ML18053A357

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Insp Rept 50-255/88-08 on 880303-0404.Violations Noted.Major Areas Inspected:Followup of Previous Insp Findings, Operational Safety,Maint,Surveillance,Physical Security, Generic Ltrs,Info Notices & Quarterly Mgt Meeting
ML18053A357
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/22/1988
From: Burgess B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18053A354 List:
References
50-255-88-08, 50-255-88-8, GL-86-07, GL-86-7, IEB-88-001, IEB-88-1, IEIN-87-021, IEIN-87-023, IEIN-87-024, IEIN-87-034, IEIN-87-040, IEIN-87-041, IEIN-87-042, IEIN-87-21, IEIN-87-23, IEIN-87-24, IEIN-87-34, IEIN-87-40, IEIN-87-41, IEIN-87-42, NUDOCS 8805030349
Download: ML18053A357 (12)


See also: IR 05000255/1988008

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I II

Report No. 50-255/88008(DRP)

Docket No. 50-255

Licensee:

Consumers Power Company

212 West Michigan Avenue

Jackson, MI

49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, Michigan

Inspection Conducted:

March 3 through April 4, 1988

Inspectors:

Approved By:

E. R. Swanson

N. R. Wil 1 i ams en

T. V. Wa~.9 ch,1

.

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Reactor Projects Section 2A

Inspection Summary

License No. DPR-20

Date

Inspection on March 3 through April 4, 1988 (Report No. 50-255/88008(DRP))

Areas Inspected:

Routine, unannounced inspection by resident inspectors and

Region III staff of followup of previous inspection findings; operational

safety; maintenance; surveillance; physical security; radiological protection;

bulletins; generic letters; information notices; and quarterly management

meeting.

Results:

Of the areas inspected two violations were identified.

The first

involves inadequate evaluation and documentation of an issue involving an

unreviewed safety question.

The second involves an improperly performed

surveillance test where technician performance was not adequate .

8805030349 880422

PDR

ADOCK 05000255

Q

DCD

1.

2 .

l -

DETAILS

Persons Contacted

Consumers Power Company (CPCo)

D. P. Hoffman, Plant General Manager

  • J. G. Lewis, Technical Director
  • W. L. Beckman, Radiological Services Manager
  • R. D. Orosz, Engineering and Maintenance Manager
  • R. M. Rice, Operations Manager
  • D. W. Joos, Administrative and Planning Manager

C. S. Kozup, Licensing Engineer

  • R. A. Vincent, Plant Safety Engineering Administrator
  • D. J. Malone, Licensing Analyst
  • R. E. McCaleb, Quality Assurance Director

R. A. Fenech, Operations Superintendent

T. J. Palmisano, Plant Engineering Supervisor

  • Denotes those present at the Management Interview on April 4, 1988.

Other members of the Plant staff, and several members of the Contract

Security Force, were also contacted briefly.

Followup on Previous Inspection Findings:

(Closed) Violation 255/85003-21(DRP):

A QA audit had an inadequate

categorization of

110bservations

11 compared to

11 Findings

11 ; furthermore,

it appeared that Observations that required corrective actions were not

being tracked.

The licensee has amended his definition of

110bservation

11

and will continue to classify Observations and Findings according to

their significance.

However, those Observations that are considered to

be conditions adverse to quality and not corrected prior to the issuance

of the report will be documented on an Action Item Record (AIR) and

tracked to completion and trended via the Corrective Action System.

The licensee states that procedures are in place to assure personnel

follow-up on AIRs and to perform a completion review prior to closeout

of the document.

The inspector reviewed a number of QA audit reports and

the categorization of Observations and Findings and "conditions adverse

to quality" seems adequate.

This Violation is closed.

(Closed) Open Item 255/85013-08(DRP):

Failure of the 2400 volt breakers

to effect a fast transfer of vital loads to the startup transformer.

This open item was the result of failures documented in LERs 84001,

84015, -and 85005.

The event described in LER 85031 also involved the

failure of the 2400 volt breakers to transfer load,

LER 85031 was closed

in Inspection Report 255/88005, Paragraph 9, and that closure satisfies

Open Item 255/85013-08, also.

This Open Item is closed .

2

(Open) Open Item 255/85030-02(DRP):

Revise Test Procedure R0-65 so that

the testing of the both HPSI train check valves will be congruent with

ASME Code Section XI, Article IWV-3522, which states that the pressure

differential for equivalent flow shall be no greater than that observed

during the preoperational test.

