05000272/LER-1980-069, Forwards LER 80-069/03L-0

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Forwards LER 80-069/03L-0
ML18085A524
Person / Time
Site: Salem 
Issue date: 01/14/1981
From: Uderitz R
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18085A525 List:
References
NUDOCS 8101200357
Download: ML18085A524 (2)


LER-1980-069, Forwards LER 80-069/03L-0
Event date:
Report date:
2721980069R00 - NRC Website

text

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(} PS~G e Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone_2Q1/430-7000 --*

Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region 1 631 Park Avenue January 14, 1981

.. _I~.ing of Prussia, Pennsylvania 19406

~-*: - -_*

- Dear Mr. Grier:**

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 80-69/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 80~69/03L.. This report is required within thirty (3 0),days of the occurrence.

CC:

~

Sincerely yours,

-~ - %/"

,{/{ ;~"'*;!~4 R. A. Uderl:tz General Manager -

Nuclear Production Director, Office of Inspection

. and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies)

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  • !***--~ -**~* *" **.---** ~:-*--*,**---..*--w--.. _,...---~-* - *----- -* *- - -*-

Report Number:

80./03L Report Date:

Occurrence Date:

January 14, 1981 12/23/80 Facility:

Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, NJ 08038 IDENTIFICATION OF OCCURRENCE:

  1. 13 Steam Generator Channel II Steam Flow Failed High CONDITIONS PRIOR TO OCCURRENCE:

Mode 2 Startup _ 8 Rx Power 5 x 10 A

DESCRIPTION OF OCCURRENCE:

While performing routine startup operations, #13 Steam Generator Channel II steam flow failed high.

Action Statement 3.3.1.1-7 was entered at 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br /> which allows continued startup and/or power operation to ~ontinue until performance of the next required channel functional test provided the inoperable channel is placed in the tripped condition within one hour.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment Malfunction ANALYSIS OF OCCURRENCE:

Upon investigation, it was determined that the Multiplier/Divider Unit (Hagan Model 112) in the channel had failed.

CORRECTIVE ACTION

The defective Hagan Module was replaced with a spare.

The replacement unit was calibrated and a satisfactory functional test performed.

The Action Statement was terminated at 1147 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.364335e-4 months <br /> on December 23, 1980.

FAILURE DATA:

  • Hagan Controls Multiplier/Divider Unit -

Model 112 Prepared By W. J. Steele Manager -

Sal?m Generating Station SORC Meeting No.

81-01