 1993, was* documented in NRC
IR 93-26. An initial Part 3 (closure) inspection was documented in IR 96-11.
A public meeting was held on November 12, 1996, to discuss PSE&G plans to
complete the Salem Unit 2 MOV program, as well as to discuss the unresolved
issue of MOV program status in the context of 10 CFR 50.9(b). The slides .
presented by PSE&G during the November 12th meeting are attached to this
inspection report. The purpose of this more recent inspection was to review
PSE&G's corrective actions for the findings from IR 96-11 and to again address
~losure of the GL 89-10 program at Salem Unit 2.
El .2
Summary Status of Generic Letter 89-1 O MOVs
a.
lnsi:~ctior Scope
In GL 89-10, the NRC requested notification within 30 days after the MOV design-
basis reviews, analyses, verifications, tests, and inspections have been completed.
In a letter dated March 20, 1995, PSE&G notified the NRC that the committed
programmatic actions taken to address Items a through h of GL 89-1 0 had been
completed at Salem Unit 2. The inspectors reviewed PSE&,G's S-C-VAR-NEE-1.117,
. "Generic Letter 89-10 Closure Summary for the Motor Operated Valve Program as
.Implemented at Salem Unit 2," Rev. 0, and documents associated with all MOVs in
the GL 89-10 program. Using these documents, a valve s~mple was selected that
included examples of all methods used to demonstrate design-basis capability .
. b.
Observations and Findings
PSE&G used several methods to demonstrate MOV design-basis capability which
included verification by:
Valve-specific dynamic test at, or near, design-basis conditions,
Valve-specific test, linearly extrapolated to design-basis conditions,
In-plant information *obtained from .dynamic tests on similar MOVs. and
Electric Power Research lnstitute's (EPRI) Performance Prediction Model
(PPM) applied to MOVs that were not practicable to test.
PSE&G had dynamically tested 46 of the 94 MOVs in the GL 89-10 population at.
Salem 2. PSE&G provided information for the 94 MOVs which were grouped into
16 l'v10V families. The inspectors reviewed special test pack<;1ges and engineering
evaluations for the following MOVs:
22SJ40
2RH1
2CC136
22SJ33
21SJ113
(Family 2)
(Family 6)
(Family 5)
(Family 1)
(Family 3)
E1 .3
MOV Sizing and Switch Settings
a.
Inspection Scope
29
Safety Injection Pump to Hot Leg Isolation Valve
Reactor Coolant System (RCS) Hot Leg to
Residual Heat Removal (RHR) Suction Header
Valve
Reactor Coolant Pump (RCP) Motor Bearing
Cooling Water Outlet Valve
Safety Injection Pump Suction Valve
Containment Spray Pump Discharge Isolation
Valve
The inspectors reviewed valve packages that established the thrust requirements
for MOVs in their GL 89-10 program. These documents included thrust calculations
and test evaluation packages associated with the selected MOVs. PSE&G's
methods for determining minimum thrust requirements were documented in Motor
Operated Valve Program - Appendix 6 "MOV Mechanical Capability Review,"
Rev. 4, dated June 7, 1994, and EE: A.-O-ZZ-MEE-0609, "MOV Program Position
Papers," Rev. 5, dated April 9, 1996. The purpose of this review was to assess
the licensee's justifications for assumptions used in MOV thrust calculations which
form the basis for determining the design-basis* requirements.
b.
Observations and Findings
PSE&G's thrust calculations typically utilized the standard industry equations.
Mean seat diameter was used to calculate valve seat area. Valve factors were
based on the in-plant test results or other industry sources as specified by the
licensee's grouping methodology. A stem friction coefficient of 0.20 was used for
determination of actuator output thrust capability. The licensee applied margin to
account for diagnostic equipment uncertainty, torque switch repeatability, 1*oad
sensitive behavior, and potential valve degradations.
Valve Factor and Grouping
PSE&G classified Salem MOVs into valve families Qased on manufacturer, type, and
ANSI pressure class rating. Some families contained a range of valve sizes.
PSE&G attempted to use in-plant data for justification of valve factors for non-
9ynamically tested MOVs. However, PSE&G did not have* sufficient in-plant test
results to .adequately .cover all valve groups. During the program review, the
inspectors noted that the licensee initially did not provide adequate justification_for
MOVs in Families 6 and 9. However, further discussion resolved -the inspector's
comments as follows:
_-;.
30
Family 6: 14" Copes Vulcan 2500psi Parallel Double Disk Gate Valves
This family consisted of the RCS hot leg-to-AHR suction header valves
(2RH1 and 2RH2). PSE&G was unable to obtain in-plant or applicable
industry data for these valves. To address this issue, the licensee reviewed
the "separate effects" friction test program that.was conducted by EPRI as
part of the Performance Prediction Program (PP~). A friction coefficient of
0.55 was selected based on an expected operational water temperature of
200-300° F. This justification was not considered adequate for program*
closure because the EPRI separate effects testing was only one of many
parts of what the NRC reviewed regarding the PPP.
After discussion with the inspectors, PSE&G revised its valve factor for
these valves to 0;61 which was based on the maximum value experienced
during dynamic in-situ testing at Salem Unit 2. Also, PSE&G intended to
modify valve 2RH1 prior to restart to make it comparable to valve 2RH2~
thereby improving its actuator capability. While both valves were shown to
have adequate design basis capability, the inspectors noted that the valve
factor basis for these valves was still weak and' could be better support~d in
the long term. Based on PSE&G's irtent to pursue an improved valve factor
basis for these valves as part of their periodic verification program an'd
.
modifications to be performed prior to restart, the inspectors concluded that
these valves wer.e acceptable for GL 89-10 closure. An inspector followup
item will track implementation of. issue 2RH 1 and 2. (IFI- 50-J11 /97-03-03)
Family 9: 3" & 4" Velan Flex Wedge Gate Valves
The inspector's comments for this family focused on the power operated
relief valve (PORV) block valves (2PR6 and 2PR7) and the RCP thermal
barrier isolation valves (2CC131 and 2CC190). PSE&G modified the PORV
block valves to operate them based on limit switch control. * The
modification provided ari "available" valve factor (i.e., functional upper limit)
of 0.61 to close the valve. Given this apparent capability, use of a 0.2 stem
friction coefficient, and the application of actuator pullout efficiencies, the
inspectors considered the current settings of the PORV block valves to be
adequate. _However, the inspectors requested PSE&G to confirm the
technical adequacy of the basis for valve factor, and to address any potential
non-predictability for the PORV block valves as part of Salem Unit 2's
periodic verification program. PSE&G agreed and stated* that they will
review the possibility of applying the EPRI PPM methodology for these
valves. An inspector followup item will track implementation of this issue
for valves 2PR6 and 7. (IFI 50-311197-03-04)
For the RCP thermal barrier isolation valves (2CC131 and 2CC190), the
licensee used EPRI PPM test data in a unique manner to determine a
bounding valve factor of 0.64. The unique treatment of the EPRI PPM test
data was described in a vendor (MPR Associates) calculation that was
included as Attachment 24 to PSE&G's Engineering Evaluation S-C-VAR-
31
NEE-111 7. The statistical approach utilized in this calculation was not
endorsed in the NRC's safety evaluation of the EPRI PPM, and was
considered to be unacceptable for GL 89-10 closure.
PSE&G revised the valve factor to 0.54 which was based on the highest
value obtained from testing similar Salem Unit 2 valves. Both valves were
still shown to have positive thrust margins, with 2CC 1 31 the least at 8 % ..
While the inspectors considered this acceptable for GL 89-10 closure,
PSE&G was requested to take measures at the first opportunity to improve
the actuator capability for these MOVs. The inspectors also requested
PSE&G to confirm the technical bc:1sis of the valve factor, and to address any
potential non-predictability for these valves as part of periodic verification.
PSE&G agreed and stated that they will review the possibility of applying the
EPRI PPM methodology for these valves. An inspector followup item will
track implementation of this issue for valves 2CC131 and 190; UFI 50-
311/97-03-05)
Load Sensitive Behavior
Attachment 19 of the Unit 2 Closure Summary documented a statistical analysis of
75 data points, an average load sensitive behavior of 3. 7% and a standard
deviation of 9.6%. Based on this analysis, the licensee's error analysis added 4%
directly as a bias margin and 21 % as a random value that was included with other
uncertainties using the square root sum of the squares method. The inspectors
found the licensee's analysis and load sensitive behavior margin to be acceptable
- for non-dynamically tested MOVs at Salem Unit 2.
Stem Friction Coefficient
PSE&G recently completed a comprehensive stem friction coefficient review of the
results from in.:plant testing. Based on this study, PSE&G increased Unit 2's
assumed stem friction coefficient value from 0.15 to 0.20. The inspectors found
the licensee's stem friction coefficient justification to be acceptable for* Salem
. Unit 2.
.
Degradation Margin
NRC Inspection Report 50-311 /96-11 noted that the licensee's margin to address
potential future valve degradations may not exist if other uncertainties were large
enough to consume the fixed 30% margin that was used to account for these
uncertainties. Recently PSE&G revised their setup methods to include a 5% bias
margin to account for degradations as a part of their standard error analysis.
Results from Salem's periodic verification program will be used to revise this 5%
margin if necessary. The inspectors found this approach to be acceptable .
