05000272/LER-1980-046-03, /03L-0:on 800810,during Routine Operation,Steam Generator Level Feed flow-steam Flow Mismatch Circuit 12 Failed.Caused by Failure of Comparator in Circuit.Unit Replaced & Tested Satisfactorily

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/03L-0:on 800810,during Routine Operation,Steam Generator Level Feed flow-steam Flow Mismatch Circuit 12 Failed.Caused by Failure of Comparator in Circuit.Unit Replaced & Tested Satisfactorily
ML18082B146
Person / Time
Site: Salem PSEG icon.png
Issue date: 09/04/1980
From: Murphy M
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082B145 List:
References
LER-80-046-03L, LER-80-46-3L, NUDOCS 8009120428
Download: ML18082B146 (1)


LER-1980-046, /03L-0:on 800810,during Routine Operation,Steam Generator Level Feed flow-steam Flow Mismatch Circuit 12 Failed.Caused by Failure of Comparator in Circuit.Unit Replaced & Tested Satisfactorily
Event date:
Report date:
2721980046R03 - NRC Website

text

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LICENSEE EVENT REPORT

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((ill I During routine operation, it was determined that 12 Steam Generator Level Feed

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Flow-Steam Flow mismatch circuit had failed.

Action Statement 3.3.1.1 was entered

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SUBCODE

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((((] I The comparator in the circuit had failed.

The unit was replaced and tested satis-factorily.

The Action Statement was terminated at 0201 hours0.00233 days <br />0.0558 hours <br />3.323413e-4 weeks <br />7.64805e-5 months <br /> on August 12, 1980.

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NUMBER r:;:;.., TYPE

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80 PERSONNEL INJURIES

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NUMBER DESCRIPTION~

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9 11 12 L.OSS OF OR DAMAGE TO FACILITY '43' TYPE

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