ML17157C355
| ML17157C355 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 05/26/1993 |
| From: | Jason White NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17157C353 | List: |
| References | |
| 50-387-93-07, 50-387-93-7, 50-388-93-07, 50-388-93-7, NUDOCS 9306080058 | |
| Download: ML17157C355 (35) | |
See also: IR 05000387/1993007
Text
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UNITED STATES NUCLEAR REGULATORY COMMISSION
REGION I
Inspection
Report Nos.
50-387/93-07; 50-388/93-07
License Nos.
Licensee:
Pennsylvania Power and Light Company
2 North Ninth Street
Allentown, Pennsylvania
18101
Facility Name:
Inspection At:
Susquehanna
Steam Electric Station
Salem Township, Pennsylvania
Inspection
Conducted:
March 30, 1993 - May 10, 1993
Inspectors:
G. S. Barber, Senior Resident Inspector,
D. J. Mannai, Resident Inspector, SSES
R. K. Mathew, Reactor Engineer, D
S
B. J. M'Dermott,
ct
En in
r RP
Approved By:
J. Wh', Chief
R
or Projects Section No. 2A,
Date
Ins
tion Summa:
This inspection report documents routineand reactiveinspections
(during day and backshift hours) of station activities, including: plant operations; radiation
protection; surveillance and maintenance;
and safety assessment/quality
verification.
Findings and conclusions are summarized in the Executive Summary.
One violation was
identified pertaining to improper HPCI system valve lineup.
Section 2.2.1 pertains.
One
non-cited violation was identified concerning Reactor Protection System {RPS) overvoltage
setpoints.
Section 7.2.1 pertains.
Details are provided in the full inspection report.
9306080058
930527
ADOCK 05000387
Q
EXECUTIVE SUMMARY
Susquehanna
Inspection Reports
50-387/93-07; 50-388/93-07
March 30, 1993
- May 10, 1993
Operations (30702, 71707, 71710)
During the period, the inspector performed an engineered
safety feature (ESF) walkdown of
the Unit 1 High Pressure
Coolant Injection (HPCI) system.
The inspector determined the
system was capable of performing its intended safety function. However, the inspector found
the system lineup improper.
The inspector discovered
a containment boundary valve that
was closed, but not locked, as required.
The inspector also identified that the HPCI steam
admission valve was leaking by the seat.
Section 2.2.1 pertains.
The inspector identified oil levels slightly below the standstill level on several (10 of 16)
pump motor bearings on emergency service water and residual heat removal service water
pumps.
Electrical maintenance
concluded the oil levels were acceptable.
However, the
inspector identified a non-licensed operator training weakness during a review of the matter.
Section 2.2.2 pertains.
Maintenance/Surveillance
(61726, 62703)
The licensee generally exercised good control of maintenance
and surveillance activities.
The inspector identified minor procedural adherence
weaknesses
and a lack of complete
worker knowledge regarding safe use of a material during observation of a maintenance
activity. Section 4.4.2 pertains.
Bailey 740 millivoltconverters are used as class 1E isolators.
These converters can be
procured specifically for their isolation capability or for general applications.
To use a
general application converter for an isolation function, certain internal jumpers had to be
preset.
The inspector reviewed the isolation applications for both types of converters and
found them acceptable.
Section 4.4.1 pertains.
Engineering/Technical Support (71707, 92720, 93702)
The inspector discovered that the original overvoltage setpoint for the Unit 1 "B" Reactor
Protection System (RPS) power supply was questionably established.
The Main Steam
Isolation Valve (MSIV) AC solenoids were originally limited to a maximum of 125 vac.
The
current setpoint of 129.5 vac would have allowed voltage above the maximum design at the
A 1988 letter from the vendor revised the MSIV AC solenoid
maximum design voltage to 132 vac.
However, the licensee was not justified in operating
. 'Pe
with the current setpoint from 1982 to 1988.
This was a non-cited violation. The inspector
also noted that the licensee does not have a mechanism
to ensure that vendor initiated
changes to design information are included in plant information systems.
The licensee has
agreed to review the need, for a design input checklist or some other mechanism to ensure
that changes or clarifications to plant design information are adequately captured in plant
information systems.
Section 7.2.1 pertains.
Safety Assessment/Assurance
of Quality (40500, 90712, 92700, 92701)
The inspector reviewed two Licensee Event Reports during the period.
Section 8.1 pertains.
The Susquehanna
river exceeded flood stage during March and April. The licensee's actions
relative to preparing for, monitoring of, and responding to, river flooding was good, though
some minor procedural weaknesses
were observed.
