Similar Documents at Salem |
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LER-1980-008, /03L-0:on 800129,maint Was Performed on Inboard Containment pressure-vacuum Relief Valve lVC6 Using nonsafety-related Procedures & Nonqualified Parts.Caused by Omission on List of safety-related Control Valves |
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| 2721980008R03 - NRC Website |
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v Report Number:
Report Date:
Occurrence Date:
80-08/03L 2/15/80 1/29/80
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Facility:*
Salem Generating Station Public Service Electric & Gas Company Hancocks Bridge, NJ 08038 IDENTIFICATION OF OCCURRENCE:
Non-Safety Related Procedures Applied to Safety Related Equipment CONDITIONS PRIOR TO OCCURRENCE:
Modes 1, 2, 3, 4, 5 and 6 DESCRIPTION OF OCCURRENCE:
During January 1979, maintenance was performed on 1VC6, inboard 10" containment pressure-vacuum relief valve, using non-safety related procedures and non-qualified parts.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
An investigation indicates that 1VC6 was incorrectly classified as a non-safety related control valve on the safety related equipment list (our Reference Project Directive 7).
ANALYSIS OF OCCURRENCE:
Valve 1VC6 was designated as a safety related component during the design and construction phas.e of Salem Unit No. 1.
There is proper documentation that the valve was purchased and installed as safety related equipment.
The engineering disciplines in subsequently compiling the list of control valves, in an apparent oversight, did not classify 1VC6 as a safety related control valve.
During January 1979, maintenance was performed on the valve using non-safety related parts and procedures.
Subseqeunt testing of the valve, after the maintenance, verified that the valve performed its intended function as required.
During the recent refueling outage, the valve was damaged while attempting to block it in the open position during performance of the integrated leak rate test.
The valve was removed and subse-quently sent to the manufacturer.
In examining the valve, the manufacturer identified the extent of damage done during the integrated leak rate test and discovered that the parts used in our maintenance work, presumably during January 1979, were not the same as those originally furnished.
They then notified Publip Service.
An investigation was initiated to determine the cause of the incorrect parts being used.
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- LER 80-08/03L CORRECTIVE ACTION:
Due to the work being done by the manufacturer on the Unit No. 1 valve, the Unit No. 2 valve was put in its place.
The Unit No. 2 valve has had no corrective maintenance performed on it and, there-fore, remains a fully qualified safety related valve.
The original Unit No. 1 valve is being restored to a fully qualified condition by the manufacturer and will be placed in Unit No. 2.
As corrective action for the oversight in incorrectly classifying the valve, the Engineering Department is currently reviewing all safety related control valves to confirm the accuracy of their classification.
If any discrepancies materialize, the station personnel will review maintenance records and take the necessary corrective action to ensure that all components are fully qualified.
The Salem Master Equipment List will be revised to indicate the correct classification of equipment.
FAILURE DATA:
Not Applicable Prepared By P. Moeller Manager 2 Salem Generating Station SORC Meeting No.
12-80
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NRC£._c;>RM_~6 e LICENSEE EVENT REPORT U.S. NUCLEAR REGULATORY COMMISSION (7-i'71
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[)))) I The inboard 10" containment pressure-vacuum relief valve, 1VC6, was repaired in January 1979, maintenance was performed using non-safety related procedures and [QJ1] I non-qualified parts.
During the recent refueling outage, the valve was damaged and sent to the manufacturer for repairs.
During the manufacturer's repairs, he
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identified parts were used that were not the same as those originally furnished.
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CAUSE
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @
42 43 44 47 DJ)) I The valve, 1VC6, due to an apparent oversight was not listed as a safety related control valve.
During January 1979, it was repaired with non-safety related parts and procedures.
The Unit 2 valve was used as a replacement and it has not had o:r::IJ I corrective maintenance, therefore, maintaining its qualification.
