ML18038B582

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Insp Repts 50-259/95-60,50-260/95-60 & 50-296/95-60 on 951015-1118.Violations Noted.Major Areas Inspected: Operations,Maint & Surveillance Testing Activities & Unit 3 Restart Activities
ML18038B582
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 12/12/1995
From: Lesser M, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B580 List:
References
50-259-95-60, 50-260-95-60, 50-296-95-60, NUDOCS 9512190099
Download: ML18038B582 (98)


See also: IR 05000259/1995060

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report Nos.:

50-259/95-60,

50-260/95-60,

and 50-296/95-60

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

.

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

October

15 - November

18,

1995

1

Inspector:

eonar

.

er

,

,

endor

es>

ent

nspector

J.

Munday, Resident

Inspector

R. Musser,

Resident

Inspector

M. Morgan, Resident

Inspector

Approved by:

ar

.

esser,

rane

se

,

Reactor Projects,

Branch

6

Division of Reactor Projects

lz n./tJ

ate

1gne

SUMMARY

Scope:

This routine resident

inspection

involved inspection on-site in the areas of

operations,

maintenance

and surveillance testing activities, Unit 3 restart

activities including observation of management

assessments

for restart

and

major testing activities,

review of the component

and piece part qualification

system

and review of open items,

including several

Three Mile Island Action

items.

The remainder of NRC open items for restart of Unit 3 were closed.

Several

hours...of. backshift coverage

were routinely worked during most work

weeks.

Deep backshift inspections

were conducted

on November

10,

12 and

18.

p-Q> g~fj,'4;;-

".<<~~a W

95i2i90099 95i2i2

PDR

ADOCK 05000259

8

PDR

Enclosure

2

'I

i5

Results:

One violation and two noncited violations were identified.

Operations:

One violation was identi.fied involving failure to follow configuration control

procedures.

Unit 3 scram discharge

volume vent and -drain valves were found

incorrectly gagged

open.

A NRC inspector identified that the discharge

volume

high level

scram function was incorrectly bypassed.

Although existing plant

conditions

reduced

the safety significance of both incidents,

these

examples

were significant deficiencies

involving plant configuration.

(VIO 296/95-60-

01, Failure to Follow Config8fation Control Procedures

Resulting in

Misalignment of Scram Discharge

System

Components,

paragraph

2.3)

A noncited violation was identified involving a loss of shutdown cooling flow

on Unit 3.

Fuel

had not yet been

loaded into the core.

Planning

and review

processes

were not conducted

in accordance

with procedural

requirements

during

troubleshooting of reactor protection

system equipment.

(NCV 296/95-60-02,

Loss of Shutdown Cooling Flow, paragraph

2.2)

Final verification of the licensee's

readiness

to load fuel in Unit 3 was

performed through detailed

reviews of selected

important equipment conditions

and confirmation of incorporation of regulatory requirements

into procedures.

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For several

key systems,

all open items were reviewed

and the systems

were

confirmed to be ready for fuel loading.

Maintenance

backlogs

were noted to be

small.

Emergent

equipment

issues

continued to be addressed

appropriately.-

All required TS.surveillances

were completed prior to fuel loading.

Overall

drywell conditions at drywell closeout

were regarded

as very good.

(paragraphs

6.1;I and 6.1.2)

Observation of the Nuclear Safety Review Board

and senior'management

assessment

of the readiness

to restart Unit 3 indicated that

a comprehensive

review was performed

by the groups.

(paragraph

6.1.3)

Maintenance

and Surveillance:

Inspection of completed Unit 3 maintenance

work orders indicated that post

maintenance

testing

and environmental qualification requirements

were being

met.

Documentation of completed

work was adequate.

'(paragraph

3.2. 1)

The Unit 3 containment

integrated

leak rate test,

diesel

generator

load

acceptance

testing,

and primary system hydrostatic

testing were well planned

and implemented.

(paragraphs

3.2.2, 6.2.1,

and 6.2.3)

Plant Support:

Inspectors

noted several

instances

in, whi.ch securi.ty guard monitoring of

personnel

access

lanes

.was not. vigorous.

The .observations

were communicated.

to plant management

and corrective actions

were promptly'initiated.

(paragraph

4)

t

l~

Engineering

and Technical

Support:

One noncited violation was identified.

The licensee initially concluded that

a failure of the "A" diesel generator'id

not have to be incorporated into the

diesel

generator reliability calculations.

NRC inspectors identified that the

failure was required to be included in the calculations.

(NCV 260/95-60-03,

Failure to Perform Diesel

Generator Reliability Determination,

paragraph

5.2)

A detailed review of the Component

and Piece Part gualification Program for

Unit 3 was completed.

The pro'gram fully met regulatory commitments

and

adequate

controls were present

on qualified equipment

replacement

parts.

Good

conditions were noted in the,-storage

warehouse.

(paragraph

7)

I

I

f

1.0

Persons

Contacted

Licensee

Employees:

'REPORT:DETAILS

T.

J.

R.

  • J

T.

  • C
  • J
  • G

R.

J.

R.

G.

  • E

S.

J.

  • p

T.

D.

  • S

J.

  • H.

Abney, Unit 3 Nuclear Assurance

and Licensing Manager

Brazell, Site Security Manager

Coleman.,

Radiological Controls Manager

Corey,

Chemistry

and Radiological Controls 'Manager

Cornelius,

Emergency

Preparedness

'Manager

Crane, Assistant Plant Manager

Johnson,

Site guality Manager

Jones,

Unit,3 Startup

Manager

Little, Operations

Superintendent

Machon, Site Vice President,

Browns Ferry

Maddox, Maintenance

and Modification Manager

Moll, Plant Operations

Manager

Pierce,

Technical .Support

Manager

Preston,

Plant Manager

Rudge, Site Support

Manager

Sabados,

Chemistry Manager

Salas,

Licensing Manager

Shriver, Nuclear Assurance

and Licensing

Manager.

Stinson,

Recovery

Manager

Wetzel., Acting Compliance Licensing Manager

White, Outage 'Manager

.

Williams, Engineering

and Materials Manager

Other licensee

employees

or, contractors

contacted

included licensed reactor

operators,

auxiliary'perators,

craftsmen,

technicians,

and

public safety

officers;

and quality .assurance',

design,

and engineering

personnel.

NRC Personnel:

  • L. Wert,,Senior Resident

Inspector

J: Hunday,

Resident

Inspector

R. Musser,

Resident

Inspector

  • M. Morgan, Resident

Inspector

J. Williams,

NRR Project Manager

G.

Wiseman,

DRS Inspector

G. HcDonald,

DRS Inspector

P. Fillion, DRS Inspector

F. Jape,

Senior Project Manager,

DRP

B. Rogers,

NRR Special

Inspection

Branch

S. Rudisail,

DRS Inspector

D. Nelson,

NRR Inspection

Program Branch

H. Janus,

Resident .Inspector,

Brunswick

H; Whitener=,

DRS Inspector

P. Byron, Resident

Inspector,

Brunswick

R. Aiello, Inspector,

DRS

W

0

'0

NRC Officials/Hanagement

onsite:

W. Russell, Director, Office of Nuclear Reactor Regulation

S. Varga, Director, Division of Reactor Projects,

NRR

S. Ebneter,

Regional Administrator,

Region II

J. Johnson,

Acting Deputy Regional Administrator,

Region II

"Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the last

paragraph.

2.0'lant Operations

(71707,

92901,

40500)

2. 1

Operations

Status

and Observations

Unit 2 operated

at power for the entire period.

On October

18,

1995

TVA

commenced

loading of fuel into the Unit 3 reactor vessel.

Loading was

completed

on October 29.

On November 2, reactor vessel

reassembly

was

completed.

Unit 3 containment

leak rate

and

RPV hydrostatic testing

was

performed during November 5-11.

The vessel

was disassembled

to correct

a

problem with two misaligned fuel support pieces.

On November

16 and

17 the

Unit 3 vessel

and drywell were reassembled..

Activities within the control

rooms were monitored routinely.

Inspections

were conducted

on day and night shifts, during weekdays

and

on weekends.

Observations

included control

room manning,

access

control, operator

professionalism

and attentiveness,

and adherence

to procedures.

Th'

inspectors

noted that operators

were cognizant of plant conditions

and were

attentive in'heir duties.

Due the approaching

Unit 3 restart,

the inspectors

have emphasized

review of issues that have potential effects

on the operation

of the other unit. Instrument readings,

recorder traces,

annunciator

alarms,

operability of nuclear instrumentation

and reactor protection system channels,

availability of power sources,

and operability of the Safety Parameter

Display .

System were monitored.

Control

room observations

also included emergency

core

cooling system lineups,

primary and secondary

containment integrity, reactor

mode switch position,

scram discharge

volume valve positions,

and rod movement

controls.

Daily discussions

were held with plant management

and various

members of the

plant operating staff.

One of the inspectors

attended

the daily Plan of the

Day meetings.

Plant tours were taken throughout the reporting period

on

a

routine basis.

Observations

included valve position

and system alignment,

snubber

and hanger conditions,

containment isolation alignments,

instrument

readings,

housekeeping,

power supply

and breaker alignments,

radiation

and

. contaminated

area controls,

tag=control-s

on.-equipment-,.

work activities in

progress,

and radiological protection controls.

Paragraph

6. 1 describes

t

specific reviews conducted just prior to Unit 3 fuel loa'ding

and startup

activities.

II

i

During this report period the licensee

and the inspector noted examples of

deficiencies

involving second party verification.

On October 31,

1995, the

licensee identified .that

a hold order card

was not properly second party

verified while placing

a clearance.

BFPER951643

was written to document this

event.

On November 7,

1995, the inspector noted confusion concerning the

requirements

of performing second party verification while observing

an

SLC

.operability test.

Conversations

with various Operations

personnel

.indicated

that there

was

a lack of understanding

on the requirements

of second party

verification and

how it is actually performed.

This was discussed

with

Operations

management

'who stated that action

had already

been taken to provide

additional training and restated

the expectations

of management

regarding

second party verification.

The inspectbrs

continued to perform periodic tours of the Unit

1 reactor

building.

On October

19,

1995,

an inspector identified three pipes

(one inch

diameter)

located in the Unit

1 reactor building that had direct communication

outside of the building.

The pipes

were funnel drain pipes from fire

protection deluge valves which drained to the reactor building roof drain

lines.

The inspector felt air discharging

from the funnels which indicated

that outside air was blowing through the roof drains into the building.

Operations

was contacted

and engineering

was requested

to investigate.

The

openings

were found to not have

been

accounted for'in the secondary

containment

breach

program,

however,

when the breaches

were

added to the

recorded existing breaches,

the result

was not an excessive

amount of

secondary

containment

openings.

BFPER951567

was initiated to document

and

correct this condition.

On November

13 and

14,

1995, the senior resident

inspector contacted six local

officials and informed them of the Unit 3 restart

planned for November

19.

The officials included: the mayors of Athens, Moulton,

and Decatur,

as well as

the commissioners

of Limestone,

Morgan,

and Lawrence cdunties.

The inspector

did not receive .any negative

comments or concerns

from the officials..

2.2

Unit 3 Loss of Shutdown Cooling Flow

On October

13,

1995, while troubleshooting

a problem with the

RPS system,

an

automatic isolation of the

Loop II RHR inboard injection valve, 3-FCV-74-67,

occurred

when the

B RPS

MG set

was manually tripped.

Following the isolation

the

B RPS bus

was re-energized

and the injection valve reopened.

At the time

of the event the loop was in the shutdown cooling mode of operation,

however,

no fuel was in the reactor

vessel.

The shutdown cooling suction valves did

not isolate

because

the isolation function had been defeated

in accordance

with the troubleshooting

work order,

WO 95-18774-00.

It was not recognized

by

those involved with the activity that the injection valve would also receive

an isolation signal.

Operations

reported the event to the

NRC in accordance

with 10CFR50.72(b)(2)(ii)

and initiated BFPER951505.

The inspectors

reviewed..the

WO and. noted.-that- it was not planned

as

a high

risk- activi'ty;

SSP-6-..2,

Mai'ntenance

Management

System,, section 3.8.6,.

describes

a high risk activity as

one which has

an inherent increased risk for

causing reactor

scrams,

ESF actuations,

or transients.

It states

that

activities involving logic systems

such

as

RPS or PCIS that can directly or

I

0

indirectly cause isolations

are to .be considered

to be high risk.

Additionally, troubleshooting activities where the causes

of the malfunctions

are not well understood

are to be considered

high risk.

The procedure

requires that high risk activities include additional

planning considerations

and approvals

by the Operations

Manager,

Operations

Superintendent,

Maintenance

Manager,

Duty Plant Manager,

and Technical

Support

Manager prior

to starting work.

The inspector could not conclude that the event would not

have occurred

had the activity been considered

high risk but it was concluded

,that the troubleshooting activities would have received

much mor e review prior

to the work commencing.

An Incident Investigation

was initiated and concluded that the event

was

caused

by inadequate

coordination of activities, technical deficiencies

in the

troubleshooting

plan,

and inadequate

control of the types of activities that

can

be performed from a troubleshooting

plan.

Discussion with the licensee

indicated that the troubleshooting

plan did not receive the proper reviews

and

approvals prior to commencing work.

The safety significance of this event is

small.

Although shutdown cooling was in service,

no fuel was located in the

reactor vessel

and shutdown cooling was not being used to remove decay heat.

This failure to follow plant procedures

constitutes

a..violation of minor

significance

and is 'being treated

as

a Non-Cited Violation, consistent with

Section

IV of the

NRC Enforcement Policy.

This matter is identified as

NCV

50-296/95-60-02,

Loss of Shutdown Cooling Flow.

. Following the event,

on October

16,

1995, licensee

management

issued

a site

dispatch stating that there would be

a site wide seventy-two

hour quiet time

in which little physical

work 'would be performed.

The plant management

stated

that the purpose of the quiet time was to assess

the activities for the future

and to completely "switch gears"

from. a recovery .mode to an operating

mode.

2.3

Components

Out Of Expected Position

On October 30,

1995, the Unit 3 reactor

mode switch was placed in a "Shutdown"

position for containment

integrated

leak rate testing

(CILRT).

The mode

switch positioning caused

the expected

reactor

scram;

however, it was noted

that all eight

SDV vent and drain valves failed to close during the scram.

Upon further investigation,

the valves were found to be in a gagged

("dogged")

open and, therefore,

they could not close

upon receipt of the scram signal.

The valves were not in an ungagged position

as prescribed

in the

SDV system

equipment

alignment checklist.

The

SDV vent

8 drain valves,

(3-FCV-085-0082,

0082A, 0083,

0083A,

0037C,

0037D,

0037E

and 0037F),

have handwheels

which are

actually mechanical

stops or "dogs".

The handwheels

can

be used to manually

open the valves,

but .the valves will then

be "blocked" in an open position.

The handwheels

cannot block the valves from opening

when placed in a closed

position;

however,

they can prevent closure if "dogged" in the open position.

A "dogged" position is

a ful-ly counterclockwise

("open"), direction with

threads visible between the handwheel

and the valve body.

An "undogged"

position -is

a ful-ly"clockwise ("closed" ) direction with no threads, visible.

=between" the 'handQheel--and=valve

body;

When"the valves were later"ungagged'

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they-operated-properly-.

Despite

a detailed investigation,

the inspection

-period, the licensee

was not able to determine

the specific cause .of'he

misposi,tioned valves.

l

t

ll

5

On November 6,

1995,

an

NRC inspector.,

during

a routine inspection of control

room activities,

noted that the Unit 3

SDV High Level

Scram switch was in the

"Bypass" position.

On November 3, the unit reactor

mode switch'had

been

repositioned

from "Refuel" .to "Shutdown", in order to comply with

prerequisites

of a scheduled

CILRT.

An expected

scram

was later reset;

however,

the

SDV High Level Bypass switch was not returned to normal until the

mispositioning

was observed

by the

NRC inspector.

The mode switch was in

"Shutdown"

and all rods were fully inserted.

However,

TS require that this

scram function be operable.

The switch was not in the "Normal" position

as

prescribed for in the

SDV system

equipment checklist.