The licensee agreed to revise the
procedure to correct the noted weaknesses.
Section 8.3 pertains.
Temporary Instruction TI-2515/112 required inspector review of licensee programs that
evaluate changes in population distribution and site proximity hazards.
In the course of this
review, the licensee initiated their own review and submitted an FSAR update. PAL did
not identify any significant changes.
The licensee did not have a formal program in place
prior to the TI issuance.
Currently, a formal program is being implemented to periodically
review and evaluate changes to the site environ.
The inspector concluded the licensee-
initiative was a strength.
Section 8.4 pertains.
TABLEOF CONTENTS
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EXECUTIVE SUMMARY ..
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SUMMARYOF OPERATIONS.......
1.1
Inspection Activities..........
1.2
Susquehanna
Unit 1 Summary....
1.3
Susquehanna
Unit 2 Summary....
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OPERATIONS
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2.1
Inspection Activities...............................
2.2
Inspection Findings and Review of Events
2.2.1
Unit 1 High Pressure
Coolant Injection System ESF Walkdown
2.2.2
Safety Related Pump Motor Bearing Oil Levels
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3.
RADIOLOGICALCONTROLS
3.1
Inspection Activities..............
.3.2
Inspection Findings
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MAINTENANCE/SURVEILLANCE
4.1
Maintenance and Surveillance Inspection Activity.........
4.2
Maintenance Observations ................;...'...
4.3
Surveillance Observations
4.4
Inspection Findings
4.4.1
Class 1E Isolation Capability of the Bailey 740 Millivolt
Converter.......... ~..................
4.4.2
Thermo-Lag Repair Unit 1 Remote Shutdown Panel...
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Inspection Activity... ~.... ~..............
5.2
Inspection Findings
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SECURITY
6.1
Inspection Activity........
6.2
Inspection Findings
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Table of Contents (Continued)
7.
ENGINEERING/TECHNICALSUPPORT
7.1
Inspection Activity............ ~............ ~.........
7..2
Inspection Findings
7.2.1
Reactor Protection System Overvoltage Setpoint ...........
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8.
SAFETY ASSESSMENT/QUALITYVERIFICATION.............
8.1
Licensee Event Reports.............................
8 ~2
Open Items ......
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8.2.1
(Closed) Unresolved Item 50-387/89-21-02, RCIC and HPCI
Rupture Disc NCRs on Post Work Testing Inadequate
8.2.2
(CLOSED) Unresolved Item 50-387-90-21-01, Firewatch
Rounds Not Completed As Required
8.2.3
(Closed) Violation 50-387/91-06-01, Inservice Test Program
0mlsslon
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Susquehanna
River Flooding
8.4
(Closed) Temporary Instruction (TI) 2515/112 - Licensee Evaluations
of Changes to the Environs Around Licensed Reactor Facilities
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9.1
Resident Exit and Periodic Meetings.........
9.2
Inspections Conducted By Region Based Inspectors
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1.
SU5&IARYOF OPERATIONS
1.1
Inspection Activities
Details
The purpose of this inspection was to assess
licensee activities at Susquehanna
Steam Electric
Station (SSES) as they related to reactor safety and worker radiation protection.
Within each
inspection area, the inspectors documented
the specific purpose of the area under review, the
scope of inspection activities and findings, and appropriate conclusions.
This assessment
is
based on actual observation of licensee activities, interviews with licensee personnel,
independent calculation, and selective review of applicable documents.
'bbreviations are used throughout the text.
Attachment
1 provides a listing of these
abbreviations.
1.2
- Susquehanna
Unit 1 Summary
Unit 1 began the inspection period at 100% power.
One unplanned power reduction
occurred during the period,
Five planned power reductions were scheduled
on weekends for
balance of plant repairs.
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On March 31, the normal level control valve for the "4C" feedwater heater failed
closed, causing high level in the "4C" feedwater heater.
automatically isolated.
Operators reduced power to 80% in accordance with ON-147-
001; Loss of Feedwater Heating Extraction Steam, and isolated the "C" feedwater
heater string per the requirements of OP-144-001,
Condensate
and Feedwater System.
Power was returned to 100% on April 1 following repairs to the feedwater heater
drain valve.
On April2, power was reduced to 98% to test and adjust feedwater level control.
Similar testing was previously performed at 60%, 70%, and 80% power on March
26-29.
Power was returned to 100% on April 3 at 4:30 a.m.
On April 3 at 6:50 a.m., power was reduced to 60% for additional feedwater heater
valve repairs.
Power was returned to 100% on April 4 following the valve repairs.
