ML18016A981

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Announces Safety Sys Design & Performance Capability Insp Scheduled for 990719-23 & 0802-06,under Insp Rept 50-400/99-11.Forwards Info Requested for HHSI & Lhsi Sys
ML18016A981
Person / Time
Site: Harris 
Issue date: 05/28/1999
From: Landis K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Scarola J
CAROLINA POWER & LIGHT CO.
References
NUDOCS 9906140206
Download: ML18016A981 (81)


See also: IR 05000400/1999011

Text

CATEGORY 2

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

CESSION NBR:9906140206

DOC.DATE: 99/05/28

NOTARIZED: NO

DOCKET 'I

ACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina

05000400

AUTH.NAME

AUTHOR AFFILIATION

LANDIS,K.D.

Region

2

(Post

820201)

RECIP.NAME

RECIPIENT AFFILIATION

SCAROLA,J.

Carolina Power

& Light Co.

SUBJECT: Announces safety sys design

& performance capab'ility insp

scheduled for 990719-23

6 0802-06,under

insp rept

50-400/99-11.Forwards

info requested

for HHSZ

& LHSZ sys.

DISTRIBUTION CODE:

IEOlD

COPIES

RECEIVED:LTR J

ENCL J

SIZE:

TITLE: General

(50 Dkt)-Insp Rept/Notice of VioOLation Response

NOTES:Application for permit renewal filed.

05000400

RECIPIENT

COPIES

ID CODE/NAME

LTTR ENCL

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ZD CODE/NAME

LAUFER,R.

COPIES,

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INTERNAL: ACRS

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ERNAL: LMITCO MARSHALL

NRC PDR

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NUDOCS FULLTEXT

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NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DZSTRZBUTZON LIS:

OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU QR YOUR'ORGANIZATION

CONTACT THE DOCUMENT CONTR(

DESK

(DCD)

ON EXTENSION 415-2083

TOTAL NUMBER OF COPIES

REQUIRED:

LTTR

17

ENCL

17

May 28, 1999

Carolina Power 8 Light Company

ATTN:

Mr. James Scarola

Vice President - Harris Plant

Shearon Harris Nuclear Power Plant

P. O. Box 165, Mail Code: Zone

1

New Hill, NC 27562-0165

SUBJECT:

SAFETY SYSTEM ENGINEERING INSPECTION (NRC INSPECTION REPORT

NO. 50-400/99-11)

Dear Mr. Scarola:

The purpose of this letter is to announce

a safety system design and performance capability

inspection at your Harris facilitywhich is scheduled

for July 19 - 23 and August 2 - 6, 1999. The

inspection will be conducted using Inspection Procedure 71111, "Safety System Design and

Performance Capability", and willsupport the pilot for the new inspection oversight process.

A

team of six inspectors will perform the inspection.

The designated team leader, Joseph J.

Lenahan, will make arrangements

with your staff to discuss the inspection plan in more detail.

The inspection objective will be to evaluate the capability of the high head safety injection

(HHSI) and low head safety injection (LHSI) systems to perform safety functions required by

their design bases.

The team will require the information outlined in the enclosure for the HHSI

and LHSI systems to review in preparation for the inspection.

Please contact Mr. J. Lenahan at

(404) 562-4625 prior to preparing the requested information. This information will be needed by

July 6, 1999,

in order to support the inspection effort.

Thank you for your cooperation in this matter.

Ifyou have any questions regarding this

inspection, please contact Mr. K. Landis at (404) 562-4605 or Mr. J. Lenahan.

Sincerely,

Original signed by Joseph Lenahan for

Kerry D. Landis

Kerry D. Landis, Chief

Engineering Branch

Division of Reactor Safety

Docket Nos. 50-400

License Nos. NPF-63

Enclosure:

Information Requested for High Head Safety Injection (HHSI) and

Low Head Safety Injection (LHSI) Systems

cc w/encl: (See page 2)

9906i40206

990528

PDR

ADOCK 05000400

8

PDR

CP8L

cc w/encl:

Terry C. Morton, Manager

Performance Evaluation and

Regulatory Affairs

CPB 9

Carolina Power & Light Company

P. O. Box 1551

Raleigh, NC 27602-1551

Chris L. Burton

Director of Site Operations

MC: Zone1

Carolina Power & Light Company

Shearon Harris Nuclear Power Plant

P. O. Box 165

New Hill, NC 27562-0165

Bo Clark

Plant General Manager-Harris Plant

Carolina Power 8 Light Company

Shearon Harris Nuclear Power Plant

P. O. Box 165

New Hill, NC 27562-0165

Donna B. Alexander, Manager

Regulatory Affairs

~

Carolina Power 8 Light Company

'Shearon Harris Nuclear Power Plant

P. O. Box 165, Mail Zone

1'ew

Hill, NC 27562-0165

Johnny H. Eads, Supervisor

Licensing/Regulatory Programs

Carolina Power & Light Company

Shearon Harris Nuclear Power Plant

P. O. Box 165, Mail Zone

1

New Hill, NC 27562-0165

William D. Johnson

Vice President 8 Corporate Secretary

Carolina Power 8 Light Company

P. O. Box 1551

Raleigh, NC 27602

John H. O'eill, Jr.

Shaw, Pittman, Potts 8 Trowbridge

2300 N. Street, NW

Washington, DC 20037-1128

Mel Fry, Director

Division of Radiation Protection

N. C. Department of Environmental

Commerce & Natural Resources

3825 Barrett Drive

Raleigh, NC 27609-7721

Karen E. Long

Assistant Attorney General

State of North Carolina

P. O. Box 629

Raleigh, NC 27602

Public Service Commission

State of South Carolina

P. O. Box 11649

Columbia, SC 29211

Chairman of the North Carolina

Utilities Commission

P. O. Box 29510

Raleigh, NC 27626-0510

Robert P. Gruber

Executive Director

Public Staff NCUC

P. O. Box 29520

Raleigh, NC 27626

Vernon Malone, Chairman

Board of County Commissioners

ofWake County

P. O. Box 550

Raleigh, NC 27602

Richard H. Givens, Chairman

Board of County Commissioners

of Chatham County

P. O. Box 87

Pittsboro, NC 27312

CP&L

3

Distribution w/encl

L. Plisco, Rll

B. Bonser, Rll

J. Coley, Rll

R. Laufer, NRR

R. Baldwin, Rll

J. Lenahan, Rll

D. Jones, Rll

D. Thompson, Rll

PUBLIC

NRC Resident Inspector

U. S. Nuclear Regulatory Commission

5421 Shearon Harris Road

New Hill, NC 27562-9998

QFFIGE

SIGNATURE

NAME

DATE

RII:DRS

nahan:pd

/99

RII:DR

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I

5/

/99

RII:DRP

BBonser

/99

5/

/99

5/

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0

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NO

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0

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GIALREGQRD c

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DOGUMENT NAME:S ADRS'iEBiHARSSEI1.WPD

INFORMATIONREQUESTED FOR THE HIGH HEAD SAFETY INJECTION (HHSI)

AND LOW HEAD SAFETY INJECTION (LHSI) SYSTEMS

Site specific administrative procedures related to standard operation, abnormal operation,

and emergency operation of the HHSI and LHSI systems.

Design criteria for the HHSI and LHSI Systems in addition to support systems and

interfaces.

HHSI and LHSI Technical Specification requirements and associated

surveillance

test/calibration procedures.

HHSI and LHSI systems piping and instrumentation drawings; one line diagrams;

electrical schematics; wiring and logic diagrams.

A list of engineering calculations (Electrical, Instrumentation and Controls and

Mechanical/Nuclear) applicable to the HHSI and LHSI systems.