Problem Evaluation Report 951687 noted that, during the month of October., six

similar conditions involving instances

of equipment mispositioning were

reported.

An attachment

to the above

PER was reviewed

by the inspectors

and

it was noted that

a search of the database

was performed

by the licensee to

identify similar configuration control

PERs

on Units-2

8

3 over the last

thirteen months.

Sixteen

"component mispositioning"

PERs were found and were

generically classified

as "loss of status control".

While several

licensee

actions

have

been

performed to resolve this issue,

others

must

be performed to

reinforce facility procedural

requirements

and expectations

of both Operations

and Maintenance

personnel.

At. the close of this report, the licensee

was

evaluating, the overall subject for corrective action.

These

two examples of failure to mainta'in adequate

unit system configuration

control represent

a violation.

This issue is identified as

VIO 296/95-60-01;

Failure to Follow Configuration Control Procedures

Resulting in Misal.ignment

of SDV System. Components.

One violation and

one noncited violation were identified.

3.0

Maintenance Activities and Surveillance Testing

(62703, .92902,

61726,

92901,

37551,

92903)

3. 1.1 Maintenance

Observations

Maintenance activities were .observed

and/or reviewed during the reporting

period to verify that work was performed

by qualified personnel

and that

approved

procedures

in use adequately

described

work that was not within the

skill of the trade.

Activities, procedures,

and work requests

were examined

to verify proper authorization to begin work, provisions for fire hazards,

cleanliness,

exposure control,

proper return of equipment to service,

and that

limiting conditions for operation

were met.

The following maintenance activities were reviewed

and witnessed

in whole or

in part:

WO 95-00312-00

'RCIC Minimum Flow Valve Motor Inspection.

On November=l.l=,

1995, the inspector witnessed electrical

maintenance

personnel

perform portions of an inspection

and -cleaning of the 2-MTR-071'-0034,

RCIC

-Minimum Flow Valve motor.

The inspector

observed

the craft pull back

il

0

0

insulating tape to inspect connectors,

verify l.ug tightness,

and ensure

the

wiring insulation

was not damaged.

The torque switch setting

was verified to

be acceptable

as

was the general

overall condition of the switch.'ollowing

completion of the activity the inspector verified the housing cover .was

properly oriented. when installed.

The maintenance

.personnel

appropriately

used the proper procedures.

Cleanliness

requirements

were adhered to.

The

inspector

noted

no discrepancies

with this activity.

Section

6 of .this report describes

additional specific maintenance activities

monitored

by the inspectors.

3. 1.2 Maintenance

Work Order Reviews

The inspectors

reviewed several

recently completed

maintenance

work orders

associated

with Unit 3 maintenance activities to verify that the work was

properly controlled

and post'aintenance

testing

was satisfactory.

WR 293089,

WO 95-15441-01,

and 95-15441-00:

These

work packages

addressed

"rolled leads" involving the- drywell control air

compressor

inboard

and outboard drywell suction valves.

Discussions

were held

with the Unit 3 Restart

Manager,

the involved system engineer,

and Ma'intenance

management

regarding

some aspects

of the packages.

WR 293089

was written on 8/30/95 to disposition Test deficiency TD-2 on Post

Modification Test 3-PHT-032-.043:

Functional. Testing of Valves 3-FCV-032-0062

and 0063.

(At steps

7.3. 13. 1 the "63" val.ve local handswitch operated

backwards,

at step 7.4.13. 1 the "62" valve would not operate

from the local

switch.),

The inspector

.noted .that the problems

and the

WR actions

were

logged

on the chronological test log in the test -package.

'he

WR was assigned

as a,priority 2 "immediate attention"

and the Restart

'Manager authorized

the work to be performed in parallel with the planning.

The inspector verified that this is permitted

by SSP-6.2.

The work was

performed

on August 30,

1995.

The work was documented

in detail

(lead

by

lead, including second

checks)

on the

WR form.-and included

a simple functional

~

test.

The opening of the junction box was recorded

on Attachment

5 of EII-0-

OOO-TCC106, Troubleshooting

and Configuration Control of Electrical

Equipment.

(Box was left "unsealed",on

August 31.)

PMT-BF-032.043

was- subsequently

completed

on August 31.

The inspector verified that the steps of the

PHT that

were re-performed

also served

as

a post maintenance

"functional test" after

the electrical

leads

were connected.

Inspector obtained

copy of Potential

Drawing Deficiency

(PDD)95-441.

This

PDD was initiated on August 31,

1995 to correct the connection

diagram for the

valve leads.

(The schematic

drawing was correct.)

WOs 95-15441-00

and -Ol were subsequently

planned.

These work orders

were

signed-.off on. September-

15;

1995.

Usually,

WOs are=planned

much:more-quickly.

if "in parallel" with the work.

Although it is not specificall'y set forth in

. the

SSP, it is expected that planning "in parallel"

be performed's

the work

is being done.

In this case, -restoration -of operabi.lity was not,a concern.

i1

0

The

WO packages

included the

Form SSP-235s

required for all of the worked

Eg

components,

the

PDD,

and completed

sheets

out of the EII-0-000-TCC106

procedure.

The,inspector noted that the functional test

was N/A'd in the

WOs

and suspected

that this was because

the "actual work" was done

as noted

on the

WRs (8/31/95)

and the

WO paperwork

was completed

as "documentation of

completed actions"

on September

14-15.

The actions required

by the

Form 235s

(Eg maintenance

sheets)

and the TCC106 sheet for resealing of the junction box

were completed

on September

14-15.

The system engineer

and maintenance

management

confirmed that this was what had occur red.

The inspector

questioned

maintenance

management

as to why the workers did not simply

document that the wire connection activities had

been

completed

on August 31

as recorded

on the

WR instead of writing the steps

out again with the

September

14 date.

Maintenance

management

indicated that this practice will

be reviewed.

In summary,

the inspector

concluded that the work was controlled in accordance

with the procedures.

All Eg work requirements

were completed

and documented

as required.

On operable

equipment

such

as Unit 2, the

same

sequence

could

occur except that the planning would be more in "parallel" and the

WO

completed

more timely since the equipment would remain inoperable until the

WO

was completed.

WO-95-01888-03

and WO-94-02123-00:

This work was to disconnect/reconnect

a

RHR heat

exchanger

discharge

valve and

temperature

sensor

so that the

RHRSW piping could be replaced.

The inspector

'eviewed

the

EMS .data

base

and noted that 3-FCV-023-0034 is not flagged

as

Eg

in EMS.

However, the motor actuator

(3-MVOP-023-0034) is coded

as

Eg.

The actual

work performed section of WO-95-01888-03'stated

that the valve

cables

were reterminated

and conduits replaced

by

WO 94-02123-00.

The

inspector obtained

a copy of this

WO.

The

WO clearly identified the actuator

as

Eg and the required

SSP

Form 235s were completed.

Post maintenance

testing

of the val.ve was included in the

WO and was accomplished

by an approved

procedure.

WO-94-16769-00:

This

WO involved troubleshooting

an unexpected

annunciator

window response

during

a test.

The equipment

involved was Unit 3 load shed circuitry.

The

inspector

reviewed the referenced

procedure,

EII-O-OOO-TCC106, Troubleshooting

and Configuration Control of Electrical

Equipment

and noted that it provides

methods for documenting/controlling electrical

lead lifts and other electrical

maintenance activities.

WR 230242

was initiated on October

16,

1995, to support completion of Stage

6

of.

DCN. 21284,

The actual

work performed section. of. the

WO described

activities performed October

17,

1994 to October 23,

1994,

then the activities

were initiated again

on March 6,

1995 to test

changes

made

by

DCN F33386 for

t

W21284.

The

WO contained

a detailed

45 page attachment

which-was- used. to-.

guide the troubleshooting/testing

activities starting. on March 6,

1995.

The

attachment

included prebriefing, specific acceptance

criteria,. and. speci,fic

0

0

8

step-by-step

method

of, testing.

The. attachment

was completed

on March 6,

1995.

WO 94-16769 work activities were completed

on June

21,

1995 when leads

to a relay were rol.led.

The inspector verified that'.PMT 268.001 functionally

tested

the circuitry and it was completed

on July 19,

1995 (after the work was

done).

The inspectors

concluded that the activities were adequately controlled

and

regulatory requirements

were met.

3.2

Surveillance Obsyrvations,

Surveillance tests

were reviewed

by .the inspectors

to verify:procedural'.and

performance

adequacy.

Testing .was witnessed

to ensure that approved

procedures

were used, test equipment

was calibrated,

prerequisites

were met,

test results

were acceptable,

and system restoration-was

completed.

3.2. 1 Routine Surveillance Testing

i

2-SI-4.4.A.l

Standby Liquid Control

Pump Functional. Test

On November 7,

1995, the inspector witnessed

the'performance of this

surveillance.

This test operates

each

SLC pump to verify the proper flow rate

can

be obtained

and the vibration levels are acceptable.

During the

surveillance the inspector noted that step 7.5. 10 did not receive

second party

verification prior to its performance

as required.

The step required the

isolation of a drain valve when

a specified

amount of water is drained

from

the system.

It did not appear

to the inspector as,a

step requiring this type

of verification nor one in which 'the verification could reasonably

be

performed.

The inspector questioned

both the

AUO performing the test

and

an

ASOS observing

about this step.

They stated that the step should not be

required to be second party verified because it. was not

a critical step

and

.

was required to be performed

when

a parti'cular setpoint

was reached.

If a

second party verification,;were performed the setpoint would have:been

exceeded

prior to its'erformance.

The licensee

stated that the procedure

would be

reviewed

and .revised to delete

any unnecessary

second party verifications.

including the one for-this step.

While operating

pump

2A to verify flow requirements

the

pump discharge

hose

rig started leaking

an excessive

amount

and the

pump was secured.

The hose

was repaired,

the test tank refilled, and the test restarted.

The inspector

noted the operators

contacted

the main control- room to apprise

them of the

situation,

backed

up in the procedure to the appropriate

step,

and

recommenced

performance of the surveillance.

The inspector considered this process

to be

well communicated'nd

coordinated.

During the surveillance

the operator

noted

that the green

"pump off" light flickered on and off. It was determined that

the socket

was loose

and

WR C285369

was initiated to correct the condition.

It was also noted that the red

"pump. running" light was dim.

The operator

removed the bulb and determined that- it-was= not the-same-type

bulb as the

green light.

Engineering

was contacted <o determine

what- bulb -should-be-

i'nstalled for these. l,ights but was unable to identify a particul.ar,

requirement.

Operations initiated

a

PER to address this issue.

No further

discrepancies

were noted during .the, performance .of this procedure.

0

.3-SI-4.6.B.1-4

Reactor Coolant Chemistry

On November

7,

1995, the inspector witnessed

the sampling

and analyzing of

reactor coolant for conductivity in accordance

with this procedure.

The

continuous conductivity monitor was =-inoperable

and Technical Specifications

requires

a reactor coolant sample

be analyzed for conductivity 'every eight

hours

under these conditions.

The inspector

witnessed

the sample

being drawn

and analyzed.

Proper radiological protection requirements

were observed.

The

conductivity was acceptable for the existing plant conditions.

No

discrepancies

were identified during the performance of this activity.

3-SI-4.2.C-4(B)

Instrumentation

That Initiates

Rod Blocks/Scrams

Source

Range Monitors

(SRM) Calibratio~ And Functional

Test

On October

14,

1995,

the .inspector witnessed

portions of the performance of

this surveillance.

The test

had previously been performed with the .exception-

of the discriminator high threshold/high, voltage calibration port'ion.

Performance of this section required that

a neutron source

be located close to

the

SRM detector.

The .inspector verified that the test equipment

was properly

calibrated,

the appropriate

reviews

had

been obtaine'd prior to performance,

and the proper procedure

was being used.

The procedure

was

on revision

0 and

had not yet been validated.

It was therefore

necessary

to validate it during

'this performance.

The technicians

performing the surveillance .identified that

step 7. 11.34 incorrectly operated

component

Z32-Rl.

The performers

determined

that the correct

component

was PS21-Rl.

This was considered

to be

an obvious

minor error and the surveillance

was completed

as written.

Following the

conclusion of the surveillance the inspector:verified that this discrepancy

was identified on the

new procedure, validation form.

No.further discrepancies

were identified with this activity.

Additional routine surveillance testing activities conducted

on Unit 3 in

preparation for,.restart were, observed

and are discussed

in paragraph

4.2.

3.2.2

Unit 3 Integrated

Leak Rate Test

The inspectors

reviewed test documentation

and witnessed test activities to

determine that the Unit 3 primary containment

integrated

leak rate test

(CILRT) was performed in accordance

with 10 CFR 50, Appendix J,

Primary

- Reactor Containment

Leakage Testing for Mater Cooled

Power Reactors;

ANSI

N45.4 - 1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.4 - 1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

American National Standard,

Leakage

Rate Testing of Containment

Structures for Nuclear Reactors;

Browns Ferry Nuclear Plant Technical

Specifications 3.7/4.7.A.2.a-f,

Unit 3; test procedure 3-SI-4.7.A.2.a-f,

Primary Containment

Integrated

Leak Rate Test;

and,

Bechtel Topical Report,

'BN-TOP-l, Rev.

1, Testing Criteria for Integrated

Leakage

Rate Testing of

Primary Containment Structures for Nuclear

Power Plants.

Selected

sampling of the licensee's .activities which were inspected

included:

(-1:)'- review-.of the test 'procedure to verify that the procedure

was properly

approved

and conforms with'-the regul'atory requirements

listed-above;

(2)

observation of test performance to determine that test preparat'i'ons

were

completed,

special

equipment

was installed,

and appropriate

data

was recorded;

0

10

and (3) preliminary evaluation of test results'o verify that leak rate limits

were met.

From review of the test procedure 3-SI-4.7.A.2.a-f,

and associated

technical

instructions 3-TI-173 and 3-TI-179 the inspectors

concluded that the licensee

had incorporated

the essential

elements of the regulations into the procedure

and instructions.

Procedure 3-SI-4.7.A.2.a-f contained

adequate

instructions

for venting, draining and alignment of systems to establish

boundary

conditions, identification of systems to remain operable for safe

shutdown of

the;reactor,

and .acceptance

criteria for a short duration test

and

a '24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

test which were consistent

with the regulations.

Technical instructions

provided detailed instructions for installation, location,

and determination

of weighing factors for instrumentation

and data recording setup.

The

technical

instructions

also required inspection of the accessible

areas

o'

containment for degradation

and delineated

.the leakage

surveys to be performed

during the test.

The inspectors

reviewed the instrument calibrations, verified that selected

penetration

alignments

were correct,

observed that appropriate

data were

recorded

and processed,

and evaluated

the test results.

The containment

integrated

leak rate data analysis

program used

by Browns

Ferry had the capability of analyzing the data in accordance

with BN-TOP-I for

a short duration total time test

and .in =accordance

with ANSI N45.4 and

Appendix J for a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> total time or mass point test.

The inspectors

evaluated

the data

and determined that the all acceptance

criteria for

termination of the leak rate measurement

were met in a 10.2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> short

duration test with an uppei

95K confidence leak rate (includes

measurement

error) of 1.06 wt. percent pe'r'ay of the'ontainment,air

at Pa.

The

allowable limit for,Browns Ferry Unit 3 for the test is 0.75

La or 1.5 wt.

percent

per day.

Subsequent

to the containment

leak rate measurement,

a supplemental

test must

be performed to verify the ability of the CILRT instrumentation to measure

a

change in leak rate..

An acceptable

method is specified in Appendix

C of ANSI .

N45.4 which involves establishing

an additional

known leak rate

on the

containment

and verifying the

known change

by measuring

the .overall leak rate.

The licensee

performed

a 5.3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> supplemental

test

and measured

the composite

leakage of 2.84 wt. percent -per day which-was well within the acceptable

range

of leakage.

+I

The inspectors

concluded that .the licensee

had demonstrated

the leak tight

'ntegrity

of the primary containment

as required

by the regulations.

The test

was well planned'and

implemented.

During a previous inspection,

NRC Report 95-08, the inspectors

had reviewed

six -design

changes

associated

with plant modifications to meet Appendix J test

requirements. and-found'that-*the-modifications

were properly implemented.