.;.
~ ..
. j
. (
- ~
1
. !
c.
El.4
a.
32
Linear Extrapolation
The inspectors reviewed Section 4.4.5 of the Unit 2 Closure Summary which
contained PSE&G's justification for use of linear extrapolation to account for
differences between dynamic test conditions and design-basis conditions. PSE&G's
justification was based on results from EPRl's PPM. The inspectors did not identify
any concerns with the licensee's general method for extrapolating test results.
However, the inspectors requested that PSE&G review the NRC~s Safety Evaluation
(SE) by the Office of Nuclear Reactor Regulation of Electric Power Research
Institute Topical Report TR-103237,
11EPRI Motor-Operated Valve Performance
Prediction Program,
11 dated March 15, 1996, and EPRl's latest recommendations
related to use of linear extrapolation. The licensee's review was requested to
ensure that adequate disk loading was obtained during testing at Salem Unit 2, and
in*order to improve the reliability of wide extrapolations.
Conclusions
The justifications for key program assumptions were complete and the applied valve*
factors for Salem Unit 2 MOVs were adequate for GL 89-10 closure. These
conclusions were based on the understanding that PSE&G would pursue actions for
certain MOVs in Families 6 and 9 in conjunction with the periodic verification
program for Salem Unit 2 MOVs. * These additional evaluations were agreed to be
formalized in a revision of the Salem Unit 2 GL 89-10 closure summary document
S-C-VAR-NEE-1117.
The inspectors noted that progress was achieved since the previous NRC inspection
as reported in NRC Inspection Report 50-311 /96-11 . The inspectors also noted
that NC.DE-PS.ZZ-0033(0), "Motor Operated Valve Programmatic Standard and
Appendices,
11 was not consistent with PSE&G' s current margin and error analysis
assumptions, as presented in the Salem 2 GL 89-10 Closure Summary document.
Design-Basis Capability
Inspection Scope
The inspectors reviewed dynamic test evaluation packages that were performed in
accordance with Appendix 14 of the Motor Operated Valve Programmatic Standard
and associated test reports for the selected MOVs. The purpose of this review was
to assess P5E&G's efforts to establish des!gn-basis ~apability for all MOVs in Salem
Unit 2's GL 89-10 program.
b. . Observations and Findings
Reactor Coolant System Hot Leg-to-Residual Heat Removal Suction Header MOVs
During the initial review of Salem Unit 2's Closure Summary document, the
ir1spectors noted that the RCS Hot Leg to RHR Suction Header Valve (2RH 1 -
Family 6) had an identified 1 % thrust margin. As noted in Section E1 .3 of this
- ._
.,
33
report, the licensee had applied a 0.55 valve factor which was inadequately
justified. Further, the inspectors noted that the margin calculation for 2RH1 did not
include any margin for load sensitive behavior (because of limit switch control), or
valve degradation. However, as discussed in Section E1 .3, after further discussion
with the inspectors, the licensee changed the approach to demonstrating design
basis capability by adopting a higher valve factor and agreeing to perform
modifications prior to restart of Salem Unit 2. The inspectors concluded that this
was acceptable for these valves for GL 89-10-closure.
Thrust Margin Improvement
The inspectors noted that several Salem Unit 2 MOVs were scheduled for margin
improvements. However, the following MOVs. had adequate basis for the applied
thrust requirements, but had low thrust margins and were identified by the
inspectors to ensure that they are included in PSE&G's margin improvement plans:
. 2CC136
21BF13
22CC16
22BF13
2SJ4
2SJ5
The licensee was requested to review this list and to include these MOVs as part of .
their margin improvement program. PSE&G personnel agreed to conduct this
review. Closure of these MO Vs under the generic letter program was considered
contingent upon the licensee's agreement .to improve the margin of these MOVs as
part of Salem Unit 2's long term MOV program (IFI 50-311197-03-06).
Pratt Butterfly Valves
'*
Family 16 consisted of 8" and 24" Pratt butterfly valves. The licensee used the
EPRI PPM butterfly model to develop the torque requirements for these valves.
Further, the licensee has initiated Minor Modification package No. S-96-019 to
change the spring packs which will increase the output capability for the four 24"'
valves. However, these modifications were not complete at the time of the
inspection. PSE&G has scheduled these modifications to be completed prior to
restart of Salem Unit 2. The inspectors concluded that the methodology for setting
the torque switches for these valves was acceptable for GL 89-10 closure .
. MOV Thermal' Overloads
During a rncent inspection of the component cooling system as reported in NRC
Inspection Report 50-311 /96-81, the inspectors found that design change DCP
2EC-3249 installed thermal overload (TOL) relay heaters on MOV circuits that were
different than the design basis calculation ES-18.006. The inspectors requested
confirmation that the correct heater sizes were used in the MOV program, NC.DE-
PS.ZZ-0033 (Q). Appendix 5, Electrical Capability Review, of this MOV program
document presented the methodology establishing the degraded voltage factor for
the MOV program analyses. The MOV group maintains a separate file for each
valve in which the TOL heater resistance is used in part of the analysis to determine
the voltage at the valve motor.
..
34
In response to the inspector's concern, PSE&G compared the as-installed TOL
heaters with the TOL heaters used in the analyses. PSE&G identified spray additive
isolation valve 2CS14 and RCP motor and bearing cooling water valve 2CC118
with heaters that were a smaller size than used in the analyses and, because of
their increased resistance, would result in a lower degraded voltage factor than that
used in the MOV program analysis of record. PSE&G reran the analyses for 'these
two valves and reviewed the results with the inspectors. The results of the
reviews indicated that the degraded. voltage factors would decrease by 2 % but the
- valves were still capable of developing sufficient torque under the new degraded
voltage conditions.
PSE&G prepared AR 970116087 to document this discrepancy.
c.
Conclusions
The inspectors concluded that PSE&G had adequately demonstrated design basis
capability for Salem Unit 2 MOVs such that the NRC review of GL 89-10 could be
closed. This inspection also closes NRC Restart Issue 111.a.23, Adequacy of Motor
Operated Valve Program. This conclusion was based on the understanding that
PSE&G would pursue actions for certain MOVs in Families 6 and 9 in conjunction
with the periodic verification program for Salem Unit 2 MOVs.
El .5
Pressure Locking and Thermal Binding
a.
Inspection Scope
The inspectors reviewed the evaluation of gate valves susceptible to pressure
locking (PL) and/or thermal binding (TB) which the licensee had completed in
response to GL 95-07, "Pressure Locking and Thermal Binding of Safety-Related
Power-Operated Gate Valves." As indicated in the licensee's response to GL 95-07.
dated February 13, 1996, PSE&G identified 8 valves (21 CS2, 22CS2, 2SJ 1 2,
2SJ13, 2SJ1, 2SJ2, 21 SJ113, and 22SJ113) that were considered to be
susceptible to PL for Salem Unit 2. In addition, PSE&G identified 4 valves
(21CC16, 22CC16, 2PR6, and 2PR7) that were considered to be susceptible to
thermal binding for Salem Unit 2.
b.
Observations and Findings
PSE&G in_dicated that holes were drilled in 6 of the 8 valves that were susceptible
to PL. In addition, PSE&G modified the procedures for the 21 CS2 and 22CS2
valves to include valve cycling after surveillance testing. The inspectors concluded
that the licensee's modifications were adequate to address the susceptibility of PL
for the modified valves.
PSE&G also indicated that TB concerns were addressed for the PORV block valves,
PR6 and PR7, by modifying the MOV control circuit from torque control to limit
control. It was noted that the unwedging force was significantly decreased
following the modification. The MOV static test trace from the diagnostic
35
equipment (i.e., VOTES) indicated approximately 2673 lbs. of unwedging force for
the PR6 valve. A calibration error of 40% was added to the unwedging force;
therefore, the unwedging force for PR6 was recalculated to be about 3842 lbs.
The inspectors were not able to verify the unwedging force for PR7 due to
diagnostic sensor problems.
By letter dated July 1, 1996, the NRC staff asked PSE&G to supply additionai
information concerning their submittal in response to GL 95-07. By letters dated
August 7 and 30, 1996, PSE&G provided a response to the staff's request for
additional information. PSE&G indicated that the RH-26 valves were not within the
population of valves considered to have a safety-related or important to safety
function to open; therefore, the licensee did not evaluate the susceptibility to PL for
~he RH-26 valves. The inspectors noted that PSE&G's position concerning 2RH26
remained the same during this inspection as it was not included in the scope of the
GL 89-10 program (see Section E1 .2). Regarding the PORV block valves PR6 and
PR7, PSE&G indicated that an evaluation of these valves under conditions
associated with a steam generator tube rupture had been completed. The licensee.
concluded that there was a negligible effect on the required unwedging thrust for
the PR6 and PR7 as a result of a steam generator tube rupture. Accordingly, the
licensee concluded that there was no increase in the required thrust associated with
the PL scenario. PSE&G indicated that valve specific evaluations were performed
with respect to valve and system function; however, no specific training had been
conducted regarding modifications.
