05000272/LER-1980-069-03, /03L-0:on 801223,steam Generator 13 Channel II Steam Flow Failed High.Caused by Failure of Multiplier/ Divider Unit,Hagan Model 112.Unit Replaced,Calibr & Tested

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/03L-0:on 801223,steam Generator 13 Channel II Steam Flow Failed High.Caused by Failure of Multiplier/ Divider Unit,Hagan Model 112.Unit Replaced,Calibr & Tested
ML18085A526
Person / Time
Site: Salem 
Issue date: 01/14/1981
From: Steele W
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18085A525 List:
References
LER-80-069-03L, LER-80-69-3L, NUDOCS 8101200359
Download: ML18085A526 (1)


LER-1980-069, /03L-0:on 801223,steam Generator 13 Channel II Steam Flow Failed High.Caused by Failure of Multiplier/ Divider Unit,Hagan Model 112.Unit Replaced,Calibr & Tested
Event date:
Report date:
2721980069R03 - NRC Website

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1 [UIJ I During routine startup operation, #13 Steam Generator Channel II Stearn Flow failed

!))I] I high.

Action Statement 3.3.1.1-7 was entered at 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br />.

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

43 44 47 D:JIJ !The Multiplier/Divider Unit (Hagan Model 112) in the channel had failed and was [III] I replaced with a spare.

The replacement unit was calibrated and a functional test Li1iJ I was satisfactorily performed.

The Action Statement was terminated at 1147 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.364335e-4 months <br /> on IJJIJ I December 23, 1980.

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