Engineering is [III] I reviewing all systems for proper valve classification and any discrepancies will be 1
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| 05000311/LER-1980-001-03, /03L-0:on 800522,when OL Received,Fire Barriers Were Open Due to Recent Removal of Electrical Cables,Pipes & Welding Cables.Cause Not Stated.Barriers Were Verified Sealed Prior to Core Load | /03L-0:on 800522,when OL Received,Fire Barriers Were Open Due to Recent Removal of Electrical Cables,Pipes & Welding Cables.Cause Not Stated.Barriers Were Verified Sealed Prior to Core Load | | | 05000311/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000272/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000272/LER-1980-001-03, /031-0:on 800101,axial Flux Difference Determined to Be Outside Target Band.Caused by Signal Output Failing High.Signal Isolator Was Replaced & Axial Flux Difference Monitor Recalibr | /031-0:on 800101,axial Flux Difference Determined to Be Outside Target Band.Caused by Signal Output Failing High.Signal Isolator Was Replaced & Axial Flux Difference Monitor Recalibr | | | 05000311/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000272/LER-1980-002-03, /03L-0:on 800104,discovered That Functional Tests of Power Range Neutron Flux Low Trip Setpoint When Greater than 25% Power Had Not Been Performed Since 1976.Caused by Lack of Procedures for Tests | /03L-0:on 800104,discovered That Functional Tests of Power Range Neutron Flux Low Trip Setpoint When Greater than 25% Power Had Not Been Performed Since 1976.Caused by Lack of Procedures for Tests | | | 05000311/LER-1980-002-03, /03L-0:on 800526,during Routine Surveillance, Emergency Diesel 2B Could Not Be Fully Loaded.Caused by Three Pins Stuck in Fuel Injectors.Pins Were Unstuck & Diesel Tested Satisfactorily.Insp Order Has Been Initiated | /03L-0:on 800526,during Routine Surveillance, Emergency Diesel 2B Could Not Be Fully Loaded.Caused by Three Pins Stuck in Fuel Injectors.Pins Were Unstuck & Diesel Tested Satisfactorily.Insp Order Has Been Initiated | | | 05000272/LER-1980-002, Forwards LER 80-002/03L-0.Previous Transmittal Included Incorrect LER Attachments | Forwards LER 80-002/03L-0.Previous Transmittal Included Incorrect LER Attachments | | | 05000272/LER-1980-003-03, /03L-0:on 800203,air Particulate Detector Pump Seized,Rendering Detector Inoperable.Caused by Normal Degradation of Pump.Pump Replaced | /03L-0:on 800203,air Particulate Detector Pump Seized,Rendering Detector Inoperable.Caused by Normal Degradation of Pump.Pump Replaced | | | 05000272/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000311/LER-1980-003, Has Been Cancelled | Has Been Cancelled | | | 05000272/LER-1980-004, Forwards LER 80-004/03X-1.Detailed Event Analysis Encl | Forwards LER 80-004/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000311/LER-1980-004-03, /03L-0:on 800610,during Routine Surveillance,Both Safety Injection Pumps Were Made Operable at Less than 312 F in Rcs.Caused by Lack of Procedure to Limit Max Number of Operable Safety Pumps | /03L-0:on 800610,during Routine Surveillance,Both Safety Injection Pumps Were Made Operable at Less than 312 F in Rcs.Caused by Lack of Procedure to Limit Max Number of Operable Safety Pumps | | | 05000272/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000311/LER-1980-005-03, /03L-0:on 800622,during Preparation for Heatup, Position Indication & Mechanical Operation of Pressurizer Overpressure Protection Valves Gave False Indication & Failed to Reseat.Possibly Caused by Foreign Matl in Valve | /03L-0:on 800622,during Preparation for Heatup, Position Indication & Mechanical Operation of Pressurizer Overpressure Protection Valves Gave False Indication & Failed to Reseat.Possibly Caused by Foreign Matl in Valve | | | 05000272/LER-1980-005-03, /03L-0:on 800117,containment Pressure Allowed to Increase Above Limit.Design Change 1EC-0474,not Incorporated,Would Have Raised Alarm Setpoints on Containment Particulated Monitors.Setpoints Readjusted | /03L-0:on 800117,containment Pressure Allowed to Increase Above Limit.Design Change 1EC-0474,not Incorporated,Would Have Raised Alarm Setpoints on Containment Particulated Monitors.Setpoints Readjusted | | | 05000311/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000311/LER-1980-006-03, /03L-0:on 800625,residual Heat Removal Pump Was Discovered to Have Been Previously Improperly Assembled. 