The inspectors noted that PSE&G utilized the services of MPR Associates, who
developed an .analytical method to determine a maximum inertial thrust limit below
which TB should not be a concern for the 21CC16, 22CC16, 2PR6, and 2PR7
valves ...* In reviewing the MPR analysis, the inspectors determined that the test data
that was used for this analysis did not completely validate the model to determine
the susceptibility to TB for the PR6 c>~1 PR7 valves. In addition, the inspectors
found that MPR's key assumption in their calculations for deriving a PLfTB model
may not adequately consider transient or steady state temperature gradients in the
valve .body or valve disk.
The MPR analysis included an analytical method that was utilized to demonstrate
that the actuators on the PORV block valves, PR6 and PR7, could develop adequate
thrust to overcome pressure locking. PL thrust requirements for these valves were
calculated by a method of the MPR analysis. The inspectors independently
calculated the thrust required to overcome PL and determine the actuator capability
for the PR6 and PR7 valves and concluded that the actuators were able to develop
the thrust required to overcome PL.
The inspectors noted that a response to one item of the RAI was still required by
the licensee and had not been submitted. The licen~ee indicated that a response to
this item would be submitted to the NRC in th~ near future .
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c.
Conclusions
The inspectors did not find any immediate safety or operability concerns regarding
' -)
any Salem Unit 2 MOVs. PSE&G's modifications and other actions to address PL
and TB in the short term were acceptable. However, in the long term for satisfying
GL95-07, PSE&G was requested and agreed to determine and confirm at the
earliest opportunity that the unwedging force for 2PR7 is comparable to 2PR6.
Also, PSE&G was requested and agreed to further discuss and resolve with the
NRC questions regarding assumptions and test validation of the MPR Associates PL
and TB analytical model.
El .6
MOV Failures. Corrective Actions, and Performance Trending
a.*
Inspection Scope
b.
The inspectors reviewed two recent MOV fanures concerning component cooling
(CCI water "alve 22CC3 and service wat'3r valve 22SW17. The inspectors
evaluated the causes of the failures, implications of the failures for similar MOVs,
and the comprehensiveness of the corrective actions. These failures were then
reviewed within the context of. PSE&G's methodology to track and trend MOV
performance as described in the MOV program procedure Appendix 18, "MOV
Tracking and Trending Assessment."
Observations and Findin*gs
Torque Switch Failure of 22CC3
During differential pressure (DP) testing of the CC pump discharge header isolation
valve 22CC3 using a variable transformer (i.e., VARIAC) to simulate degraded
voltage conditions, the torque switch failed to open even though the valve closed.
The motor stalled at a torque value of about 5 ft-lb below the torque switch trip
value of 352 ft-lb. The license*e disassembled the actuator and found no significant
mechanical conditions which confirmed the initial thoughts that the actuator was
not the cause of the failure. PSE&G also reviewed the VOTES diagnostic trace,
disassembled the motor, and found no abnormalities. The motor was then sent to
Liberty Technologies for further evaluation off site. Tests of the motor were not
conclusive in determining why the motor stalled during the DP test.
PSE&G replaced the motor on 22CC3 and performed the DP test successfully.
However, PSE&G is still evaluating the 22CC3 failure under an open Action Request
and has postulated that the motor may have stalled because of loose cable
connections associated with the variac used for this degraded voltage test. Further
motor disassembly and inspection was being evaluated to better define the root
cause of the problem. The inspectors concluded that PSE&G was evaluating this
problem consi~tent with the requirements of the GL 89-10 program .
f'
37
Incorrect Torque Switch Setting of 22SW17
Service water isolation valve 22SW17 is a limit-seated butterfly valve which has a
torque switch wired in series with the limit switch. The torque switch is generally
not actuated and it is set to trip at maximum allowable torque for component
protection. On September 4, 1996, PSE&G operations closed 22SW17 under
dynamic loading but did not receive the closed indication. While the valve fully
closed, there appeared to be an indication problem. Operations informed the Salem
MOV program manager who initiated corrective actions to review this and other
similar MOVs for this problem.
On November 1, 1996, during DP testing, 22SW17 failed to fully close on its limit
.switch. Action Request 961101135 was issued to take appropriate corrective
actions. PSE&G discovered that the torque switch setting was erroneously set to
1.0 in lieu of the correct setting of 1.5 for both the open and close directions. This
setting prematurely deenergized the motor causing the valve to stop before
reaching its full closed position. In the subsequent investigation, the licensee
- determined that maintenance personnel had removed the valve and actuator to the
maintenance shop and inadvertently changed the torque switch setting during
"bench testing" in the shop. PSE&G concluded that the incorrect torque switch
setting was due to human error in that new personnel were at fault for not restoring
the torque switch to its proper setting. The inspector noted that the lack of
independent verification of maintenance activities involving torque switch settings
during the maintenance shop work contributed to the failure of 22SW17.
As corrective actions per AR 9611001135, PSE&G was verifying the torque switch
setpoint for each of the limit-seated butterfly valves and other limit seated valves.
In addition, PSE&G will revise the MMIS data base -by providing only the maximum
torque value *and torque switch setting for limit-seated MOVs. This should
eliminate erroneous use of the minimum torque setpoint which is not applicable for
limit-seated MOVs.
The inspectors considered the corrective action for the 22SW17 valve to be
adequate. However, it was noted that the licensee could enhance its independent
verification process in its MOV maintenance procedures. The inspectors considered
this to be an area of weakness requiring thorough licensee evaluation before
closeout of AR 9611001135. The inspectors had no further comments.
Tracking and Trending
The inspectors verified that the licensee has an adequate program, in place, to
annually examine pertinent MOV documentation for trending purposes. *The
inspectors noted that a detailed database was implemented in order to track MOV
test data and MOV failures. The inspectors noted that overall parameters for
monitoring MOV performance were well-de:fined and properly implemented for
tracking and trending purposes. The annual MOV review will be fully documented
in accordance with the requirements of the Salem corrective action program.
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c.
Conclusions
The inspectors concluded that PSE&G was adequately addressing MOV
performance problems by taking appropriate corrective actions. PSE8tG had
developed a good MOV tracking and trending program.
E1. 7
Post Maintenance Testing
a.
Inspection Scope
The inspectors reviewed Salem's MOV post maintenance testing (PMT) practices as
described in procedure NC.NA-AP.ZZ-0050(0), "Station Testing Program."
b.
Observations and Findings
The inspectors verified that the licensee's procedure adequately described the
process of identifying PMT and ensured that components or systems perform as
intended when returned to service, following corrective or preventive maintenance
activities. In addition, PSE&G adequately defined maintenance activities which
would create the need for a PMT of the affec1:ed component or system.
c.
Conclusions
The inspectors concluded that PSE&G *established and implemented an adequate
MOV PMT program as recommended by GL 89-10.
E1 .8.
MOV Program Administration
a.
Inspection Scope
b.
The inspectors reviewed the governing MOV program procedure NC.DE-PS.ZZ-
0033(0) and supporting appendices throughout the inspection and observed how
the various implementing procedures were controlled to fulfill program
requirements. This review included the licensee's efforts regarding periodic
verification of MOV design basis capability in response to GL 96-05.
Observations and Findings
PSE&G prepared a sound Engineering Evaluation s.-C-VAR-NEE-1117 to present the
Salem Unit 2 MOV information in an organized manner for this inspection. The
MOV staff demonstrated a thorough understanding of the MOV issues in presenting
the MOV program for closure. The inspectors requested that PSE&G formally
revise Engineering Evaluation S-C-VAR-NEE-1117 to include the changes discussed
during this inspection. Consistent with the Salem Quality Assurance program
requirements, PSE&G recognized the need to update the MOV program procedure
NC.DE-PS.ZZ-0033(0) and associated MOV calculations to be consistent with the
information presented during this inspection .
..
39
The inspectors reviewed Salem's MOV periodic verification program as describe in
procedure EE:S-C-VAR-NEE-1117, Rev. 0. The inspectors verified that PSE&G has
a surveillance work order in place to perform a recurring task for static testing each
MOV of the GL 89-1 0 program every 5 years or 3 refueling outages, whichever is
later.
PSE&G is in the process of determining periodic verification plans for performing
dynamic tests of GL 89-10 valves. The inspectors noted that the licensee intends
to perform some dynamic testing. This item will be further reviewed under GL 96-
05.
c.
Conclusions
E1 .9
a .
b.
The inspectors concluded that PSE&G was implementing adequate administrative
controls for the Salem Unit 2 MOV program. PSE&G prepared a sound engineering
evaluation to present the Salem Unit 2 MOV information in an organized manner for
this inspection.
Containment Fan Cooling Unit Service Water Isolation Valve Testing
Inspection Scope(37751)
The inspector reviewed the licensee's plan for operation of the containment fan
cooling units (CFCUs) during a planned Unit 2 Mode 4 entry.
Observations and Findings
The inspector attended a Station Operations Review Committee (SORC) meeting
and learned that station management planned to enter Mode 4 with two CFCU
units operational and with the SW cooling supply isolated and drained for three
CFCUs. The CFCUs were removed from service to support installation of a design
change package intended to resolve generic service water (SW) pressure transient
concerns identified in NRC Generic Letter 96-06.
The SORC approved an operability determination which demonstrated that 2 CFCUs
were adequate to support the potential containment cooling requirements for the
Mode 4 entry.
The inspector noted that one SORC member questioned whether the drained SW
cooling lines presented a containment integrity concern.