A list of plant modifications to the HHSI and LHSI systems implemented since plant

licensing.

A list of Adverse Condition Reports and Condition Reports initiated since 1990 affecting

the HHSI and LHSI systems.

List of current open temporary modifications and operator work arounds involving

operation of the HHSI and LHSI systems.

System Health Report and Performance Trends for the HHSI and LHSI systems.

Maintenance Rule Performance criteria for the HHSI and LHSI systems.

Documentation of corrective and preventive maintenance activities, including the

maintenance rule event log, performed on the HHSI and LHSI systems in the past 12

months.

Copies of applicable sections of changes to the UFSAR (which have yet to be docketed)

for the HHSI and LHSI systems.

An index of drawings for the HHSI and LHSI systems.

Copies of self-assessment

performed on the HHSI and LHSI systems in the last 24

months.

The system description and operator training module for the HHSI and LHSI systems.

PRA Fault Tree Data for the HHSI and LHSI systems.

Enclosure

Distribution Sheet

Distri95.txt

Priority: Normal

From: Elaine Walker

Action Recipients:

RidsNrrPMRLaufer

RidsNrrDlpmLpdii2

R Laufer

NRR/DLPM/LPD2-2

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Paper Copy

Paper Copy

Internal Recipients:

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External Recipients:

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Paper Copy

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Paper Copy

Paper Copy

Total Copies:

Item: ADAMSDocument

Library: ML ADAMS"HQNTAD01

ID: 003694160

Subject:

IR-99-008 Harris - Integrated

~

~

Page

1

Distri95.txt

Body."

ADAMS DISTRIBUTIONNOTIFICATION.

Electronic Recipients can RIGHT CLICKand OPEN the firstAttachment to View

the Document in ADAMS. The Document may also be viewed by searching for

Accession Number ML0036941 60.

IE01 - General (50 Dkt)-tnsp Rept/Notice ofViolation Response

( for use by HQ)

Docket: 05000400

Page 2

\\ ~

NR 20

20gg

Carolina Power 8 Light Company

ATTN: Mr. James Scarola

Vice President - Harris Plant

Shearon Harris Nuclear Power Plant

P. O. Box 165, Mail Code: Zone

1

New Hill, NC 27562-0165

SUBJECT:

NRC INTEGRATED INSPECTION REPORT 50-400/99-08

Dear Mr. Scarola:

On February 19, 2000, the Nuclear Regulatory Commission (NRC) completed an inspection at

your Shearon Harris facility. The enclosed report presents the results of that inspection.

The

results of that inspection were discussed with you and other members of your staff on

February 24, 2000.

The inspection was an examination of activities conducted under your license as they relate to

safety and compliance with the Commission's rules and regulations and with the conditions of

your license.

Within these areas, the inspection consisted of a selective examination of

procedures and representative

records, observations of activities, and interviews with personnel.

Based on the results of this inspection, the NRC has determined that a low risk significance

violation of NRC requirements occurred. The issue was entered into your corrective action

program, and is discussed

in the summary of findings and in the body of the attached inspection

report. This issue, which involved the failure to maintain the required water level above stored

fuel assemblies,

was determined to involve a violation of NRC requirements, but because of its

low safety significance the violation is not cited. Ifyou contest this non-cited violation you should

provide a response within 30 days of the date of this inspection report, with the basis for your

denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC

20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of

Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and

the NRC resident inspector at the Shearon Harris Nuclear Power Plant.

CP8L

2

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be placed in the NRC Public Document Room.

Sincerely,

/RA/.

Brian R. Bonser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket No.:

50-400

License No.:

NPF-63

Enclosure: Integrated Inspection Report

cc whencl: (See page 3)

~ ~ 0

CP8L

V

q ~

cc w/encl:

Terry C. Morton, Manager

Performance Evaluation and

Regulatory Affairs

CPB 9

Carolina Power & Light Company

Electronic Mail Distribution

Chris L. Burton

Director of Site Operations

Carolina Power & Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

Robert J. Duncan

Plant General Manager-Harris Plant

Carolina Power 8 Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

Donna B. Alexander, Manager

Regulatory Affairs

Carolina Power 8 Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

Johnny H. Eads, Supervisor

Licensing/Regulatory Programs

Carolina Power 8 Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

William D. Johnson

Vice President 8 Corporate Secretary

Carolina Power 8 Light Company

Electronic Mail Distribution

Peggy Force

Assistant Attorney General

State of North Carolina

Electronic Mail Distribution

Public Service Commission

State of South Carolina

P. O. Box 11649

Columbia, SC 29211

Chairman of the North Carolina

Utilities Commission

P. O. Box 29510

Raleigh, NC 27626-0510

Robert P. Gruber

Executive Director

Public Staff NCUC

P. O. Box 29520

Raleigh, NC 27626

Vernon Malone, Chairman

Board of County Commissioners

of Wake County

P. O. Box 550

Raleigh, NC 27602

Richard H. Givens, Chairman

Board of County Commissioners

of Chatham County

Electronic Mail Distribution

Distribution w/encl: (See page 3)

John H. O'eill, Jr.

Shaw, Pittman, Potts 8 Trowbridge

2300 N. Street, NW

Washington, DC 20037-1128

Mel Fry, Director

Division of Radiation Protection

N. C. Department of Environmental

Commerce 8 Natural Resources

Electronic Mail Distribution

MAR-17-2888

89:48

NRC

HARRIS PLANT

9193628E'AB

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OFFICIALRECORD COPY

DOCUMENT NAME'. C:U-ILESURF

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TOTAL P.81

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DOCUMENT NAME: G:WARRISNeport$ 9 08.wpd

1

I

U. S. NUCLEAR REGULATORYCOMMISSION

REGION II-

Docket No:

License No:

50-400

NPF-63

Report No:

50-400/99-08

Licensee:

Carolina Power & Light (CP8L)

Facility:

Shearon Harris Nuclear Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill, NC 27562

Dates:

November 21, 1999 - February 19, 2000

Inspectors:

Approved by:

J. Brady, Senior Resident Inspector

R. Hagar, Resident Inspector

D. Thompson, Safeguards

Inspector (Sections 3PP1, 3PP2, and

4OA2)

J. Kreh, Emergency Preparedness

Inspector (Section 1EP1 and

4OA2)

A. Hutto, Resident Inspector, H.B. Robinson Plant (Section 1EP1)

B. Bonser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Enclosure

'

I

SUMMARYOF FINDINGS

Shearon Harris Nuclear Power Plant, Unit 1

NRC Inspection Report 50-400/99-08

The report covers a thirteen-week period of resident inspection.

In addition, it includes the

results of announced inspections by a regional safeguards

inspector and a regional emergency

preparedness

inspector.

The significance of issues is indicated by their color (GREEN, WHITE, YELLOW, RED) and was

determined by the Significance Determination Process as discussed

in the attached summary of

the NRC's Revised Reactor Oversight Process.

Barrier Integrity

~GREEN. A non-cited violation was identified for multiple failures to maintain Spent Fuel

Pool water level 23 feet above stored boiling water reactor (BWR) fuel assemblies

as required

by Technical Specification 3.9.11.

Licensee Event Report (LER) 50-400/1999-01-00 had

reported that nine BWR assemblies

had not been fullyseated in the spent fuel storage racks

because

on each of the affected assemblies,

a channel fastener had caught on the top of the

storage racks.

The safety significance of the violation is low because the depth of the water

above the top of the active fuel was never less than 23 feet. Therefore, the violation did not

affect the ability of the water barrier to absorb 99 per cent of the assumed

iodine gap activity that

could be released from a rupture of an irradiated fuel assembly.

