ML18059A557

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Forwards Monthly Operating Rept for Nov 1993 for Palisades Nuclear Plant & Revised Monthly Operating Rept for Oct 1993 for Palisades Nuclear Plant
ML18059A557
Person / Time
Site: Palisades Entergy icon.png
Issue date: 12/03/1993
From: Kluskowski P
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML18059A558 List:
References
NUDOCS 9312100166
Download: ML18059A557 (5)


Text

consumers Power.

POWERING lllllCHlliAN"S PROGRESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Covert, Ml-49043 December 3, 1993 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LICENSEE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO 50-255 Enclosed is a copy of the Monthly Operating Data and Summary of Operating Experience for the Palisades Nuclear Plant for the month of November, 1993.

If you have any questions or concerns, please feel free to contact me at

{616) 764-8913, extension 0113.

Sincerely, PJ Kl uskowski Reactor Engineer CC: DPHoffman, P26-117B JMartin, USNRC JLKuemin, Palisades Resident Inspector, Palisades DRHahn, Div of Rad Health Services, Lansing, MI BWJorgensen, Michigan Dept of Labor, Lansing, MI JPadgett, Michigan Public Service Commission Records Center, INPO, Atlanta, GA RWTaylor, CE, Palisades MPKnopp, Palisades SMMcintyre, Pl3-121 Region III Administrator, USNRC Document Control, 950*22*35*10/L Cycle 11 Reports

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OPERATING DATA REPORT DOCKET NO 50-255 DATE 11-30-93 COMPLETED BY MMVanWagner TELEPHONE (616)764-8913 OPERATING STATUS:

NOTES:

1. UNIT NAME Palisades
2. REPORTING PERIOD: 931101-931130
3. LICENSED THERMAL POWER (MWt) 2530.0
4. NAMEPLATE RATING (GROSS MWe) 811. 7
5. DESIGN ELECTRICAL RATING (NET MWe) 805.0
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe) **770
7. MAXIMUM DEPENDABLE CAPACITY (NET MWe) **730
8. IF CHANGES OCCUR IN CAPCITY RATINGS (ITEM NUMBERS 3 AND 7) SINCE LAST REPORT GIVE REASONS:
9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe):
10. REASONS FOR RESTRICTIONS, IF ANY:

This Month Yr-to-Date Cumulative

11. HOURS IN REPORTING PERIOD 720.0 8016.0 192423.0
12. NUMBER OF HOURS REACTOR WAS CRITICAL 660.8 3963.4. 107696.0
13. REACTOR RESERVE SHUTDOWN HOURS
14. HOURS GENERATOR ON-LINE 558.0 3851.0 103057.6
15. UNIT RESERVE SHUTDOWN HOURS
16. GROSS THERMAL ENERGY GENERATED (MWH) 1242336.0 9490239.0 221786211. 0
17. GROSS ELECTRICAL ENERGY. GENERATED (MWH) 409540.0 3108940.0 69999123.0
18. NET ELECTRICAL ENERGY GENERATED (MWH) 386643.0 2955916.0 65992996.0
19. UNIT SERVICE FACTOR 77.5% 48.0% 53.6%
20. UNIT AVAILABILITY FACTOR 77.5% 48.0%. 53.6%
21. UNIT CAPACITY FACTOR (USING MDC NET) 73.6% 50.5% 51.1%*
22. UNIT CAPACITY FACTOR (USING DER NET) - 66.7% 45.8% 42.6%
23. UNIT FORCED OUTAGE RATE 0.0% 9.9% 29.8%
24. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):
25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: November 6, 1993
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

    • Based on condenser backpressure
  • Weighted Average (635 MWe used as MDC Net prior to October 1985)

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO 50-255 UNIT Palisades DATE 12/03/93 COMPLETED BY MMVanWaqner MONTH NOVEMBER 1993 TELEPHONE (616)764-8913 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe Net)

1. 0 17. 19129
2. 0 18. 19146
3. 0 19. 19091
4. 0 20. 19210
5. 0 21. 19111 .
6. 836 22. 19123
7. 0 23. 19130
8. 1483 24. 19159
9. 6657 25. 19162
10. 7737 26. 18964
11. 13864 27. 19348
12. 14716 28. 19138
13. 15860 29. 19227
14. 19152 30. 19106
15. 19095
16. 19187 INSTRUCTIONS:

On this format, list the average daily unit power level in MWe-NET for .each day in the reporting month. Compute to the nearest whole megawatt.

DOCKET NO 50-255 UNIT Pa 1i sades DATE 12/02/93*

COMPLETED BY MMVanWagner **

REPORT MONTH NOVEMBER 1993 TELEPHONE (616)764-8913 UNIT SHUTDOWNS AND POWER REDUCTIONS No. Date Type 1 Duration Reason 2 Method of Licensee System Component Cause & Corrective 4 6 (Hours) Shutting Event Code Code Action to 3

Down Reactor Report # Prevent Recurrence 02 930604 s 176.4 c

l. 2. 3. 4. 5.

F: Forced Reason: Method: Exhibit G - Instructions Exhibit I - Same Source S: Scheduled A-Equipment Failure (Explain)  !'"Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriciion 4-0ther (Explain) (NUREG-0161)

[-Operator Training & License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain)

SUMMARY

OF OPERATING EXPERIENCE FOR OCTOBER 1993 Initial criticality for Cycle 11 was attained on November 3, 1993 at 1109.

The plant went off-line at 0731 to repair an EHC leak on November 5, 1993.

Return to power took p1ace at 0944 on November 6, 1993. On November 6 the turbine was taken off-line at 2105 to perform overspeed trip testing. The test failed, repairs were made, and the turbine was returned to service November 8 at 0534. At 1419, the turbine was taken off- 1ine, the overs peed test was reperformed satisfactorily and the turbine was back on-line at 1705.

The outage officially ended at this time. Full power was reached by approxi-mately 2030 on November 13, 1993 and continued for the remainder of the month.

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