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Inverter Does Not Have Automatic Transfer Switch as Originally Designed | | | 05000311/LER-1980-007-03, /03L-0:on 800709,during Normal Operations,Motor Bearing Thermocouple for 21 Containment Fan Coil Unit Indicated High.Caused by Normal Wear on Bearing.Bearing Replaced in Kind & Fan Coil Unit Tested Satisfactorily | /03L-0:on 800709,during Normal Operations,Motor Bearing Thermocouple for 21 Containment Fan Coil Unit Indicated High.Caused by Normal Wear on Bearing.Bearing Replaced in Kind & Fan Coil Unit Tested Satisfactorily | | | 05000311/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000272/LER-1980-007, Forwards LER 80-007/03X-2.Detailed Event Analysis Encl | Forwards LER 80-007/03X-2.Detailed Event Analysis Encl | | | 05000272/LER-1980-007-03, /03X-1:on 800128,design Deficiency Found in Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7.Caused by Failure to Include Valve in Piping Spec Break.Valve Seismically Qualified | /03X-1:on 800128,design Deficiency Found in Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7.Caused by Failure to Include Valve in Piping Spec Break.Valve Seismically Qualified | | | 05000311/LER-1980-008-03, /03L-0:on 800710,during Routine Containment Entries,Entry Into Action Statement 3.6.1.3 Resulted from Excessive Leak Rate.Caused by Gaskets Being Moved from Seating Surface Due to Improper Operation.Gaskets Reseated | /03L-0:on 800710,during Routine Containment Entries,Entry Into Action Statement 3.6.1.3 Resulted from Excessive Leak Rate.Caused by Gaskets Being Moved from Seating Surface Due to Improper Operation.Gaskets Reseated | | | 05000272/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000272/LER-1980-008-03, /03L-0:on 800129,maint Was Performed on Inboard Containment pressure-vacuum Relief Valve lVC6 Using nonsafety-related Procedures & Nonqualified Parts.Caused by Omission on List of safety-related Control Valves | /03L-0:on 800129,maint Was Performed on Inboard Containment pressure-vacuum Relief Valve lVC6 Using nonsafety-related Procedures & Nonqualified Parts.Caused by Omission on List of safety-related Control Valves | | | 05000311/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000311/LER-1980-009-03, /03L-0:on 800709,during RCS Heatup,Steam Generator Flow & Pressure Channel Response Inadequate.Bistables Placed in Tripped Mode.Caused by Closed Isolation Valve from Main Steam Piping Preventing Normal Operation.Valve Opened | /03L-0:on 800709,during RCS Heatup,Steam Generator Flow & Pressure Channel Response Inadequate.Bistables Placed in Tripped Mode.Caused by Closed Isolation Valve from Main Steam Piping Preventing Normal Operation.Valve Opened | | | 05000272/LER-1980-009, Forwards Updated LER 80-009/03X-2 | Forwards Updated LER 80-009/03X-2 | | | 05000311/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000272/LER-1980-009-03, Small Leak Found in Telltale Drain 6 in Spent Fuel Pit.Caused by Leaking Welded seams.Half-round Channels Welded Over Leaking Welds | Small Leak Found in Telltale Drain 6 in Spent Fuel Pit.Caused by Leaking Welded seams.Half-round Channels Welded Over Leaking Welds | | | 05000272/LER-1980-010-03, /03L-0:on 800206,while Reviewing Procedure,Found That,During Load Test on Manipulator Crane Prior to Fuel Movement on 790425,test of 3,220 Lbs Performed Instead of 3,250 Lbs Per Tech Spec.Procedure Will Be Revised | /03L-0:on 800206,while Reviewing Procedure,Found That,During Load Test on Manipulator Crane Prior to Fuel Movement on 790425,test of 3,220 Lbs Performed Instead of 3,250 Lbs Per Tech Spec.Procedure Will Be Revised | | | 05000272/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000311/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000311/LER-1980-010-03, /03L-0:on 800709,during RCS Heatup at 1,700 Psig, Channels I & II for Pressure Indication Failed to Respond. 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