The preoperational testing was done with

the flow going into all four loops and the flow thru each check valve

being measured.

However, the present version of the test procedure calls

for the check valves being tested one at a time, hence putting the full

head of the pump across just one check valve until it opens.

The licensee

has stated that they are evaluating a revision to Test Procedure R0-65

such that the pressure differential across the check valves during testing

will be congruent with the pressure during preoperational testing.

(Closed) Unresolved Item 255/86005-02(DRP):

Licensee to submit a study

and planned corrective action for Region III review by June 30, 1986,

regarding the problem of local leak rate test failures.

The study

results and the corrective action plan were submitted on time.

(Closed) Open Item 255/86035-157(DRP):

Improve the testing of the High

Pressure Safety Injection (HPSI) pumps through a combination of better

instrumentation and enhanced procedures.

As reported in Inspection

Report 87032, the improved procedures had been completed but a vibration

problem with the newly-installed precision-type discharge pressure gauges

still remained.

The licensee has now corrected the vibration problem and

this Open Item is closed.

(Closed) Unresolved Item 255/87005-08(DRP):

Licensee could not identify

the relief valve which protects against overpressure on the Low Pressure

Safety Injection pump discharge line, if there were thermal expansion of

the water in the line due to a sudden increase in room temperature.

The

necessity for such a relief valve is documented in FSAR Section 6.1.2.2,

Paragraph 6.

Relief Valve RV-3162 (see Drawing 203, Sheet 2, Rev. 8,

3/13/87) has been identified by the licensee as the valve which provides

the necessary protection.

This item is closed.

(Closed) Unresolved Item 255/87005-09(DRP):

Five instrument isolation

valves, which the Engineered Safeguards System Checklist required to be

positioned open, were missing from Drawing M-203 Sheet 2 (Revision 4).

Four of the missing valves had been added to M-203 as Rev. 7 and the

fifth valve was added whe-ri~ Rev. 9 was issued.

The inspector also

verified that all five valves are in the Equipment Data Base of the

Advanced Maintenance Management System.

(Closed) Open Item 255/87018-03:

Facility Change 623; Auxiliary Feedwater

Nozzle Modification.

The inspection report identified a concern about

the lack of consideration of differential thermal stresses on the steam

generator internals caused by removal of the sparger.

The licensee

1 s

re-evaluation report concludes that the auxiliary feedwater will be

sufficiently warmed by either the secondary side water or, if the water

level has dropped to expose internals, by the wall of the steam generator.

The inspector reviewed the drawing of the steam generator and internal

configuration to verify these feedwater heating methods.

3

(Closed) Open Item 255/87018-04:

Facility Change 576; Install 2

11 Auto

Isolation Valve on Penetration No. 33.

Historically, this issue was

discovered in 1982 when a discrepancy between the containment isolation

requirements of the FSAR and the operating procedures was discovered.

A

letter of {nterpretation was sent to the NRC explaining that since other

nuclear plants have Technical Specifications (TS) allowing certain manual

containment isolation valves to be open during plant operation, that

Palisades intends to continue sampling the Safety Injection Tanks through

the series, manual, containment isolation valves.

The licensee also

committed to submit a TS change request to formally resolve the issue.

This penetration was listed in Table 5-2 of the original FSAR as a Class

C-3 penetration.

Class C-3 includes penetrations that

11 *** are never

opened during power operation.

These lines contain two normally closed

manual valves in series.

A mechanical lock on each valve will ensure the

valve is not left open or inadvertently opened during power operation.

11

Since this penetration must be opened at least monthly to perform the

sampling of the Safety Injection Tanks required by the Technical

Specifications, it should have been Class C-2 which would require two

automatic isolation valves in series.

This is what this facility change,

as approved by the PRC, would have accomplished.

The safety evaluation,

which received appropriate reviews, did not identify that the discrepancy

was an unreviewed safety question (URSQ).

This constitutes a violation

of 10 CFR 50.59 requirements to document the bases for a determination

that an URSQ does not exist or receive Commission approval for the change

(violation 255/88008-0l(DRP)).

The prior inspection report raised the concern that the modification, as

described in the safety evaluation and facility change package reviewed

and approved by the PRC, was not completed and the remaining incomplete

portion was aborted without being re-evaluated and approved by PRC.

The

portion that was not completed included the automatic isolation that was

needed to conform to the FSAR.

In response to the open item another

evaluation was performed and concluded that this penetration, as

presently modified, conforms to the FSAR.