The inspector subsequently reviewed the updated final safety analysis report
(UFSAR) Table 6.2.-13 which stated, in part, that the SW containment isolation
vc..lves had been exempted from Appendix J, Type C ler;ik rate testing since the
valves were normally open to support CFCU operation. The inspector questioned
whether the basis for the leak rate test exemption as described i.n the UFSAR
remained applicable with the SW lines drained and isolated .
40
The licensee subsequently prepared, and the SORC approved a 10 CFR 50.59
safety evaluation to revise the UFSAR to clarify the basis for not Type C leak rate
testing the SW isolation valves. The 10 CFR 50.59 concluded that these valves did
not meet any of the required categories of valves subject to Type C testing. The
approved 1.0 CFR 50.59 adequately addressed the inspector's UFSAR compliance
concern.
The inspector noted, however, that NRC follow-up was required to get a fully
satisfactory response to the containment integrity question raised at the first SORC
meeting. The inspector concluded that the ineffective follow-up demonstrated a
weak safety perspective by station management.
c
Conclusions
SORC approved a 10 CFR 50.59 which adequa'tely addressed inspectors concern
regarding the UFSAR commitments for Type C leak rate testing the CFCU SW
cooling line containment isolation valves. Station management demonstrated a
, weak safety perspective by not ensuring an appropriate response to the
containment integrity question raised at the SORC meeting.
E1.10 Surveillance 'Effectiveness
a.
Inspection Scope (61726)
Inspectors monitored Salem staff response to an identified surveillance deficiency.
b,
Observations and Findings*
As a result of a proposed modification to the control circuitry for automatic
operation of the pressurizer Power Operated Relief Valves (PORVs), a system
- manager discovered that the surveillance procedure for the Pressurizer Overpressure
Protection System (POPS) did not completely test the operation of the automatic
controls. The surveillance procedure previously required operators to turn off each
chann.el of POPS while technicians inserted a test signal on the input of the circuit.
As a result, plant staff had not demonstrated that the output relays actuated as
required. The plant staff immediately developed a method to test the circuit from
input to output and successfully demonstrated operability of the POPS. The
inspectors considered the previous failures to completely demonstrate operability of
POPS a non-cited violation, since PSE&G shut down both Salem units to correct
long-standing plant deficiencies subjected to NRC enforcement action, and because
the Salem staff identified the violation, and took appropriate corrective action. In
addition, .the violation stemmed from procedure inadequacies existing prior to the
Salem shutdown.
The inspectors noted that the Salem Technical Specification Surveillance
Improvement Project, phase 2, would probably have detected this type of
surveillance deficiency. Since Salem management has not scheduled completion of
TSSIP phase 2 until the end of 1997, the inspectors considered it probable that, if
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41
not for the implementation of the PORV control circuit modification, Salem staff
would have detected the lack of a complete POPS surveillance until well after
Salem Unit 2 restart .
c.
Conclusions
As a result of a proposed modification, an alert system manager discovered an
incomplete surveillance of the circuit for automatic operation of the Pressurizer
Overpressure Protection System. Plant staff immediately devised and completed an
effective test. The inspectors noted that TSSIP, phase 2, scheduled for completion
in late 1997, would have probably discovered this defici~ncy.
Miscellaneous_ Engineering Issues
ES. 1
Control Room Ventilation Modification Testing
a.
Inspection Scope. (71707)
Inspectors observed engineering staff actions to insure that the newly modified
control room ventilation system met design requirements.
b.
Observations and Findings
During the inspection period, the Salem staff expended considerable effort to --
demonstrate that the ventilation system could develop the required positive
pressure in the control room area compared to air pressure in adjacent rooms and
the outside air pressure. Although plant management and staff considered the
possibility of a license change request to change the licensing basis requirement for
differential air pressure, they decided instead to make the system perform as
designed. As a result of trouble-shooting activities, such as temporarily covering
ventilation dampers to assess air leakage from the control room envelope, plant
staff discovered that the switchgear and penetration area ventilation system
(SPAVS) pressurized the rooms adjacent to the control room area. The Salem staff
identified and corrected the leak paths allowing SPAVS to pressurize areas adjacent
to the control room. The engineers subsequently demonstrated the ability of the
control room ventilation system to perform its design basis function.
c.
Conclusions
The inspectors concluded that the engineering staff conducted appropriate trouble-
shooting to determine the cause of control room ventilation performance problems.
The Salem managers properly elected to correct system deficiencies rather than
change the licensing basis for control room ventilation. As a result .of considerable
effort, the engineering staff successfully demonstrated the ability of control room
ventilation to perform its design function .
E8.2
E8.3
a.
42
(Closed) Unresolved Item 50-272 & 311/95-17-02
The inspectors previously identified that a commitment to install a concrete curb at
- the entrance fo each Salem Unit 1 and 2 Emergency Diesel Generator (EOG)
cubicle, contained in a July 26, 1978 letter from PSE&G to the NRC, had not been
implemented. The purpose of the curbs was to prevent the potential spread of
. diesel fuel to areas outside of the individual cubicles .. The failure to implement the
commitment to install the curbs was interpreted as a weakness in the licensee's
commitment management processes.
The inspector toured the EOG cubicles at Salem Units 1 and 2 and noted that
curbs, fabricated from steel angle (approximately 3 inches high) with caulking, had
.been installed. at the entrance to each Unit 2 EOG cubicle; no curbs had been
installed at the Salem Unit 1 EOG cubicles. The licensee indicated that the caulking
is resistant to diesel fuel oil.
The inspector reviewed the process that the licensee used to change the
commitment from installation of concrete curbs to installation of caulked steel
curbs. In response to a request from the inspector, the licensee provided "FORM.,4,
NUCLEAR BUSINESS UNIT; COMMITMENT CHANGE EVALUATION SUMMARY
FORM" Which addresses the EOG curb commitment change and was approved on
November 1, 1996. The "FORM -4" is an enclosure to the licensee's procedure
NC.NA-AP.ZZ-0035(0), Revision 5, dated December 27, 1995 and is* to be used in
Step 5.1.4 for "Changes to commitments made to the NRC in response to GLs,
Notices of Violations (NOVs), Inspection Report Followup Items, and Bulletins."
The inspector noted that "FORM-4" follows the process of the "NEI Guidelines for
Managing NRC Commitments - Revision 2", dated December 19, 1995 that was
endorsed by NRC letter dated January 24, 1996. Based upon the review of the ... :
subject "FORM 4", the inspector found the change in commitment, and installation
of the caulked steel curb, to be acceptable.
The inspector noted that the licensee had closed the commitment tracking form for
the Unit 1 and 2 commitment without implementing the installation of curbs at the
Unit 1 EOG cubicles. The licensee responded to this finding by opening a new*
commitment, using the Commitment Manager database, to assure installation of the
curbs at Unit 1 . Based upon installation of the curbs at Unit 2 and the commitment
to install the curbs at Unit 1, this item is closed.
NRC Restart Item 111.1, Unresolved Items 50-272&311 93-80-06, 07, and 08
(Open) - Appendix R jumpers and program discrepancies, including fire barrier
Inspection Scope
NRC Inspection Report 50-27 2, 311 /93-80, identified nine Unresolved Items. This
inspection addresses three of these items: URI. 272/311-93-80-06, non-
conservative assumptions, licensee using only one spurious operation per fire
incident; URI 272/311-93-80-07, requirement to perform repairs for Hot Shutdown
--~
b.
c.
43
contrary to SER statement; and URI 272/311-93-80-08, licensee method of
protecting equipment from damage by fire.
Observations and Findings
By letters dated August 2, 1993, and October 26, 1993, the licensee submitted
additional information. By letter dated January 25, 1996, the staff sent its
evaluation which concluded that Salem's safe shutdown capability was
unacceptable because redundant trains of equipment necessary to achieve and
maintain hot shutdown conditions may be damaged by a single fire and the
licensee's analysis for fire-initiated spurious signals was inconsistent with the
established staff positions promulgated in Generic Letters 81-12 and 86-10.
By letters dated June 19, 1996, and December 2, 1996, the licensee committed to
implement certain modifications to resolve the NRC concerns. The modifications
are needed to meet the requirements of Appendix R to 10 CFR Part 50. These
include the installation of isolation transfer switches for the required safe shutdown
functions controlled by the alternative shutdown system and the modification of the
control circuits for certain motor operated valves in order to resolve the concern
about multiple hot-short spurious damage from associated circuits in the fire area.
The licensee proposed to implement all of the modifications prior to restart of Unit
1, and, for Unit 2, during the first refueling outage following restart. In response to
an NRC request, the licensee provided, in a letter dated February* 18, 1 991,
compensatory. measures that will be taken until the modifications are implemented
on Unit 2.
By letter dated March 17, 1997, the staff determined that reliance on
these compensatory measures is not appropriate to provide adequate protection of
public health and.safety, and, therefore, concluded that the modifications are
- required to be in place prior to its restart.
Conclusions
Pending satisfactory implementation of the modifications proposed by the licensee
in its letters of June 19, 1996, and* December 2, 1996, the staff concludes that
URI 272/311-93-80-06, -07, and -08 remain open. The basis for this conclusion is
contained in the NRC letter dated. March 17, 1997.
