ML17252B525

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LER 78-030/01T-0 for Dresden, Unit 2 Re During Startup Operation, the a LPCI and Core Spray Subsystem Were Inadvertently Rendered Inoperable
ML17252B525
Person / Time
Site: Dresden Constellation icon.png
Issue date: 05/12/1978
From: Stephenson B
Commonwealth Edison Co
To: James Keppler
NRC/RGN-III
References
BBS LTR 78-828 LER 78-030/01T-0
Download: ML17252B525 (3)


Text

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  • Commonwe. Edison Dresden Nuclear wer Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 May 12, 1978 BBS Ltr /178~828 James G. Keppler, Regional Director*

Directorate.of.Regulatory Operations - Region III U.S. Nuclear.Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137.

Repor~~ble;Otcurrence Repo~t ff78~030/01T-0 Docket 11050-237 is hereby submitted *to your office in accordance.with Dresden Nuclear Power Station Technical Specification 6.6.B.l.(f), personnel error which prevents ~r could prevent, by itself, the fulfillment of.the functional requirements of . syste!Tls required. t6 .cope with accidents analyzed in. the SAR.

  • St phenson*.

Statio.n Superintendent*

Dresden Nuclear Power Station

. BBS/deb*

  • Enclosure*

cc: Director of Inspectiofi & Enforcement*

Director of Management Information & Program Control File/NRC

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NRC FORM 366  :,,, .. U.S .. NUCLEAR REGULATORY COMMISSION.

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  • LICENSEE EVENT REPORT

eoNTROL BLOCK: .____.__..._I_ ....1_*__..I_"'_.-_.I_ _.10 * (PLEASE PRINT OR TYPE)iALL REQUIRED INFORMATION) 6

~ I I I LI DIR Is I 2 101 0 o I - I o I o I o I o I o I - Io Io IG)l 4 11 11 11 I 1 l©I I 10 7 8 9 LICENSEE COOE 14 15 LICENSE NUMBER 25

  • 26 LICENSE TYPE :JO 57 CAT 58 CON'T
  • ITEJ 7 8

-~~~~~~ L!J© 1 oI s.10 I o I o I 2 I 3 60 . . 61 .* DOCKET NUMBER.

I 1 101 68 69 o I 4 I ~ I a I 1 I a I© I o I s I 1 EVENT DATE 74 75 REPORT.DATE

  • 1- 2..1 1_LRlG) 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES@ .

I During Unit .2 startup operations the "A" LPCI and Core Spray Subsystems were

[ITIJ inadvertantly tendered inoperable. At this time preparations were in progress on

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!Im. J. determined that the. eqtdprr.ent attendant had closed. the "A" and "B" LPCI pump and "A"

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  • Core Spray Pump. Manual Discharge ValVes on* Unit 2 instead of Unit 3. L

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7 s .9 *so SYSTEM CAUSE CAUSE ..

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COMPONENT MANUFACTURER W@W@ W@ W 101010 10 I LU@ ~ ~@) IZ 19 19 19 I@'

33 34 . 35 36 37 40 41 42 43 44. . 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

Upon discovery.of the personnel error at 0405 hours0.00469 days <br />0.113 hours <br />6.696429e-4 weeks <br />1.541025e-4 months <br /> the pump discharge valves were ITITI I returned to. their normally locked open position and verified by 0420 hours0.00486 days <br />0.117 hours <br />6.944444e-4 weeks <br />1.5981e-4 months <br />. In IJ:TIJ I addition the "A LPCI and "A" Core Sray Subsytems were satisfactorily flo~ tested. I IJJIJ 1 ** Normal Unit 2 startup then continued *. Personnel involved were admonished for OJI] their error.

7 s 9 BO FACILITY *~30 METHOD OF * ~

. STATUS  % POWER . OTHER STATUS.~* DISCOVERY . . . . . . DISCOVERY DESCRIPTION, ~* . .

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  • .45 . . 46 Operational Event - Rx Level increas.e 80 ACTIVITY, CONTENT . . r::;;-. (.;';;\
  • RELEASED OF RELEASE AMOUNT OF ACTIVITY . . LOC.ATION OF RELEASE\~.~,;:

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PERSONNEL. EXPOSURES NUMBER (::;:;\. TYPE

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PERSONNEL IN.JURIES * .. (;":;\

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~ .""). j ATTACHMENT TO LICENSEE EVENT REPORT 78-030/0lT-0 COMMONWEAL TH EDISON COMP ANY ( CWE)

DRESDEN UNIT-2 (ILDRS-2)

DOCKET 11050-237 During normal Unit 2 startup operations at 0005 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.s on April 28, 1978 the "A" Low Pressure Coolant Injection (LPCI) and "A" Core Spray. Subsystems were inadvertantly rendered inoperable. At*the time* of the event prep*arations were in progress (DOS 6600-6) **

on Unit 3 while in the shutdown condition for the Emergency Core Cooling System (ECCS) undervoltage Functional Test. Following initiation of the test, at 0405 hours0.00469 days <br />0.113 hours <br />6.696429e-4 weeks <br />1.541025e-4 months <br /> it was determined.that the Equipment Attendant (EA) had closed the "A" and "B" LPCI pump*

and "A" Core Spray Pump Manual Discharge Valves on Unit 2 instead of Unit 3. At 0420hours the Unit 2 manual discharge valves were returned to their normally locked open position and verified'. In .

addition the "A" LPCI and. "A" Core Spray S~bsystems were satisfactorily flow tested. Unit 2*startup operations continued. During the approximate four (4) hour interval. when the Au LPCI and Core Spray Subsystems were inoperable the remaining two*(2) LPCI*

pumps ~ere available to fulfill the Containment Cooling Function.

  • In additio11 the redundant 100% capacity Core Spray System was availkble*tb

. provide sufficient core cooling in the unlikely event of a loss of coolant accident. There are no previous events of a similar nature at Dresden~

A subsequent review of the event with the appropriate operations personnel revealed that the. Equipment Attendant (EA) assigned to

.Unit 3 for specific valving operations involving the ECCS test mistakenly closed the three discharge valves.discussed previously on Unit 2

  • the personne:i, involved were admonished regarding* the{r errors.

At this time, -an investigative .committee ha*s been assigned to fur'ther

--i~~~stigate th~ event and provide recommendations to prevent .. *a.

  • re.Qccurence.

A supplemental report will . be sub.mittea

. . I following .the investigation!

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