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LER-1977-046, /03L-0:on 770626,during Mode 2 Operation,Station Power Transformer Became Inoperable Due to Protective Relay Operation.Caused by Personnel Error in Not Tagging Breaker Failure |
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| 2721977046R03 - NRC Website |
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LICENSEE EVENT REPORT a 77-46/03L 7/12/77 CONTROL BLOCK 6
LICENSEE LICENSE EVENT NAME LICE:NSE NUMBER TY~E TYPE
@KIJNIJ!S!G!Sl~l jplol-IOIOIOIOIOl-IOlgJ 14111 ll ll lJo ~
REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT DATE lol1l CON'T LJ__j llJ LLJ I 0 I 5 I 0 I - I 0 I 2 I 7 I 2 I l 0 I 6 I 2 16 I 7 I 7 I I 0 I 7 I 1 I 2 l 7 I 7 I
~
57 58 59 60 61 68 69 74 7560
EVENT DESCRIPTION
@TIJIDuri.ng Mode 2 operation, the No. 2 Station Power Transformer l'ecame. fooner--l eo 7
8 9
@))jable due to protective *relay operation.
7 8 9 Both offsite transmission lines d
~land the No. 1 SPT was operable throughout this eve.nt.
The electrical li~eub t7J-7 8 9 [Qli]!was restored to normal arnl action statement 3.8.1.1 was t en1ii rl 2 t ed.
Th~_§__]
w 1
a s
~lis the first event of this type.
(77-lo.6/03L) 7 B 9 SYSTEM CODE
@J?J1E IA I 7
8 9 10 CAU5£ CODE lAJ 11 CAUSE DESCRIPTION COMPONENT CODE IT IR IJ~ INJS-1EJ 12 17 PRIME COMPONENT SUPPLICR lLJ 43 COMPONENT MANUFACTURER IW I 1 I? Io I 44 47 VIOLATIOI*~
LNJ 48 loTal l 9Personnel error in not tagging. the Breakc::r Failure~ and Crouris Protec,_L!._QJJ_]
d
~
~I circuit out of service durj_1;.g breaker___t..c...~.. ti.JJ.Y.,....... r.EUJ.. c;""r1 1*b:i s r~,r..c.DJ.*~ *~-----~
- 7.
8 9
£0
~
~
7 09
~
[ill]
f9AC"11 l"!"V STATUS LEJ.
% POWE.R I o Io In I 0TH"::_'8STATUS I Rx: 10 amps 7
0 9
FORM OF 10
- 12.
13 ACTIVITY CONTENT RE.LEASED OF F.ELEA5E G:liJ
!_0_j
~
.<\\MOUNT OF ACTIVITY N/A 7
8 9
10 11 PERSONNEL EXPOSURES 01scovE.r-1v ~i::-5.:,r;,1ri-r10N IBreab:'.r Testir.;; i11 Progress I
~46~
.. :...........--'---~--'--'--'-....C.....--"--'-LL----.....,,a5 LOCATION OF '<ELE;*<,(
N T / __ A _______ j 6-0 NUMbEP.
TYPE
DESCRIPTION
~IO IO IO I l.ZJ
~N:..:..../...:..:."l';.:;___ _________________ -,J 7
8 9 11 12 13 bO PERSONNEL INJURIES NUMOER
DESCRIPTION
~1010101 N-A 7
8 9 11 12 OFFSITE CONSEQUENCES VislL..---------------!N:.!L..~A=-------------------------d LOSS OR DAMAGE TO FACILITY r.T:1 TYPE
DESCRIPTION
~IZI I N/A 1
a'"g'-'
~,o~---------:..:.L.~:..........-------------------------......_..,;
PUBLICITY Gli]L.-_________ ~l,Lti..........--------------------:::
7 8 9 80 ADDITIONAL FACTCRS
~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~
7 8 9 00 NAME:
T. L. Soencer
.. ~ ___ _
PHONE: (609)365-7000 Ext. Salem 528
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| 05000000/LER-1977-020-03, /03L:on 770404,RCS Leakage Determined to Be Greater than 10 Gpm.Caused by Packing Leakage Past Stems on RTD Bypass Throttle Valves 13RC20 & 14RC20.Valves Placed on Backseat & Stem Leakage Decreased | /03L:on 770404,RCS Leakage Determined to Be Greater than 10 Gpm.Caused by Packing Leakage Past Stems on RTD Bypass Throttle Valves 13RC20 & 14RC20.Valves Placed on Backseat & Stem Leakage Decreased | | | 05000272/LER-1977-032-03, /03L-0:on 770418,during Mode 1 Operation, Protective Relay Operation Caused Loss of 5024 500-kV Transmission Line.Caused by Smoke from Forest Fire 36-37 Miles from Facility | /03L-0:on 770418,during Mode 1 Operation, Protective Relay Operation Caused Loss of 5024 500-kV Transmission Line.Caused by Smoke from Forest Fire 36-37 Miles from Facility | | | 05000272/LER-1977-032, Forwards LER 77-032/03L-0 | Forwards LER 77-032/03L-0 | | | 05000272/LER-1977-037-03, /03L:on 790514,during Mode 1 operation,5023 500-kV Transmission Line Tripped.Caused by Forest Fire Between Towers 36/1 & 36/3 | /03L:on 790514,during Mode 1 operation,5023 500-kV Transmission Line Tripped.Caused by Forest Fire Between Towers 36/1 & 36/3 | | | 05000272/LER-1977-037, Forwards LER 77-037/03L-0 | Forwards LER 77-037/03L-0 | | | 05000000/LER-1977-038-03, /03L:on 770519,RCS Leakage Determined to Be Greater than 10 Gpm from Stem Leakoff on Manual Isolation Valves 1PS24 & 1PS28 for Pressurizer Spray Valves.Caused by Packing Leakage.Valves Will Be Repacked at Next Outage | /03L:on 770519,RCS Leakage Determined to Be Greater than 10 Gpm from Stem Leakoff on Manual Isolation Valves 1PS24 & 1PS28 for Pressurizer Spray Valves.Caused by Packing Leakage.Valves Will Be Repacked at Next Outage | | | 05000272/LER-1977-045, Forwards LER 77-045/03L-0 | Forwards LER 77-045/03L-0 | | | 05000272/LER-1977-045-03, /03L-0:on 770626,during 100% Generator Trip Test, 5024 500-kV Transmission Line Became Inoperable.Caused by Bus Sections 1-5 & 5-6 Breaker Flashover Nhc Iia Relay Remaining Energized.Relay Removed from Svc | /03L-0:on 770626,during 100% Generator Trip Test, 5024 500-kV Transmission Line Became Inoperable.Caused by Bus Sections 1-5 & 5-6 Breaker Flashover Nhc Iia Relay Remaining Energized.Relay Removed from Svc | | | 05000272/LER-1977-046-03, /03L-0:on 770626,during Mode 2 Operation,Station Power Transformer Became Inoperable Due to Protective Relay Operation.Caused by Personnel Error in Not Tagging Breaker Failure | /03L-0:on 770626,during Mode 2 Operation,Station Power Transformer Became Inoperable Due to Protective Relay Operation.Caused by Personnel Error in Not Tagging Breaker Failure | | | 05000272/LER-1977-046, Forwards LER 77-046/03L-0 | Forwards LER 77-046/03L-0 | |
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