This conclusion is based

on the updated FSAR that was revised in the Fall of 1987 to match the

modified penetration.

The basis for this FSAR change was the 1982

licensee letter interpreting the TS, to which the NRC had never formally

responded since they were expecting a TS submittal for review.

By not

completing this change and revising the FSAR, the licensee has granted

itself an exception to the approved criteria in the FSAR.

(Closed)

Open Item 255/87018-05:

Facility Change 445-2; Install Motor

Operators on MSIV Bypass Valves.

The inspection report identified a

deficiency in the safety evaluation, in that it did not address

inadv~rtent or spurious operation of the motor-operated valve.

The

re-evalu~tion addresses this issue satisfactorily .

4

(Closed)

Open Item 255/87018-06:

Facility Change 676; Supports for

Nozzle of HC 23 -3

11 adjacent to SIRW Tank.

The inspection report found

that this evaluation did not address any seismic consideration or any

loss in safety margin because of the degraded pipe.

The re-evaluation

identifies that seismic stresses both for the OBE and SSE were included

in the analyses but not explicitly mentioned in the original evaluation.

With regard to the margin of safety, the re-evaluation concluded that the

margin of safety is not reduced but no satisfactory basis is provided.

However, discussions with the licensee determined that this modification

is temporary until the next refueling outage.

The piping will then be

restored to a condition equivalent to the original design.

(Closed)

Open Item 255/87018-07:

Facility Change 564; Addition of

Alternate Safe Shutdown Panel C-150A.

The evaluation for this change did

not address separation or isolation of the instrumentation or controls

for class IE circuits. It also did not assess whether any of these items

should be added to Technical Specifications.

The re-evaluation states

that the panel is located in the left channel penetration room and all

class IE circuits for the panel are left channel.

It also states that

Technical Specifications for this equipment have been proposed in a

submittal to NRC dated November 21, 1985.

(Closed)

Open Item 255/86035-153:

Upgraded Training. An upgraded

training program was conducted in 1988. The training program slides,

training material and the revised Procedure No. 3.07, Rev. 1, Safety

Evaluations, were reviewed by the inspector.

Both the training material

and the procedure include pending FSAR changes, Technical Specification

changes, design changes, and License Amendments as resource material to

be used by the evaluator.

A listing of these pending changes is maintained

current.

The training slides do not specifically address the qualifications

of the designated evaluation reviewer.

However, the training and the

final examination, as well as Procedure 3.07, include these qualifications,

i.e., the reviewer be a PRC member or alternate.

The revised procedure

satisfactorily takes into account the weaknesses identified in Inspection

Report 255/86035.

Approximately 150 personnel have been trained with this revised procedure

and upgraded training program.

An additional 60 to 90 people from the

General Office are going to be trained also.

The licensee is planning to

provide requalification training on a 2 year frequency.

One violations and no deviations were identified.

3.

Operational Safety

a.

Routine Inspections

The inspectors observed control room activities, discussed these

activities with plant operators, and reviewed various logs and other

operations records throughout the inspection.

Control room indicators

and alarms, log sheets, turnover sheets, and equipment status boards

were routinely checked against operating requirements.

Pump and

5

valve controls were verified to be proper for applicable plant

conditions.

On several occasions, the inspectors observed shift

turnover activities and shift briefing meetings.

Tours were conducted in the turbine and auxiliary buildings, and in

the central alarm station to observe work activities and testing in

progress and to observe plant equipment condition, cleanliness, fire

safety, health physics and security measures, and adherence to

procedural and regulatory requirements.

A portion of the inspection

activities were conducted at times other than the normal work week.

An ongoing review of licensee corrective action program items at

the Deviation Report level was performed.

b.

Boric Acid System

Background

During a routine NRC inspection in June of 1980, the inspector

identified that the concentrated boric acid (BA) system was

susceptible to a single active failure preventing BA addition during

accident conditions.

Power supplies to flowpath valves and the BA

pumps (P-56A, P-56B) are such that during a Main Steam Line Break

(MSLB) accident with loss of offsite power and failure of the 1-1

Diesel Generator, the the only concentrated BA flowpath is from the

11T-53A

11 BA storage tank, thru pump P-56A to the suction of the

charging pumps.

If either the T-53A storage tank or the P-56A pump

are inoperable, then no BA flowpath exists to perform the _function

of making the reactor subcritical (USAR G.1.2.1, 14.4).

