05000272/LER-1980-013-03, /03L-0:on 800227,during Routine Surveillance,Temp Maintained by Heat Trace Circuit 603 Found to Be 142 F Instead of 145 F.Caused by Pipe Insulation Erosion.Heat Tracing Repaired & Piping Reinsulated

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/03L-0:on 800227,during Routine Surveillance,Temp Maintained by Heat Trace Circuit 603 Found to Be 142 F Instead of 145 F.Caused by Pipe Insulation Erosion.Heat Tracing Repaired & Piping Reinsulated
ML18081B271
Person / Time
Site: Salem PSEG icon.png
Issue date: 03/27/1980
From: Murphy M
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18081B266 List:
References
LER-80-013-03L, LER-80-13-3L, NUDOCS 8004010348
Download: ML18081B271 (1)


LER-1980-013, /03L-0:on 800227,during Routine Surveillance,Temp Maintained by Heat Trace Circuit 603 Found to Be 142 F Instead of 145 F.Caused by Pipe Insulation Erosion.Heat Tracing Repaired & Piping Reinsulated
Event date:
Report date:
2721980013R03 - NRC Website

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Nf'C POIHll 315 CJ.771 U. I. NUCLEA" REGULATO"Y COMMISSION LICENSEE EVENT REPORT CONTROL ILOCK: I J (!)

CPUASE PRINT oA rvn ALL RIOUIRED INFO"MATIONI lN IJ uL~!ECUJ'E I 1,j@tp I a 1-I o ~cEL~JJM,!Ro I - lo I o~!@.4 I ~J1;SE1T~JE1 J©l1 c:lT J@

CON"T ror;i*

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IO 11 DOCKET NUMIER 18 19 IVENT OATE l*

lli flEl'ORT CATE ID IVENT DESCRl"10N AND PROBABLE CONSEQUENCES@

((II] !At 1500 during a rgutine suryeillance the temperature maintained Ill!) 1by heat trace circuit 603 was found to be 142°F instead of 145°F.

Action

~

1statement 3.5.4.2 was entered, The circuit was repaired and the action

[)))) 1statement was terminated at 0130 on February 28, 1980.

At 1500 on

([))].!February 28, 1980_, a second circuit, 601, was found inoperable and the UJ]J 7

i cmJ 1

I 1action statement was entered.

Circuit 601 was repaired and the action 1statement was terminated at 2025 on February 28, 1980.

I IYSTEM

CAUSE

CAUSE COMP.

VALVE CODE CODE IUllCODE COMl'ONENT CODE IUllCODE IUBCODE I EfB I@ m.J@ llLJ@ IH IE I AIT IE IR I@ t:_j@) ~@

I ID 11 12 13 18 18 20 t:::'I LE R IRO CVENT YEAR

\\:.!I 11ePORT is 1 o 1 NUMBER 1

22 IEOUENTIAL OCCURRENCE flEl'ORT flEl'ORT NO.

COOE TYl'E I

I 10 11 I 3 I I/I Io 13 I LIJ l=J 23 2*

26 21 28 29 30 31 ACTION FUTURE EFFECT IHUTDOWN Gil ATTACHMENT N'RD-4 PRIME C.OMP.

llEVISION NO.

L.QJ 32 COMl'()fjENT MANUFACTURER eo TAKEN ACTION ON l'L.ANT METHOD HOURS ~ SUBMITTED FORM :.ue.

SUl'PLIER

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UJ@ Jo I 010 I I W@ W@ L!J@

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CAUSE DESCRl"10N AND CORREC"r&VE ACTIONS @

Cl [II)) I A boric acid solution dripped from 'valves onto th~e:......;;;a~f~f~e~c~t~e-d=-~~~~~~.......

IIIIJ piping, and caused the pipe insulation to errode away.

The heat tracing CiID then became shorted.

The heat tracing was repaired and the piping was DJ)) I reinsulated.

At a future outage the valves will be repaired.

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FACILITY

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METHOD OF A

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0 10 12 1:1 DISCOVERY DISCOVERY DESCRll'TION ~

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ACTIVITY CONTENT t:::\\

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7 I

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LOCATION Of fliLEASE NA IO PlllSONNEL IXl'OSURES Q

NUMllEP. ~

TYl'E t.=:i\\ DHCll1"10N ~

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N_A ___________________ __,

1 I

I 11 12 13 PERSONNEL INJURIES

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NUMllE R DESCRll'TIONl!!J rr:TIJ I 010 I Ol@)'--~~~~N_A~~~~~~~~~~~~~~~~~~~~-'

7 I

I 11 12 LOSS OF OR DAMAGE TO FACILITY r.3' TYPE DESCRll'TION

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NA IIIIJ L!J@).i--~~~~~~~~~~~~~~~~~~~~~~~~~~---'

1 I

I 10 ID IO l'UILICITY f::-.

ISSl.JJDc,;'\\ DESCRll'TION ~

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