Similar Documents at Salem |
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LER-1980-020, Forwards LER 80-020/03L-0 |
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| 2721980020R00 - NRC Website |
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Public Service Electric and Gas Company 80 Park Place Newark. N.J. 07101 Phone 2011430-7000 Mr. Boyce H. Grier Director of USNRC May 12, 1980 Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
Dear Mr. Grier:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 80-20/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 80-20/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours, j,_,Q/1~
F. P. Librizzi General Manager -
Electric Production
.CC:
Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control (3 copies)
'L\\H~OI' s..:m1n:
Report Number:
80-20/03L Report Date:
5/12/80 Occurrence Date:
4/11/80 Facility:
Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Auxiliary Feedwater Valve, 14AF10, Out of Position CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 100%
Unit Load 1140 MW DESCRIPTION OF OCCURRENCE:
At 1308 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.97694e-4 months <br />, the Resident NRC Inspector discovered 14AF10, the manual isolation discharge valve of 13 Auxiliary Feed Pump to 14 Steam Generator, closed.
The valve position was verified and locked open, its normal position, immediately upon notification to the Senior Shift Supervisor.
This valve, 14AF10, is required to be open by Technical Specification 3.7.l.2(b) which requires the steam driven pump and the associated flow path to be operable or be in Hot Shutdown within the next 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
A complete system flow path verification was performed by an unlicensed operator, with a second independent verification performed by the Shift Technical Advisor, all valves were found to be in their required positions.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
Personnel error.
An operator closed 14AF10 and started to close 13AF10 for a troubleshooting investigation of the steam driven Auxiliary Feed Pump governor control when he was informed to keep those valves open.
In his haste to continue his work assignments, he apparently failed to reposition the 14AF10 valve to locked open.
When a second operator performed a system valve lineup, he apparently recognized 14AF10 was locked and assumed it was open when it was indeed locked closed.
ANALYSIS OF OCCURRENCE:
On April 10, 1980, at 1627 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.190735e-4 months <br />, ll-14AF10 and ll-14AF11 valves were closed in preparation for a 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> endurance test of 13 Auxiliary Feed Pump.
At 1735 hours0.0201 days <br />0.482 hours <br />0.00287 weeks <br />6.601675e-4 months <br />, the endurance test was aborted 15 minutes after its start due to AFP governor control hunting.
All valves were positioned to their normal position at approximately 1855 hours0.0215 days <br />0.515 hours <br />0.00307 weeks <br />7.058275e-4 months <br /> while Performance Department personnel investigated the governor control
LER 80-20/03L 2 -
problems.
At 1915 hours0.0222 days <br />0.532 hours <br />0.00317 weeks <br />7.286575e-4 months <br />, a test run was requested by Instrument and Controls.
To perform the test run, an operator was assigned to manually start the pump.
He started to close ll-14AF10's.
He was informed, after closing 14AF10 and starting to close 13AF10, by the Nuclear Control Operator, that the AFlO valves were to remain open and ll-14AF11 control valves were to be shut from the control room.
13AF10 was opened, but in haste 14AF10 apparently was left locked closed, an abnormal position.
At the completion of the test, a different operator was directed to realign the sys-tem and perform a valve lineup verification of the system.
Ap-parently, when checking 14AF10 and seeing it locked, he assumed it was locked open and noted that on the valve lineup.
The valve line-up was completed, and 13 Auxiliary Feed Pump was returned to oper-ability at 2150 hours0.0249 days <br />0.597 hours <br />0.00355 weeks <br />8.18075e-4 months <br />.
The system remained untouched until 1308 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.97694e-4 months <br /> the following day when the Resident NRC Inspector reported his find-ings.
CORRECTIVE ACTION
The valve was positioned properly and two independent valve lineups were completed for the system valves to ensure its operability.
A task force was commissioned by the Public Service Electric and Gas Company to perform an independent investigation of the occurrence and to submit positive recommendations.
Further action will be taken upon completion of the evaluation now being conducted.
Our response to the NRC inspection addressing this item will serve as a supple-mental report and provide definitive actions that will be implemented.
FAILURE DATA:
None Prepared By M. J. Murphy
~~~~~~~=---=--~~~-
Manager -
SORC Meeting No.
