Similar Documents at Salem |
|---|
|
LER-1979-016, /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2721979016R03 - NRC Website |
|
text
,,*
Report Number:
Report Date:
Occurrence Date:
Facility:
79-16/03L 3-5-79 2/20/79 Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
No. 14 Containment Fan Coil Unit Inoperable CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 1 Reactor Power 100%
DESCRIPTION OF OCCURRENCE:
At 1842 hours0.0213 days <br />0.512 hours <br />0.00305 weeks <br />7.00881e-4 months <br />, No. 14 containment fan coil unit was started in slow speed and secured three minutes later due to no indication of service water flow.
Performance personnel were notified and tests performed showed no service water flow in either fast or slow speed.
The fan coil unit was declared inoperable and the Action Statement for Technical Specification 3.6.2.3 was implemented.
Rework of the service water flow control valve and retests to verify service water flow were completed at 0020, 2-21-79, and the Action Statement was terminated.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of this occurrence was a burned out coil in solenoid valve SV-630 which supplies either closing air or flow control air to 14 SW223, the service water flow control valve for No. 14 C.F.C.U.
SV630 was found inoperable in a position which kept 14 SW223 shut.
The coil is believed to have burned out during the slow speed start at 1842 hours0.0213 days <br />0.512 hours <br />0.00305 weeks <br />7.00881e-4 months <br />.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.6.2.3 Action Statement requires that with one group of containment cooling fans inoperable, restore the inoperable fan group to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
No. 14 C.F.C.U. was returned to service within six hours.
No. 11, 12, 13 and 15 C.F.C. units were available throughout this occurrence.
CORRECTIVE ACTION
The burned out coil on SV-630 was replaced and Surveillance Procedure SP(O) 4.6.2.3.A was performed to verify operability of the fan coil unit and service water flow indication.
LER 79-16/03L FAILURE.DATA:
Solenoid Valve SV-630 ASCO Solenoid Valve Company Prepared by A. W. Kapple Manager 2 Salem Generating Station SORC Meeting No.
13-79
1(7-77)
LICENSEE EVENT REPORT
. ~C~NTROL BLOCK: !---'-_...... _._!_._I._.__-!I(!)
(PLEASE PRINT OR TYP. REQUIRED INFORMATION) 6
!IE] I N IJ I s I G I s I 1 IG)I o I o I -1 o Io I o I o I o I - I o I o !(DI 4 I 1 I 1 I i I i 101 I I© 7
8 9
LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T la I 1 I 7
8
- ~:~~~ LIJ© I o I s I o I o I o I 2 ! 7 I 2 IG)I o I 2 I 2 I o I 1 I 9 I© I o I 3 Io I s I 2 I 9 I G) 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES@)
[§))] I During normal operation, after starting No. 14 Contairunent Fan Coil Unit, the [2:1))
Control Operator observed zero service water flow through the unit.
The unit was
~
secured and T/S 3.6.2.3 Action Statement was implemented.
Performance Department
[£))]
reworked a solenoid control valve and the unit was returned to service.
SP(O) iifil 4.6.2.3a was performed and-verified No. 14 Containnent Fan Coil Unit operabj.lity.
[§]2J No. 11, 12,* 13 and 15 CFC units were operable throughout this occurrence.
This is
[)))) I the third occurrence of this type (78-85, 79-01).
7 8 9 [9Jil 7
8 SYSTEM CODE Is I cl@
9 10
!':'::\\
LER'RO LVENTYEAA v..:J REPORT I 7 I 9 I NUMBER 21 22
CAUSE
CAUSE COCE SUBCCCE COMPONENT COCE Llj@ ~@IV !AIL [VIO !Pl@
11 12 13 18 SEQUENTIAL OCCURRENCE REPORT NO.
CODE I I Io I l I 6 I I_......,
I o I 3 I
~
~
~
v
~
~
COMP.
SUBCOOE
~@
19 REPORT TYPE
~
30 VALVE SUBCODE
~@
20 1=1*
31 REVISION NC. w 32 80 ACTION FUTURE TAKEN ACTION ON PLANT METI-IOD HOURS SUBMITTED FORM l>UB.
EFFECT SHUTDOWN
~
ATTACHMENT NPAD-4 PRIME COMP.
SUPPLIER COMPONENT MANUFACTURER W@W@ UJ@
L!J@
I 0_10 I 01 I 1.!J@
L!.J@
33 34 35 36 37 40 41 42
~ I A 14 I 9 j 9 I@*
CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @
43 44 47 I The cause was a burned out coil in solenoid valve 630 which supplies control air for o:::IlJ 14SW223, the service water flow control valve for No. 14 C.F.C.U.
The burned out o::IIJ coil was replaced and the C.F.C.U. was tested satisfactorily.
o:m 1
a 9 FACILITY
~30 STATUS
% POWER OTI-IER STATUS \\.:::;:!