EB.4
(Closed) Unresolved Item 50-272&311 /96-06-02: failure to perform a 10 CFR
50.59 safety evaluation for a degraded emergency diesel generator jacket water
after-cooler heater condition regarding the UFSAR requirements. The jacket water
after-cooler heater was inoperable for approximately one year yet Salem engineers
performed no safety evaluation. Subsequently, engineers performed a safety
evaluation for this condition and prepared a UFSAR change request to clarify the
function of the after-cooler heater. The inspector reviewed the safety evaluation
and the UFSAR change request and found they satis~actorily resolved this issue.
Management resolved the generic issue of tir.ieliness and adequacy of the 10 CFR
50. 59 process as part of the response to NRC Restart Issue Ill. 11, Engineering
Problem Resolution, Including Safety Evaluations (NRC Inspection Report 50-
272&311 /96-16). This unresolved item is closed.
'*
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EB.5
(Closed) Violation 50-272&311 /96-07-04: failure to evaluate a deviation and
submit a report within 60 days of discovery per 1 OCFR21. On March 15, PSE&G
published an industry report that described recent failures of safety related 4. 16 KV
breakers. PSE&G staff did not report this as required by 1 OCFR21 until July 1,
1996. Salem staff provided and documented training for licensing, operations, and
engineering personnel to heighten awareness of reporting requirements and to
improve inter-departmental communication. Additionally, Salem management
performed a review of corrective action documents for Salem and Hope Creek to
identify any other potentially reportable deficiencies and found none. The inspector
considered the corrective actions adequate. This item is closed.
EB.6
(Closed) Unresolved Item 50-272&311/96-12-03: AHR minimum flow line flow
_indicator was described in the UFSAR but does not exist in the plant. The inspector
reviewed UFSAR change notice No.96-154 and the 10 CFR 50. 59 Safety
Evaluation for the change. The change deleted the informat.ion in UFSAR Section
6.3.5.3 regarding the AHR minimum flow line flow indication. The inspector
concluded that this was a satisfactory resolution to the conflict between the
UFSAR anq the existing plant configuration. The inspector noted that Salem staff
had not yet made this change to the UFSAR but the existence of the change notice
provided reasonable assurance the staff will make the change. This item is closed.
EB.7
!Closed) Unresolved Item 50-272&311/96-07-01: a fuel handling building sump
pump unot running" alarm was mentioned in the UFSAR but does not exist in the.
plant. The inspector reviewed UFSAR change notice No. 96-1 21 and the 10 CFR
50.59 Safety Evaluation for the change. The change removed the reference to the
alarm and provided additional information regarding monitoring of the sump level.
The inspector concluded that this was a satisfactory resolution to the conflict
between the UFSAR and the existing plant configuration. The inspector noted that
Salem staff had not yet made this change to the UFSAR but the existence of the
change notice provided reasonable assurance the staff will make the change. This
item is closed.
EB.8
(Closed) Violation 50-311196-13-01: failure to perform the required lnservice
Inspection of the pressurizer spray nozzle inner radius. On August 19, 1996, Salem
staff determined that, contrary to the requirements of Technical Specification 4.0.5., engineers had not performed the first 10 year inspection of the pressurizer
spray nozzle inner radius weld. The inspector reviewed PSE&G's response to this
violation and reviewed documents which provided evidence of the corrective action
taken. The inspector found that engineers performed the inspection and the results
were satisfactory. Management reviewed the Salem Unit 2 lnservice Inspection
database for first 10 year inspections and found one additional pressurizer weld
that engineers had not inspected. In the LEA Salem staff issued as a result of this *
event, the licensee committed to perform a similar review for Salem Unit 1 prior to
mode 6. The cause of the missed inspections was insufficient administrative
control of the computer data input and review. Previously, a vendor was
responsible for the data base. Presently, Salem staff controls the database. Also,
the database now has inherent program controls linking completed inspections with
the inspection schedule, thus providing an extra measure of precaution to prevent
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45
missing inspections. The inspector concluded that response and corrective action
to this violation was satisfactory.
This item is closed.
EB.9
(Closed) Unresolved Item 50-272&311 /96-01-04: update FSAR to state that full
core off-load is a routine practice during refueling outages. During an inspection, an
NRC inspector pointed out that although full core off-load is routine during refueling
outages at Salem 1 &2, the FSAR referred to the practice as "unusual". Since
then, Salem staff has amended the FSAR to state "The system design considers the
need to totally unload a reactor at the time when spent fuel is in the fuel pooL"
The inspector considers this resolution acceptable. This item is closed.
EB.10 (Closed) Inspector Followup Item 50~272&311 /96-08-07: update FSAR to state
~hat full core off-load is a routine practice during refueling outages. This issue is
identical to Unresolved Item 50-272&311/96-01-04. This item is closed.
The inspectors updated or closed the following items which had been identified in
past MOV program inspections. These items had been identified in Inspection
Report 50-272/311/96-11).
EB.11 (Closed) Violation 50-311/96-11-01: In NRC Inspection Report 50-311/96-11
violations were identified concerning inadequate test *control measures during
dynamic testing conducted on valves 2CV68 and 2CV69 (Charging Header Stop
Valves). The inspections determined that the differential pressures assumed by the
dynamic test analysis were uncertain because: 1) the upstream pressure
instruments did not account for the presence of pressure control valves located
between the pressure instruments and the test valves, and 2) the test procedure
specified the use of a downstream pressure gage with an abnormally wide range
which provided insufficient sensitivity for the expected test conditions. More
importantly the que~tionable test data obtained was used as the valve factor basis
for. the PORV block valves (2PR6 and 2PR7).
In response to the violation, PSE&G issued Performance Improvement Request No.
00960725067 dated July 29, 1996, and took the following actions:
PSE&G was no longer using the Charging System (2CV68 and 2CV69) testing to
justify the valve factors for the* PORV block valves. (See Section E1 .3 of this
report.)
PSE&G personnel retested 2CV68 and 2CV69 and was able to reduce the effect of
the upstream pressure drop contributed by pressure control valve 2CV71 . This
testing resulted in reasonable valve factors except for one test that was still
abnormally low. PSE&G personnel were unable to explain this result.
Licensee personnel reviewed other Unit 2 dynamic tests to identify if similar test
control mistakes were made. Flow paths were reviewed to identify flow
restrictions and f)ressure instrument locations were evaluated to assess the
adequacy of the pressure data that w*as obtained. Plant walkdowns were also
performed in some cases. This review revealed other cases where the pressure
\\
46
instrument locations and the system alignment could be improved. Based on this
review, proposed changes to the dynamic test procedures were under consideration
at the time of this inspection. PSE&G personnel considered these changes fo be
enhancements and the existing testing results were not seriously affected by the
existing test alignments. Also, a revision was made to the test evaluation
procedure to prompt the technician to review the pressure data and ensure that the
observed pressures are reasonable. The inspectors noted that a further procedure
cau.tion may be appropriate to review overall test conditions and data acquisition
when test results appear to be abnormal. Finally, licensee personnel stated that
they intend to use continuous pressure data acquisition during future tests (where
possible) to improve accuracy of test results.
_To assess these licensee's actions, the inspectors reviewed a dynamic test
performed on 22SJ.40 in November 1994, where the apparent valve factor was
0.11. The inspectors noted that the downstream pressure gauge was left closed
during the closing stroke. This was done because the pressure gauge range was
limited to 100 psig and leaving it on line would have damaged the gauge. Licensee
personnel justified this action because the system flow discharged into the reactor
cavity and the back pressure present at the outlet of the test valve was a function
of the cavity water level which would have had no significant change and hence
minimal impact on the test results. While this item was not identified or
documented as part of the licensee's review and corrective actions, the inspectors
concluded that PSE&G took adequate corrective actions to resolve the concerns
regarding this violation which is now closed.
ES. 12 !Closed) lnsoector Followup Item 50-311196-11-02: Complete load sensitive
behavior study for Salem Unit 2. To establish an adequate load sensitive behavior
margin for MOVs that cannot be dynamically tested, the licensee was expected to
analyze Salem's dynamic test results to support the generic letter program
assumptions. This study was not available during the last inspection. However, as
- documented in Section E1 .3 of this report, PSE&G has completed an acceptable
load sensitive behavior study and has established adequate margins for MOVs at
Salem Unit 2. Therefore, the licensee's actions adequately addressed this concern.
ES.13 (Closed) Inspector Followup Item 50-311196-11-03: Complete stem friction
coefficient study for Salem Unit 2. To adequately assess MOV thrust capability
under design-basis conditions, the licensee was expected to analyze Salem's stem
friction coefficient performance to support the generic letter program assumptions.
This study was not available during the last inspection. However, as documented
in Section E1 .3 of this report, PSE&G has completed an acceptable stem friction
coefficient study for Salem Unit 2. The inspectors found the licensee's actions
acceptable and considered this item closed.
ES.14 (Closed),,lnspector r-oilowup Item 50-311196-11-04: Revise test feedback method
to include margin for valve degradation. PSE&G's methods for feeding back results
from the MOV dynamic test program did not include a specific margin for potential
valve degradations. However, as documented in Section* E1 .3 of this report,
PSE&G has revised their MOV setup methodology for Salem Unit 2 to specifically
~-
..
-~*;I
-'~
.~ -,
47
include a 5% margin for potential valve degradations. The inspectors found the
licensee's actions acceptable and considered this item closed.