During this inspection the inspectors

reviewed-two additional'lant

changes

associated

with containment leak testing

as follows:

C

IN

IO

11

RHR Suppression

Chamber

Spray Valve

(FCV 74-58)

and

RHR Recirculation

and

Pump Test Valve

(FCV 74-59)" were"'required

- to be rotated

180 degrees

to facilitate testing the valve bonnets.

The inspectors

confirmed that

this change

had

been

implemente'd

by Maintenance

under. work orders

95-

06550-00

and 95-06557-00 respectively.

Auxiliary Boiler System Valve

(HCV 12-742) required the installation of

a block valve to facilitate local leak rate testing.

The licensee

subsequently

determined that the valve and associated

piping is part of

a zinc chromate injection system which is not used.

Consequently,

under

DCN W23574A, the zinc chromate injection system including

HCV 12-742

and

associated

piping and valves were removed.

The tie-in of the Auxiliary

Boiler System to the .RCIC pump minimum flow bypass line to the

suppression

chamber

was cut,

capped

and welded outside primary

containment to preserve

containment integrity.

The inspectors

walked

down the change

and observed

the capped penetration

and confirmed

removal

on the piping and valves.

Also, the Configuration Control

Drawing 3-47E813-1 reflected the capped line and piping removal.

The inspectors

concluded that the licensee

had adequately

implemented the

above

changes

to enhance

Appendix J testing.

No violations or deviations

were identified.

~

4.0

Plant Support

(71750)

The inspectors

toured the protected

area

and noted that the perimeter fence

was intact

and not compromised

by erosion

or. disrepair.

The fence fabric was'-=.

.

verified to be intact'rid secured.

The inspectors

also observed

personnel

and'ackages

entering the protected

area

and verified they were searched

either by

special

purpose detectors

or physical

patdown.

The resident

inspectors

and

a

visiting inspector noted several

instances

in which security guard attention

was not strong during personnel

access.

During off normal hours, monitoring

of the entry lanes at the access

portal

appeared

to be less rigid than

expected.

While no regulatory requirements

were violated,

more management

attention

was needed

in this area.

The observations..were

discussed

with

security

and plant management

and corrective actions

were promptly initiated.

The inspectors will continue to monitor personnel

access

controls.

No violations or deviations

were identified.

5.0

Engineering

and Technical

Support

(37551)

5. 1

RPS Logic Problem Review

~

On October 21,

1995,

guad Cities Nuclear Plant

(a

BWR-3 similar in design to

Browns Ferry), commenced

a dual unit technical specification required

shutdown

. due

a design

problem .,in the scram discharge

volume high level reactor

scram

logi'c.

More specificall'y, the si'ngle failure criteria was not" met in that the

~

~

~

~

~

~

failure of a single

RPS subchannel- relay coupled with a high level in one

scram discharge

instrument

volume would fail to generate

a full reactor

scram

-,as required.

The inspectors

learned of this incident during

a routine review

I

0

12

of 50.72 reports

on October

24.

This information was relayed to the licensee

via the

RPS system -engineer that day.

The licensee

and the inspectors

independently verified that .this condition did not apply at Browns Ferry.

The

scram discharge

volume high level reactor

scram -logic at

BFNP is designed

such

that

a single failure of any component

coupled with a high level in a single

scram discharge

instrument

volume or both scram discharge

instrument

volumes

would result in the required reactor

scram.

Each

scram discharge

instrument

volume has four level switches

(one for each of the four RPS subchannels)

and

.

=four different

RPS logic relays for a total of eight different level switches.

and logic relays.

This review revealed that the

BFNP scram discharge

instrument

volume high level

scram logic is appropriately designed to

withstand

a single failure.

5.2

EDG Failure Not Included in

EDG Reliability Calculations

On October

10,

1995, while performing

a preventive. maintenance activity on the

A DG relay

ESTR malfunctioned which resulted

in the'DG failing to start.

The

malfunction occurred

on the third start of a redundant start test.

Investigation identified that the cause of the failure,was a,piece of tie wrap

used to bind wiring together

had fallen into the relay mechanically preventing

it from operating properly.

The tie wrap was removed

and the relay operated

satisfactorily..

The system engineer

surmised that the piece of tie wrap was

located

above 'the relay .and

had simply fallen onto the

ESTR relay.

The other

-DG relay cabinets

were inspected -.for loose tie wraps and'ther foreign debris

and

none

was found.

\\

The inspector

asked the licensee, if this event. was:considered

to be

a valid

failure to start in accordance

with O-SI-4.9.A, Diesel Generator Reliability

And Start Log.

The licensee

stated that since the

DG had two successful

'tarts

before the event occurred,

they did not consider it to be

a valid

failure.

The inspector

reviewed .the,SI

ahd .Regulator'y:Guide

1.9 and concluded

that the event met the criteria,for being considered

as

a valid failure to

start

and should

have

been included in the

DG reliability. calculation.

Following .additional discussion,

the l.icensee

reached

the

same conclusion

and

classified this event

as

a valid failure to,start.

Subsequently

0-SI-4;.9.A

was performed to determine if any additional testing

was required.

Failure to

classify this event

as

a failure to start

and perform O-SI-4.9.A is

a

violation .of plant procedures,

however,

the significance is minor.

The

DG

reliability did not change appreciably

and no additional testing

was required

due to the failure to start.

This violation is being treated

as

a Non-Cited

Violation, consistent with Section

IV of the

NRC Enforcement Policy.

This

matter is identified as. NCV 50-260/95-60-03, 'Failure To Perform Diesel

Generator Reliability Determination.

5.3

Hoisture in Drywell Penetration

Guard Pipe

During routine tours of Unit 3 one of the inspectors

observed

moisture within

the"guard: pipe on reactor building- side-of- the-:SLC system-drywell- penetration.

This condition had.-previously

been

ques'tioned

by the inspector during the

SPOC

walkdown of SLC..

On October 20, 1995,.:PER-951590-was-initiated-on

this- issue.

Technical. support personnel

reviewed the issue

and insulation

was removed.

The .water was initially attributed to condensation,

'.Several

days later, the

0

13

penetration

had dried except. for a small -amount of moisture at the drywell end

of the pipe.

The inspector noted that the re'fueling cavity had

been drained

.and questioned

engineering, personnel

on the source of the leakage.

The

inspector questioned

whether water may be leaking from the refueling cavity

bellows, which was leaking

down between the outside of the drywell liner and

the concrete shielding.

The inspector

was concerned that the construction of

the SLC:penetration

may be permitting water to leak into the penetration.

At

the end of this report period,

Engineering

was reviewing the issue.'o

immediate operability issues

were involved but potential corrosion issues

need

to be examined.

The inspectors will continue to monitor the licensee's

actions.

One noncited violation was identified.

6.0

Unit 3,Restart Activities

(37828,

61726,

62703,

87550,

92903)

(Unit 3)

The inspectors

reviewed

and observed

licensee activities involved with the

Unit 3 .restart.

This included reviews of procedures,

post-job activities,

and

completed field work; observation of pre-job field work, in-progress field

work,

and

QA/QC activities.

Detailed observation of numerous testing

acti.vities

and other system recovery activities was conducted.

6.1

Unit 3 Refueling Operations

and Preparations

~6. 1. 1 Verification of Readiness

To Load Fuel

and Restart .

The inspectors

reviewed

a portion of the various licensee

procedures

and

documents

in preparation for fuel load into the reactor vessel.

Technical

Specifications

were reviewed to identify requirements

necessary

for the

Refueling mode.

The licensees

procedures

were then verified to contain

.actions or steps

necessary

to ensure

compliance with these specifications.

Test deficiehcies

were reviewed for various post-maintenance,

post--

modification,

and surveillance activities to verify that they'were

appropriately dispositioned.

No deficiencies

were noted.

Nuclear.

Instrumentation

surveillances

3-SI-4.2.C-1.2FT,

Instrumentation

That Initiates

Rod Blocks/Scrams

APRM Functional Test With Reactor

Mode Switch Not In Run

Position

and 3-SI-4.2.C-4(A), Instrumentation

That Initiates

Rod Blocks/Scrams

SRM .Calibration

and Functional Test, were reviewed following completion.

This

review verified the acceptance criteria was satisfied

and performed

a.

comparison with the

same procedures

applicable for Unit 2.

The Unit,3

procedures

are virtually identical with the Unit 2 procedures.

This is true

for the remaining nuclear instrumentation surveillances.

The Site Master

Punchlist

was reviewed for two systems to determine if items still existed

that were either coded for fuel load

and had not been

completed or were coded

for another milestone

but should

have

been

coded for fuel load.

No

discrepancies

were noted during this review.

On-November

16, the inspector

reviewed the open items for three safety,:.related,

systems:

EECM (System 67),

HPCI (System 73),

and

RHR (System 74) to"verify-

I

C

II

14

that all required work would be completed prior to restart.

The open

WOs for

the

same

systems

were reviewed.

The

WO review revealed

the following:

~Oe ~s

ECCW

22

ll

HPCI

75

44

RHR

.

88

'59

The inspector did not identify any open items which would affect restart.

He

noted that all open lists were"very -dynamic as evidenced,

when the November .I7,-

SMPL printouts for the .three systems

were reviewed.

The updated

SMPL report

listed fewer open items.

The inspector

met with the respective

system

engineers

and their manager to discuss

changes.

The discussions

revealed that

significant changes

in the number of open items was

a function of timely

updating.

The system engineer's

system health report was also reviewed.

There

was correlation

amongst the data.

The inspector concluded that the

licensee's

review process

to address

work to be performed after startup

was

adequate.

6.1.2 .Unit 3 Drywell Closeout

Inspections

Throughout the recovery of Unit 3, the inspectors

have. monitored. the'ondition

of the Unit 3 drywell and torus.

Numerous tours were taken in both areas.

On

November 8, the inspectors

performed

a detailed

walkdown of the Unit 3 drywell

and compiled

a list,of deficiencies

needed to be corrected prior to restart of

the Unit.

These

items included

numerous

housekeeping

items,

a loose

electrical junction box cover,

a loose yoke bolt on

a

RBCCW valve, loose

~electrical outlet covers,

debris in floor drain screens,

and two sensing lines

on the

B main steam line appeared

inadequately

supported.

These

items were

turned over to the licensee's

drywell closeout .coordinator.

All items were

corrected with the exception of the sensing lines

on the main steam lines.

The sensing lines were .evaluated

as acceptable

by site engineering

personnel.

A regional str.uctural

inspector, also reviewed this issue

and determined that

the licensee's

conclusion

on this matter was acceptable.

On November

17, the

licensee

performed their:final drywell closeout inspection in accordance

with

3-GOI-200-2, Drywell Closeout.

An inspector

accompanied

.the licensee

during

the .walkdown and noted that the drywell..was in good condition and acceptable

for restart.

On:November

17,

one of .the inspectors

performed

a final drywell walkdown of

the Unit 3 drywell with the plant manager

and assistant

plant manager.

The

inspection

covered all levels of the drywell.

The condition of the drywell

was quite good.

The inspector

found

a tie wrap,

a cotton glove, several

pieces of wire,, and several

pieces of tape.

The inspection did not identify

any tools or miscellaneous

hardware.

The condition of the drywell was

among

the best that the inspector

has observed

during

a final walkdown.

Additional discussion of inspection involving drywell conditions is included

in paragraph

8. 18 of .this report.

0

15

6.1.3 Nuclear Safety Review Board/Senior

Management

Assessment

of Browns Ferry

Readiness for Unit 3 Restart

and Multi-Unit Operation

On November 7, l995, the inspectors

attended

the combined

NSRB/SMART meeting

,to monitor the licensee's .senior

managements

final review of the Browns Ferry

Site (staff, programs

and hardware)

readiness

for Unit 3 restart

and multi-

unit operation.

The site's

Vice President

presented

an overview of, the status

of the Unit 3 recovery.

Items discussed

included restart

and post-restart

.regulatory issues,

self assessments,

maintenance

backlog, plant material

condition,

power ascension

plan,

and. emerging issues.

Detailed presentations

were then

made

by the plant manager

and engineering

and materials

manager.

Topics of discussion,

in addition to th'e =above mentioned

items,

included

assessments

of the various plant departments/systems

readiness

for restart,

open engineering

issues,

and emergent restart

issues.

The emergent

issues

included the recent

component mispo'sWioning;;events,(see,paragraph

2.3)

and

a

control rod drive, problem which necessitated

the .disassembly of the reactor.

The assistant

plant manager

discussed

the work remaining

on Unit, 3 and the

licensee's

goal to have their backlog below 600 work items prior to restart.

The

ORRT team leader also

made

a presentation

to the boar@

He stated that

all of .the

ORRT issues

had

been resolved

and

made

a recommendation

to the

board

and President,

TVA Nuclear that Unit 3 be allowed to restart.

In

addition, the site

NA&L manager

discussed

all open

NRC items

as well as the

status of the

gA oversight of the recovery of Unit 3.

The

NA&L manager stated

that all .gA issues

had

been resolved

and that the unit was ready for restart

from a gA perspective.

The board/team

members

asked

probing

and pertinent questions

and received

comprehensive

and appropriate

responses.

The inspectors

perceived

the review

performed

by the

NSRB/SMART team

as thorough:and,comprehensive.

The final

resul.tant,-of

.the meeting

was

a recommendation

to the President of TVA Nuclear

that restart

be approved subject to the completion of all identified restart

items being tracked

by site -management.

6. 1.4

NRC Operational

Readiness

Evaluation

Team Issues

During the

ORAT, inspection

conducted

in October,. two issues

were identified in

which it was .determined that licensee

actions

and additional,NRC review prior

to 'Unit 3 -restart would be appropriate.

Both issues

were related to fire

protection.

The

ORAT identified that the procedural link. which instructed the operators

to

~

shut off ventilation fans to ensure that fire dampers

would close

was weak.

The instructions

were contained in the Abnormal Operating Instruction 30

series of procedures,

but there

was insufficient guidance to refer the

operators

to the AOI.

Additionally, when questioned

by ORAT inspectors,

several

operators

did not realize the importance of securing

fans to ensure

that=dampers,,go

shut..

The licensee

has revised related'procedures.

A new AOI', O'-AOI-26-1, Fire

Respons'e,

has

been written which encompasses

the AOI 30 proced'ures'in

one

procedure

and addresses

the actions to be taken

on

a fire.

The resident

inspectors

verified, that AOI 0-26-1 is present

in .the control rooms..

il

16

Operators that were questioned

on fire response

referenced

the

new AOI.

There

is

a red label

on the control

room fire panels

(Unit

1 and Unit 3) which

states

that AOI-26 is to be implemented

as required for actual fires.

The AOI

states

that actions regarding ventilation are to be taken

based

on the request

of the fire brigade leader.

The AOI contains

a list of switches to be operated

for the different areas

in the plant.

Operations

and fire leaders will be

briefed/trained

on the procedural

changes

by November 18,

1995.

Discussions

with fire protection

management

indicated that the dampers

in the reactor

buildings had

been

upgraded

such that they would shut against ventilation fan

flow if actuated.

The licensee

could not state th'at all control building

dampers

are designed to or tested to shut against

fan flow.

During the resident inspector's

review of the corrective actions,

an actual

fire occurred

(small fire in a trash

can in the turbine building).

Control

room actions

were completed

as required

by the procedures

and

PER 951722

was

initiated to address

the fire.

The inspectors

noted that the fire alarm in

the Unit 3 control

room was not of sufficient volume to be clear1y heard

above

the noise

caused

by several

ongoing activities.

The inspector

informed the

Unit 3 Restart

Manager

who responded

that the volume would be adjusted.

guestioning

by an

ORAT inspector resulted in the licensee identifying a

potential

problem involving two spurious valve failures.

The postulated

scenario

involved two

RHR valves spuriously opening during

an Appendix

R

event,

allowing

RHR pump discharge

piping to be drained. down.

The concern

was that this could cause

a water

hammer incident.

The licensee notified the

NRC operations

center of the condition.

Subsequently-,

the licensee

reviewed

the issue in more detail.