[Im L.~J@ 11 I 0 I 0 l@l.__. _ _..N""""/..-A.._ __
7 8
9 10 12 1'3 ACTIVITY CONTENT
~
RELEASED OF RELEASE AMOUNT OF ACTIVITY ITTIJ L!.I@ W@)I N/A 7
8 9
10 11 80 METI-100 OF DISCOVERY DESCRIPTION @
DISCOVERY
~@I 0Eerator Observation 44 45 46 80 LOCATION OF REL.EASE@
NiA 44 45 80 PERSONNEL EXPOSURES
~
NUMBER
~TYPE OESCRIPTION er ITI2J I a I a I o lW@~ __
N..... /_A ____________________
7 8
9 11 12.
13 PERSONNEL INJURIES C-\\
ao NUMBER OESCRIPTION~
[QI] I ol o I ol@).__ _____...,.,N_.__A..__ _____________________________ ~
8 9
11 12 LOSS OF OR DAMAGE TO FACILITY~
TYPE OESCRIPTION
':::::J BO Eli] W@
NA a 9
,*o----~--------------...... ------~-------------------------------------------------------9~0 PUBLICITY
(.';;\\
E ISSUEOC,;\\ DESCRIPTION~
NRC US ON Ly o::IIJ Lz.lei....._ __
..;.N......,A,__ ___________
II II II I II I I I I 8
9 10 68 69 eo NAMEOFPREPARER~~--~-A_.~w~*~K_a~p~p=--l_e __ ~~~
PHONE: (609)365-7000 Salem Ext.
628
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000272/LER-1979-001-03, /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | /03L-0 on 790102:during Normal Operation,The No 12 Containment Fan Coil Unit Shifted to Slow Speed,But No Indication of Svc Water Flow Was Noted.Caused by Burned Out Coil in Solenoid SV-624,supplying Control Air for 12SW223 | | | 05000272/LER-1979-001, Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | Supplemental LER 79-001/03X-1:on 790102,during Normal Operations,Containment Fan Coil 12 Shifted to Slow Speed. Operator Noticed No Indication of Svc Waterflow.Caused by Burned Out Coil in Solenoid Valve SV-624.Coil Replaced | | | 05000272/LER-1979-002-03, /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | /03L-0 on 790103:excessive Leak Rate in W1 100 Air Lock Noted.Doors Were Reworked & Airlock Returned to Operation.Seals Failed Due to Split at Vulcanized Seam. Door Seals Were Replaced | | | 05000272/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000272/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000272/LER-1979-003-03, /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | /03L-0 on 790103:containment Pressure Exceeded Tech Spec Max.Caused by Isolation of Pressure/Vacuum Relief System for Rework of 1CV6 | | | 05000272/LER-1979-004, Forwards Updated LER 79-004/03X-1 | Forwards Updated LER 79-004/03X-1 | | | 05000272/LER-1979-004-03, /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | /03L-0 on 790103:Loop 4 Channel IV Was 100 Psi Too High.Caused by Steam Pressure Transmitter Being Frozen by an Outside Air Damper Directing Cold Air Onto the Sensing Lines | | | 05000272/LER-1979-005-03, /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | /03L-0 on 790104:during Normal Operations,Position Indication for Rod 2D5 Began Oscillating.Rod Position within 12 Steps of Bank D.Caused Traced to Rod Indication Coil Stack on Reactor.Repairs Planned for Next Reactor Outage | | | 05000272/LER-1979-005, Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | Supplemental LER 79-05L/03X-1:on 790104,during Normal Operation,Individual Rod Position Indication for Rod 2D5 Began Oscillating.Cause Could Not Be Identified.Connectors Checked & RPI Coil Stack Replaced | | | 05000272/LER-1979-006-03, /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | /03L-0 on 790102:inservice Insp Data Packages Not Being Reviewed.Cause Was Lack of Administrative Control to Correlate Responsibilities of Two Station Depts.Dept Review Procedures Have Been Rewritten | | | 05000272/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000272/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000272/LER-1979-007-03, /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | /03L-0 on 790126:while Performing Channel Check of Pressurizer Level,Channel II Found 5% Lower than Others. Caused by Instrument Drift Resulting in Zero Shift in Transmitter Output | | | 05000272/LER-1979-008-03, /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | /03L-0 on 790111:during Normal Operation While Refilling Boric Acid Storage Tanks,Operator Added Improper Batch of Acid to Tanks & Pumped Concentrates Tank to Storage Tanks.Caused by Personnel Error | | | 05000272/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000272/LER-1979-009-03, /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | /03L-0 on 790112:No 13 Auxiliary Bldg Exhaust Fan Removed from Svc to Replace Motor.Caused by Worn Keyway in Drive Motor Shaft | | | 05000272/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000272/LER-1979-011, Forwards LER 79-011/01X-2 | Forwards LER 79-011/01X-2 | | | 05000272/LER-1979-011-01, /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | /01X-2 on 790116:RMS Channel Which Had Alarmed & Cleared Had Been Reset at Control Console But Not at RMS Panel.Caused by Procedure Inadequacy.Procedure Changed Initiated to Clarify Functions | | | 05000272/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000272/LER-1979-012-03, /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | /03L-0 on 790115:No 11 Steam Generator Steam Flow Channel II Failed Low.No Cause Found.Operator Took