30-80
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| 05000311/LER-1980-001-03, /03L-0:on 800522,when OL Received,Fire Barriers Were Open Due to Recent Removal of Electrical Cables,Pipes & Welding Cables.Cause Not Stated.Barriers Were Verified Sealed Prior to Core Load | /03L-0:on 800522,when OL Received,Fire Barriers Were Open Due to Recent Removal of Electrical Cables,Pipes & Welding Cables.Cause Not Stated.Barriers Were Verified Sealed Prior to Core Load | | | 05000311/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000272/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000272/LER-1980-001-03, /031-0:on 800101,axial Flux Difference Determined to Be Outside Target Band.Caused by Signal Output Failing High.Signal Isolator Was Replaced & Axial Flux Difference Monitor Recalibr | /031-0:on 800101,axial Flux Difference Determined to Be Outside Target Band.Caused by Signal Output Failing High.Signal Isolator Was Replaced & Axial Flux Difference Monitor Recalibr | | | 05000311/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000272/LER-1980-002-03, /03L-0:on 800104,discovered That Functional Tests of Power Range Neutron Flux Low Trip Setpoint When Greater than 25% Power Had Not Been Performed Since 1976.Caused by Lack of Procedures for Tests | /03L-0:on 800104,discovered That Functional Tests of Power Range Neutron Flux Low Trip Setpoint When Greater than 25% Power Had Not Been Performed Since 1976.Caused by Lack of Procedures for Tests | | | 05000311/LER-1980-002-03, /03L-0:on 800526,during Routine Surveillance, Emergency Diesel 2B Could Not Be Fully Loaded.Caused by Three Pins Stuck in Fuel Injectors.Pins Were Unstuck & Diesel Tested Satisfactorily.Insp Order Has Been Initiated | /03L-0:on 800526,during Routine Surveillance, Emergency Diesel 2B Could Not Be Fully Loaded.Caused by Three Pins Stuck in Fuel Injectors.Pins Were Unstuck & Diesel Tested Satisfactorily.Insp Order Has Been Initiated | | | 05000272/LER-1980-002, Forwards LER 80-002/03L-0.Previous Transmittal Included Incorrect LER Attachments | Forwards LER 80-002/03L-0.Previous Transmittal Included Incorrect LER Attachments | | | 05000272/LER-1980-003-03, /03L-0:on 800203,air Particulate Detector Pump Seized,Rendering Detector Inoperable.Caused by Normal Degradation of Pump.Pump Replaced | /03L-0:on 800203,air Particulate Detector Pump Seized,Rendering Detector Inoperable.Caused by Normal Degradation of Pump.Pump Replaced | | | 05000272/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000311/LER-1980-003, Has Been Cancelled | Has Been Cancelled | | | 05000272/LER-1980-004, Forwards LER 80-004/03X-1.Detailed Event Analysis Encl | Forwards LER 80-004/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000311/LER-1980-004-03, /03L-0:on 800610,during Routine Surveillance,Both Safety Injection Pumps Were Made Operable at Less than 312 F in Rcs.Caused by Lack of Procedure to Limit Max Number of Operable Safety Pumps | /03L-0:on 800610,during Routine Surveillance,Both Safety Injection Pumps Were Made Operable at Less than 312 F in Rcs.Caused by Lack of Procedure to Limit Max Number of Operable Safety Pumps | | | 05000272/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000311/LER-1980-005-03, /03L-0:on 800622,during Preparation for Heatup, Position Indication & Mechanical Operation of Pressurizer Overpressure Protection Valves Gave False Indication & Failed to Reseat.Possibly Caused by Foreign Matl in Valve | /03L-0:on 800622,during Preparation for Heatup, Position Indication & Mechanical Operation of Pressurizer Overpressure Protection Valves Gave False Indication & Failed to Reseat.Possibly Caused by Foreign Matl in Valve | | | 05000272/LER-1980-005-03, /03L-0:on 800117,containment Pressure Allowed to Increase Above Limit.Design Change 1EC-0474,not Incorporated,Would Have Raised Alarm Setpoints on Containment Particulated Monitors.Setpoints Readjusted | /03L-0:on 800117,containment Pressure Allowed to Increase Above Limit.Design Change 1EC-0474,not Incorporated,Would Have Raised Alarm Setpoints on Containment Particulated Monitors.Setpoints Readjusted | | | 05000311/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000311/LER-1980-006-03, /03L-0:on 800625,residual Heat Removal Pump Was Discovered to Have Been Previously Improperly Assembled. Caused by Either Personnel Error or Procedural Inadequacy. Pump Inspected,Repaired & Reassembled | /03L-0:on 800625,residual Heat Removal Pump Was Discovered to Have Been Previously Improperly Assembled. Caused by Either Personnel Error or Procedural Inadequacy. Pump Inspected,Repaired & Reassembled | | | 05000272/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000311/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000272/LER-1980-006-03, /03L-0:on 800123,power Was Lost to Meteorological Tower Instruments.Caused by Faulty Backup Power Inverter. Inverter Does Not Have Automatic Transfer Switch as Originally Designed | /03L-0:on 800123,power Was Lost to Meteorological Tower Instruments.Caused by Faulty Backup Power Inverter. Inverter Does Not Have Automatic Transfer Switch as Originally Designed | | | 05000311/LER-1980-007-03, /03L-0:on 800709,during Normal Operations,Motor Bearing Thermocouple for 21 Containment Fan Coil Unit Indicated High.Caused by Normal Wear on Bearing.Bearing Replaced in Kind & Fan Coil Unit Tested Satisfactorily | /03L-0:on 800709,during Normal Operations,Motor Bearing Thermocouple for 21 Containment Fan Coil Unit Indicated High.Caused by Normal Wear on Bearing.Bearing Replaced in Kind & Fan Coil Unit Tested Satisfactorily | | | 05000311/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000272/LER-1980-007, Forwards LER 80-007/03X-2.Detailed Event Analysis Encl | Forwards LER 80-007/03X-2.Detailed Event Analysis Encl | | | 05000272/LER-1980-007-03, /03X-1:on 800128,design Deficiency Found in Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7.Caused by Failure to Include Valve in Piping Spec Break.Valve Seismically Qualified | /03X-1:on 800128,design Deficiency Found in Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7.Caused by Failure to Include Valve in Piping Spec Break.Valve Seismically Qualified | | | 05000311/LER-1980-008-03, /03L-0:on 800710,during Routine Containment Entries,Entry Into Action Statement 3.6.1.3 Resulted from Excessive Leak Rate.Caused by Gaskets Being Moved from Seating Surface Due to Improper Operation.Gaskets Reseated | /03L-0:on 800710,during Routine Containment Entries,Entry Into Action Statement 3.6.1.3 Resulted from Excessive Leak Rate.Caused by Gaskets Being Moved from Seating Surface Due to Improper Operation.Gaskets Reseated | | | 05000272/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000272/LER-1980-008-03, /03L-0:on 800129,maint Was Performed on Inboard Containment pressure-vacuum Relief Valve lVC6 Using nonsafety-related Procedures & Nonqualified Parts.Caused by Omission on List of safety-related Control Valves | /03L-0:on 800129,maint Was Performed on Inboard Containment pressure-vacuum Relief Valve lVC6 Using nonsafety-related Procedures & Nonqualified Parts.Caused by Omission on List of safety-related Control Valves | | | 05000311/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000311/LER-1980-009-03, /03L-0:on 800709,during RCS Heatup,Steam Generator Flow & Pressure Channel Response Inadequate.Bistables Placed in Tripped Mode.Caused by Closed Isolation Valve from Main Steam Piping Preventing Normal Operation.Valve Opened | /03L-0:on 800709,during RCS Heatup,Steam Generator Flow & Pressure Channel Response Inadequate.Bistables Placed in Tripped Mode.Caused by Closed Isolation Valve from Main Steam Piping Preventing Normal Operation.Valve Opened | | | 05000272/LER-1980-009, Forwards Updated LER 80-009/03X-2 | Forwards Updated LER 80-009/03X-2 | | | 05000311/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000272/LER-1980-009-03, Small Leak Found in Telltale Drain 6 in Spent Fuel Pit.Caused by Leaking Welded seams.Half-round Channels Welded Over Leaking Welds | Small Leak Found in Telltale Drain 6 in Spent Fuel Pit.Caused by Leaking Welded seams.Half-round Channels Welded Over Leaking Welds | | | 05000272/LER-1980-010-03, /03L-0:on 800206,while