(Section 4OA4.2)

II

4

Re ort Details

The unit operated at 100% of rated thermal power from the beginning of this inspection period

until December 14, when the unit was manually tripped (shut down) following a failure of the "A"

condensate

pump. After repairs to that pump and several other components were completed,

the unit was,returned to full power on December 17. The unit remained at full power through the

end of the inspection period.

REACTOR SAFETY

Cornerstones:

Initiating Events, Mitigating Systems, Barrier Integrity

The inspectors reviewed the following emergent items, as described in the referenced

Work Requests/Job

Orders (WR/JOs) and/or Action Requests

(ARs), to verify that the

licensee had taken the necessary

steps to demonstrate that emergent work activities

were adequately planned and controlled to avoid initiating events, and to verify that the

licensee ensured the functional capability of accident mitigation systems:

99-AGAQ1

Feed train problems that caused

a reactor trip

00-AAAI1

A emergency diesel generator alarms due to circuit card problems

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R04

E ui ment Ali nment

For the systems identified below, the inspectors reviewed plant documents to determine

correct system lineup, and observed equipment to verify that the system was correctly

aligned:

~ Main steam system (steam generator power-operated relief valves and safety relief

valves),

k

~ "A"emergency diesel generator,

~ Residual heat removal system

~ "A"Auxiliaryfeedwater and turbine-driven auxiliary feedwater systems

0

For the emergency service water system, the inspectors reviewed various documents to

determine the correct system lineup, including plant procedures,

drawings, and the

updated Final Safety Analysis Report.

In addition, the inspectors reviewed outstanding

maintenance work requests on the system and performed a walkdown to identify any

discrepancies

between the existing system equipment lineup and the correct lineup. The

inspectors also reviewed related Condition Reports (CRs) to verify that the licensee had

properly identified and resolved equipment alignment problems that could cause initiating

events or impact mitigating system availability

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R05

Fire Protection

Ins ection Sco

e

The inspectors reviewed current action requests, work orders, and impairments

associated with the fire suppression system.

The inspectors reviewed the status of

ongoing surveillance activities to determine whether they were current to support the

operability of the fire protection system.

The inspectors also observed the fire protection

detection and suppression equipment in the cable spreading rooms, the "A"and "B"

safety-train electrical switchgear rooms, and the control room to determine whether any

conditions or deficiencies existed which would impair the operability of that equipment.

In addition, the inspectors inspected the licensee's compensatory measures that were in

place while the diesel-driven fire pump was out of service in late November.

The inspectors observed the performance of the plant fire brigade during their response

to a fire in the laundry area of the waste processing building on February 15. The fire

began in and was confined to a clothes dryer that was being used to launder anti-

contamination clothing.

Observations and Findin s

No findings were identified and documented through this inspection.

1R09

Inservice Testin

IST ofPum sand Valves

For the inservice tests listed below, the inspectors reviewed the test procedures to

ensure that the procedures were consistent with applicable American Society of

Mechanical Engineers (ASME) code requirements.

The inspectors also observed

performance of the tests and/or reviewed related records, to verify that testing was being

conducted in accordance with the'procedures.

These reviews were completed for the

following IST tests:

Number

Rev.

Title

OST-1411

OST-1104

11

"AuxiliaryFeedwater Pump 1X-SAB and 1AF-68, 1AF-106, 1AF-

87 Forward Flow Operability Test"

15

"Containment Isolation Inservice Inspection Valve Test Quarterly

Interval Modes

1 - 6"

OST-1056

6

OST-1215

21

"Containment Ventilation Isolation Valve ISI Test Quarterly

Interval" for 1CP-6

"Emergency Service Water System Operability Train "B"

Quarterly" for 1SC-37

OST-1111

12

"AuxiliaryFeedwater Pump 1X-SAB Operability Test Monthly"

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R11

Licensed 0 erator Re uglification

The inspectors reviewed licensed operator performance during the January

11 graded

emergency-plan exercise.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R12

Maintenance Rule Im lementation

For the equipment issues described in the CRs and ARs listed below, the inspectors

reviewed the licensee's implementation of the Maintenance Rule (10 CFR 50.65) with

respect to the characterization of failures, the appropriateness

of the associated

a(1) or

a(2) classiTication, and the appropriateness

of either the associated

a(2) performance

criteria or the associated

a(1) goals and corrective actions:

AR 1717

CR 98-00728

A Demineralized water system transfer pump failure (CR 99-

00038)

Duration of preventive maintenance on safety injection system

valves exceeded unavailability criteria for system 2080

1

'&

AR 16143

AR 4187

AR 8596

AH-4Afailed to start in low speed during OST -1010

Incorrect installation of the shuttle valve assembly on the "A"

preheater bypass valve air intensifier

Failure of an isolator card, in the circuit which indicates flow

rate in the."A" essential service water header

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R13

Maintenance Work Prioritization 8 Control

The inspectors reviewed the licensee's risk impact assessments

for removing from

service those components associated with the emergent work items listed in Section

1R03. The inspectors also reviewed the licensee's consideration of the risk significance

of work in the fuel handling building.

While completing the Maintenance Rule implementation inspection of a failure of the

demineralized water system transfer pump (AR 1717/CR 99-00038), the inspectors

noted that the licensee had initiated corrective action to address inappropriate work-

prioritization practices.

The inspectors reviewed the licensee's procedures for managing

the work process (ADM-NGGC-0104, "Work Management Process," Rev. 8), and for

managing risk associated with maintenance activities (WCM-001, "On-Line Maintenance

Risk Management," Rev. 6), to verify that the licensee had implemented the identified

corrective action, and that the corrective action had been effective in preventing

recurrence.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R15 0 erabilit

Evaluations

a.

Ins ection Sco

e

For the operability evaluations described in the Engineering Service Request (ESR) listed

below, the inspectors evaluated the technical adequacy of the evaluations to ensure that

operability was properly justifie and the subject component or system remained

available, such that no unrecognized increase in risk occurred:

ESR No.

Rev. No.

Title

99-00451

96-00321

99-00465

00-00016

00-00033

0

"Fire Wrap Discrepancy"

0

This evaluation was referenced in a 12-2-99 Night

Order related to an E-6B reactor auxiliary building

, exhaust fan pressure transmitter,and control problem.

"Jogging Emergency Service Water Traveling Screen

Motors"

"1BD-45 Stroke Time Evaluation"

"Operability Determination for Valves 1SP-948 and

1SP-949"

00-00045

00-00047

"[Essential Services Chilled Water] [net positive

suction head] Operability Determination"

"Controlotron Flow Measurement on [Charging/Safety

Injection Pump] Recirculation Line"

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R16 0 erator Workarounds

a.

Ins ection Sco

e

During this inspection period, several times each week, the inspectors reviewed the

licensee's list of identified operator workarounds to determine whether any identified

workarounds affected either the functional capability of the related system or human

reliability in responding to an initiating event.

During these reviews, the inspectors

specifically considered whether any identified workaround affected the operators'bility to

implement abnormal or emergency operating procedures.

In addition, the inspectors

attended a licensee meeting on November 30, in which licensee management

reviewed

each identified workaround.

The inspectors also reviewed the December 29 report of the

licensee's monthly audit of identified operator workarounds, which included the licensee's

assessment

of the cumulative impact of those workarounds.

The inspectors specifically

reviewed Workaround ¹255, "Vent Stack Radiation Monitors Become Inoperable AfterA

Reactor Trip Due To Loss Of Power."

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R19

Post Maintenance Testin

For the post-maintenance

tests listed below, the inspectors reviewed the test procedure

and either witnessed the testing.and/or reviewed test records to determine whether the

. scope of testing adequately verified.that the work performed was correctly completed and

demonstrated that the affected equipment was functional and operable.