The licensee

concluded that, while Browns Ferry

fire protection .analysis calculations did include mor'e than

one spurious

failure, regulatory requirements'did

not require

more than

one failure to be

cons'idered.

The inspector reviewed the licensee's

commitment evaluation of

this aspect of GL 86-10,

Implementation of Fire Protection

Requirements,

and

found no. discrepancies.

On November

13,

1995, the licensee- retracted

the

50.72 notification 'on this issue.

The inspectors

concluded that these

two issues

were sufficiently resolved

such

that the involved equipment

and personnel

could support the restart of Unit 3.

6.2

Unit 3 System Testing

6;-2.1

Emergency Diesel Generator

Load Acceptance

Testing

The inspector

observed testing of the

3D

EDG on October 2,

1995,

and testing

of the 3A

EDG on October

3,

1995.

The testing

was performed in accordance

with procedures

3-SI-4.9.A.l.b-4 and 3-SI-4.9.A.l.b-l, Diesel

Generator

Emergency

Load Acceptance

Test.

The inspector

reviewed the procedures,

applicable portions of the

FSAR,

and

TS requirements

before observing the

testing.

The inspector reviewed the Baseline Test Requirements

Document (2/3-

BFN-BTRD-082) and concluded'hat

the test procedures

addressed

the

requirements

adequately.

The briefing prior to each of the tests

was highly detailed.

The test

director reviewed outlines of the entire evolutioy,

The.+scussjun.--..jocluded

~c'

W

i

O.

17

the test organization,

expected

system performance,

and contingency actions.

The

SOS was involved in the briefing.

Communications

were stressed.

B'efore

beginning the 3A EDG test,

a half scram condition on Unit 2 was discussed

to

ensure that no impact between the units was involved.

Other control

room

activities were suspended'o

minimize potential interference.

During the testing,

an i.ntercom line was operating

between the Unit I/2

control

room and the Unit 3 control

room.

High levels of plant management

.were present .in the Unit 3 control

room during the tests.

The inspector noted

good oversight of the reactor operators

by the

SROs.

Running

pumps were

monitored appropriately during the test.

Test'deficiencies

and emergent

equipment

issues

were 'identified and resolution actions promptly initiated.

Manipulations of the

EDG controls~encl'UtAig";the.. paralleling activities, were

well performed.

The inspector noted that the loads;,pieced'n

the:EDGs were

well below

the load limits.

During the trip of the 'RRR pump, the

EDGs

responded

very smoothly.

The inspector:concluded .that .the testing

was

conducted

in a professional

.and highly controlled manner.

The inspector subsequently

reviewed the completed test

package for the

3A EDG

in detail during this report period.

The inspector reviewed the test recorder

printouts

and verified that the data

had

been accurately .interpreted

and

transferred to the data portions of the package.

The results

met the

acceptance

criteria.

The inspector confirmed that Test Deficiency (TD-Ol)

.which addressed

a failure of two 480 volt loads to trip on undervoltage,

was

appropriately resolved.

The inspector noted that the current

FSAR describes

the Unit 3

EDGs from the

perspective

of supporting Unit 2 operations,

not Unit 3 operations.

Licensing

management

indicated to the inspector. that

a revision to the

FSAR is planned

which would update this data.

J

The inspector reviewed the three documents

which describe

the current

LOCA

analysis for BFN: NEDC-31580P

(Safety Evaluation in Support of Extended Valve

Stroke Times for Browns Ferry Units 1,2,3),

GE calculation

EAS-49-0889

(Evaluation of Extended Diesel Generator

Ready to Load Times).,

and

BFN

calculation

ND-.90000-89062.

The inspector confirmed that the

EDG testing

~

results

were in accordance

with the .assumptions

regarding

EDG start

and load

ti~es in. the documents.

--The

EDGs were .ready for loading much faster than the

analyzed limiting times.

The inspector

concluded that the testing verified that the Unit 3

EDGs were

capable of performing their safety functions under

LOCA loading conditions.

The preparation

and planning efforts, along with the careful

and well paced

execution of the testing,

led to overall

smooth performance of the testing.

6.2.2

Unit 3 Torus Penetration

Leak Rate Testing Verification

Between

November I and November 7,, l995,.

an. inspector .performed walkdowns of

the-Uni-t-3-Torus area in order to verify that various inside

and outside

diameter

torus. penetrations-.would-be"subjected"to

leak rate testing pressures

during performance of li'censee

surveill'ance

procedure,

3-SI-4.7.A.2.'a-f;

"Primary Containment

ILRT". Mhile the,inspector

observed that the, existing

~4

il

l5

18

penetrations

would be adequately

tested,

the inspector

also noted the

following:

With the exception of three

(3) penetrations,

all other field-identified

penetrations

were not adequately identified with field markings.

Five (5) penetrations

were not identified on the licensee's

dr awing.

Also three

(3) of the field penetrations

were not accurately reflected

on the drawing; i.e.,

an inerting sample return line penetration

was

listed

as. an "instrument tube"

on the drawing.

However, with use of

both the system drawing

and drawing "change/revision

papers",

most

-'=;penetrations

.could .be found and accurately classified.

Almost all of the system penetrations

have

been verified as correctl'y

marked in accordance

with SSP-8.7

(Rev 8), "Containment

Leak Rate

Programs",

Appendix J; i.e.; the field penetration

indications. match

those penetrations

listed in SSP-8.7.

No major penetration identification deficiencies

were found by the inspector

and it was the inspector.'s

under standing, after discussions

with the system

engineer,

that field marking of these penetrations will be performed

soon.

The inspector also noted that incorporation of inspector

8 licensee-identified

drawing discrepancies

are to be'erformed

in the near future.

The inspector

intends to continue monitoring of the licensee's

progress

in this area.

6;2.3

Unit 3 Reactor

Vessel Hydrostatic Pressure

Test

One of the inspectors

observed

the conduct of Procedure .3-SI-3.3.1.B:

Hydrostatic Testing

as test pressure

was approached.

The inspector verified

that temperature

and .pressure

monitoring:.was being .performed as:required

by

TS.

The inspector verified that the temperatures

being monitored

and recorded

would confirm compliance .with TS figure 3.6-1 (curve I). 'The operator

was

knowledgeable

regarding the

TS requirements

and location of the temperature

detectors.

The inspector

noted that one narrow range suppression

chamber

water level

was slightly lower than the administration limit in Procedure

3-

SI-2 (-5.5 inches).

The SI requires

only -daily verification of torus level.

The

TS limit is -6.25 inches.

CR operators

increased

suppression

chamber

.

level in response

to the inspectors .questions.

After test pressure

of 1014

,psig was attained,

the inspector walked down the Unit 3

SDV system.

The

inspector

observed

numerous

CRD HCU packing leaks

and reported the

observations

to maintenance

personnel.

Work Requests

were initiated for

repairs.

The inspector

reviewed the completed surveillance test

package for the Unit 3

reactor vessel

hydrostatic test which was signed off on November

13,

1995.

Licensee

procedure '3-SI-3.3:I.B,

ASIDE Section

XI Hydrostatic Systen

Pressure

Test of the Reactor

Pressure

Vessel

and Associated

Piping

(ASME Section III,

Class. 152),. control:led-the-..test-.-

Four-test- deficiencies-were written to

identify six valves which 'coul'd not be cycled due to operating=limitations-.

'

~

~

~

~

~

~

~

~

~

~

~

gC inspectors

performed

a VT-2 inspection

on the reactor vessel

and associated

,piping .

They inspected

215 val.ves .and, fittings.

Fifty had leakages, in excess

of 35 drops per minute.

gC identified leaks ranging- from weeping .:gg.,one

i5

iN

0

19

gallon per minute

(gpm) for a valve packing.

Work orders

were written to

tighten fittings and to tighten or replace

valve packing.

The licensee

reduced

system leakage to a level which they expect will result in a system

leakage of less

than

one

gpm at restart.

Leakage at the

CRD under vessel

flanges

was brought to the vendor limit of less

than 30 drops per minute for

all but one flange.

Leakage at the

CRD 10-47 flange increased

when tightened.

WO 95-2086-02

was written to replace

the o-ring for CRD 10-47 which. was

completed

on November

12.

The inspector

noted that all valve manipulations

were verified to be in the specified position.

The review di.d not identify

any deficiencies.

On November

17, the inspector attended

the

JTG meeting which addressed

interim

test results for several

Power Ascension Tests.

The JTG was thorough

and

indepth questions

were asked.

There were no issues

identified which would

affect restart

but two test reports

were remanded

back to the system engineer

for clarification.

The inspector considered that the

JTG provided the

licensee

a good indepth cross discipline review of startup test issues.

6.2.4 Unit 3 Fire Protection Surveillance

and Post Modification Testing

Surveillance Instruction O-SI-4.11.G. l.a, "Inspection of Fire Rated Barriers"

was reviewed

by the inspector to verify procedural

and performance

adequacy.

The SI inspection

was performed to verify the functional status of fire rated

penetration

seals installed in the Unit 3 Reactor Building under

DCN W18196 to

support Appendix

R safe

shutdown

system separation.

The completed test

was

examined for necessary

test prerequisites,

instructions,

acceptance

criteria,

technical

content,

authorization to begin work, data-.collection,

handling of

deficiencies

noted,

and review of completed work.

The test

was inspected to

determine that approved

procedures

were available,,prerequisites

were met, the

test

was conducted

according to procedure,

and test results

were acceptable.

The SI package,

SI performance

and surveillance results

were satisfactory.

'our SI test deficiencies

were identified.

Corrective actions

had

been

initiated and given proper status.

6.3

Fire Barrier Penetration

Seals8 -+ 'v>

In the Browns Ferry Fire Protection

Report

(FPR) Section 3.0,

TVA committed to

mechanical

pipe

and electrical conduit

and cable tray penetration

seals that

are qualified by meeting criteria that:

(1) are tested

and Underwriters

Laboratory

(UL) Listed or otherwise

approved

by

a recognized

independent

testing facility; (2) the penetration

seal

design

and installation was

previously approved

by the

NRC; or (3) the seal

design

has

been evaluated

and

approved

by a qualified fire protection engineer.

In the review of penetration fire stop seals,

the inspector

used the

FPR

criteria,

Design Critetia BFN-50-799, "Fire and Pressure

Seal Selection",

and

recognized

industry penetration fire stop seal testing guidance of American

Society for Testing

and Naterial

(ASTH) Standard

E814-1988,

"Standard

Test

Hethod for Fire Tests of Through-Penetration

Fire Stops'"

and Institute of

Electrical

and Electronics

Engineers

(IEEE) Standard

634-1978,

"IEEE Standard

Cable Penetration

Fire- Stop-equal.ification Test".

The inspector reviewed the

typical

BFN mechanical

and electrical penetration

-seal installation

0

20

procedures,

installation drawings

and details, quality control

(QC)

and

quality assurance

(QA) installation records,

GL 86-10 fire protection

evaluations,

and

TVA testing data for a sample of 13 typical mechanical,

electrical conduit,

and cable tray penetration

seals identified in Attachment

1 to this inspection report.

These

seals

were reviewed to determine that the typical installed plant seal

configurations

were representative

of those .utilized in TVA's fire seal

qualification tests.

The penetration

seal

samples

were established

by an

inspector walk down of fire barriers associated

with Fire Areas 3, Fire Zones

3-1, 3-2, 3-3 and 3-4; Fire Area 16; Fire Area'9,

and Fire Area 25.

The fire

barriers

represented

10 CFR 50 Appendix

R fire barrier separation

in those

areas for required safe

shutdown

components of the

RHRSW"and <<ECCW systems.

The typical seal

sampl'es

were representative

of about

80X of the plant seal

installations.

ay

No discrepancies

were identified by the inspector in the review of the

TVA

penetration

seal installation procedures,

the

QA/QC records

associated

with

those seals

inspected,

and the penetration

seal qualification tests.

Also, no

discrepancies

were identified by the inspector

during the visual inspection of

the seal installations.

However, during the seal- review,

TVA engineerin'g

personnel

identified that the installed configuration of 'MP-3 penetration

seals

was not consistent

with the typical seal detail

dr awing 3-47E3392-628.

The top damming material for floor seal installations

was not installed

as

t

.shown in the typical detail drawing.

Additional seal material

was installed

to the top of the penetration

sleeve.

TVA BFPER951455

was written to address

the lack of the top damming material for typical NP-3 floor seal

installations.

Based

on the review of the fire:barrier penetration fire stop seals,

the

inspector

concl,uded the'-following:.

The penetration

seal qualification tests for mechanical

pipe

and

electrical

conduit seals

met minimum industry test guidelines for

significant test parameters.

The test

specimens

in qualification tests reports'were

representative

or

adequately

bounded the installed as-built, penetration

seal

configurations.

The qualification tests

bounding conditions for the significant fire

barrier penetration

seal material

and design attributes

(e.g.

type of

seal material,.sealant

density, location

and type of damming boards,

and

location

and type of penetrating

item) were clear.

The tests

sufficiently established

a fire propagation qualification rating of the

penetration

seals.

Electrical cable tray penetration

seal

desi'gn at .Browns Ferry have not

been tested/approved

by a recognized

independent- testing facility nor

tested" to-approved-industry

standards.

The. cable. tray. penetration.-seal-

design

was

based

on fire tests

conducted

by TYA and approved

by

NRC in

Part X, Fire Recovery Plan

. These tests

demonstrated

.the..adequacy

of a

ik

I~

21

seal

design that prevents

flame occurrence

on the unexposed

side of the

barrier seal for a fire condition representative

of in-plant combustible

loading.

Additional TVA engineering

evaluations

indicate'd the design

was comparable to a

UL Listed design

and acceptable.

6.4

Station Blackout Rule Unit 3 (92701)

10 CFR 50.63 requires that:plants

be able to cope with a loss of alternating

current

(AC) power sources.

Regulatory

Guide 1.155 defines which AC sources

must

be postulated

to fail, specifies the required coping duration

and

provides guidance

on how to demonstr ate that the station blackout

(SBO) rule

.. '-...has

been met.

The licensee's

latest submittal describing their approach to

meeting the

SBO rule was

made

on April 28,

1992.

The

NRCs safety..evaluation

was issued

on September

16,

1992.

On June

12 16,

1995, the

NRC con'ducted

an

on-site inspection of the

SBO rule for Unit 3.

The

NRC Inspection

Report (95-

34) states that violations or deviations

were not identified,

and lists items

that

had not been completed.

During this inspection

(October

1995) these

outstanding

SBO items for Unit 3 were addressed.

The licensee's

basic coping

strategy for SBO was to run HPCI and

RCIC systems

independent

of AC power on

.the blacked out unit and reenergize

necessary

HVAC equipment within one hour

through

"excess

capacity" diesel

generators.

The licensee's

procedures

for responding to a station blackout event were

contained

in Abnormal Operating Instruction O-AOI-57-1A, Loss of Offsite Power

(161

and

500 kV) / Station Blackout,

Rev 35, dated

September

12,

1995,

and

Transmission

Emergency

Plan,

dated

March 1,

1993.

The inspector

reviewed these

procedures

and found they met the requirements

of the .SBO rule.

The inspector verified by inspection of the:batteries

that the

new larger

batteries

required to meet the

SBO rule -had .been instal.led.

The inspector

verified through review of drawings .and inspection of;distribution panels

in

the, plant that

DC loads

had:been

removed .and/or relocated .as necessary

to

allow the batteries

to .provide the necessary, power for four hours:without'he

need for manual

shedding of loads.

=-'3he inspector verified that the battery

loading calculation supported

the design basis of multi-unit -operation

and

incorporated factors for temperature

correction,

design, margin

and aging

consistent with the

SER.

To address

the issue of loss of ventilation during

an

SBO event, the licensee

generated

Calculation MD-(0031-930059,

Control

Bay Transient Analysis - Loss

of HVAC, Rev 0, dated July 12,

1993,

and Calculation MD-N0999-890021,

Loss of

Ventilation during Station"Blackout,

Rev 3, 'dated

March 31,

1992.

The

inspector reviewed these calculations

.and observed that the temperatures

in

the control

bay,

HPCI rooms,

RCIC rooms

and the main steam tunnel

were

calculated to remain at acceptable

levels during

a postulated

SBO event.

