05000272/LER-1980-033-03, /03L-0:on 800609,while Preparing to Change Modes, Quadrant Power Tilt Ratio Was Noted to Have Not Been Completed within 7 Days.Caused by Lack of Checklist on Tickler Sys.Checklist Distributed for Initialing

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/03L-0:on 800609,while Preparing to Change Modes, Quadrant Power Tilt Ratio Was Noted to Have Not Been Completed within 7 Days.Caused by Lack of Checklist on Tickler Sys.Checklist Distributed for Initialing
ML18082A720
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/08/1980
From: Murphy M
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082A719 List:
References
LER-80-033-03L, LER-80-33-3L, NUDOCS 8007150628
Download: ML18082A720 (2)


LER-1980-033, /03L-0:on 800609,while Preparing to Change Modes, Quadrant Power Tilt Ratio Was Noted to Have Not Been Completed within 7 Days.Caused by Lack of Checklist on Tickler Sys.Checklist Distributed for Initialing
Event date:
Report date:
2721980033R03 - NRC Website

text

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I In *preparation to change modes,. it was noted the Quadrant Power Tilt Ratio (QPTR)

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continued at greater than 50% power.

The QPTR was determined on May 26, 1980.

A reactor trip occurred on June 8, 1980.

THE' QPTR should have been performed on [QJI)

June 2 but had not been performed when reviewed on June 9, 198a.

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43 44 47 CIJ:§J I The tickler system did not have a check list to ensure completion of required items.

The surveillance was completed on June 11, 1980, when conditions necessary were met o::TIJ to perform the surveillance.

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Report Number:

80-33/03L Report Date:

7/08/80 Occurrence Date:

6/09/80 Facility:

Salem Generating Station Unit 1 Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Failure to Perform a Quadrant Power Tilt Ratio CONDITIONS PRIOR TO OCCURRENCE:

Mode 3 DESCRIPTION OF OCCURRENCE:

In preparation to change from Mode 3 to Mode 2, it was determined a Quadrant Power Tilt Ratio had not been completed within the required seven days.

Power was greater than 50% within the seven

.day period just prior to the planned mode change.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Procedural Inadequacy ANALYSIS OF OCCURRENCE:

The Operations Directive Manual is used as a tickler system to remind the operators of surveillance requirements more frequent than once per seven days, but did not provide a check list to ensure their completion.

The Quadrant Power Tilt Ratio was completed on May 26, 1980 and was not completed again prior to a unit trip on June 8, 1980 due to an oversight of the need to complete the surveillance requirement.

CORRECTIVE ACTION

The Surveillance Requirement was identified as an item necessary to complete as soon as the necessary conditions were attained.

The surveillance was completed at 1937 hours0.0224 days <br />0.538 hours <br />0.0032 weeks <br />7.370285e-4 months <br /> on June 11, 1980.

A check list has been provided of all Operations Directive Manual routine items which requires each item to be performed when appli-cable and initialed indicating review and completion.

This check list becomes a part of Operations Log #1 and is reviewed by the shift licensed operators at shift relief.

FAILURE DATA:

Not Applicable Prepared By

  • __

M_._. _*J_._. -:.M-:.u_r_p.._h_y __

Manager -

Salel1?Generating Station SORC Meeting No.

47-80