Manual Control & re-established Steam Generator Level.Channel Indication Normalized within 10 Minutes | | | 05000272/LER-1979-013-04, /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | /04L on 790102:non-radioactive Waste Effluent Total Suspended Solids Exceeded Tech Specs.Caused by Abnormally High Number of Demineralized Regenerations Supporting Initial Flushes for Startup Preparation | | | 05000272/LER-1979-013, Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerat | Supplemental LER 79-013/04X-1:on 790102,during Preparation of Annual Nonradioactive Environ Operating Rept,Average 1978 Suspended Solids Concentrate in Discharge Exceeded Limit. Caused by Abnormally High Demineralizer Regenerations | | | 05000272/LER-1979-014-03, /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | /03L-0 on 790220:during Normal Operation,Radiation Monitoring Sys Channel 1R 12B Alarms Found Not Operating. Channel Later Returned to Svc & Operated Properly.Caused by Unknown Factor | | | 05000272/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000272/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000272/LER-1979-015-03, /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | /03L-0 on 790212:during Normal Operation,Noted Required Surveillance to Be Performed Every 78-h Had Not Been Done on 790210 When Scheduled.Caused by Personnel Error.Entry Made in Log Instructing Supervisor | | | 05000272/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000272/LER-1979-016-03, /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | /03L-0 on 790220:control Operator Observed Zero Svc Water Flow Through Unit.Caused by Burned Out Coil in Solenoid Valve.Coil Replaced | | | 05000272/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000272/LER-1979-017-03, /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | /03L-0 on 790219:gross Activity Surveillance of Coolant Sys & Steam Generators Was Not Performed.Caused by Personnel Error in Not Returning Gas Bottles to Storage.New Bottle Storage Pad Will Be Built | | | 05000272/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000272/LER-1979-018-03, /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | /03L-0 on 790223:auxiliary Feedwater Pump Breaker Cubicle Was Hot.Caused by Burned Out Closing Spring Charging Motor.Motor & Breaker Replaced | | | 05000272/LER-1979-020-03, /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | /03L-0 on 790225:pressurizer Level Channel II Was Declared Inoperable.Caused by non-linearity of Strain Gauge in Level Sensor Transmitter.Strain Gauge Replaced Along W/ Zero & Span Potentiometers.Transmitter Recalibrated | | | 05000272/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000272/LER-1979-021-03, /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | /03L-0 on 790302:overhead Annuciators in Control Room Alarmed,Indicating Power Range Nuclear Instrumentation Channel Failure.Caused by Failure of N41 Channel High Voltage Power Supply.Failed Power Supply Replaced | | | 05000272/LER-1979-022-03, /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | /03L-0 on 790221:during Normal Operations,While Conducting Routine Insp,Nrc Inspector Found Missed Tech Spec Surveillance Reading.Caused by Personnel Error.Surveillance Posted on Plant Status Board | | | 05000272/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000272/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000272/LER-1979-024-03, /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | /03L-0 on 790313:air Particulate Monitor Was Declared Inoperable.Caused by Failing Motor Bearings Which Led Filter Paper Drive to Slow & Activate Failed Filter Alarm.Motor Was Cleaned & Bearing Replaced | | | 05000272/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000272/LER-1979-025-03, /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | /03L-0 on 790315:during Normal Operation on 790302,retest Not Performed After 790302 Maint on Chilled Water Pump 11.Caused by Personnel Error.Procedure Reviewed & Rewritten | | | 05000272/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000272/LER-1979-026-03, /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | /03L-0 on 790318:No 13 Reactor Coolant Loop Protection Channel III Inoperable.Caused by Faulty Channel Summator Module.Summator Was Replaced | | | 05000272/LER-1979-027-01, /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | /01X-1 on 790325:while Providing Backup Protection to Hope Creek,Facility Fresh Water Tanks Were Below Tech Spec Required Levels.Caused by Poor Communications Between Facilities.Water Level Restored | | | 05000272/LER-1979-027, Forwards LER 79-027/01X-1 | Forwards LER 79-027/01X-1 | | | 05000272/LER-1979-028, Has Been Voided | Has Been Voided | | | 05000272/LER-1979-029-03, /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | /03L-0 on 790320:during Channel Functional Test High Voltage Was Found to Be Low.Caused by Breakdown of Diode in High Voltage Power Supply.Diode Was Replaced & Channel Functional Was Completed | | | 05000272/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | |
|