Also, Calculati'on

BFNAPS4-004,

Appendix .R - HVAC Review,

Rev 0, dated

December

6,

1988,

demonstrated

that temperatures

in the swi.tchgear

rooms would remain

at..acceptable

levels:during--a- postulated

SBO event.

The license

had addressed

the issue of containment isolation capability

associated

with a

SBO event through Calculation ND-N0999-890021,

Station

Blackout Equipment List, Rev 4, .dated January,2$ ,

$ 995.

,As

a result of the

0

il

22

analysis

in this calculation, certain valves are included in AOI-57-1A to be

position -perified by the operators.

The inspector

concluded that the

SER

recommendation

in the area of containment isolation valves

had

been fulfilled

by the licensee.

The inspector concluded that the licensee

had provided sufficient training to

operators

on the subject of coping with an

SBO event.

Training plans

OPL173R200

and

OPL173S116 outlined the classroom

and simulator training for

SBO.

In addition,

Job Performance

Measure

No.

166 provided for training

personnel

to observe

operators

walking through the AOI-57-lA steps

performing

realignment of power sources

to re-energize

HVAC equipment

from available

diesel

generators.

The inspector reviewed diesel

generator start

and run failure records

and

unavailability,

and observed that the target reliability was being maintained.

Overall, the inspector concluded that the licensee

had implemented the SBO-

rule for Unit 3 in accordance

with the

SER.

There were

no outstanding

items.

6.5

Appendix

R Post-Fire

Safe

Shutdown Capability Safety Evaluation Report

Follow-Up Items

NRR review of the licensee's

proposed post-fire safe

shutdown capability,

as

described

by a December

20,

1994 submittal of the Fire Protection

Report

(FPR)

for simultaneous

operation of Units

2 and 3, identified three

items which

require verification by inspection prior to restart of Unit 3.

These

items

are:

1.

Verification that the next revision to the

BFN-FPR reflects the results

of the most recent cal'culations of maximum drywell temperature.

2.

Verification of the manual

action to transfer the

RCIC system suction

from the condensate

storage

tank to the torus from outside the control

room.

3.

Verification that

new manual

actions that

may be required

as

a result of

the

RWCU system modifications have

been considered

in the licensee'.s

listing of principal

manual

actions

and time frames.

With regard to inspector follow-up item I, inspection confirmed that the

licensee

has

documented

the required

changes

to address

the maximum drywell

temperature

calculation in the

BFN FPR.

The licensee

has drafted

a

FPR

revision to incorporate the required

changes,

and is tracking these

changes

as

an open item (Punchlist

Item REC-0208) to ensure

implementation

before

BFN.

Unit 3 restart.

Inspection confirmed the changes

are appropriate.

The

licensee's

open item tracking provides reasonable

assurance

the required

changes will be completed

as required.

Therefore,

inspector.fol-low-up-item I

is closed.

t

With regard to inspector fol-low-up. item 2; the licensee

provided information

from procedure

2/3-SSI-16,

which provides instructions for the manual

actions

to transfer the

RCIC system suction to the torus.

Inspectors--confirmed

the

Ik

23

instructions

accomplish this action outside the control room.

Therefore,

inspector follow-up item 2 is closed.

For inspector follow-up item 3, the licensee

provided draft changes for

procedure

2/3-SSI-3-3,

specifying manual actions required for operation of

components

isolating high temperature

piping from low temperature

components.

The licensee

also provided draft changes

.to the

BFN FPR. addressing, the

BFN

Unit 3 configuration.

These

items are being tracked

as part of Pun'chlist

Item REC-0195.

Inspection confirmed the changes

are appropriate.

The

licensee's

open item tracking provides reasonable

assurance

the required

.'changes will 'be completed

as required.

Therefore,

inspector follow-up item 3

is closed.

These conclusions will also

be documented

in the

NRR safety evaluation of the

.'BFN post-fire safe

shutdown capability.

6.6

Review of Electrical Calculations for Unit 3 (TI 2525/lll)

The Electrical Distribution System Functional

Inspection

(EDSFI) was conducted

in 1992

and documented

in NRC Inspection

Report 50-269,

270, 296/92-15. 'he

EDSFI concentrated

primarily on Unit 2 and shared

systems.

The purpose of

this current inspection

was to review those

areas of Unit 3 electrical

systems

design not reviewed during the .EDSFI or during previous Unit 3 restart

inspections.

The sample of calculations

selected

by the inspector for this

review excluded those calculations

which had been 'inspected

in previous

inspection efforts.

These

included fuse .calculations,

thermal

overload

calculations,

and cable,ampacity

calculations.

The inspector reviewed the following calculations:

.

'D-Q0057-920034,

4 .KV and 480

V Busload

and Voltdrop

ED-Q3057-920035,

Diesel

Load Study

.ED-Q3057-920036,

480V System,

Motors and:Miscellaneous

Loads Voltage Drop

ED-Q3999-930130,

Unit 3 Slow Bus Transfer

ED-Q0057-910236,

4KV Short .Circuit

ED-Q3057-910237,

480V Short Circuit

ED-Q3082-920354,

Undervoltage Analysis of Electrical Auxiliary System During

Diesel Generator

Load Sequencing

ED-Q3999-910224,

Cable

and

Bus Protection/Breaker.

Coordination for 4KV

Switchgear

and

480

V Loadcenters.

The inspector

reviewed-.each

of these calculations for accuracy

and to ensure

the calculation

scope

encompassed

the design basis of the electrical

system.

The inspector also reviewed

each of the problems identified.'n th'

calculations to ensure that they:were .being corrected

or had

been corrected

by

0

0

I~

24

the Unit 3 restart effort;

'The inspector did not identify any calculation

errors

or

any .problems that were not being adequately

addressed.

This item is

closed for Unit 3 restart.

7.0

Procurement

Engineering

Group (IP 38703)

The object of this inspection

was to review the program

and results, of the

commitment

made in the Nuclear Program Plan

(NPP), dated October 24,

1988,

regarding Section

12.0,

Component

and Piece 3?art Qualification for Unit 3.

The original commitment stated

two goals: "

,Goal

1:

BFN will verify that 'previously. environmentally qualified.

equipment

has not been degraded

through the use of spare

and replacement

items.

'oal

2:

BFN will establish.

programs

and practices that will ensure that

,previously qualified equipment will not be degraded

in the future

through the use of spare

and replacement

parts:

Goal

2 for the evaluation 'of installed

commercial

grade .replacement

items

and

remaining inventoried commercial

grade

spare parts

was revised

as stated

below

and the Goal regarding installed material

was withdrawn based

upon Generic Letter 91-05,

issued April 9,

1991.

The revised

Goal

2 was restated

as

follows:

Establish administrative controls to ensure that in-stock commercial

grade

items will not be issued for installation in a safety-related

app1ication

unless

they have

been evaluated

in- accordance

with the

established

site procedure.

Goal

1 addressed

the qualification program for safety-related

components

in

.

10

CFR '50.49

(EQ) applications..

Goal.

2. addressed

safety-related

components

in

non-10

CFR 50.49 applications.

BFN Procurement

Engineering

Group

(PEG)

had

completed all actions,

as originally committed for Goal

1, to ensure that

previously

EQ equipment

had not been

degraded

through the use of spare or

'eplacement

parts or items.

The inspectors

reviewed the closure submittal for

Goal

1, which listed four open items which were required to be closed prior to

BFN Unit 3

EQ certification.

PEG indicated that one item, related to the

QA

closure of two PERs which was to be tracked

and closed separately,

had already

been

accomplished.

A second

item, issuance

of an EQ.binder

(Cabl-0053)

had

been completed.

The remaining

two open items, related to maintenance

work

order review,

and incorporation of field walkdown sheets

into

EQ binders,

were

targeted for completion

on November 3,

1995,

and

November 8,

1995

respectively.

These

two items were closed

by TVA as planned.

The inspectors

concurred with the completion of Goal l.

BFN had establ.ished

barriers

and procedures 'to"ensure that in.-.,stock commercial.

grade

equipment,

Goal

2 items, .will not.be issued-.for -instal.lation. in a

safety-related

application

unl.ess. they have

been evaluated

in accordance

with

SSP-10.5,

"Technical Evaluation for Procurement

Materials

and Services,"

Revision.

9. and .O-TI=.329, "Evaluation of Components

an Piece Parts

Procured

il

il

il

25

Prior to the Implementation of BFNP Commercial

Grade Dedication Program,"

Revision l.

Generic Letter 91-05,

issued April 9, 1991, states "...the

(NRC) staff does not

expect licensees

to review all past procurement."

Therefore,

TVA revised the

scope of their commitment which was issued

October 24,

1988, to exclude the

review of those

non-Eg items that were installed prior to October

1,

1988.

(The selection of October

1,

1988,

as

opposed to April 9,

1991, is

conservative.)

7.1

Summary of Actions Taken to Complete

Eg Equipment,

Goal l.

This activity was accomplished

by:

1)

Reviewing the plant's maintenance

history to identify the

activities that have replaced safety related

components

or items.

2)

Performing

an evaluation of replacement

items that have

been

installed in 10 CFR 50.49 systems.

3) 'Performing

an evaluation of the

10 CFR 50.49 inventoried

commercial

grade

(and/or ANSI N45.2) spare parts to assure that

th'eir subsequent

use will not degrade

previously qualified

equipment.

This process

was implemented

and controlled by site approved

procedure 0-TI-

329,

"Evaluation of Components

an Piece Parts

Procured Prior to the

Implementation of BFNP Commercial

Grade Dedication Program," Revision

1.

4)

Taking credit for existing programs that qualified

Eg components

by walkdown.

5)

Taking credit for Eg components qualified by evaluations.

6)

Taking credit for Eg components, replaced

by DCNs.

For all components

evaluated

by the Unit 3

Eg Project,

evaluations

were

controlled by PI 88-11,

"Preparation,

Haintenance,

and Control of

Environmental gualification

.Documentation

Packages

(EgDPs)," Revision 6,

Section 4.2.9.

7.2

Summary of Actions. Taken to Complete

Non-Eg Equipment,

Goal

2.

The original commitment approach to satisfy these

goals

had

been formulated at

a point in time when the impact

on qualification of the host components

and

plant safety at

BFN and throughout the. industry- had not been firmly

established.

Therefore,

the commitment included review of past

procurement

for items installed in the plant,

as well as items still. in inventory.

Since

that time however,

Generic Letter 91-05. had been

.issued. which established

that

licensees

were not expected to review all past

procurement

unless

problems

with a specific vendor's or supplier's

products

were found during current

procurement activities.

26

Since the time that

TVA made the original commitment,

several

other changes

had also occurred.

Primarily, the scope of items

had changed

because

a

significant number of items that were installed prior to October

1,

1988,

had

been

removed

from service

due to extensive

design modifications

and normal

maintenance

of plant equipment.

Procurement of replacement

commercial

grade

items subsequent

to October

1,

1988,

had

been specified

and accepted

so

as to

be consistent with the industry

(EPRI) guidance that was endorsed

by NRC in

Generic Letter 89-02

and later discussed

in Generic Letter 91-05.

As

procurement

engineering

processes

had improved, the population of remaining

items decreased.

Since that time, replacement

commercial

grade

items

had

demonstrated

satisfactory in-plant performance with no adverse

trend to.

suggest that items were replaced

due to inherent part defects or non-

conformance.

Improvements of site 'procurement

engineering

processes;at

BFN,

and other

activities

had

been

implemented to gain additional

assurance

that installed

commercial

grade

items:would perform as designed

and not degrade

the

qualification of their host components.

These actions

had included evaluating

commercial

grade

items to determine

the extent to which inadequate

engineeri.ng

involvement in the procurement

process

may have resulted

in either the

improper classification of items, the incorrect specification of items, or

incomplete acceptance

documentation;

and evaluating the extent

commercial

grade

items

had

been installed in applications

other than those for which they

were previously evaluated.

The resul.ts of evaluations

performed indicated that in only 3 out of

approximately

1300 reviews did previous procurement

processes

and

documentation result in items that

had degraded

the original qualification .of

their host components.

These

items were further .evaluated

under TVA's

Corrective Action Program

and none

had created

a plant operability concern.

The results

indicated that 1) commercial

grade

items were installed in safety-

related: appl;ications for which they were evaluated,

and

20 gA Level

3 items

(installed in a safety-related

component for which it was not original=ly

designed),.

were suitable .for their installed applications.

Using the

NRC guidance of Generic Letter 91-05

as

a basis,

and the assurance

gained

from years of -satisfactory in-plant performance of remaining pre-

Octobei

'1,

1988,

commercial

grade replacement

items,

BFN concluded that

further review of .installed commercial

grade

items

was

no longer necessary

to

ensure that previously qual.ified equipment

was not degraded

through the use of

these

items.

Therefore,

the original concern identifie'd in NPP Volume III had

.been resolved.

Continuous

improvements

made to

BFN procurement

processes

since October

1,

1988, extensive site-specific evaluations of past

procurement

performed to date,

and lessons

learned

from similar evaluations

in the nuclear

industry since

1988 supported

these

conclusions.

Goal

2 addressed

commercial

grade

items

(gA2 items) which were in 'inventory

and intended for safety-related

application.

The substance

of the commitment

remained

unchanged

because

the revision simply clarified the original

commitment

and provided more detail to facilTtate closure.

0

0

27

The revision allowed for closure of the commitment

by using, administrative

controls which prevent issue of commercial

grade

items for safety-related

applications

unless

they had

been evaluated for those specific end uses.

Examples of the controls which had

been applied to the items are to down-grade

to gA3 or gAO, surplus,

or put the items

on hold.

The inspectors

toured the

warehouses

and noted that the

gA2 items had

been

tagged with appropriate

hold

tags.

The revision also specified that technical

evaluations

would, meet

either plant-approved

procedure

SSP-10.5

or TI-329.

SSP-10.5

was the process

by which safety/quality-related

items were currently procured,

and met current

industry guidance.

TI-329 was the procedure

developed to evaluate

past

procurement (prior to October

1,

1988) of commercial

grade

items for use in

safety-related

applications.

7,3

Verification of the Piece Parts gualification Program

and Results

The Inspectors verified. the program

and results

by reviewing the procedures

used to accomplish the goals.

These were:

O-TI-329, "Evaluation of Components

and Piece Parts

Procured Prior to

the Implementation of BFNP Commercial

Grade Dedication Program,"

Revision

1.

SSP-10.5,

"Technical Evaluation for Procurement of Materials

and

Services,"

Revision 9.

PI-88-11,

"Preparation,

Maintenance,

and Control of the 'Eg Documentation

Packages,"

Revision 6.

SSP-10.2,

"Material Receipt

and Inspection," Revision

14.

The inspectors

met with various managers

and supervisors

involved in the

procurement

piece parts

program,

which included Nuclear Stores,

PEG,

Procurement

Engineers,

Purchasing

personnel

and gA/gE personnel.

During these

meetings

the process

and results

were described

.in detaij..and

any questions

regarding the program were satisfactorily .answered.

The inspectors

reviewed

'ssessment

NA-BF-94-114, "Special

Assessment 'of:the:Evaluation of Components

and Piece Parts

Procured Prior to the Implementation of Browns Ferry Nuclear

Plant Commercial

Grade Dedication Program," dated

September

7,

1995.

The

assessment,

performed

by guality Engineering,

was to verify that components

and spare parts associated

with 10 CFR 50.49 equipment

were being adequately

evaluated

to -ensure the

Eg status of BFN3 was not degraded.

The assessment

reviewed the scope

and adequacy of the evaluation,

contract requirements,

work

history review,

and engineering

evaluations.

The assessment

identified

several

deficiencies related to review of, supporting documentation

and

previous evaluation,

identification of references,

and work history reviews,

and documented

the deficiencies

on

PERs.

PEG had addressed

the

PERs

and

was

preparing to close

them out.

The inspectors

also discussed- the assessment

with the-'equal-i;ty,- Engineering-'personnel.

involved 'who indicated that they had

concluded that the assessment

had

shown

PEG to be adequately

meeting the

requirements

of the implementing procedure..