OST-1 024

"On-site Power Distribution

Verification"

OST -1191

OST-1007

"Steam Generator [power operated

relief valve] and Block Valve

Operability Test"

"[Chemical 8 Volume Control

System/Safety Injection] System

Operability Test Train "A"Quarterly

Interval Modes 1-4"

Test Procedure

Number

Title

MPT-M0037

"Limitorque Actuator Magnesium

Rotor Inspection"

Related maintenance task

Preventive maintenance on

refueling water storage tank to

residual heat removal pump

"B" isolation valve, 1SI-323

(AGND002)

Repair to 7.5kva

uninterruptible power supply to

the Sll instrument bus (99-

AIFJ1)

Calibration of "B" power

operated relief valve set point

(AGVH-001)

Preventive maintenance

on

the actuator for.1CS-182, an

isolation valve on the

recirculation line associated

with the A charging/safety

injection pump (PM-M0014)

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R20

Refuelin

and Outa

e Activities

The inspectors reviewed the outage plan and prioritization of the work associated with the

December 14-15, 1999, forced outage following a reactor trip. The review focused on the

work which the licensee needed to complete before achieving criticality and synchronizing

the unit to the grid. The inspectors also attended the Plant Nuclear Safety Committee

meeting that reviewed those priorities. The inspectors observed the startup process to

determine whether mode change prerequisites were followed.

~

r

.b.

Observations and Findin s

'o

findings were identified and documented through this inspection.

1R22

Surveillance Testin

a.

Ins ection Sco

e

For the surveillance tests listed below, the inspectors examined the test procedure and

either witnessed the testing and/or reviewed test records to determine whether the scope

of testing adequately demonstrated that the affected equipment was functional and

operable:

Number

Rev.

Title

OST-1124

MST-I0492

EST-221

OST-1007

MST -I0202

16

"Train "8" 6.9 KV Emergency Bus Under Voltage Trip Actuating

Device Operational Test"

16

"Diesel Generator 1B-SB Engine Control Cabinet Inspection,

Pneumatic Logic Device Replacement and Thermostat

Calibration"

9

"Type C [Local Leak Rate Test] of Containment Purge Makeup

Penetration (M-57)"

18

"[Chemical 8 Volume Control System/Safety Injection] System

Operability Test Train "A"Quarterly Interval Modes 1-4"

5

"Containment Spray Recirculation Sump 1A Level Loop

Calibration"

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R23

Tem ora

Plant Modifications

a.

Ins ection Sco

e

The inspectors reviewed the following ESRs to determine whether system

operability/availability was affected, that configuration control was maintained, and that

post installation testing was performed:

e

99-00378

99-00230

"Temporary Disable of Annunciators ALB-8/5-5Aand

5-5B." This modification disabled the C reactor

coolant pump standpipe level alarm due to a

grounding problem inside containment.

"Temporary Coredrill Cover" This modification

provided temporary fire protection and security

barriers on a vital area wall while the wall was being

modified.

b..

Observations and Findin s

No findings were identified and documented through this inspection.

Cornerstone: Emergency Preparedness

1EP1

Drill Exercise

and Actual Events

The inspectors reviewed the objectives and scenario for the Shearon Harris Nuclear

Power Plant biennial, full-participation emergency preparedness

2000 exercise to

determine whether they were designed to suitably test major elements of the licensee's

emergency plan.

During the period January 10-13, 2000, the inspectors observed and evaluated the

licensee's performance in the exercise, as well as selected activities related to the

licensee's conduct and self-assessment

of the exercise.

The exercise (rescheduled from

September 21, 1999) was conducted on January 11, 2000 from 12:30 p.m. to 5:05 p.m.

Licensee activities inspected during the exercise included those occurring in the Control

Room Simulator, Technical Support Center, Operational Support Center, and Emergency

Operations Facility. The NRC's evaluation focused on the risk-significant activities of

event classification, notification of governmental authorities, onsite protective actions,

offsite protective action recommendations,

and accident mitigation activities. The

inspectors also evaluated command and control, the transfer of emergency

responsibilities between facilities, communications, adherence to procedures,

and the

overall implementation of the emergency plan. The inspectors attended the post-exercise

critique to evaluate the licensee's self-assessment

process,

as well as the presentation of

critique results to plant management.

In addition, the inspectors observed a training drill on February 1.

Observations and Findin s

No findings were identified and documented through this inspection.

3.

SAFEGUARDS

Cornerstone: Physical Protection

3PP1

Access Authorization

The inspectors interviewed representatives

of licensee management

and escort

personnel concerning their understanding of the Behavior Observation portion of the

personnel screening and Fitness For Duty (FFD) program.

In interviewing these

personnel the inspectors reviewed the effectiveness of their training and abilities to

recognize aberrant behavioral traits.

b.

Observations and Findin'

No findings were identified during this inspection.

3PP2

Access Control

The inspectors observed access control activities on February 14 and 15, 2000, and the

seven day equipment testing on February 15, 2000.

In observing the access control

activities the inspectors assessed

whether officers could detect contraband before it was

introduced into the protected area.

Additionally, the inspectors assessed

whether the

officers were conducting access control equipment testing according to regulatory

requirements.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

4.

OTHER ACTIVITIES

4OA2 Performance Indicator Verification

Ph sical Protection Cornerstone

.1

Protected Area Securit

E ui ment Performance Indicator

The inspectors reviewed the licensee's program for the collection and submittal of data for

the Protected Area Equipment Performance Indicator(PI). Specifically, a random

sampling of the licensee's tracking, trending, and analysis of perimeter security

equipment problems coupled with alarm history logs and problem identification reports

10

sampling of the licensee's tracking, trending, and analysis of perimeter security

.equipment problems coupled with alarm history logs and problem identification reports

were reviewed.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

.2

Personnel Screenin

Pro ram Pl

The inspectors reviewed the licensee's program for the collection and submittal of data for

the Personnel Screening Program Pl. Specifically, a random sampling of logged events

relating to the access authorization personnel screening program were reviewed.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

.3

Fitness For Dut

FFD /Personnel Reliabilit Pro ram Pl

a.

Ins ection Sco

e

The inspectors reviewed the licensee's program for the collection and submittal of the

semiannual FFD/Personnel Reliability Program Pl, laboratory error reports, and a

random sampling of logged events relating to the FFD program.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

Emer enc

Pre aredness

Cornerstone

.4

Emer enc

Res

onse Or anization

ERO Drill/Exercise Pl

a.

Ins ection Sco

e

On November 30, 1999, the inspectors assessed

the accuracy of the Pl for ERO drill and

exercise performance (DEP) through review of documentation relative to an ERO full-

scale drill held on October 14, 1999, and two licensed-operator requaiification (LOR) drills

conducted on October 20, 1999.

In addition, the inspectors reviewed and discussed the

licensee's methodology for calculating the DEP Pl.

t

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1

I

l

h

11

.5 '.

ERG Drill Partici ation PI

On November 29, 1999, the inspectors assessed

the accuracy of the Pl for ERO drill

participation through review of source records for selected individuals (approximately

10 percent) from the roster of key ERO personnel as of September 30, 1999.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

.6

Alert and Notification S stem Reliabilit

Pl

a.

Ins ection Sco

e

On November 29, 1999, the inspectors assessed

the accuracy of the Pl for alert and

notification system (ANS) reliability through review of the licensee's records of annual full-

cycle tests, quarterly growl tests, and biweekly silent tests of its siren system in the

10-mile radius around the Harris Plant.

Records from January

1, 1998 to the present

were selectively reviewed, with a focus on test results since June 1, 1999.

b. 'Observations and Findin s

No findings were identified and documented through this inspection.