As in 1980,

Technical Specification (TS) 3.2 requires that only one BA transfer

pump be operable, and allows either of the BA storage tanks to be

out of service for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

With either T-53A or P-56A out of

service the system is single failure prone, and the susceptible

condition can exist for Tank T-53A for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or indefinitly for

the pump P-56A.

Licensee resolution of this issue took the form of verbal

commitments to submit appropriate technical specifications, and

implementation of Standing Order No. 28 which directs the selection

of T-538 for routine BA usage.

The potential inoperability of pump

P-56A was apparently not an immediate concern because it was supposed

that the charging pump could draw water through the idle pump.

The

licensee actions were reviewed and approved by the NRC and the NRC

requested submittal of appropriate TS.

E1tent

On March 7, 1988, the system engineer recognized the incongruity of

the lack of a pump Limiting Condition for Operation and the importance

of the operability of P-56A during the above MSLB scenario.

He also

recalled that the P-56A pump had been out of service from October 19

through November 9, 1987 for maintenance and initiated a Deviation

Report.

6

The Licensee decided that the event was not reportable under lOCFR

50.72 in that it did not constitute an unanalyzed condition nor a

condition that could have prevented the fulfillment of a safety

function of a system needed to investigate the consequences of an

accident.

This decision was based on an informal evaluation of the

MSLB analysis which indicated that adequate margin was provided by

the actuation of a single High Pressure Safety Injection (HPSI)

pump. Using similar logic, the licensee does not plan 'to submit an

LER.

The licensee's reinitiation of corrective action on the pump

operability is a result of a more conservative view and the

realization that prior assumptions were not validated by testing.

Specifically, it has not been demonstrated that the charging pumps

can draw-adequate BA flow through an. idle pump, and the pump being

inoperable (as during 1987) may result in the isolation of the BA

fl owpa th.

The licensee revised the Standing Order No. 28 on April 8, 1988

to direct treatment of the P-56A transfer pump as required to be

operable at all times when the reactor is critical. A modification

to the power supplies which will eliminate the single failure

concern is planned for the 1988 refueling outage.

A TS submittal

is also expected by the end of 1988.

Conclusion

Removal of the A train concentrated boric acid system from service

is contrary to the current MSLB analysts assumptions.

An engineering

evaluation by the licensee concluded that adequate reactivity control

is provided by the HPSI system; however, this evaluation is not

substantiated by test data.

c.

Inadvertent Auxiliary Feedwater Pump Start

On March 27, 1988 at about 12:50 p.m., the C sensor channel of the

Auxiliary Feedwater Actuation System (AFAS) lost power.

The AC

power into the power supply was verified energized, but no DC output

was indicated.

At 1:30 p.m. the channel was bypassed.

Later, at

11:25 p.m., operators were attempting to reset lights on one of the

two actuation channels and inadvertently pressed the test button,

actuating the AFAS and starting the P-8A AFW pump.

After control

room operators verified that the actuation was spurious, the pump

was turned off.

No steam generator level control problems resulted,

and the licensee determined that the amount of cold water injected

was not deleterious from a thermal stress standpoint.

Corrective actions planned by the licensee will address the human

error from both the knowledge/training aspect and procedural and

human factors considerations.

7

d.

Safety Injection Sequence (SIS) Failure Evaluation

An engineering review by the licensee determined that a loss of

coolant accident coincident with loss of offsite power and a single

active failure of one channel of the SIS relays would result in

either of the following consequences.

The service water (SW)

non-critical header isolation (CV-1359) would not close and only the

P-7B service water pump would start.

Failure of the other channel

would result in two service water pumps running, but a containment

air cooler service water valve (CV-0867) would .not close.

Evaluations by the licensee determined that the susceptibility to

the postulated single failure is acceptable based on other cooling

systems availability (containment spray); the delayed need for

cooling to the Component Cooling Water heat exchangers after sump

recirculation (20 minutes); and adequate time and procedures

controlling operator action.

The NRC had reviewed these susceptibilities under the SEP topic IX-3

review, and also following recent SW System testing and flow balancing

in 1986/early 1987 and found them acceptable.

Additional review will be conducted of the planned LER.

No violations or deviations were identified.

4.

Maintenance

The inspectors reviewed and/or observed the following selected work

activities and verified whether appropriate procedures were in effect

controlling removal from and return to service, hold points, verification

testing, fire prevention/protection, radiological controls, and

cleanliness where applicable:

a.

