Similar Documents at Salem |
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LER-1979-031, /03L-0 on 790329:100 Elevation Containment Personnel Air Lock Failed to Pass Leak Rate Test.Caused by Split Inner Door Seal Snagged by Some Object Passing Through Door.Seal Replaced |
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| 2721979031R03 - NRC Website |
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text
Report Date:
Report Date:
Occurrence Date:
79-31/03L 4/27/79 3/29/79 Facility:
Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Containment Personnel Air Lock Elevation 100 Inoperable CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 1 Reactor Power 100%
DESCRIPTION OF OCCURRENCE:
At 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, the containment personnel air lock elevation 100 failed to pass a leak rate test.
Technical Specification 3.6.1.3.b Action Statement was implemented.
Maintenance Department personnel repaired the inner door and surveillance 4.6.1.3 was performed to verify opera-bility.
The Action Statement was terminated at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The caus~ of this occurrence was a split inner door inner seal which appeared to have been snagged by some object passing through the door.
There was no other damage to the door sealing surface or operating mechanism.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.6.1.3 requires that with an air lock inoper-able, restore the air lock to operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or be in at least hot standby within the next six hours and in cold shutdown within th~ following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
The air lock was repaired and returned to service within 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> and 30 minutes.
CORRECTIVE ACTION
The air lock inner door inner seal was replaced and the door was adjusted for a proper seal.
A satisfactory leak rate test was per-formed before returning the air lock to service.
FAILURE DATA:
Containment Personnel Air Lock Chicago Bridge & Iron Company Prepared by A. W. Kapple SORC Meeting No.
29-79 7905040~<-\\-\\
NRC~FORM 356 (7-77). '
LICENSEE EVENT REPORT e NUCLEAR REGULATURY COMMISSION CONTROL BLOCK: !--....._.....__....._ ____.___,J 0 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI 0
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- 5 1..ICENSE NUMBER 25 26 i..ICENSE TYPE JO 57 CA7 58 CON'T [IT1J 7
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74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
I During normal operation, at 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, the 100 elevation containment personnel air lock failed to pass a leak rate test.
The air lock was declared inoperable and the Action Statement for T/S 3.6.1.3 was implemented.
The inner door was repaired and surveillance 4.6.1.3 was performed to verify operability.
The air lock was returned to service at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> and the Action Statement was terminated.
This is
~ the fourth occurrence of this type.
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47 r1:l]J j The cause of this occurrence was a split inner door inner seal which appeared to havej D:IIJ been snagged by some object passing through the door.
No other damage to the door o::::IIJ I sealing surface or operating mechanism was detected.
The seal was replaced and the [JJ]J I door adjusted for a proper seal.
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| 05000272/LER-1979-001-03, /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | | | 05000272/LER-1979-001, Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | | | 05000272/LER-1979-002-03, /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | | | 05000272/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000272/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000272/LER-1979-003-03, /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | | | 05000272/LER-1979-004, Forwards Updated LER 79-004/03X-1 | Forwards Updated LER 79-004/03X-1 | | | 05000272/LER-1979-004-03, /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | | | 05000272/LER-1979-005-03, /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | | | 05000272/LER-1979-005, Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | | | 05000272/LER-1979-006-03, /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | | | 05000272/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000272/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000272/LER-1979-007-03, /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | | | 05000272/LER-1979-008-03, /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | | | 05000272/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000272/LER-1979-009-03, /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | | | 05000272/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000272/LER-1979-011, Forwards LER 79-011/01X-2 | Forwards LER 79-011/01X-2 | | | 05000272/LER-1979-011-01, /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | | | 05000272/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000272/LER-1979-012-03, /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | | | 05000272/LER-1979-013-04, /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | | | 05000272/LER-1979-013, Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerat | Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerations | | | 05000272/LER-1979-014-03, /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | | | 05000272/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000272/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000272/LER-1979-015-03, /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | | | 05000272/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000272/LER-1979-016-03, /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | | | 05000272/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000272/LER-1979-017-03, /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | | | 05000272/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000272/LER-1979-018-03, /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | | | 05000272/LER-1979-020-03, /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | | | 05000272/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000272/LER-1979-021-03, /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | | | 05000272/LER-1979-022-03, /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | | | 05000272/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000272/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000272/LER-1979-024-03, /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | | | 05000272/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000272/LER-1979-025-03, /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | | | 05000272/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000272/LER-1979-026-03, /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | | | 05000272/LER-1979-027-01, /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | | | 05000272/LER-1979-027, Forwards LER 79-027/01X-1 | Forwards LER 79-027/01X-1 | | | 05000272/LER-1979-028, Has Been Voided | Has Been Voided | | | 05000272/LER-1979-029-03, /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | | | 05000272/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | |
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