The inspectors reviewed the licensee actions following the December 14, 1999, manual reactor trip following the loss of the "A"condensate

pump. The inspectors evaluated the

response of the mitigating systems and whether required notifications had been made.

b.

Observations and Findin s

Allmitigating systems performed as required.

No findings were identified and

documented through this inspection.

4OA4 Other

Closed

Licensee Event Re ort LER: 50-400/1999-009-00:

Reactor Trip and Auxiliary

Feedwater Actuation. The December 14, 1999, manual reactor trip resulted from low

steam generator level. The low steam generator level was caused by the loss of the "A"

condensate

pump motor, due to a ground fault, resulting in loss of the "A"feed train. The

total loss of one feedwater train resulted in a condition where steam generator levels

could not be maintained even with a designed runback of reactor power. Operators

AI

0

12

- manually tripped the reactor when steam generator levels approached the automatic trip

setpoint.

Allmitigating systems performed as designed.

No findings were identified and

documented through this inspection.

Closed

LER: 50-400/1999-001-00:

Spent Fuel Pool water level not maintained greater

. than 23 feet above stored boiling water reactor (BWR) fuel assemblies.

This LER

reported a violation of Technical Specification 3.9.11 for failing to maintain spent fuel pool

water level 23 feet above the top of the fuel assemblies..

Nine BWR fuel assemblies

had

not been fullyseated

in the spent fuel storage racks because

a fuel assembly channel

fastener had caught on the top of the fuel rack. The licensee's review of operating logs

showed that Technical Specification 3.9.11 had not been met on numerous occasions

from August 14, 1997, until January 6, 1999. This violation is being treated as a non-cited

violation, consistent, with the Interim Enforcement Policy for pilot plants.

This violation is

in the licensee's corrective action program as Condition Report 99-00050.

This violation

is designated as NCV 50-400/99-08-01, Spent Fuel Pool water level not maintained

greater than 23 feet above stored fuel assemblies.

The inspectors considered that this violation could have significance with respect to the

potential release of radioactive materials only ifit affected:

~

the frequency of a significant event that could cause a release of radioactive materials

from a stored fuel assembly,

the availability or operability of a system or feature designed to mitigate the effects of

such a release, and/or

4

~

the integrity of a system or feature that acts as a barrier against such a release.

The inspectors assessed

the impact of this violation in each of those areas, as follows:

General

The inspectors noted that the only effect of this violation was that several fuel

assemblies were not fullyseated in their respective channels in the spent fuel racks

because the assemblies were suspended

approximately 4 inches above the bottom of the

rack by interactions between assembly channel fasteners and the walls of the spent fuel

rack channels.

The tops of the affected assemblies thus extended approximately 4

inches higher in the pool than they would have ifthe assemblies

had been fullyseated.

Th

iii d

h

lii'hh

dpi

documented

in ESR 99-00013, "Evaluation of Boiling Water Reactor Fuel Assemblies

Supported by Channel Fastener," Revision 0, and noted that the licensee determined that

a seismic event or breaking of the channel fastener could cause or allow the suspended

fuel assemblies to fall unimpeded to the bottom of the racks.

However, the licensee also

determined that such a fall would not affect the structural integrity of either the affected

assembly or the rack channel into which the affected assembly would fall. The inspectors

found that the licensee's determination included a sound technical basis, and that the

conclusions were adequately supported.

Since the only effect of this violation would not

increase the likelihood of damage to an affected assembly, the inspectors concluded that

13

this violation did not increase the frequency of a significant event that could cause a

release of radioactive materials from a stored fuel assembly.

Miti atin

s stems

The inspectors visually examined the fuel pool configuration, and

observed that no part of any system or feature designed to mitigate the effects of events

, in the fuel pool is located at or near the tops of the spent fuel racks.

The only effect of the

,violation was.that the tops of the affected assemblies extended approximately 4 inches

higher in the pool than they would ifthe assemblies

had been fullyseated,

and since no

part of a mitigating system is located at or near the area that could be affected by the

violation, the inspectors considered that the violation had no effect on any system or

feature designed to mitigate events in the fuel pool.

Th

I

Id

dh

hi

Il

I

I

Ih

against the release of radioactive materials from the Spent Fuel Pool, as follows:

hf:Th

T

h

TP

f

2

dpf

f

2

h

p

the fuel assemblies.

The Technical Specification bases state that a minimum water

depth of 23 feet above the top of the active fuel is required to satisfy the licensing-

basis requirement for removing 99% of the assumed

iodine gap activity that could be

released from a rupture of an irradiated fuel assembly.

The inspectors considered the

reason the Technical Specification value was measured at a point above the top of

the active fuel was because

it is easier to measure from the top of the fuel assembly.

The top of the active fuel is not readily observable from the outside of the fuel rods.

The licensee's analysis calculated where the theoretical top of the active fuel was and

determined that the subject violation did not reduce the depth of water above the fuel

to less than the 23 foot value in the licensing basis.

The inspectors concluded that the

subject violation did not have any measurable affect on the effectiveness of the fission

product absorbing water barrier.

Th

Il

I

I df

If

II

hf

approximately 4 inches above the assembly positions assumed

in fuel pool

subcriticality analyses.

The inspectors noted that during the period of this violation,

the Spent Fuel Pool configuration included two barriers to prevent criticality: one

barrier was that a neutron-absorbing

material had been incorporated into the rack

channel walls, and the other was that a relatively high concentration of a neutron-

absorbing material (> 2000 ppm Boron) had been dissolved in the water in the pool.

2

The licensee's evaluation showed that the active portion of the fuel was still

surrounded by neutron absorber in the 4 inch extended position. The Boron

concentration in the pool was essentially unchanged during the period of the violation.

Consequently, the inspectors considered that there had been no effect on the

subcriticality barrier.

Assembl

Inte rit

The licensee's visual examination of the spent fuel racks, as

documented

in the subject ESR, revealed that the violation had not damaged the

integrity of either the affected assemblies or the corresponding rack channels.

0

I

Because the subject violation:

14

~

had no effect on the frequency of any initiating event,

~

had no effect on any mitigating system or feature,

~

did not have any measurable

affect on the effectiveness of any barrier against the

release of radioactive materials,

the inspectors concluded that the risk significance of the subject violation was well below

the threshold for increased regulatory response,

and have therefore designated its risk

significance as GREEN.

.3

Closed

LER: 50-400/1999-002-00:

Reactor trip due to not removing a temporary device

from a relay following calibration. The non-safety relay caused a loss of production but

did not introduce a safety issue.

All mitigating systems performed as designed.

.4

Closed

LER: 50-400/1999-006-01: Containment Isolation Valve Technical Specification

Noncompliance.

This item was addressed

in Inspection Report 50-400/99-04 and

included in violation 50-400/99-04-03.

.5

Closed

LER: 50400/1999-004-00:

Unit trip due to the degraded condition of a steam

generator water level flow control valve. This reactor trip was reviewed in Inspection

Reports 50-400/99-01 and 50-400/99-02.

.6

Closed

VIO: 50-400/01014:

The inspectors reviewed the proposed and implemented

corrective actions that the licensee had taken to avoid further regulatory concerns with the

Access Authorization Program and determined that the corrective actions were

acceptable.

4OA5 Mana ement Meetin s

.1

Exit Meetin

Summa

The inspectors presented the inspection results to members of licensee management

on

February 24, 2000. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any of the material examined during the

inspection should be considered proprietary.

No proprietary information was identified.

