05000272/LER-1980-039-03, /03L-0:on 800702,while Starting 12 Containment Fan Coil Unit,No Svc Water Flow Indicated.Cause Unstated. Solenoid Valve Replaced & Unit Verified Operable

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/03L-0:on 800702,while Starting 12 Containment Fan Coil Unit,No Svc Water Flow Indicated.Cause Unstated. Solenoid Valve Replaced & Unit Verified Operable
ML18082A799
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/23/1980
From: Murphy M
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082A798 List:
References
LER-80-039-03L, LER-80-39-3L, NUDOCS 8007290729
Download: ML18082A799 (1)


LER-1980-039, /03L-0:on 800702,while Starting 12 Containment Fan Coil Unit,No Svc Water Flow Indicated.Cause Unstated. Solenoid Valve Replaced & Unit Verified Operable
Event date:
Report date:
2721980039R03 - NRC Website

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NRC FORM366 (7-77) e LICENSEE EVENT REPORT U.*

CLEAR REGULATORY COMMISSION CONTROL BLOCK: !--_.,...,..........___...____._...,........___,l~

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

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IN I J Is I GI s I 1 JG)I 0 I 0 I - I 0 I 0 I 0 I 0 I 0 I - I 0 I 0 1014 7

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LICENSEE CODE 14 15 LICENSE NUMBER 25 26 I i I i I i I i 101 I I 0 LICENSE TYPE 30 57 CAT 58 CON'T CIT1J

~~~~ Ll.l© I o I 5 I o Io I o i 2 I 1 1 2 101

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8 60 61

. DOCKET NUMBER 68 69 01 1 I o I 2 I 0 I o I@ I o I 1 I 2 I 3 I a I a I G)

EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

[TIIJ I Upon_: starting 12 Contairunent Fan Coil Unit (FCU), it was observed there was no

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((ill IIIIJ liill [ill]

service water flow indication.

At 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br />, the FCU was declared inoperable and Action Statement 3.6.2.3 was entered (78-85, 79-1, 79-16, 80-22, 80-24).

7 8 9 rTIIl 7

8 SYSTEM CODE Is IB I@

9 10 G\\ LER:RO CVENTYEAR

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REPORT I 8 I 0 I NUMBER 21 22

CAUSE

CAUSE CODE SUBCODE COMPONENT CODE L!.J@ LI@ jv IA I LIV IE I XI~

11 12 13 18 SEQUENTIAL OCCURRENCE REPORT NO.

CODE I

I 1013191 1......-1 IOl31 23 24 26 27 28 29 COMP.

SUBCODE

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19 REPORT TYPE L!J 30 VALVE SUBCODE

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20 l.=l 31 ACTION FUTURE EFFECT SHUTDOWN

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ATTACHMENT NPR0-4 PRIME COMP.'

SUPPLIER REVISION NC.

L9J 32 COMPONENT MANUFACTURER 80 TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM SUB.

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

43 44 47 DJ)) I The solenoid valve, SV-624, was replaced from stock.

The FCU was verified operable and the Action Statement was terminated at 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> on July 3, 1980.

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FACILITY

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STATUS

% POWER OTHER STATUS v::::J Gm~@ 1110I0 l@l ___

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10 12 l'J 44 ACTIVITY CONTENT

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RELEASED OF RELEASE AMOUNT OF ACTIVITY ~

[QI] ~@) W@I N/A

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10 11 44 PERSONNEL EXPOSURES

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so METHOD OF A

DISCOVERY DISCOVERY DESCRIPTION ~

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45 46 80 LOCATION OF RELEASE @

N/A 45 80 NUMBER

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DESCRIPTION

ETIJ I o I o I oJ~@.___ __

.-..N"-"A ______________________ _

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9 11 12 13 PERSONNEL INJURIES

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NUMBER DESCRIPTIOJ\\J~

ETIJ I 0 I 0 I 0 l@..__ ____......;N~A'------------------------

8 9

11 12 LOSS OF OR DAMAGE TO FACILITY f.i'3\\

TYPE

DESCRIPTION

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80

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PUBLICITY f,;;;\\

NRC USE ONLY ISSUED~ DESCRIPTION~

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68 69 80 ;

NAME (i~R-lPARER M. J. Murphy PHONE: ___

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