0

0

28

In addition, the inspectors

reviewed several

evaluations that

PEG had

performed of inventoried

10 CFR 50.49 replacement

.items

and concluded that

PEG

had performed

adequate

evaluations

.in accordance

with applicable the

procedures.

Examples

as the reviewed evaluations

are

as follows:

Evaluation U3IEG-006, dated July 8,

1995, for Valcor Solenoid Valve

Model V526-529-2,reviewed

several

components

including

a switch block

assembly, coil, and ceramic rectifier.

For the Valcor components,

PEG

had concluded that the

POs for the replacement

items

had not imposed the

proper documentation

requirements for use in 10 CFR 50.49 applications,

the components

were not qualified for use in a

10 CFR 50.49 environment,

and .placed the inventoried components

in surplus.

Evaluation U3IEG-007, Revision 1, dated

September

27,

1995,

reviewed

a

Rosemount

Pressure

Transmitter

Model

1153 Series

B which included

an

electronic

assembly

hardware kit, adjustment

screw kit, valve stem,

and

sensor, module.

PEG had concluded that the

Rosemount transmitter

components

were acceptable

for Eg applications.

Evaluation U3IEG-004, Revision

1, dated August 25,

1995,

reviewed

SOR

Flow Switches

Models 103AS-B212-NX-JJTTX6,

103AS-B202-NX-JJTTX6',

and

103AS-B803-NX-JJTTX6, which included components

o-ring and cov'er

gaskets'.

PEG had concluded that the

SOR Flow Switch components

were

acceptable

for Eg applications.

A walk-through inspection .of the warehouse

was also conducted.

The warehouse

space

was impressive in that"it,was very clean.,an

wel,l organized.

Material

and items were labeled

and tagged

These discussions

and review of procedures listed, above,

review .of Assessment

NA-BF-94-114 and discussion with gE personnel,

review of the

PEG evaluations

for inventoried

Eg parts,

arid inspection of the warehouses

led the inspectors

to concl'ude that the program in place

was adequate

and satisfactory to

complete the goals.

Based

on the procedures

reviewed, discussions

with licensee

personnel

and

observations

by the inspectors it is concluded that the commitment,

as

amended,

.in the

NPP is satisfied sufficiently for restart of Unit 3.

The

ongoing program to release

gA2 items

on hold currently held in inventory is

acceptable

as

a basis of control to ensure qualification of installed

materials or parts.

7.4

Procurement of Structural Material

By TVA From Mid-South Nuclear

A potential

problem was identified during an

NRC inspection of Mid-South

Nuclear,

Report

No. 99901270/95-01,

dated. September.-27,-

1995, related to the

purchase

of 2 inch, schedule

160,

ASME SA-106,

Grade

B piping.,

The .problem

identified that the -possibility existed-that all cri'tica1 characteristics

required to dedicate commercial'rade

materials for safety-related:

appl-ications

may-not have-been

appropriately

addressed.

IS

0

0

29

The

NRC report,

No. 99901270/95-01',

was received

by TVA Corporate

on October

23,

1'995,

but had not yet been distributed

by TVA to

BFN such that

BFN had no

knowledge of the potential

problem.

The report findings were discussed

with

PEG management

and it was discovered that

a section of the pipe in question

had

been released for a safety-related

application in BFN Unit 3.

Immediately

upon discovery the licensee

segregated

and tagged the remaining pipe in

inventory to prevent further

use

and the operation shift supervisor,

on duty

was notified of the discovery.

PER 951611

was prepared to initiate corrective

actions.

The licensee

determined that the

critical characteristics

test that was

lacking .was

a tensile properties test.

Therefore

a section of the inventoried

p1pe

was submitted to TVA's central laboratory for performance of this test.

The'test

was performed

on October 27,

1995,- and the results obtained

met the

tensile properties for ASME SA-106,

Grade

B, schedule

160 specifications for

seamless

carbon steel

pipe.

'ven though the material

was determined

acceptable

for use at

BFN, the

remainder of pipe was transferred to the scrap yard..

By scrapping

the

, material

and receiving acceptable

test results,

the

BFN PER 951611

was closed

and

removed

from the Unit 3 restart list.

TVA Corporate Materials Engineering

Group has

issued

a separate

PER,

CHPER 950128, to evaluate this problem from a

generic view and extent of condition.

One hundred

ASME Section III purchases

from Mid-South Nuclear for the past yea'r were identified and from these

20

were examined in detail to determine if any code compliance

problems existed.

.Results

were negative,

that is no code compliance

problems were identified.

Therefore this issue is resolved

as it relates to BFN3 restart.

No violations or deviations

were identified.

I

8.0

Review of Open

Items

(92700)

(92901)

(92902)

(92903)

(92904)

(TI2515/65)

~

.

g.

he

open items listed below were reviewed to determine if the information,

provided met

NRC requirements.

The determinations

included the verification

of compliance with TS and regulatory requirements,

and addressed

the adequacy

of the event description,

the corrective actions

taken',

the existence of

potential generic problems,

compliance with reporting requirements,

and the

relative safety significance of each event.

Additional in-plant reviews

and

discussions

with plant personnel,

as appropriate,

were conducted.

8. 1

(CLOSED)

LER 260/95-002,

Reactor

Scram Resulting

From A Turbine Trip Due

To A Sensed

Generator

Load Unbalance Condition Caused

The Actuation Of

The

ESF System.

On February 9,

1995,

a reactor

scram occurred

when the main turbine tripped

due to a stator cooling leak causing operation of a generator field ground

relay.

The water was leaking from the cooling water supply. mani.fold for the

generator rectifier"and. dripped onto rectifier electrical

components -creating

an electrical

path to ground.

The leak was repaired

and potentially damaged

=--components. were- repaired or replaced.

Preventive maintenance'o.

inspect

cooling water components

susceptible

to degradation

has

been

scheduled

to be

performed every eighteen

months.

In addition, the licensee

defeated

the main

0

30

generator

and turbine trip functions which are generated

by the operation of

the generator field ground relay.

The annunciator function due to this

condition is, unaffected.

This will allow time for operator action,to isolate

the ground

and perform repairs withou't experiencing

a generator

and turbine

trip.

8.2

(CLOSED)

LER 260/95-004,

Reactor

Scram Resulting

From Personnel

Error

During Surveillance Testing

Caused

The Actuation Of The

ESF System.

On March 30,

1995,

a reactor

scram occurred during the performance of

surveillaTfce"-2'-.".SI-4;"2.'B-'ATU(C), Core

and Containment

Cooling Systems, Analog

Trip Unit Functional Test,

which tested

among other things, the

ATWS

initiation logic.

The event

was the result of a personnel

error in which a

test performer prematurely turned the

ATWS test switch from the Test position

to the Normal position.

Personnel

action was taken against the individual

involved in the event.

.Labels

were attached

to the switches identifying them

as having unit scram hazard potential.

In addition the licensee

deleted the

ATWS logic test from 2-SI-4.2.B-ATU(A, B,

C,

and D).

This test is not

required

by technical. specifications,

however,

the licensee

intends to write a

separate

test to be performed every eighteen

months.

The initiation of this

test is being tracked

by the licensee's

tracking system

and is scheduled

to be

completed prior to the completion of the next Unit '2 refueling outage.

8.3

(CL'OSED)

LER 260/94-007,

Noncompliance

With IOCFR50 Appendix

R Results

In Unit 2 Being Outside Its Design Basis

And In A Condition not Covered

By The 'Plants Operating Instructions.

'On September

29,

1994, 'the licensee

identi.fied that

IEC Bus

2B which supplies

a Unit 2 suppression

pool level indication would be made unavailable

due to a

fire occurring in Fire Area 18.

Upon discovery of this condition, the

licensee

entered

a Unit 2 Appendix

R limiting condition of operation

which

established

compensatory

measures.

Long term corrective actions

included

revising the Safe

Shutdown

Program to correct the compensatory

measures

for

loss of IK Bus

2B and revised the calculations

and procedures

to allow the

use..of the alternate

feed to I8C Bus .2B for a fire occurring in Fire Area 18.

In addition,

a comparative

r5view twas 'per'formed

between the Appendix

R Safe

Shutdown

Progr'am

and the Appendix

R calculations. to identify any other

potential discrepancies.

Those identified .were also corrected.

8.4

(CLOSED) (Unit 3)

LER 259/88-12,

Battery Failui e Concurrent with

LOP/LOCA Prevents

Automatic Start of Residual

Heat

Removal

Pump.

This

LER describes

a design

problem with electrical

systems identified by the

licensee

during

a design review;

The identified problem was that failure of

one battery would result in loss of DC power to one division of RHR system

logic and thereby

cause

the voltage sensing circuitry within the logic to

incorrectly enable the

RHR pump breaker to close onto

a dead

bus.

Therefore,

during the

10 second diesel

generator

start=-time-fol-lowing-a-.LOP-, the

RHR

breaker would close onto

a dead

bus.

At the

same time; there would-be

a trip

t

signal present -from-the- undervol-tage

load shed relays.

Simultaneous trip and

close signals

cause

the anti-.pump circuit to lockout the breaker.

The

corrective action

was to wire a normally closed contact from the undervoltage

il

31

load shed relays into the close circuit of the

RHR pumps 4o prevent closing

onto

a dead

bus regardless

of the functionality of%he

RHR system 'logic.

Then,,since

one

RHR pump in each division receives

a start signal

from the

RHR

system logic of both divisions, the failure of any one

DC power supply would

'ot

result in failure to start of both

RHR pumps of a division.

The inspector

verified the logic change

by reviewing the schematic wiring diagrams for the

RHR,pump motor breakers..

LER 88-12

was closed for Unit 3.

8.5

(CLOSED) (Unit 3)

LER 259/88-40,

Inadequate 'Design Controls Result in

the Backup Control

System Not Meeting Design Requirements.

This

LER addressed

problems identified by the licensee

during

a design review

with the as-installed

Backup Control System,

the requirements for which are

described

in FSAR Section 7.18.

The physical separation

requirements, of the

'Backup Control System are enveloped

by the Appendix

R requirements.

The

licensee

had

a special

program'to

address

Appendix R,

and this was reviewed

and inspected

by the Staff (refer to

NRC Inspection

Report 95-37).

Corrective

actions for this

LER were superseded

by the Appendix .R-.program.

'During this

inspection period,

the, inspectors

selected

a few corrective .action

modifications at random for implementation veWification.

From Design

Change

Notice W21814, the inspector verified that the transfer switches for valves 3-

PCV-001-0018,

-0019,

-0031

and -0179 were moved from the backup control

panel

to local panel

3-LPNL-25-0658.

LER 88-40 was closed for Unit 3.

8.6

(CLOSED) (Unit 3)

LER 259/89-25,

Design Errors. in 250

VDC Electrical

System Results in Unanalyzed

Condition.

=-'This

LKR involved three problems with the single failure criterion and

electrical

systems.

One problem applied to Unit 3.

RHR containment isolation.

valves 3-'FCV-74-47 (outboard)

and 3-FCV-74-48 (inboard)

have independent

power

supplies,

the .outboard is

DC powered

and the inboard is .AC powered.

However,

the inboard valve logic circuit power had been taken .from the

same

source

as

the motive power for the outboard

valve,:RNOV 3B, thus .violating the single

failure criterion.

'Review of system operation indicates that this failure

would represent

an unanalyzed

condition.

The corrective action

was to take

motive power for the outboard valve, 74-47,

from RHOV 3A.

This was consistent

~

with the overall division separation

scheme.

The inspector verified that the

power source

change

had

been

implemented 'by reviewing one-line diagrams

and

inspecting the distribution panels in the plant.

'LER 89-25 .was closed for

Unit .3.

8.7

(CLOSED) VIO 259,260,296/95-38-01,

Inadequate

Drawing And Procedures

r

The violation addressed

failure to have appropriate

procedures

and/or drawings

for activities that affected quality including Thermo-Lag installation.

The

inspector

reviewed the corrective actions for the Thermo-Lag issues

identified

in TVA's reply to the

NOV dated

September

6,

1995.

The inspector

concluded

that the- drawing

and procedure

revi'sions affecting the material control

and

installation of the Thermo-Lag adequately

addressed

.the violation-.=

Additional

review of Thermo-Lag design

comparison to Watts Bar details identified no

significant discrepancies.

The corrective actions

associated

with electrical

relay contact drawings were reviewed.

This violation .i.tern is=,closed';. '-

0

32

8.8

(CLOSED)

TI 2500/20,

Rev. '2, Inspection to,Determine

Compliance with

ATWS Rule,

10 CFR 50.62.

(CLOSED)

TI 2515/95,

Inspection

For Verification of BWR Recirculation

Pump Trip, Multi-Plant Action Item C-02.

The inspection for these

items covered the remaining .issues identified in IRs

259,

260, 296/95-22, specifically,. additional reviewof testing and"procedures

.upon completion of the ATWS/ARI/RPT modifications

on Unit "3 prior to recovery.

The modifications were tested

in accordance

with ECN P0126', 'Mechanical to

Analog Transmitter Trip System

(ATTS) modification, Post Modification Test

(PHT),

PMT-116 and

DCN W19321A, ARI/RPT Modifications,

PHT-258.

The ATTS

modi'fication replaced

old style mechanical

pressure

and differential pressure

indicating switches with more rel,,iable electronic

components

and included

many

other instruments

in addition to those .associated

with the

ATWS modifications.

PHT-116 functionally tested

the modification from the sensor to the analog

trip units

(ATUs).

PHT-258 functionally tested

the remainder, of the

ATWS

modification from the

ATUs to the actuating

components, i.e., the

recirculation

pump trip. breakers

and the control rods hydraulic control units

(HCUs).

The testing

was completed

October

10,

-1995.

The inspector reviewed the

completed

PMTs for completeness

and satisfaction of the pre-determined

~acceptance

criteria.

The inspector considered

the 'PMTs to be comprehensive

and to have successfully

demonstrated

the desired functionality of the

modifications.

An error in the design of the. ARI portion of the modification was revealed

during the

PHT.

Numerous intermittent fuse failures in the power circuit to

the ARI solenoid valves occurred.

The licensee ultimately attributed this

problem to the absence, of a .suppressor

diode around the solenoid coils..

Without the suppressor

diodes,

discharging the coils upon reset of the ARI

actuation

would degrade

the upstream fuses.

After several

actuation resets,

the fuses

would blow, disabl.ing subsequent

initiations for the affected

HCU.

The licensee

determined that .the

same problem had been revealed during the

Unit 2

ATWS PHT, but had not been factored into the modification for Unit 3.

Upon installation of the suppressor

.diodes for each

ARI solenoid valve, the

testing

was successfully

conducted.

The inspector'erified that appropriate surveillance instructions

(SI) existed

to satisfy the Technical 'Specification surveillance

requirements for periodic

actuation

instrumentation calibrations

.and functional tests.

The surveillances

were verified to be current

and entered into the licen'see's

surveillance

scheduling

process

with the correct frequencies.

The

TS required daily

instrument

channel

checks required

by TS 4.2.B for LIS-3-58A-D and

LS-3-58A-D=-

were verified to be included in the routine surveillance

procedures.

The inspector verified that Emergency Operating Instructions correctly

directed-manual

actuation of ARI in the event of ATWS in'dications.

.The.',Unit

3,

ATWS/ARI/RPT fs fiinctionally,equivalent to 'the Unit 2 system.

All training

-.

received

by the operators:for.'.Unit

2 is directly .applicable to Unit 3.

0

is,'

33

The Unit 3

SLC system

has

been established,

OPERABLE with the boron

concentration verified to be within the Technical Specification required

range.

.Based

on the above information, section 4.05 of TI 2500/20 is considered

closed.

IR 259,

260, 296/90-33

documented

inspection of the

ATWS related

gA

requirements

of Generic Letter 85-06 for Unit 2.

Inasmuch

as the

gA program

is common to both Units 2 and 3,

no further action is required to verify 'the

existence of gA program attributes for Unit 3.

Thus, section 4.06 of TI

2500/20 is considered

closed.