15

PARTIALLIST OF PERSONS CONTACTED

. B. Bonser, Chief, Reactor Projects Branch 4

R. Laufer, Harris Project Manager, NRR

Licensee

D. Alexander, Regulatory Affairs Manager

K. Altman, Major Projects Manager

C. Burton, Site Operations Director

B. Clark, Harris Plant General Manager at the beginning of this inspection period

R. Duncan, Harris Plant General Manager at the end of this inspection period

R. Field, Nuclear Assessment Manager

T. Hobbs, Acting Operations Manager

J. Holt, Outage and Scheduling Manager

G. Kline, Harris Engineering Support Services Manager

T. Natale, Training Manager

K. Neushaeffer, Plant Support Services Manager

J. Scarola, Harris Plant Vice President

B. Waldrep, Maintenance Manager

E. Wills, Environmental & Radiation Control Manager

I~

16

~Oened

ITEMS OPENED, CLOSED, AND DISCUSSED

50400/1 999-08-01

Closed

NCV

Spent Fuel Pool water level not

'aintained

greater than 23 feet above

stored fuel assemblies

(Section 40A4)

50-400/1 999-009-00

50400/1 999-001-00

50-400/1 999-002-00

50-400/1 999-006-01

50-400/'I 999-004-00

50<00/1 999-08-01

50-400/01014

LER

LER

LER

LER

LER

NCV

VIO

Reactor Trip and AuxiliaryFeedwater

Actuation (Section 40A4)

Spent Fuel Pool water level not

maintained greater than 23 feet

above stored BWR fuel assemblies

(Section 40A4)

Reactor trip due to not removing a

temporary device from a relay

following calibration (Section 40A4)

Containment Isolation Valve

Technical Specification

Noncompliance (Section 40A4)

Unit trip due to the degraded

condition of a steam generator water

level flowcontrol valve

(Section 40A4)

Spent Fuel Pool water level not

maintained greater than 23 feet

above stored fuel assemblies

(Section 40A4)

Failure to comply with the

Regulations in 10 CFR Part 73 and

the provisions of the Harris Security

Program related to the Access

Authorization Program in four

examples (Section 40A4)

Discussed

None

'

1

17

NRC's REVISED REACTOR OVERSIGHT PROCESS

The federal Nuclear Regulatory Commission (NRC) revamped its inspection, assessment,

and

enforcement programs for commercial nuclear power plants. The new process takes into

account improvements in the performance of the nuclear industry over the past 25 years and

improved approaches

of inspecting safety performance at NRC licensed plants.

The new process monitors licensee performance in three broad areas (called strategic

performance areas): reactor safety (avoiding accidents and reducing the consequences

of

accidents ifthey occur), radiation safety (protecting plant employees and the public during routine

operations), and safeguards

(protecting the plant against sabotage or other security threats).

The process focuses on licensee performance within each of seven cornerstones of safety in the

three areas:

Reactor Safety

~ Initiating Events

~ Mitigating Systems

~ Barrier Integrity

~ Emergency Preparedness

Radiation Safety

~ Occupational

~ Public

Safeguards

~ Physical Protection

To monitor these seven cornerstones of safety, the NRC uses two processes

that generate

information about the safety significance of plant operations: inspections and performance

indicators.

Inspection findings willbe evaluated according to their potential significance for

safety, using the Significance Determination Process,

and assigned colors of GREEN, WHITE,

YELLOWor RED. GREEN findings are indicative of issues that, while they may not be desirable,

represent little effect on safety. WHITE findings indicate issues with some increased importance

to safety, which may require additional NRC inspections.

YELLOWfindings are more serious

issues with an even higher potential to effect safety and would require the NRC to take additional

actions.

RED findings represent an unacceptable

loss of safety margin and would result in the

NRC taking significant actions that could include ordering the plant shut down.

Performance indicator data willbe compared to established criteria for measuring licensee

performance in terms of potential safety.

Based on prescribed thresholds, the indicators will be

classified by color representing incremental degradation in safety: GREEN, WHITE, YELLOW,

and RED. The color for an indicator corresponds to levels of performance that may result in

increased NRC oversight (WHITE), performance that results in definitive, required action by the

NRC (YELLOW), and performance that is unacceptable

but still provides adequate protection to

public health and safety (RED). GREEN indicators represent performance at a level requiring no

additional NRC oversight beyond the baseline inspections.

The assessment

process integrates performance indicators and inspection so the agency can

reach objective conclusions regarding overall plant performance.

The agency will use an Action

Matrix to determine in a systematic, predictable manner which regulatory actions should be taken

18

C

based on a licensee's performance.

As a licensee's safety performance degrades,

the NRC will

take more and increasingly significant action, as described in the matrix. The NRC's actions in

response to the significance (as represented

by the color) of issues willbe the same for

performance indicators as for inspection findings.

More information can be found at: http://www.nrc.gov/NRR/OVERSIGHT/index. html.

> ~

I

Distri17.txt

Distribution Sheet

Priority: Normal

From: Esperanza

Lomosbog

Action Recipients:

RidsNrrPMRLaufer

RidsNrrDlpmLpdii2

R Laufer

NRR/DLPM/LPD2-2

Internal Recipients:

TTC

C-TNN

RidsOgcRp

RidsNrrDripRexb

RidsNrrDipmOlhp

RidsNrrDipmIipb

RidsManager

RidsEdoMailCenter

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2 .FILE

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OGC

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NRR/DIPM/OLHP

NR

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DEDRO

ACRS

Copies:

1

1

1

1

1

1

1

1

1

1

1

1

1

1

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1

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1

1

1

1

1

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OK

OK

Not Found

Not Found

Not Found

OK

OK

OK

OK

OK

OK

OK

Not Found

Not Found

Not Found

OK

Not Found

Not Found

Not Found

Not Found

Not Found

Not Found

Not Found

External Recipients:

NRC

PDR

NOAC

INEEL Marshall

Not Found

Not Found

Not Found

Total Copies:

Item:

ADAMS Package.

Library:

ML ADAMS"HQNTAD01

ID: 003670960

Subject:

General

(SO Dkt)-Insp Rept/Notice of Violation Response

Page

1

odp:

DR ADOCK 05000400

0

Distri17.txt

Docket:

05000400,

Notes: Application for permit renewal filed.

Page

2.

December

17,1999

EA 99-273

Carolina Power 8 Light Company

ATlN: Mr. James Scarola

Vice President - Harris Plant

Shearon Harris Nuclear Power Plant

P. O. Box 165, Mail Code: Zone

1

New Hill, NC 27562-0165

SUBJECT:

NRC INTEGRATED INSPECTION REPORT 50-400/99-07

Dear Mr. Scarola:

On November 20, 1999, the NRC completed an inspection at your Shearon Harris facility. The

enclosed report presents the results of that inspection.

The results of that inspection were

discussed with you and other members of your staff on November 23, 1999.

The inspection was an examination of activities conducted under your license as they relate to

reactor safety, radiation safety, verification of performance indicators, and compliance with the

Commission's rules and regulations and with the conditions of your license.

Within these areas,

the inspection consisted of a selective examination of procedures and representative

records,

observations of activities, and interviews with personnel.

As identified in the report, no findings

were identified during this inspection.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be placed in the NRC Public Document Room (PDR).

Sincerely,

(Original signed

by B.