Main Feed Pump Turbine

11 K-7A

11

Steam Trap Drain Line Repair

( FWS-24801705).

b.

Troubleshooting AFAS Channel C Power Failure (FWS 24801931).

c.

Fan V-24B Thermostat Replacement (SPS-24703560, SC-87-298).

d.

Replacement Of Temperature Indicator Number 1487 on 1-2 Diesel

(EPS-24800192).

~

e.

Replacement Of Instrument Hoses On 1-2 Diesel Control Panel

(EPS-24703195).

f.

Lubrication Of Fan V-24D (VAS 24706074).

No v1olations or deviations were identified.

8

5.

Surveillance

The inspectors reviewed surveillance activities to ascertain compliance

with scheduling requirements and to verify compliance with requirements

relating to procedures, removal from and return to service, personnel

quilifications, and documentation.

The following test activities were

inspected:

a.

b.

c.

d.

ME-12

MI-39

DW0-1

SH0-1

Battery Checks.

Auxiliary Feedwater Actuation System Logic Test.

Daily Control Room Surveillance.

Operators Shift Surveillance.

During performance of the AFAS Logic Test, the technicians were observed

to be conducting the test improperly and had signed off steps where

correct actuation logic had not occurred.

The technicians had not

performed this monthly test recently and were apparently unfamiliar with

the required output from the actuation module.

An incorrect test button

was being pressed.

This was apparently due to a combination of confusion

and poor labeling.

(This same poor labeling contributed to the AFAS

actuation discussed in Paragraph 3.c.) The technicians had both signed

off the procedure indicating that three status lights had lighted when

they had not.

The technicians apparently believed that they had obtained

the required output indication and called the system engineer when the

inspector questioned the results.

The INPO certified training program

provided documented on-the-job training qualification for the performance

of surveillance tests, but the certification was based on the satisfactory

performance of a selection of tests which did not include MI-39.

ANSI

Standard N18.7-76 section 3.3 states that training shall

11 *** assure that

suitable proficiency is achieved and maintained.

11

It was also noted that

although an inadvertent actuation had occurred during the performance of

the test on September 1, 1987, that corrective action action identified

to improve the procedure had not been included in the January, 1988

biennial review.

The above constitutes a violation of the TS procedural

compliance requirements of section 6.8.1 as outlined in the Appendix

(Violation 255/88008-02(DRP)).

One violation and no deviations were identified.

6.

Physical Security

The inspectors observed physical security activities at various

locations throughout the protected and vital areas including the Central

and Secondary Alarm Stations.

Periodic observations of access control

actiiities including proper personnel identification, badging and

searches of personnel, packages and vehicles were conducted.

The

inspectors verified appropriate security force staffing and operability

of search equipment.

Protected and vital area boundaries were toured

to verify maintenance of integrity.

Illumination was verified to be

adequate to support patrol and Closed Circuit Television (CCTV) monitor

observations.

CCTV monitor clarity and resolution were also observed.

The inspectors periodically verified that appropriate compensatory

measures were taken for degraded or inoperable equipment and breached

boundaries.

9

No violations or deviations were identified.

7.

Radiological Protection

The inspectors made observations and had discussions concerning

radiological safety practices in the radiation controlled areas

including: verification of radiation levels and proper posting; accuracy

and currentness of area status sheets; adequacy of and compliance with

selected Radiation Work Permits and high radiation procedures; and the

ALARA (As Low As is Reasonably Achievable) program.

Implementation of

dosimetry requirements, proper personnel survey (frisking) and

contamination control (step-off-pad) practices were observed.

Health

Physics logs and dose records were routinely reviewed.

The licensee has completed the testing phase of the PCM-lA personnel

contamination monitors and has developed a policy for dealing with the

expected low levels of contamination that will now be identified.

These

devices are viewed as a positive enhancement to the Radiation Protection

Program.

No violations or deviations were identified.

8.

NRC Bulletins

(Closed) NRC Bulletin 88-01:

Defects in Westinghouse Circuit Breakers.

The licensee determined that none of the subject breakers are in use in

IE applications at Palisades.

Two DS-416 breakers are in use supplying

the asphalt solidification system for which appropriate reviews and

actions will be taken separate from the NRC Bulletin requirements.

The

licensee

1 s response was dated March 14, 1988.

9.

Generic Letter 86-07

On March 20, 1986 the NRC issued Generic Letter 86-07, transmitting

NUREG-1190 regarding the November 21, 1985 San Onofre Unit 1 loss of

power and water hammer event.