8.9

(CLOSED) Review of ATWS Issues for Generic Letter 83-28 Items 4.5.'2

and

'4.'5;3:(IP 37700)

The inspector

reviewed the licensee

actions

completed for Generic Letter (GL) 83-28 for Unit 3 restart.

Item 4.5 of the

GL identified

a

NRC position that

required on-line functional testing of the .reactor trip system,

including

independent

testing of the diverse'trip features.'n

TVA submittal

dated

March 15,

1984 in response

to the

GL,

TVA delineated

the Browns Ferry testing

requirements

for the reactor protection system.

The channel

functional

testing

scheme

was described with the frequency

and scope of this testing

used

as

TVA basis for not modifying the system to enhance testability..

The Safety Evaluation. (SE). issued

September

2,

1986 in response

to the

.

previous submittal

documented

a conclusion that

TVA had demonstrated

a

sufficient basis for:not requiring modification of the backup

scram function

to provide for on-line testability.

However, the

SE identified a requirement

to test the backup

scram function during refueling outages

and such testing

should

be included in,the Technical Specifications.

The inspector

reviewed

'he testing requirements

for the backup

scram function.

This festing is

included in Surveillance Instruction '3-SI-4. 1.A. 1, Reactor Protection

System

Mode Switch in Shutdown Functional Test. This test is required during

refueling outages.

Item 4.5.3 of .the

GL required confirmation from all licensees

that

on line

testing of the reactor trip system

was being performed.

The

NRC Safety

Evaluation Report

(SER) for Item 4.5.3 of the

GL was issued

August 17,

1990.

The conclusion of this report stated that the current test intervals are

sufficient to provide high reliability. All licensing actions

were considered

complete for Item 4.5.3 for Browns Ferry Unit 3.

Items 4.5.2

and 4.5.3 of the

GL '83-28 are complete.

The i'nspector

determined

that the licensee

actions

were adequate

for addressing

the items identified in

the GL.

This item was closed.

.8. 10

(CLOSED) IFI 296/95-37-02,

Performance of Simulated

Shutdown for an

.Appendix

R .Event

On September

7,

1995, the inspectors

accompanied

operations

personnel

on

a

walk through of -a simulated Appendix

R fire in fire area

16 (control

bay,.

II

0

II

34

including control room).

This effort was intended to be training on the

combined

U2/U3 SSIs

as well as

a enhancement

of the procedures.

This area is

regarded

as the most challenging safe

shutdown scenario

due the extensive

number of in-plant activities required.

Operators

simulated

performance of

plant activities

on Units '2 and

3 while the simulator was shutdown

as the "non

fire" unit.

The inspectors

(and operators)

noted

numerous differences

between

the labels

on the instal.led equipment

and the procedures.

The procedures

had

been through validation.

The inspectors

discussed

with licensee

management

-their conclusions that the exercise

involved more procedural validation effort

rather than operator training and verification of time .requirements.-

Following this initial observation, it was concluded that the inspectors

would

observe

an additional

safe

shutdown exercise drill scenario to ensure

the

licensee

properly demonstrated their ability to remotely shutdown the units

during

an Appendix

R event

and to verify the noted labeling problems

were

corrected.

On September

28,

1995,

a group of. four inspectors

observed

another

performance

of an exercise

involving the training of operations

personnel

in the use of

the Unit 2/3 Safe

Shutdown Instructions.

Again, Safe

Shutdown Instruction

2/3-SSI-16,

Control Building Fj.re on Elevation

593 through Elevation 617,

was

demonstrated.

A majority of'he previously noted labeling issues

had

been

corrected.

However, the inspectors

noted that

some Unit 2 "20 minute" actions

were accompl'ished

exactly at the

20 minute'ime limit. After these

concerns

were communicated to the licensee,

plant management

concluded that the drill

was unsatisfactory.

Site engineering

stated that there is some margin in the

20 minute requirement,

however,

the inspectors

noted that existing

SER for

Appendix

R exemptions refers to 20 minutes.

Following this demonstration,

the

licensee

stated that SSI 2/3-SSI-16 would be revised

by adding

an additional

remote operator for Unit 2.

Additionally, all of the Unit 2/3 SSIs would be

revised to address

multiple impedance faults.

On October 25,

1995, the residents

again observed

.the licensee's

performance

.of an Appendix

R Safe

Shutdown simulation for a fire in the control bay.

This

demonstration

involved simulating the remote

shutdown of both

U2 and

U3 from

their respective

remote

shutdown panels.

All labeling deficiencies

were

corrected."

The. licensee

revised. 2/3-SSI-16 for the control

bay which resolved

the inspectors

concerns

related to timeliness of Unit 2 remote operator

actions

(20 .minute).

The licensee

successfully

demonstrated their ability

(through the simulated. exercise)

to remotely shutdown Units

2 and

3 with the

Safe

Shutdown Instructions.

The SSIs for Unit 3 operation will be issued

prior to restart.

Based .on the inspectors

review,of this matter, this IFI is

.

closed.

8. 11

(CLOSED) THI Action Item 296/II E.4.2,

Containment Isolation

Dependability

Items

1 through 4, Diverse Isolation.

The .inspector

performed

a review of the licensee's

activities associated. with

this item-. --These-activit;ies=-are-:related:=to-those

for NRC Bulletin 80-06,

Engineered

Safety Feature

Rest"Control's;

which was closed-for Unit 3 in IR 95-

22.

Tlie licensee

was committed to ensuring that the containment isolation.

system design

complied with the requirements

of the Standard

Review Plan,

Section 6.2.4.

fl

35

The inspector

reviewed the applicable. Safety Evaluation Report issued

by the

NRC 'on January

5,

1995.

This

SER contained

an evaluation of information

provided in response

to NUREG-0737, -Item II.E.4.2.

The report evaluated

the

design of the containment isolation systems for BFN Units

1 and

3 and

compared

them to the previously evaluated

Unit 2 design.

The report concluded that the

containment isolation systems for Units

1 and

3 were acceptable

and that

no

differences

in Appendix J,

Primary Reactor Containment

Leakage Testing were

identified between the units.

The inspector reviewed supplemental

information

provided

by TVA concerning additional differences

between Units

2 and

3 and

noted that final

NRC acceptance

of the Unit 3 system configuration

was granted

in a letter dated October

18,

1995.

The inspector reviewed the system modifications associated

with this item

performed

under

DCN W17185A.

Field work on this modification was completed

on

August 25,

1994.

The inspector

noted that this work was previously inspected

and documented

in

NRC IR 95-16.

This .DCN installed the containment isolation

status

system,

as well as the modifications to TIP system required

by NRC

Bulletin 80-06.

As noted in IR 95-16, the remaining activities to be

inspected

involved the completion of post modification testing

and revision of

impacted

procedures

necessary

for return to operation.

The inspector

reviewed

the required post modification,testing

and noted that it included:

a number of

different valve and relay functional tests; circuit continuity checks

remote

position indication tests;

PCIS logic functional tests;

and the verification

of Containment Isolation System Status

(CISS) computer points.

The inspector

reviewed the completed test results

and noted that the various system

responses

were within the established

acceptance criteria

and that .any test

deficiencies

were identified, evaluated,

and corrected.

The inspector

determined that the post modification tests .appeared

adequate

to ensure that

the system performs

as designed.

During review of the:,post modi'fication

testing,

the inspector

noted that

a small portion of the testing

remained to

be completed.

This testing involved verification of CISS computer points for.

system which had

been turned over to operations.

Based

on .a schedule to

complete these activities,

the inspector

found the post modification testihg

acceptable for closure of this item.

The inspector

reviewed

a selected

number of procedures

.impacted

by the above

noted modifications to verify that the licensee

has completed all required

procedure revisions.

The .inspector

noted that the licensee

had completed all

procedure

revisions required

by the implementation

on

DCN W17185A.

The

inspector's

review of revised

procedures

confirmed that the licensee

had

adequately

revised =the procedures

to reflect the changes

associated

with the

modification.

Based

on

a review of the completed activities, the inspector

has determined

that the licensee

has satisfactorily completed all requirements

associated

with this .commitment,

and considers this item closed.

8. 12

(CLOSED)

TMI Action Item 296/I.L.E.4.2,, Containment

Isolati.'on

Dependabil.ity Item 6, Containment

Purge Valves.

The licensee

has completed the following actions to ensure that the

Containment

Purge isolation valves

met the criteria of '.Branch Technical

il

11

36

Position

CSB 6-4.

BFN Unit 3 containment isolation system design

compliance

with Branch Technical Position

CSB 6-4 has

been evaluated

and accepted

by'the

NRC in a letter to TVA dated July 1,

1985.

Calculations

analyzing the effects

of a

LOCA occurring while purging the Containment

and impacts

on the Reactor

Building ductwork, Secondary

Containment,

and Standby

Gas Treatment

systems

were completed satisfactorily in 1991.

The stroke times of the containment

purge isolation valves were reduced

through the implementation of ECN P0384.

This

ECN replaced

the solenoid valves

and supply tubing for the valves

and was

.completed in September of 1993.

Debris screens

were installed

on the

'ontainment

purge lines in August of 1981 through the implementation of ECN

P0428.

Lastly, the containment

purge isolation valves were"replaced

under

DCN

W18233,

completed in September

1993.

The replacement

valves

have

a different

seat

design resulting in better sealing capability and requiring lower valve,

operator torque.

The licensee

has completed all of the actions

noted

above in

fulfillment of i.ts commitment to Branch Technical

Position

CSB 6-4.

The inspector

has reviewed

and evaluated

the licensee's

efforts as various

activities have

been completed.

The inspector

reviewed the implementation of

the system modifications

and documented this review in NRC IR 95-16.

Following the completion of these modification activities, the remaining

actions to be reviewed involved the implementation of post modification

testing

and procedure revisions.

The inspector

has reviewed the post

modification test activities associated

with ECNs

P0384

and

P0428

and

DCN

W18233.

These test activities included:

remote operation

and 'indication;

LLRT; leak'esting;

and closure/stroke

time testing.

The inspector

has

reviewed the results of ,these completed test activities

and noted that test

deviations, were properly identified, evaluated

and- corrected.

The inspector

noted the testing reviewed

appeared

adequate

to ensure

proper operation of the

systems.

The final area,to

be inspected

involved

a review of:procedures 'to ensure that

'all impacted procedures

were properly 'updated.

The inspector reviewed the

modification packages,

associated

documentation

and noted that the licensee

has completed all procedure revisions required for return to operation.

The

inspector reviewed the current revisions of selected

procedures

to ensure that

.,

these activities have

been

completed'.

The inspector noted that the procedures

reviewed

had all been properly modi.fied to,reflect the changes

associated. with

the plant modifications.

'Based

on

a review of the completed activities, the inspector

has determined

that the licensee

has satisfactorily completed all requirements.

associated

,with this commitment,

and considers this item closed.

8. 13

(CLOSED)

IFI 296/94-18-02, .Condition of Unit 3 Containment Coatings,

During the performance of a containment

coatings

inspection in August,

1994,-

the

NRC determined that containment

coatings

were being properly controlled at

Browns Ferry.

However, at the time of that inspection -effort, over 4000

square feet of Unit 3 containment

coatings

were not- DBA"qualified.

The=.-

licensee's

calculations. stated-that

only 157 square feet .of unqualified-

(uncontrolled) coatings

could exist within primary containment

and not exceed

il

II

37

the 65 percent

ECCS suction strai'ner

blockage criteria.

The above stated IFI

was

open pending resolution of this matter.

On November 6,

1995, following extensive evaluation

and effort to reduce

certain coatings to a dry film thickness of (0.003", the total

amount of

unqualified (uncontrolled) coatings within. Unit 3 primary containment

was

reduced to 118.2 square feet as delineated

in the Unit 3. Primary Containment

Uncontrol,led Coatings

Log (Calculation

Number MD-93303-940038).

The log also

stated that the application of Valspar

78 coating to stainless

steel

was

now

DBA qualified therefore allowing the coating to remain

on the

SRV T-quenchers

and other stainless

steel

surfaces within containment.

The inspector reviewed-

the calculation (uncontrolled coatings log) and found it to be acceptable.

In

addition, the inspectors

toured the drywell

(November 8)

and the torus (prior

to fil.,l:ing),,:and found the condition of the coatings to be acceptable.

Based

on .this Ye'0'i'ew, XPe, inspectors

have determined that the coatings within Unit 3

primary containment

are'acceptable

for Unit 3 restart

and this item is

considered

closed.

8. 14

(CLOSED) TMI Action Item II.F.1.2.D (Formerly II.F. 1.4)

Containment

Pressure

(Accident) 'Monitor (Unit 3).

As presented

in IR 95-31,

some review of this item was previously conducted.

However, the issue

remained

open pending,

equipment calibration/testing

inspections,

instrumentation string functional'testing,

and following

approvals of related pressure

component testing,

maintenance,

and operating

procedures.

An inspector

reviewed/observed

closure activities for the

'remaining .issues

and noted the following:

Instrument string testing for the wide range .accident:monitoring strings

(PT-64-160A 5 160B)

was performed.on

October

16

8 17,

1995 .and results,

received/reviewed

October 30,,were satisfactory.

Based

upon this review and examination of related

component

procedures,

TMI

Action Item II..F.1.2.D, (.II.F.1.4), is closed for Unit 3.

8. 15

(CLOSED)

TMI Action Item II.K.3.18, A'utomatic Depressurization

System

(ADS) Logic Modification '(Unit .3).

Previous review of this item was addressed

in IR 95-43.

However, the issue

remained

open pending,

additional inspection of ADS component operability,

performance of ADS functional testing, testing of the

ADS logic and completion

of proposed

changes

to plant maintenance/testing

and operations

procedures.'n

October 23,

1995, logic train "A" testing

was performed,

on October

24,

"B"

testing

was perfo'rmed

and results,

received

and reviewed

on October 31, were

found to be satisfactory.

An inspector

reviewed closure activities for the

remaining issues

and noted the following:

The improved,

ADS timer met the::prescribed

Unit 3'echnical

Specification

(Section 3.2.B.) setpoint;.of: 95. (+/.-7).-seconds..--

-.-

"New" initiation logic inhibit switches

operated

as designed.

0

38

The "new" ADS logic train time delay relays operated

as designed.

Mhen the manual

"A"/"B" keylock switches

were operated,

the "new" alarm;

"ADS LOGIC BUS A OR

B INHIBITED", functioned

as designed.

Based

on these

reviews,

THI Action Item II.K.3.18, is closed for Unit 3.

8.16

(CLOSED) THI Action Item I.D.2 (Specifically Action Item I.D.2.2

Installation)

Safety Parameter

Display System

(SPDS - Unit 3).

Previous review of this item was addressewd

in IR 95-22.

However, the issue

remained

open pending completion of a licensee

Post Hodification Test

(PHT)

229 and::a status .of Unit 3 system tie-in to the Integrated

Computer

System

(ICS).

The

PHT,

a test of thermocouple, digital signal

and "sequence-of-event"

inputs into the

ICS neutron monitoring instrumentation strings,

was

performed

November 7,

1995.

Results of this testing

was received

and

'reviewed

November

8 and found to be satisfactory.

System tie-in to the

ICS.was

completed

November 7.

Remaining action plan issues for TI2515/65 - 3.02.b.(2)

[Equipment

Calibration],

and 3.02.b.(3)

[Operability) - have

been adequately

addressed

by the licensee.

Based

on these

reviews,

THI Action Item I.D.2 specifically, I.D.2.2

("Installation" ) - is closed for Unit 3.

8.17

(CLOSED)

GSI 75

(HPA B085);

GL 83-28,

"Required Action Based

On Generic

Implications Of Salem

ATWS Events",

Section 1.2, "Post-Trip Review (Data

and Information Capability)" (Unit 3).

Licensee

computer capability to record data pertinent to a unit reactor trip

~is

an integral part/capabil1ty of the previously mentioned Unit 3 SPDS.

2'apabilities of assessing

"'sequence-.of-events",

"variable time-histories",

and

"unscheduled

reactor

shutdown probable-cause"

are met with the installed

system.

Based

upon present

status of the installed Unit 3 system

and closure

of the prior THI Action Item, Item I.D.2, this capability issue,

(GSI 75), is

also addressed

and closed for Unit 3.