ES. 1 5 (Closed) Violation 50-311196-11-05: Incorrect assumpt_ions in. the mechanical
design calculations for the residual heat removal suction header valves {2RH1 and
2) resulted in low torque switch settings. The incorrect settings for these risk
significant pressure isolation valves created the possibility that they might not close
under design-basis conditions since the torque switch was wired in series with the
limit switch for these limit-controlled MOVs. PSE&G responded to the Notice of
Violation by letter LR-N96332 dated November 1, * 1996 that stated the corrective
actions to be taken to prevent recurrence.
- .The inspector specifically verified that PSE&G had .corrected the mechanical design
calculations for 2RH1 and 2 such that the torque switch settings would not prevent
full closure of these MOVs. A heavier spring pack had to be installed for 2RH 1
since the required torque output was beyond the capability of the original spring
pack. Both valves were then static tested satisfactorily with diagnostics to assure
their operability. The inspector also verified that the licensee had checked other
limit controlled MOVs, including butterfiy valves, and confirmed that they were not
impacted similarly. Additional remarks concerning the switch settings and
capability of these MOVs are included in Sections E1 .3 and E1 .4 of this report. The
inspector concluded these actions to be appropriate for closing out this item.
E8.16 !Closed) Inspector Followup Item 50-311196-11-07: Request for PSE&G to
increase the capability of marginal MOVs. This issue was addressed again in this
report as discussed in Section E1 .4. PSE&G has agreed to review measures to
improve the capability of certain MOVs in conjunction with periodic verification
. efforts in response to GL 96-05. The inspectors concluded that these actions were
acceptable for closing this item.
E8.17 (Closed) Inspector Follow Item 50-311196-11-08: Verify MOV switch setting
requirements for Pratt service water system butterfly valves. PSE&G had not
verified the adequacy of vendor-provided torque requirements for the Pratt butterfly
valves that were located in Salem Unit 2's service water system. None of these
valves were practicable to test in situ under dynamic conditions. As documented in
Section E 1 .4 of this report, the licensee used the EPRI PPM butterfly model to
develop the torque requirements for these valves. Based on PSE&G's application of
the PPM in accordance with EPRl's guidance and the NRC's safety evaluation (as it
relates to use of the butterfly model), the inspectors found the licensee's actions
acceptable and considered this item closed.
E8.18 (Closed) Inspector Followup Item 50-311196-11-09: An independent assessment of
the Salem MOV program to evaluate its readiness for closure was conducted in
August 1995 by two individuals who were MOV project members at another
nuclear f~cility. The as*.;essment appeared to be highly constructive with strengths
and weaknesses noted and various recommendations presented for assuring Salem
MOV program closure. However, PSE&G had not established firm management
controls for providing action plans or addressing the other items in the independent
- "
48
assessment report. Action Request (AR) 960725184 was issued to evaluate the
independent assessment, incorporate any appropriate recommendations, and
complete any necessary changes to the Salem MOV program by October 25, 1996.
The inspector reviewed PSE&G's actions to resolve this AR and determined that no
new issues were identified in this subsequent review of the MOV program
independent assessment. PSE&G was adequately addressing the various
recommendations of the independent assessment. The inspector concluded that
this issue was resolved.
E8.19 (Open) Unresolved Item 50-311196-11-10: Resolve configuration control issues
regarding the impact on the MOV program due to p!ant modifications and EOP
changes. In June 1996 PSE&G identified a problem concerning past plant changes
that had been implemented without appropriate consideration given to the impact
ori MOV design~basis setpoint documents. These plant changes included design
change packages, temporary modifications, and emergency operating procedures.
PSE&G issued AR 96060711 6 to identify comprehensive corrective actions to
evaluate and correct potential problems. The inspector reviewed the findings and
status regarding these corrective actions and determined that, while substantial
progress has been made to resolve this configuration control issue, AR 96060711 6
has not been completed. The licensee considAred that this AR had been completed
to provide the assurance that there were no MOV configuration control issues that
could impact existing MOV switch settings. The inspector noted that the NRC
identified TOL issue on MOVs in Section E1 .4 of this report, although only one
instance and concluded to have minor safety consequences, challenges the
thoroughness of PSE&G's corrective actions of AR 960607116. This item will
remain unresolved pending PSE&G's uncompleted actions to address all engineering
areas exposed to the configuration control issues in this AR.
E8.20 (Closed) Unresolved Item 50-311196-11-11: PSE&G had submitted an MOV
program closure letter on March 20, 1995, for Unit 2 and had not amended this
letter. In light of this fact and the nature and extent of the findings in NRC
Inspection Report 50-311 /96-11, a question regarding compliance with 10 CFR
50.9, "Completeness and Accuracy of Information" was raised. This issue was
identified as an Unresolved Item. The issue was discussed at a public meeting held
on November 12, 1996, between PSE&G and the NRC. PSE&G indicated that
engineering evaluation A-O-ZZ-MEE-0926 served as a technical basis for the Salem
Unit 2 MOV program closure letter. PSE&G m_aintained that then:i was no
significant negative information that developed subsequent to the March 20, 1995
letter which would have warranted an amended response. MOV changes that were
- made were considered to be minor enhancements to improve performance and were
not significant deviations from the MOV program technical basis.
The inspector determined that the design verifier of engineering evaluation A-0-ZZ-
MEE-0926, in accordance with the recommendation of the licensing engineer
responsible for the March 20, i 995 letter, had prepared an internal memorandum
on March 9, 1995, which summarized the technical basis for how PSE&G had
completed requested actions a. through h. of GL 89-1_ 0. In reviewing this *
document and based on interviews with the cognizant technical and licensing staff
',
49
personnel responsible for the March 20, 1995 letter, the inspector concluded that
there were no clear factors regarding MOVs subsequent to this letter that would
have warranted an amended response. In this regard the inspector noted that the
MOVs of most concern in the internal memorandum of March 9, 1995, were PR6
and 7 and CC131 and 190 and these MOVs continued to be discussed during this
inspection. The inspector concluded that PSE&G has been closely monitoring the
performance and capability of these MOVs which is consistent with the intent of
GL 89-10. In summary, the inspector concluded that the question regarding
compliance with 10 CFR 50.9 had been resolved in that there was not a compliance
problem. This unresolved item is closed.
ES.21 Review of Updated Final Safety Analysis Report !UFSARl Commitments
A *recent discovery of a licensee operating their facility in a manner contrary to the
UFSAR description highlighted the need for a special focused review that compares
plant practices, procedures, and/or parameters to the UFSAR descriptions. While
performing the inspections documented in this report, the inspector reviewed the
applicable portions of the UFSAR that related to the areas inspected. The
inspectors verified that it was consistent with the observed* plant practices;
procedures, and/or parameters.
P8.1
!Closed) Unresolved Item 50-272&311 /96-15-03: description of backup radiological
instrumentation in Salem's Emergency Plan was incorrect.* The Emergency Plan
incorrectly stated that radiologicalinstrumentation was available in the Training
Center laboratory for use as backup to the Emergency Off site Facility, however,
technicians did not calibrate that instrumentation. Salem management revised the
Emergency Plan to state that backup equipment is available at the station and at
other licensed facilities such as Peach Bottom or Limerick. The inspector found this
)
solution acceptable. This item is closed.
j
P8.2
!Closed) Unresolved Item 50-272&311 /96-15-04: description of media training
program in Salem's Emergency Plan was incorrect. Salem staff revised the
Emergency Plan to accurately describe the present method of informing local media
personnel cf emergency plan activities. The present method is to send local media
ar1 information calendar followed by a phone call inviting them to the annual
emergency preparedness exercise. The inspector found the resolution*to be
satisfactory. This item is closed.
P8.3
(Closed) Violation 50-272 & 311 /94-112-05014: incomplete reporting of
information to the NRC regarding the April 7, 1994 inadvertent safety injection
event. The Salem Emergency Plan required that operators report specific
information to the NRC within 60 minutes. The required information includes
systems affected, actuations and their initiating signals, causes, effect of event on
' .
50
the plant, and actions taken or planned. The inspector verified that the Emergency
Plan, Attachment 5, now provides clear guidance regarding technical information
which must be included when reporting emergency events. Also, Attachments 6
and 7 allow operators to assign an additional communicator if necessary.
Additionally, in December 1996, NRC inspectors observed mini-drills for
Salem/Hope Creek and found that "Offsite notifications were timely, and
professionally completed" (NRC Inspection Report 50-272&311 /96-18 has details).
Inspectors also verified that training modules used to qualify and requalify
designated communicators provided sufficient information relative to reporting. The
inspector concluded Salem staff took appropriate action to resolve this violation.
This item is closed.
P8.4 .!Closed) Violation 50-272 & 311/95-81-04: inadequate equipment to support the
emergency response. In October 1995, the control room overhead annunciator
alarm system failed and the system provided no indication that the failure had
occurred. This condition rendered the equipment inoperable so that PSE&G staff
was not able to meet the requirements of the Emergency Classification Guide
(ECG). Section 10 of the ECG requires an alert declaration if "Loss of most or all
( > 75%) overhead annunciators (excluding a scheduled test or maintenance activity
for which preplanned compensatory measures have been implemented) and fifteen
minutes have elapsed since the loss of annunciators."