R. Bonser)

Brian Bonser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket No.:

50-400

License No.:

NPF-63

Enclosure:

Inspection Report

cc whencl: (See page 2)

CP8L

cc w/encl:

Terry C. Morton, Manager

Performance Evaluation and

Regulatory Affairs

CPB 9

Carolina Power & Light Company

Electronic Mail Distribution

Chris L. Burton

Director of Site Operations

Carolina Power 8 Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

Bo Clark

Plant General Manager-Harris Plant

Carolina Power & Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

Donna B. Alexander, Manager

Regulatory Affairs

Carolina Power 8 Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

Johnny H. Eads, Supervisor

Licensing/Regulatory Programs

Carolina Power 8 Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

William D. Johnson

Vice President 8 Corporate Secretary

Carolina Power 8 Light Company

Electronic Mail Distribution

Peggy Force

Assistant Attorney General

State of North Carolina

Electronic Mail Distribution

Public Service Commission

State of South Carolina

P. O. Box 11649

Columbia, SC 29211

Chairman of the North Carolina

Utilities Commission

P. O. Box 29510

Raleigh, NC 27626-0510

Robert P. Gruber

Executive Director

Public Staff NCUC

P. O. Box 29520

Raleigh, NC 27626

Vernon Malone, Chairman

Board of County Commissioners

of Wake County

P. O. Box 550

Raleigh, NC 27602

Richard H. Givens, Chairman

Board of County Commissioners

of Chatham County

Electronic Mail Distribution

Distribution w/encl: (See page 3)

John H. O'eill, Jr.

Shaw, Pittman, Potts 8 Trowbridge

2300 N. Street, NW

Washington, DC 20037-1128

Mel Fry, Director

Division of Radiation Protection

N. C. Department of Environmental

Commerce 8 Natural Resources

Electronic Mail Distribution

CP8L

Distribution w/encl:

R. Laufer, NRR

PUBLIC

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DOCUMENTNAME: G:WARRISNopoh$ 9 07.wpd

TOTAL P.81

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

License No:

50-400

NPF-63

Report No:

50<00/99-07

Licensee:

Carolina Power 8 Light (CP8 L)

Facility:

Shearon Harris Nuclear Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill, NC 27562

Dates:

October 10 - November 20, 1999

Inspectors:

J. Brady, Senior Resident Inspector

R. Hagar, Resident Inspector

E. Testa, Senior Radiation Specialist (Sections 2PS2, 2PS3,

4OA2.1, and 4OA2.2)

Approved by:

B. Bonser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

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Enclosure

SUMMARYOF FINDINGS

Shearon Harris Nuclear Power Plant, Unit 1

NRC Inspection Report 50400/99-07

The report covers a six-week period of resident inspection.

In addition, it includes the results of;

an announced inspection by a regional radiation specialist.

No findings were identified during this inspection period.

0

Re ort Details

The plant operated at 100% of its licensed power level throughout this inspection period, except

on November 6, when power was reduced to 80% for approximately 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> to enable testing

of the main turbine control valves. After those valves were successfully tested, the plant was

returned to 100% power.

REACTOR SAFETY

Cornerstones:

Initiating Events, Mitigating Systems, Barrier Integrity

1R01

Adverse Weather Pre arations

R

The inspectors reviewed the licensee's preparations for cold weather as described in

procedure AP-301, "Adverse Weather," Revision 24, to verify that those preparations

limited the risk of weather related initiating events, ensured accessibility to accident

mitigation system equipment, and adequately protected accident mitigation systems from

adverse weather effects.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R

a.

Ins ection Sco

e

The inspectors reviewed the following emergent items, as described in the referenced

Work Requests/Job

Orders (WR/JOs) and/or Action Requests (ARs), to verify that the

licensee had taken the necessary steps to demonstrate that emergent work activities

were adequately planned and controlled to avoid initiating events, and to verify that the

licensee ensured the functional capability of accident mitigation systems:

AR 8767

High suspended

particulate matter in the emergency diesel'generator

fuel-oil day tank

99-AIFM1

Diesel-driven fire pump lube oil contamination

b.

Observations and Findin s

No findings were identified and documented through this inspection.

0

1R04

E ui mentAli nment

S

For the main feedwater system, the inspectois reviewed plant documents to determine

correct system lineup, and observed equipment to verify that the system was correctly

aligned. The inspectors also reviewed related Condition Reports (CRs)to verify that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact mitigating system availability.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R05

Fire Protection

The inspectors reviewed current ARs, work orders, and impairments associated with the

fire suppression

system.

The inspectors reviewed the status of ongoing surveillance

activities to determine whether they were current to support the operability of the fire

protection system.

In addition, the inspectors observed the fire protection detection and

suppression equipment in the A & B switchgear rooms to determine whether any

conditions or deficiencies existed which would impair the operability of that equipment.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R09

Inservice Testin

of Pum

s and Valves

Ins ection Sco

e

For the inservice tests listed below, the inspectors reviewed the test procedures to

ensure that the procedures were consistent with applicable American Society of

Mechanical Engineers (ASME) code requirements.

The inspectors also observed

performance of the tests and/or reviewed related records, to verify that testing was being

conducted in accordance with the procedures.

These reviews were completed for the

following IST tests:

Number

Rev.

Title

OST 1018

8

"Main Steam Isolation and Main Feedwater Isolation Valves

Operability Test Quarterly Interval Mode 1"

EST 229

0

"Remote Position Indication Test for 1SP-62"

OST 1214

20

"Emergency Service Water System Operability Train A

Quarterly Interval Modes 1-2-3-4"

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R12

Maintenance Rule Im lementation

For the equipment issues described in the CRs and ARs listed below, the inspectors

reviewed the licensee's implementation of the Maintenance Rule (10 CFR 50.65) with

respect to the characterization of failures, the appropriateness

of the associated

a(1) or

a(2) classification, and the appropriateness

of either the associated

a(2) performance

criteria or the associated

a(1) goals and corrective actions:

Document

Title/Descri tion

CR 99-01695

1-4A1 Feeder Breaker Failure

CR 99-01699

E-61-A Low Flow Trip

CR 98-02984

'A'rain Residual Heat Removal Pump inoperability

AR 4187

AR 8233

'A'reheater Bypass Valve Shuttle Valve Sleeve Assembly

Containment Ventilation Isolation Radiation Monitor Functional

Failure

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R13

Maintenance Work Prioritization & Control

The inspectors reviewed the licensee's assessments

of the risk impacts of removing

from service those components associated with the emergent work items listed in

Section 1R03. The inspectors also reviewed the licensee's consideration of the risk

significance of work in the fuel handling building.

0

4

b.

Observations and Findin s

The inspectors observed that the licensee's on-line risk-assessment

tool was not

applicable to activities in the fuel handling building, since it only can be used to assess

the risks associated with operating the plant with fuel in the reactor vessel.

The

inspectors also observed that the shutdown risk-assessment

tool was not being used

while the reactor was operating.

Therefore, the licensee's programs and procedures did

not require the licensee to conduct appropriate risk assessments

for activities in the fuel

handling building. The licensee initiated AR 0008170 to address this observation.

No

findings were identified and documented through this inspection.

1R15 0 erabilit

Evaluations

a.

Ins ection Sco

e

For the operability evaluations described in the Engineering Service Requests (ESR)

listed below, the inspectors evaluated the technical adequacy of the evaluations, to

ensure that operability was properly justified and the subject component or system

remained available, such that no unrecognized increase in risk occurred:

99-0220

99-00437

0

Reactor Vessel Level Indication System (RVLIS) Train B

Plasma Display

E-88-B Operability Determination

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R16 0 erator Workarounds

S

The inspectors reviewed the operator work-around titled "Manual fillof the 'O'eactor

Coolant Pump standpipe", to determine whether the functional capability of the related

system or human reliability in responding to an initiating event was affected. The-

inspectors specifically considered whether the workaround affected the operators'bility

to implement abnormal or emergency operating procedures.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

0

1R19

Post Maintenance Testin

For the post-maintenarice tests listed below, the inspectors reviewed the test procedure

and either witnessed the testing and/or reviewed test records to determine whether the

scope of testing adequately verified that the work performed was correctly completed

and demonstrated that the affected equipment was functional and operable:

Test Procedure

Number

Rev.