8. 18

(Closed, for U3 Restart)

Bulletin 93-02

and 93-02,

Supplement

1, Debris

Plugging of Emergency

Core Cooling Suction Strainers

Bulletin 93-02

(and supplement

1) were issued

by the

NRC to notify the

operators

of light water reactors of the potential for debris plugging of ECCS

suction strainers.

This inspection, documents

the licensee's

readiness

to

restart Unit 3 as it relates to thi's matter.

The corrective actions

performed,

for Unit 3 are equivalent to those

performed

on Unit 2 and previously accepted

by the Office- of 'Nuclear Reactor Regulation.

The inspectors

reviewed the

correspondence

related to this bulletin.

.In addition, the inspectors

performed

a detailed

walkdown of the Unit 3 drywell for temporary

and

4

IS

39

permanently installed fibrous material.

During the walkdown, the inspectors

noticed that the fibrous material

permanently installed inside various drywell

penetrations

(the

NRC was -informed of these penetrations

in correspondence

related to this Bulletin) was in a condition such that the insulation

was

flush with inboard side of the penetration.

The inspector discussed

this

matter with site engineering

personnel.

The engineers

stated that this

material

would be "trimmed back" such that the fibrous material

remaining

within these penetrations

would be shielded

in the event of an accident'nd

thereby minimizing the possibility of the material

being transported

to the

suppression

pool.

The inspectors verified the fibrous material

had

been

trimmed back.

No temporary or any additional

permanently installed fibrous

material

.was identified by the inspectors.

In addition,

the. inspectors

verified that the Unit 3,EOIs appropriately .addressed

ECCS

pump

NPSH concerns.

Also reviewed were the operator lesson

plans

and simulator scenario. addressing

ECCS suction strainer .plugging.

These

were found to be acceptable.

Lastly,

the inspectorgccompan'ied.

the licensee

on the final drywell closeout,

performed in accordance

with 3-GOI-200-2, .Drywell Closeout,

and found no

fibrous material.

Based

on these reviews,

the inspectors

determined that the

actions required

by Bulletin 93-02 (including supplement I) were accomplished

satisfying the requirements

for the restart of Unit 3.

8.:19

(Closed, for U3 Restart)

'Bulletin 95-02,

Unexpected

Clogging of a

Residual

Heat

Removal

(RHR)

Pump 'Strainer While Operating in Suppression

Pool

Cool.ing Mode

Bulletin 95-02 was issued

by the

NRC (on October

17,

1995) to notify the

operators of boiling water reactors of the potential for debris plugging of

RHR suction strainers while 'operating in the suppression

pool cool.ing mode.

'his inspection

documents

the licensee"s

readiness

to restart. Unit 3 as it

relates to this matter.

During the recovery of Unit 3, the inspectors

have

'closely

monitored the licensee's

actions related to the torus.

This included

a detailed inspection of the .torus prior to filling (which included

cleanliness

of the entire pool area

and strainers

and inspection of coa4ings).

Following torus fill, the licensee

had

an event in which a vacuum bag

became

lodged in the 3A,core spray

pump.

,As

a result of this matter,

the licensee

performed

.a complete

underwater

inspection,and

vacuuming of the torus.

The

licensee

also stated that they would perform an additional inspection of the

torus just prior to the units restart.

The licensee

responded

to this

bulletin in..a letter to the

NRC on November

15.

On November

16, the licensee

compl'eted

a complete

underwater

vacuuming of the torus including

a cleaning of

the,ECCS suction strainers.

Material

removed from the torus included the

remnants of the previously discussed

vacuum

bag

and silt from piping corrosion

products.

Following the vacuuming of the torus, the licensee

ran

2

RHR pumps

for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> in the suppression

pool cooling mode,

which pumped

an equivalent

of almost three times the torus volume through the

ECCS suction strainers.

Upon completion of the torus flush, di.vers- reinspected

and video" taped the

conditi'on of- the-'ECCS suction: strainers-.-

The strainer s were found to be-

essentially free of any debris.

In addition to these actions,

the licensee's

response

to this bulletin was

reviewed

by .NRR and discussed

in,phone call with the licensee

on November

16;

40

NRR -found that the licensee's

response

was satisfactory

pending the results of

the flushing and reinspection

discussed

above.

NRR was advised of the

satisfactory

underwater .inspection results

on November

17 and concurred that

no issued

remained preventing the restart of Uni.t 3 related to bulletin 95-02.

Based

on these

reviews, the inspectors

determined that the actions required

by

Bulletin 95-02 were accomplished

satisfying the requirements for the restart

of Unit 3.

, e

8.20

(CLOSED) 296/IFI 95-31-06: Potential

Unit 3

Eg Program Deficiencies

Eg

ISSUES

During a guality Assurance

assessment

of the .Unit 3 IOCFR50.49 Environmental

guaTification Program,

a number of findings wer e made which brought the

effectiveness

of the Unit 3 program into question.

The predominant finding

dealt with the fact that

some Unit 3'g equipment

was potentially wo} ked as

non-Eg.

To determine the extent of the condition, the licensee

formed

an

incident- investigation

team.

The team determined that

a window of

vulnerability existed

from November,

1992,

(time at which recovery workplan

write began) until July,

1994,,when

a revision'to the site standard

practice.

controlling the

Eg program at

BFN (SSP 6.5)

was issued.

The

SSP 6.5 revision

laid out

a program to install, modify,, and .maintain all equipment designated

as

Eg in accordance

with 10 CFR 50.49 requirements.

The licensee

performed

a,

review of work plans

and work orders ~performing work on

Eg components

during

the window of vulnerability to ensure that components requiring environmental

qualification are baselined

as such.

The review wa's performed

on

a system

basis

as part of the

SPOC activities.

The licensee

performed incident investigation

BFPER950469 to address

the

issue.

The inspectors

reviewed

BFPER950469

and verified the corrective

actions

incl.uded completion of the Unit 3 50.49 list and

gMDS Manual'.and

revision of SSP 6.5.

Beginning the

Eg workplan effort prior to finalizing the

50.49 list and.

gMDS Manual also .occurred

on the Unit 2 recovery effort and was

the subject of a Unit 2 lessons

learned

item.

The Unit 2 lessons

learned

item

was not addressed

and

a Unit 3

Eg work,plan

and work.order review .was required

to baseline

the Unit .3

Eg program.

The incident investigation concluded that

the root cause

was inadequate

management

fol.lowup 'and monitoring of

activities.

-Procedure

TI-339,

Eg Review Project,

was prepared to implement the work

order/work plan review.

The work activities were categorized

into one of six

classes.

Class I items were activities which are periodically performed

and

the licensee verified the satisfactory'erformance

of the last activity

for'he

baselining effort.

Class

2 items were. activities which were controlled

independent of the

Eg status of the equipment.

Class

3 items were activities

which could be affected 'by .a work plan or work order.

Work plans

and work

orders

were reviewed for these

items.

Class

4 items were activities which

could

be affected

by. a work. order but not- a- work- plan.

Work-orders- were"

reviewed, for these

items.

Class

5 items were activities which were

recommended

not required-maintenance

activities in the--gMDS- manual..

Class-6---

items were activities which"were verified to .be-completed

or work orders

were

performed to complete the activity in lieu of a review of closed work

plans/work orders.

0

0

The completed

Eg system baseline

packages for systems 32,.69,

70,

and

90 were

reviewed.

The inspectors verified. that the

Eg components

in the system

packages

included .those

components listed in

EMS for the system.

The

qualification maintenance

items listed in the system

packages

were compared to

the activities listed in the

gMDS Manual.

No di,screpancies

were noted.

The

packages

were prepared

in accordance -with TI-339 and the activity

classifications

and detailed work order/work plan evaluations

were,acceptable.

Twenty-one selected activities were reviewed

and the inspectors verified that

the

WO/WP implemented the

gMDS requirements for the listed equipment.

No

discrepancies

were noted.

The inspectors

determined that the corrective

actions for IFI 95-31-06 were completed. -;This;item is closed.

9.0

Exit:Interview (30703)

t'la, sP"

The inspection

scope

and findings were summarized

on November 29,

1995, with

those, persons

indicated in paragraph

1 above.

The inspectors

described

the

areas

inspected

and discussed

in detail the inspection findings listed below.

Although proprietary material,was

reviewed during the inspection,

proprietary

information is not contained

in this report.

Dissenting

comments

were not

received

from the licensee.

Item Number

Status

VIO 296/95-60-01

Open

NCV 296/95-60-02

Closed

NCV 260/95-60-03

Closed

'-"VIO 259,'260,296/

Closed

95-38-01

Descri tion

Failure to Fol.low Approved Configuration Control

Procedures

Resulting in Misalignment of SDV

System

Components.

Loss .of Shutdown Cooling .Flow.

Failure -to,perform Diesel 'Generator Reliability

Determination.

Inadequate

Drawing and Procedures.

LER 259/88-12

Closed

Battery Fai-lure Concurrent with LOP/LOCA

Prevents, Automatic .Start of Residual

Heat

Removal

Pump.

(Closed for. Unit 3)

LER 259/88-40

Closed

Inadequate

Design Controls Result in the Backup

Control System Not Meeting Design Requirements.

(Closed for.Unit 3)

LER 259/89-25

Closed

TI 2500/20,- Rev.2 Closed

Design Errors in .250

VDC Electrical

System

Results in Unanalyzed Condition.

(Closed for

Unit 3)

Compliance- with ATWS Rule,

10 CFR 50.62.

TI 2515/95

Closed

42

BWR Recirculation

Pump Trip, Multi-Plant Action

Item C-02.

LER 260/95-002

Closed

LER 260/95-004

Closed

LER 260/94-007

Closed

Reactor

Scram Resulting

From A Turbine Trip Due

To A Sensed

Generator

Load Unbalance

Condition

Caused

The Actuation Of The

ESF System.

Reactor

Scram Resulting

From Personnel

Error

During Surveillance Testing

Caused

The Actuation

Of The

ESF System.

Noncompliance With lOCFR50 Appendix

R Results

In

Unit 2 Being Outside Its Design Basis

And In A

'Cendition not Covered

By The Plants

Operating

Instructions.

GL 83-28

Closed

Review of ATWS Issues for Generic Letter 83-28

Items 4.5.2

and 4.5.3

IFI 296/95-37-02

Closed

TMI Action Item

Closed

296/II E.4.2

TMI Action Item

Closed

296/II.E.4.2

IFI 296/94-18-02

Closed

TMI Action Item

Closed

II.F.1.2.D

(Formerly II.F.1.4)

TMI Action Item

Closed

II.K.3.18

TMI Action Item

Closed

I.D.2 (Specifically

Action Item I.D.2.2

Installation)

GSI 75,

MPA B085

Closed

BU-93-02

8

Supp

1

Closed

Performance of Simulat'ed

Shutdown for an

Appendix

R Event.

Containment Isolation Dependability

Items

1 through 4, Diverse Isolation.

Containment Isolation Dependability

Item 6,

Containment

Purge Valves.

Condition of Unit 3 Con'tainment Coatings.-

Containment

Pressure

(Accident):Monitor

,(Unit 3).

l

Automatic Depressurization

System

(ADS) Logic

Modification (Unit 3).-

Safety Parameter

Display 'System

(SPDS - Unit 3).

Required Action Based

On Generic Implications Of

Salem

ATWS .Events,

Section 1.2, Post-Trip Review

(Data

and Information Capability) (Unit 3).

Debris Plugging of Emergency

Core Cooling

Suction Strainers

(Closed for Unit 3 restart).

0

'BU-95-02

Closed

43

Unexpected

Clogging of a Residual

Heat

Removal

(RHR)

Pump Strainer While Operating in

Supression

Pool Cooling Mode (Closed for Unit 3

restart).

IFI 296/95-31-06

Closed

Potential

Unit 3

Eg Program Deficiencies

Eg

Issues.

i

0

10.0

ADS.

ANSI

AOI

APRM

ASME

ASOS

ASTM

ATTS

ATU

ATWS

AUO

BFNP

BWR

CISS

CILRT

DBE

DCN

DG

EDG

ECCS

ECN

EECW

EDSFI

EPRI

EQ

'EQDP

ESF

FPR

FSAR

GE

GL

GSI

HPCI

HVAC

ICS

IEEE

IFI

IR

kV

La

LER

LOCA

MPA

NCV

NPP

NRR

NRC

NSRB'

oIIAT

.Acronyms and Initialisms

.Automatic Depressurization

System

American National Standards

Institute

Abnormal Operating Instruction

Average

Power

Range Monitor

American Society of Mechanical

Engineers

Assistant Shift Operations

Supervisor

American Society for Testing

and Material

Analog Transmitter Trip System

Analog Trip Units

Anticipated Transient Without

Scram'uxiliary

Unit Operators

Browns Ferry Nuclear Plant

Boiling Water Reactor

Contai.nment Isolation System Status

Containment

Integrated

Leak Rate Testing

Design Basis

Event

Design

Change Notice

Diesel

Generator

Emergency Diesel

Generator

Emergency

Core Cooling System

Engineering

Change. Notice

Emergency

Equipment Cooling Water

Electrical Distribution System Functional

Electric Power Research

Institute

Environmental Qualification

Environmental Qualification Documentation

Engineered

Safety Feature

Fire Protection

Report

Final Safety Analysis Report

General Electric

Generic Letter

Generic Safety Issue

High Pressure

Coolant Injection

Heating, Ventilation,

and Air Conditioning

Integrated

Computer System

Institute of Electrical

and Electronics

Inspector Follow-up Item

Inspection

Report

Kilovolts

Allowable leakage

in wt. percent

per

day

Licensee

Event Report

Loss of Coolant Accident.

Multi-Plant Action Item

Non-Cited Violation

Nuclear Performance

Plan

Nuclear- Reactor Regulation

Nuclear.'Regulatory.

Commission.

Nuclear Safety Review .Board

Operating Instruction

Operational

Readiness

Evaluation

Team

Inspection

Packages

t

0

i

ORRT

Pa

PDD

PDR

PER

PMT

PORC

QA

QC

RCIC

RHR

RHRSW

RI-

RMOV

RPS

RWCU

SBO

SDV

SER

SI

SLC

SMART

SPDS

SRM

SRO

SSI

SSP

TI

TMI

TS

TVA

UL

USI

V

VIO

WO

WR

't-

Operational

Readiness

Review Team

Containment Accident Pressure

Potential

Drawing Deficiency

'Public Document

Room

Problem Evaluation Report

Post Maintenance/Modification Test

Plant Operations

Review Committee

Quality Assurance

Quality Control

Reactor

Core Isolation Cooling

Residual

Heat

Removal

Residual

Heat .Removal Service

Water System

Resident

Inspector

Reactor Motor Operated

Valve

Reactor Protection

System

Reactor

Water Cleanup

Station Blackout

Scram Discharge

Volume

Safety Evaluation Report

Surveillance Instruction

Standby Liquid Control

Senior Management

Assessment

of Readiness

for Restart

Team

Safety Parameter .Display System

Source

Range Monitors

Senior Reactor Operator

Safe

Shutdown Instructions

Site Standard Practices-

Temporary Instruction

Three Mile Island

Technical. Specifications.

Tennessee

Valley Authority

Underwriters L'aboratory

Unresolved Safety Issue

'Volts

Violation

Work Order

Work Request

Weight percentage

of containment

0

i

G.Wiseman

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btsmd Conduh Seal Teat

No. SSNN0.75417A

R35835474

R3583$ 480

R358354S1

R3583$ 482

R35835483

R358354%

Reactor BuMny.

FZ34 to

FZ 3 2/ 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

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lboc<<r BOMOS.

FZ 3Q ao

FZ 3 1/ 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

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pipe tkrovyh 4

above h

concrete Soot

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loam

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3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> Se<<<<et/

CTP 1001A, Peneiedrn

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Reactor BuMny,

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FZ3 T/1 hour

Reactor, BOMny.

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eon<<sto Se<<

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Nnlrnwn 8

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FZ 34 to

FZ 3 1/ 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

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eonddt <<e pbyyad to

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Can+ Brdr5ny.

FA 18 to

FA 1SI 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

2

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Attachment

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4

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