During this event all inplant ac power was

lost for* 4 minutes; all steam generator feedwater was lost for 3 minutes;

a severe water hammer caused by check valve failures was experienced; all

indicated steam generator water levels dropped below scale; and the

reactor coolant system experienced an unnecessary cooldown transient.

The inspector verified that the licensee 1 s program for review and

assignment of action was appropriately implemented, and that sufficient

distribution of the information concerning the event had been accomplished.

Of the actions identified as a result of the event, the only action

remaining relates to the check valve failures.

The licensee has

incorporated the guidance and recommendations of INPO SOER 86-03 and

the EPRI document,

11Application Guidelines for Check Valves in Nuclear

Power Plants

11 , into their Valve Improvement Pr9gram.

Under contract to

Palisades, Combustion Engineering has completed an evaluation of the flow

criteria for each check valve identified in the program.

Additional

evaluation criteria are being considered along with various methods for

verifying check valve integrity and condition in the formulation of the

continuing program.

10

Specific actions are being tracked under Action Item Record A-SA-87-10,

which has an assigned completion date of December 1, 1988.

10.

Information Notices

The inspector reviewed licensee action on the following Information

Notices in order to verify receipt, appropriate review, distribution, and

timely corrective actions.

(Closed) IN 87-21:

11Shutdown Order Issued Because Licensed Operators

Asleep While On Duty

11 *

The licensee and individual licensed operators

received the IN, but no action was documented as having resulted from the

information.

(Closed) IN 87-23:

"Loss of Decay Heat Removal During Low Reactor Coolant

Level Operation".

Action on this IN and INPO SER 15-87, resulted in a

number of procedural enhancements and a modification to provide an alarm

indicating impending loss of shutdown cooling.

(Closed) IN 87-24:

"Operational Experience Involving Losses of Electrical

Inverters

11 *

Fans had been added as a result of prior Pali sades events

and inverter replacement is planned.

(Closed) IN 87-34:

11 Single Failures in Feedwater Systems".

Action on

this issue, specifically the low pressure suction trip subsystem, is

still not complete, but tracked under the licensee's corrective action

program.

(Closed) IN 87-40:

"Backseating Valves Routinely to Prevent Packing

Leakage".

The licensee's evaluation references Administrative Procedure

4.02 "Equipment Control" as providing adequate instructions concerning

the proper method for backseating valves and for the identification of

valve damage.

Distribution was not made to the operator requalification

training program or to the "read and sign" file since the licensee had

taken action after a similar Palisades event.

(Closed) IN 87-41:

Circuit Breakers

11 *

size.

"Failures of Certain Brown Boveri Electric (BBE)

Palisades does not have any BBE breakers of the 4KV

(Closed) IN 87-42:

11Diesel Generator Fuse Contacts".

Palisades PT fuse

drawers were found to already have the knife switch contacts recommended

by GE as corrective action.

During the review of the above IN 1 s it was determined that the Training

Revision Tracking Committee was functioning, meeting weekly with

multidiscipline membership, and making acceptable determinations as to

which generic communications are desirable for inclusion into the

various plant training programs.

Action on IN 1 s continues to be assigned

and tracked by the Plant Safety Engineering group.

No violations or deviations were identified.

11

11.

Management Meeting

A quarterly management meeting to review the status and progress of the

Palisades plant was conducted on March 31, 1988 at the Palisades site.

Consumers* Power Company (CPC) was represented by Messrs. 0. P. Hoffman,

J. G. Lewis, W. E. Garrity, K. W. Berry and others of the staff; and the

NRC was represented by Messrs. E. G. Greenman, W. G. Guldemond, M. P.

Phillips, B. L. Burgess, T. V. Wambach, and others of the staff.

The

meeting consisted of presentations by CPC covering an update on the

corrective action plan to restore the original design margin to the

Component Cooling Water and Service Water Systems, the scope of work

planned for the 1988 refueling outage, and a summary of the last INPO

evaluation.

12.

Management Interview

A management interview was conducted on April 4, 1988, upon conclusion of

the inspection.

The scope and findings of the inspection were discussed.

The inspector emphasized the importance of timely corrective action and

management oversight as the keys to preventin_g licensing roadblocks and

violations like the ones discussed in Paragraphs 2 and 5.

The inspector

also discussed the likely information content of the inspection report

with regard to documents or processes reviewed by the inspectors during

the inspection.

The licensee did not identify any such documents/processes

as proprietary .

12