Title

OST-1038

10

"Sampling, Chemical Addition and

Main Steam Drain Systems ISI

Valve Test Quarterly Interval

Modes 1-4"

Related maintenance task

Repair of Target Rock reed

switch

FPT-3010

OST-1024

8

"Engine Driven Main Fire Pump

Operability Test Weekly Interval

Modes: All"

8

"On-site Power Distribution

Verification Weekly Interval

Modes 1-6"

Diesel driven fire pump fuel

leak

Repair of Sll inverter

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R22

Surveillance Testin

For the surveillance tests listed below, the inspectors examined the test procedure and

either witnessed the testing and/or reviewed test records to determine whether the scope

of testing adequately demonstrated that the affected equipment was functional and

operable:

Number

Rev.

Title

EST-0221

OST 1045

MST- I0143

8

"Type C Local Leak Rate Test of Containment Purge Make-up

Penetration (M-57)"

14

"ESFAS Train B Slave Relay Test Quarterly Interval

Modes 1-4"

6

"Steam Generator A Narrow Range Level Loop (L-0474)

Operational".

OST-1111

OST-1122

12

"AuxiliaryFeedwater Pump 1X-SAB Operability Test Monthly

Interval Modes 1-3"

2

"Train A 6.9 KV Emergency Bus Undervoltage Trip Actuating

Device Operational Test and Contact Check Modes 1-6"

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R23

Tem ora

Plant Modifications

Ins ection Sco

e

The inspectors reviewed the temporary plant modification described in ESR-00378,

Revision 0, Temporary Disable of Annunciators ALB-8/5-5Aand 5-5B, to determine

whether its implementation had adversely affected the operability and/or availability of

the affected system.

(The disabled annunciators are associated with a standpipe

associated with seal leakoff flowfrom the reactor coolant pump pressure seals.)

b.

Observations and Findin s

No findings were identified and documented through this inspection.

Cornerstone: Emergency Preparedness

.

1EP1

Drill Exercise

and Actual Events

The inspectors observed an emergency response training drill conducted on October 14,

to verify licensee self-assessment

of classification, notification, and protective-action-

recommendation development.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

C),

2.

RADIATIONSAFETY

Cornerstones:

Public Radiation Safety

2PS2

Radioactive Material Shi

in

8

The inspectors reviewed and observed the licensee's performance in the radioactive

material shipping area.

Spent fuel handling and shipping records were reviewed to

ensure that doses to the public associated with fuel shipments and onsite storage were

minimized.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

2PS3

Radiolo ical EnvironmentalMonitorin

Pro ram

The inspectors reviewed the licensee's performance in implementing the

Radiological Environmental Monitoring Program, as required by Technical

Specifications and the Offsite Dose Calculation Manual.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

4

OTHER ACTIVITIES

40A2

Performance Indicator Verification

.1

Occu ational Radiation Safet

Performance Indicator Verification

'

The inspectors verified the Occupational Exposure Control Effectiveness performance

indicator (Pl) for the Occupational Radiation Safety Cornerstone through September

1999. The inspectors reviewed data reported to the NRC and sampled plant records in

the corrective action program.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

.2

Public Radiation Safet

Performance Indicator Verification

The inspectors verified the RETS/ODCM Radiological Effluent Occurrence Pl for the

Public Radiation Safety Cornerstone through September,

1999. The inspectors

reviewed data reported to the NRC, plant calculations, and selected independent offsite

dose calculations and observations.

The inspectors also sampled related plant records

in the corrective action program.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

.3

Reactor Safet

Performance Indicator Verification

The inspectors verified the Pls listed below through September,

1999.

Cornerstone

Performance Indicator

Mitigating Systems

Barrier Integrity

Safety System Unavailability, Emergency AC Power

Safety System Unavailability, High Pressure Safety Injection

Safety System Unavailability, Residual Heat Removal

Safety System Unavailability, AuxiliaryFeedwater

Safety System Functional Failures

Reactor Coolant System Specific Activity

Reactor Coolant System Leakage

Containment Leakage

To verify the performance indicator data, the inspectors reviewed Licensee Event

Reports, information contained in the licensee's maintenance-rule

database,

plant

chemistry data, operator logs, and containment leak rate test results.

b.

Observations and Findin s

During the inspection, several minor errors were identified in the Pl data for each safety

'ystem

unavailability performance indicator submitted to the NRC.

The licensee

documented those errors in Action Request (AR) 008984.

The licensee also found some

errors in the calculation of the containment leakage performance indicator. The licensee

documented those errors in AR 008908008908

Correcting the errors did not result in either a

change of Pl color or a significant change in the Pl value.

Since these errors were not

significant in that no change in the NRC's action would have resulted from this data, and

were not willfulthis is a minor violation not subject to formal enforcement action.

For the other Pls verified through this inspection, no findings were identified and

documented.

40A4

Other

Closed

Escalated Enforcement Item EEI 50-400/99-010-01

99-010-02

99-010-03

99-010-04

and 99-010-05: Access authorization apparent violations. By letter EA 99-

273 dated November 23, 1999, access authorization EEls 50400/99-010-01, 99-010-02,

99-010-03, and 99-010-04 were dispositioned as four examples of a violation associated

with a GREEN issue for the Harris facility. This violation is identified as 50400/01014,

failure to comply with the regulations in 10 CFR Part 73 and the provisions of the Harris

Physical Security Program related to the Access Authorization Program.

EEI 50-400/99-

010-05 was dispositioned as a violation of minor significance and was not subject to

formal enforcement action.

4OA5 Mana ement Meetln s

Exit Meetin

Summa

The inspectors presented the inspection results to members of licensee management

on

November 23, 1999. The licensee acknowledged the findings presented.

I

The inspectors asked the licensee whether any of the material examined during the

inspection should be considered proprietary.

No proprietary information was identified.

10

PARTIALLIST OF PERSONS CONTACTED

NRC

B. Bonser, Chief, Reactor Projects Branch 4

R. Laufer, Harris Project Manager, NRR

Licensee

D. Alexander, Regulatory Affairs Manager

A. Barbee, Acting Training Manager

C. Burton, Director of Site Operations

B. Clark, Harris Plant General Manager

J. Cook, Outage Manager

R. Field, Nuclear Assessment

Manager

T. Hobbs, Acting Operations Manager

J. Holt, Outage and Scheduling Manager

G. Kline, Harris Engineering Support Services Manager

J. Scarola, Harris Plant Vice President

B. Waldrep, Maintenance Manager

E. Wills, Environmental 8 Radiation Control Manager

11

~Oened

ITEMS OPENED, CLOSED, AND DISCUSSED

50-400/01014

VIO

Failure To Comply With The Regulations In 10 CFR Part 73 And The Provisions Of The Harris Physical

Security Program Related To The Access

Authorization Program In Four Examples.

Closed

50-400/99-010-01

50-400/99-010-02

50400/99-010-03

50-400/99-010-04

50<00/99-010-05

EEI

EEI

EEI

EEI

EEI

Failure To Review And Evaluate Background

Information For Persons Granted Unescorted

Access (Section 4OA4).

Continuation OfThe Granting Unescorted Access

Authorization (Section 4OA4).

Failure To Maintain Original Data On Which The

Licensee Granted Unescorted AAAuthorization For

Five Years (Section 4OA4).

Failure To Log Safeguards

Events Within 24 Hours

Of Discovery (Section 4OA4).

Failure To Document Individuals'raining In

Accordance With Licensee Requirements (Section

4OA4).

Discussed

None

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