PSE&G staff addressed this issue in their response to NRC Restart Issue 11.40,
Overhead Annunciator Failures. NRC staff conducted a recent inspection to review *
PSE&G's actions to resolve these equipment problems and the inspectors concluded
the corrective action was satisfactory for Salem Unit 2. The inspector documented
the results of that inspection in Inspection Report 50-272 & 311 /96-13 .. Because
the issue is closed for Salem Unit 2 and is being tracked to completion for Unit 1 by
NRC Restart Issue 11.40, this violation is closed.
V. Management Meetings
X1
Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management at the
conclusion of the inspection on March 19, 1997. The licensee acknowledged the findings
presented.
Licensee representatives were informed of the purpose and scope of the MOV inspection
at an entrance meeting conducted on January 13, 1997. Findings were discussed
periodically with the licensee throughout the course of the inspection. The inspectors met
with the principals listed below on January 17 and January 24, 1997 at which time a final
exit meeting with the licensee was conducted to summarize preliminary inspection
findings. The licensee acknowledged the preliminary findings and conclusions, with no
exceptions taken. The bases for the inspection conclusions did not involve proprietary
information, nor was any such information included in this inspection report, except for the
MPR Associates TB and PL analyses reviewed by NRR and referred to in Section E1 .5.
' .
51
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
X3
Management Meeting Summary
On February 5, 1997,Mr. Leonard J. Callan, NRR Executive Director for Operations visited
the Salem site. A copy of the licensee handout is attached .
INSPECTION PROCEDURES USED
Tl 2515/109:
Inspection Requirements for Generic Letter 89-10, Safety-Related
Motor-Operated Valve Testing and Surveillance
IP 37551:
Onsite Engineering
IP 50001:
IP 61726:
Steam Generator Replacement Inspection
Surveillance Observations
IP 62707:
Maintenance Observations
Plant Operations
IP 71707:
- IP 92901:
Followup - Plant Operations
ITEMS OPENED, CLOSED, AND DISCUSSED
- Opened
50-272&311 /97-03-01
50-311197-03-02
. operator trafning and qualification
IFI
management commi<::ment process
!:>0-3 l 1 /97-03-03
50-311197-03-04
50-311197-03-05
IFI
verify commitment regarding 2RH1 and 2.
IFI
verify commitment regarding 2PR6 and 7.
IFI
verify commitment regarding 2CC 131 and 1 90.
Closed
50-272&311/95-024
LER
50-311 /96-09 _
LER
50-272&311 /93-23
VI Os
(EA, 94-003: 01013, 01023,
01033,01043,01053,
01063, 01073 & 01083)
EA94-112: 04013
EA94-112: 05014
272&311/93-15-04
50-272&311/94-14-02
50-272&311 /95-07-03
50-272&31; /95-17-02
50-272&311 /95-17-03
50-272&311 /95-80**01
"Technical Specification Violations: differential
pressure of the fuel handling building ventilation
system" (discussed in 50-272 and 311 /96-06
fourteen day followup report regarding 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />
shift for operations personnel
failure to follow procedures
PSE&G staff provided inadequate training
incomplete reporting of information to the NRC
regarding April 7, 1994 inadvertent safety
injection event
corrective action program weaknesses
failure to provide adequate training to
maintenance personnel
failure to follow procedures
failure to implement a commitment to install a
concrete curb at the entrance to each Salem
Unit 1 and 2 EOG cubicle
evaluation of corrective action regarding Salem
Unit steam generator tube inspection
weaknesses
~--~
-:J
- )
. ~
~,
- *.
2
50-272&311/95-81-04
inadequate equipment to support the emergency
response
50-272&311/96-01-01
failure to follow procedures
50-272&311 /96-01-02
failure to follow procedures
50-272&311/96-01-04
update FSAR to state that full core off-load is a
routine practice during refueling outages
50-272&311/96-06-01
failure to follow procedures
50-272&311 /96-06-02
failure to perform a 10 CFR 50.59 safety
evaluation
50-272&311/96-07-01
a fuel handling building sump pump"not running"
alarm was mentioned in the UFSAR, but does
not exist in the plant
50-27_2&311 /96-07-04
failure to evaluate a deviation and submit a
report within 60 days of discovery per 10 CFR
21
50-272&311 /96-08-05
inadequate procedures
50-272&311 /96-08-06
Salem Unit 2 operating license does not permit
1 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> operating shifts
50-272&311 /96-08-07
IFI
update FSAR to state that full core off-load is a
routine practice during refueling outages
50-311/96-11-01
Inadequate test control and application of MOV
test data
50-311196-11-02
IFI
Basis for load sensitive behavior margin used in
thrust calculations
50-311196-11-03
IFI
Basis for stem friction coefficient used in thrust
calcul.ations
50-311 /96-11-04
IFI
Basis for valve degradation margin used in thrust
calculations
50-311196-11-05
Inadequate design control of switch settings for
MOVs 2RH1 and 2
50-311196-11-07
IFI
Request to improve thrust margin for selected
MO Vs
50-311196-11-08
IFI
Evaluate torque requirements for Pratt butterfly
valves
50-311 /96-11-09
IFI
PSE&G to evaluate and document response to
MOV program independent assessment
50-311/96-11-11
Resolve question regarding Salem Unit 2 MOV
program completion in the context of 10 CFR
50.9(b)
50-272&311/96-12-03
AHR minimum flow line flow indicator was
described in UFSAR, but does not exist in the
plant
50-311 /96-1 3-01
failure to perform the required inservice
inspection of the pressurizer spray nozzle inner
radius
50-272&311/96-'!5-02
failure to follow procedures
-
50-272&311 /96-15-03
50-272&311 /96-15-04
50-272&311 /96-17-01
Discussed
50-272&311 /93-80-06
50-272&311 /93-80~07
50-272&311 /93-80-08
50-311/96-11-10
3
description of backup radiological
instrumentation in Salem's Emergency Plan was
incorrect
description of media training program in Salem's
Emergency Plan was incorrect
failure to perform a safety evaluation in
accordance with 10 CFR 50.59
non-conservative assumptions, licensee using
only one spurious operation per fire incident
requirement to perform repairs for Hot Shutdown
contrary to SER statement
licensee method of protecting equipment from
damage by fire
review PSE&G's corrective actions to resolve
design interface problem regarding impact on
MOVs from modifications and EOP changes
. ' . '
- ~i
- ~
- ~
..
-i
cc
CFR
CFCU
DP
ECG
ECG
EOG
EMIS
GL
IR
LCO
MMIS
MO Vs
NBU
NO Vs
NRC
PL
PPP
PSE&G
SR Os
TOL'
TS
TSSIP
WIN
LIST OF ACRONYMS USED
Augmented Inspection Team
Action Request
Action Tracking System
Corrective Action Program
Component Cooling
Code of Federal Regulations
Containment Fan Cooler Unit
Differential Pressure
Emergency Classification Guide
Emerg~ncy Classification Guide
Equipment Malfunction Identification System
Electric Power Research Institute
Generic Letter
.Inspection Report
Limiting Condition for Operation
Measuring and Test Equipment
Managed Maintenance Information System
Motor-Operated Valves
Management Review Committee
Nuclear Business Unit
Notices of Violations
Nuclear Regulatory Commission
Public Document Room
Performance Improvement Request
Post Maintenance Testing
Power Operated Relief Valve
Performance Prediction Model
Performance Prediction Program
Public Service Electric and Gas
Reactor Coolant Pump
Safety Evaluation
Senior Reactor Operators
Thermal Overload
Technical Specifications
Technical Specification Surveillance Improvement Program
Updated Final Safety Analysis Report
Work-it-Now
- .
- .
-
.
ATTACHMENT
PUBLIC SERVICE ELECTRIC AND
.GAS
SALEM.NUCLEAR GENERATIN~G
STATION
GENERIC LETTER 89-.10 PROGRAM
.
.
..
lfff/
PURPOSE OF MEETING
A) DISCUSS UNRESOLVED ITEM FOR THE MOV
PROGRAM CLOSURE
B) DISCUSS ACTIONS REQUIRED BY PSE&G
BEFORE RESTART
(A)
GENERIC LETTER 89-10
CHRONOLOGY OF EVENTS
MOVEng.
Sukm 1&2
Comments on
Sah:m 2
\\'k!gin
PECO 111ird
Assessment
I lope Creek
Sulcm I
Closure
extended
Party*
presentc:d to
assessment to
Assessm.:nl
closure
Oulngc shifts
Closure
?'-
Letter
shutd0\\\\11
Assessment
PSE&GMgt.
Mgt.
Report issued
inspc:ction
to Unit 2
Letter
lnsr
3/20/95
611195
8/25/95 -
9n/95
9/28/95
10/5/95
Feb-96
3/15/96
6/25/96
112
8/31/95
11:
I
I
I
I
I
I
.