Reviewing Procedure,Found That,During Load Test on Manipulator Crane Prior to Fuel Movement on 790425,test of 3,220 Lbs Performed Instead of 3,250 Lbs Per Tech Spec.Procedure Will Be Revised | /03L-0:on 800206,while Reviewing Procedure,Found That,During Load Test on Manipulator Crane Prior to Fuel Movement on 790425,test of 3,220 Lbs Performed Instead of 3,250 Lbs Per Tech Spec.Procedure Will Be Revised | | | 05000272/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000311/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000311/LER-1980-010-03, /03L-0:on 800709,during RCS Heatup at 1,700 Psig, Channels I & II for Pressure Indication Failed to Respond. Caused by Broken Fuse Cap on Channel I & Improper Valve Lineup on Channel Ii.Fuse Cap Replaced & Valve Opened | /03L-0:on 800709,during RCS Heatup at 1,700 Psig, Channels I & II for Pressure Indication Failed to Respond. Caused by Broken Fuse Cap on Channel I & Improper Valve Lineup on Channel Ii.Fuse Cap Replaced & Valve Opened | | | 05000311/LER-1980-011-03, /03L-0:on 800710,during Routine surveillance,2C Vital Bus Undervoltage Trip Relay Failed to Meet Spec.Caused by Variation in Ambient Conditions Resulting in Relay Trip Setpoint Changing from Preset Mode.Relay Reset | /03L-0:on 800710,during Routine surveillance,2C Vital Bus Undervoltage Trip Relay Failed to Meet Spec.Caused by Variation in Ambient Conditions Resulting in Relay Trip Setpoint Changing from Preset Mode.Relay Reset | | | 05000272/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000311/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000272/LER-1980-011-03, /03L-0:on 800212,during Air Lock Leakage Test, Found Leakage Above Tech Spec Limit.Caused by Gasket Being Jarred from Seating Channel.Gasket & Seating Surface Cleaned.Gasket Reinstalled | /03L-0:on 800212,during Air Lock Leakage Test, Found Leakage Above Tech Spec Limit.Caused by Gasket Being Jarred from Seating Channel.Gasket & Seating Surface Cleaned.Gasket Reinstalled | | | 05000311/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000272/LER-1980-012-03, /03L-0:on 800205,air Particulate Detector Was Declared Inoperable When Shear Pins & Microswitch Failed. Caused by Normal Degradation of Pins & Probable Bump of Switch by Personnel.Pins Replaced & Switch Repaired | /03L-0:on 800205,air Particulate Detector Was Declared Inoperable When Shear Pins & Microswitch Failed. Caused by Normal Degradation of Pins & Probable Bump of Switch by Personnel.Pins Replaced & Switch Repaired | | | 05000272/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000311/LER-1980-012-03, /03L-0:on 800713,during Routine Surveillance, Auxiliary Feedwater Pump 23 Found Inoperable.Caused by Jammed Control Valve Linkage Due to Loose Nut.Linkage Set Free,Nut Installed & Pump Tested Satisfactorily | /03L-0:on 800713,during Routine Surveillance, Auxiliary Feedwater Pump 23 Found Inoperable.Caused by Jammed Control Valve Linkage Due to Loose Nut.Linkage Set Free,Nut Installed & Pump Tested Satisfactorily | | | 05000272/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000311/LER-1980-013-03, /03L-0:on 800714,during Routine tour,21 & 22CS6 Spray Header Isolation Valves Were Found Cleared & Tagged in Closed Position.Caused by Facilitation of Performance of Surveillance Test After Which Valves Were Not Repositioned | /03L-0:on 800714,during Routine tour,21 & 22CS6 Spray Header Isolation Valves Were Found Cleared & Tagged in Closed Position.Caused by Facilitation of Performance of Surveillance Test After Which Valves Were Not Repositioned | | | 05000311/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000272/LER-1980-013-03, /03L-0:on 800227,during Routine Surveillance,Temp Maintained by Heat Trace Circuit 603 Found to Be 142 F Instead of 145 F.Caused by Pipe Insulation Erosion.Heat Tracing Repaired & Piping Reinsulated | /03L-0:on 800227,during Routine Surveillance,Temp Maintained by Heat Trace Circuit 603 Found to Be 142 F Instead of 145 F.Caused by Pipe Insulation Erosion.Heat Tracing Repaired & Piping Reinsulated | |
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