{1}
{2}
{3}
11/12/96
- . '! .**
(A)
(tJBASIS FOR SALEM 2 CLOSURE
SUBMITTAL
CLOSURE LETTER SENT 3/20/95 UPON COMPLETION OF 2R08
. ITEMS A THROUGH H CONSIDERED COMPLETE
. DOCUMENTATION FOR EACH VALVE EXISTED IN
INDIVIDL)AL EVALUATIONS
ENGINEERING EVALUATION A-O-ZZ-MEE-0926 ISSUED 12/23/94
JUSTIFIED AfSUMPTIONS BASED ON ANALYSIS OF EPRI DATA
. 0.5 VALVE FACTOR
. 0.15 STEM COEFFIC.JENT
. 30 o/o MARGIN
DP TESTING JUSTIFIED THAT PROGRAM ASSUMPTIONS WERE
GOOD PREDICTORS OF VALVE THRUST REQUIREMENTS
. EXCEPTIONS WERE EVALUATED ON A CASE BY CASE
BASIS BY APPROVED PROCEDURES AND THE TARGET
THRUST WA~ INCREASED
1sEe FIGURE 1)
I f/f2)§g
. . . ... *-
. . .. ~ -* '.:_ ~ ....... "......
. .
~--*.
'
\\ ...
TARGET THRUST BASED ON 0.5 VALVE FACTOR AND 30% MARGIN Vs. MEASURED
THRUST AT HARD S!:AT CONTACT.
-**--*--.. -* .. ---
---*---------------*---*---**-*---**--**-*** -- ............... _**----*--*----*--**---................. . .................... *--- .... *-****--*----.
-*---. -*--*----*--...... ___ _
Figure 1
- .,.
1111/
... :'. ...
(A)
(2) REASON FOR THIRD PARTY
ASSESSMENT
.* ..* j,
,.,
ASSESSMENT WAS REQUESTED AS PART OF A REVIEW OF ALL
ENGINEERING PROGRAMS FOR RESTART IN AUGUST, 1995
THE MOV PROGRAM WAS ONE OF THE PROGRAMS THAT WAS
REVIEWED
THERE WERE NO SPECIFIC CONCERNS REGARDING THE MOV *
PROGRAM WHICH INITIATED THE ASSESSMENT REQUEST
11111
(A)
(2) THIRD PARTY ASSESSMENT
RESULTS IDENTIFIED STRENGTHS, WEAKNESSES AND RISKS TO
CLOSURE
RESULTS COMMUNICATED TO MANAGEMENT
. PRESENTATION BY PECO TO PSE&G MANAGEMENT 9/7/95
. MOV ENGINEER MEMO SUMMARIZED RESULTS 9/28l95
. FINAL REPORT ISSUED 10/5/95
RESULTS NOT ENTERED INTO CORRECTIVE ACTION PROGl~AM
NEW PROGRAM
. UNDER A STARTUP AND LEARNING CURVE
. PROGRAM WEAKNESSES WERE NOT CONSIDERED
ACTIONS TAKEN IN RESPONSE TO WEAKNESSES WERE Nor
WELL DOCUMENTED
. . .
1111/
.(..,: .... *--*-'*
(A)
- (2) RESPONSE TO THIRD PARTY
ASSESSMENT
ADDITIONAL STATIC AND DP TESTING WAS SCHEDULED
PRESENTATION WAS MADE TO MRC IN SEPTEMBER, 1995 (MTG.95-035). IMPORTANCE OF ADDITIONAL STATIC AND DP
TESTING TO SUPPORT CLOSURE WAS EMPHASIZED
THE REVISED CLOSURE DOCUMENT COMPLETION WAS BASED
ON THE OUTAGE SCHl;DULE. COMPLETION DATES SLIPPED
AS THE OUTAGE SCHEDULE CHANGED. THE LAST PUBLISHED
DUE DATE WAS 6/30/96
THE EXISTING SALEM 2 CLOSURE DOCUMENT EE: S-C-ZZ-MEE-
0906 WAS SUPERSEDED BY EE: S-C-VAR-NEE-1117
SCHEDULED TO BE COMPLETED BY NOVEMBER 30,1996
1111/
(A)
. (2) SALEM RESTART PLANS
.
.
(SEPTEMBER, 1995)
CLOSURE FOCUS SHIFTED FROM EPRI AND INDUSTRY DATA
TO SALEM SPECIFIC DATA FOR JUSTIFICATION OF
.
ENGINEERING ASSUMPTIONS.
~
A SIGNIFICANT AMOUNT OF ADDITIONAL STATIC TESTING
WAS SCHEDULED TO INCREASE MARGIN
. UNIT I - 36 STATIC VOTES TESTS, 4 'VALVE INTERNAL
DCP's, 3 SPRING PACK I GEAR RATIO DCP's
.
. UNIT 2 - 30 STATIC VOTES TESTS
ADDITIONAL DP TESTING WAS SCHEDULED TO PROVIDE
. GREATER CONFIDENCE IN ENGINEERING ASSUMPTIONS
. UNIT 1 - 16 DP TESTS SCHEDULED
. UNIT 2 - 11 DP TESTS SCHEDULED
..
'>
(A)
(3) BASIS FOR SALEM 1 CLOSURE
SUBMITTA.L
GL 89-10 ITEMS A THROUGH H WERE CONSIDERED COMPLETE. AS PART OF THE
IMPROVEMENT PLAN, ADDITIONAL TESTING WAS SCHEDULED TO INCREASE.
MARGIN
LICENSING WAS REQUESTED TO PROVIDE UNIT 1 SCHEDULE INFORMATION TO
ENABLE NRC TO INITIATE THE CLOSURE REVIEW PROCESS.' YNIT 1 WAS THE
LEAD RESTART UNIT AT THAT TIME
TENTATIVE MID-JULY, 1996 CLOSURE INSPECTION DATE WAS ESTABLISHED IN
FEBRUARY, 1996 BASED ON COMPLETION OF UNIT 1 MOV WORK IN EARLY
APRIL, 1996
RESTART PRIORITY SHIFTED IN MARCH, 1996 FROM UNIT 1 TO UNIT 2. ALTHOUGH
ITEMS A THROUGH H WERE CONSIDERED COMPLETE, MARGIN ENHANCEMENT
ACTIVITIES WERE NOT COMPLETED
THE NRC WAS NOT REQUESTED TO RESCHEDULE THE CLOSURE INSPECTION
BASED ON THE CHANGE IN THE LEAD RESTART UNIT
SALEM UNIT 1 CLOSURE LETTER ISSUED JUNE, 1996
- --**it.
~
) .
SUMMARY
SALEM CLOSURE BASED ON DP TEST RESULTS AND INDUSTRY
EXPERIENCE
SALEM STAFF BELIEVED THAT THE ISSUES IDENTIFIED IN THE
THIRD PARTY ASSESSMENT DID NOT CHALLENGE THE ABILITY
TO CLOSE GL 89-10
PSE&G FAILED TO CONSIDER THE IMPACT OF THE CHANGE OF
THE LEAD RESTART UNIT AND SCHEDULE SLIPPAGE ON THE
SCHEDULE FOR THE CLOSURE
~ .
.--
.
f
(B)
ACTIONS REQUIRED FOR SALEM 2
RESTART
TEST CONTROL VIOLATION (CV68 & 69)
. TEST PROCEDURES REVISED
. VALVES RE-TESTED
. NO GfNERIC ISSUES WERE DISCOVERED
. -UNIT 2 COMPLETED - SEPTEMBER, 1996
DESIGN CONTROL VIOLATION (RH1 & RH2)
. CALCULATIONS REVISED
. VALVES RE-TESTED
. NO GENERIC ISSUES WERE DISCOVERED
. UNIT 2 COMPLETED - AUGUST, 1996
il/12fo&
m
.1;
. -*~
,_.'(_r~: *' .
. - .
-' .. ,. ... .
. ... *,_- .. **'*
~.:.': -* .
(B)
ACTIONS REQUIR~ED FOR SALEM 2
RESTART
CLOSURE DOCUMENT
-
ENGINEERING EVALUATION TO BE APPROVED BY NOV. 30,
1996
>> BASIS FOR ENGINEERING ASSUMPTIONS
>> JUSTIFICATION FOR VALVE FAMILIES
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UNIT 2 CALCULATIC?N REVISIONS, IF REQUIRED, TO BE
.-COMPLETE BY MODE 2
.
- ~*'-*'
- "~:.
(B)
ACTIONS REQUIRED FOR SALEM 2
RESTART
JUSTIFICATION FOR VALVES IN UNIT 2 FAMILIES 3 AND 9.1 WILL
BE ENHANCED PRIOR TO MODE 6 .
CONFIGURATION CONTROL
-
OVER 400 DCP's REVIEWED WITH MINIMAL IMPACT - .
COMPLETE
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REVISED EOP's AND AOP's REVIEWED WITH MINIMAL
IMPACT - COMPLETE
-
TRAINING OF OPERATIONS PROCEDURE WRITING STAFF
TO PREVENT RECURRENCE - COMPLETE
STATUS OF ADDITIONAL DIFFERENTIAL PRESSURE TESTING
16 UNIT 2 VALVES TESTED, THE ONE TEST REMAINING
REQUIRES THE CONDENSATE SYSTEM TO BE IN SERVICE.
V'JILL COMPLETE PRIOR TO MODE 3.
1111/
(B)
ACTIONS REQUIRED*FOLLOWING
SALEM 2 RESTART
REVISE AND UPDATE MOV PROGRAM DOCUMENTATION FOR
ENHANCEMENTS BY MARCH 31, 1997
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CALCULATION REVISIONS
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PROGRAM DOCUMENTATION ENHANCEMENTS