On April 8, power was reduced to 80% and the "B" feedwater heater string was
isolated to plug tube leaks in the "3B" feedwater heater.
Power was returned to
100% on April 11.
On April23, power was reduced to 60% to rework the auxiliary steam supply to the
steam jet air ejector (SJAE) pressure control valve actuator.
The licensee identified
- that the pressure control valve actuator required rework and auxiliary boiler steam
leak repairs were necessary
while preparing to repair a SJAE main steam supply valve
leak.
Power was returned to 100% on April 25.
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On April 30, power was reduced to 60% to repair the SJAE main steam supply valve,
Power was returned to 100% on May 1.
Operators conducted several other routine power reductions during the period to facilitate
surveillance testing.
No reactor scrams or ESF actuations occurred during the inspection
period.
Unit 1 finished the inspection period at 100% power.
1.3
Susquehanna
Unit 2 Summary
Unit 2 began the inspection period at 100% power.
On April 18, the "C" reactor feed pump
turbine tripped due to test circuit limit switch problem during emergency governor and trip
lockout testing.
A reactor recirculation runback was received, reducing power to 65%.
Following additional testing of the "C" reactor feed pump turbine, power was returned to
100% on April 19.
On April 22, during an investigation of "4C" feedwater normal level control valve, the "4C"
feedwater heater level rose which resulted in an automatic isolation of extraction steam.
Operators reduced power to 80% in accordance with ON-247-001, Loss of Feedwater
Heating Extraction Steam, and isolated the "C" feedwater string per the requirements of OP-
244-001, Condensate
and Feedwater System.
Power was returned to 100% on April 23
following repair of the feedwater heater level control valve.
Operators conducted several other routine power reductions to facilitate surveillance testing.
No reactor scrams or ESF actuations occurred during the inspection period.
Unit 2 finished
the inspection period at 100%.
2.
OPERATIONS
2.1
Inspection Activities
The inspectors verified that the facility was operated safely and in conformance with
regulatory requirements.
Pennsylvania Power and Light (PP&L) Company management
control was evaluated by direct observation of activities, tours of the facility, interviews and
discussions with personnel,
independent verification of safety system status and Limiting
Conditions for Operation, and review of facility records.
These inspection activities were
conducted in accordance with NRC inspection procedure 71707.
The inspectors performed 12.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> of deep backshift inspections during the period.
These
deep backshift inspections covered licensee activities during between
10:00 p.m. and 6:00
a.m. on weekdays,
and weekends
and holidays.
2.2
Inspection Findings and Review of Events
2.2.1
Unit 1 High Pressure
Coolant Injection System ESF Walkdown
During the period, the inspector performed an Engineered Safety Feature Walkdown of the
Unit 1 High Pressure
Coolant Injection (HPCI) system to independently verify the status of
the system.
The inspector utilized the Risk-Based Inspection Guide for the Susquehanna
HPCI system during the walkdown.
The inspector performed the following during the ESF walkdown:
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Reviewed in-service test (IST) data
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Performed walkdown checklist contained in NUREG/CR-5392 Risk Based Inspection
Guide for the Susquehanna
Station HPCI System
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Verified key components
on mechanical and electrical checklists (CL) to
independently verify system lineup
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Reviewed work authorization system printout to identify existing deficiencies in the
system
Verified housekeeping
conditions
Verified combustible materials controls
Reviewed system instrumentation to determine ifthe process parameters
were
adequate
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Compared as-built configuration to as-built drawings
The inspector identified the following significant deficiencies during the walkdown:
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Valve 155F092 HPCI turbine exhaust vacuum breaker test valve found not locked as
required by the system checklist;
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Valve HV-155F001 HPCI turbine steam supply valve, leaking by the seat;
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Valve 155F036 HPCI steam trap outlet isolation valve, packing leak;
The inspector identified the following minor deficiencies:
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Oil leaking from MOV actuators for HV155F012 HPCI.minimum flow valve to
suppression
pool and HV155F066 HPCI turbine exhaust to suppression
pool;
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Several motor control center (MCC) covers mounting screws not properly fastened in
place - elevation 683'eactor Building;
1Y226 208/120 volt instrument distribution panel covers not secured - elevation
683'eactor
Building;
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Mirror insulation dented on HPCI discharge piping around valve HV152F007, HPCI
pump discharge valve elevation 670',
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Insulation missing from 3 1/2'ection of HPCI discharge piping elevation 670',
Valve HV155F079 HPCI turbine exhaust inboard vacuum breaker valve MOV manual
handwheel
has missing dust cap;
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Half of the lighting burned out in the HPCI pipe routing area (area 28 elevation
670');
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Loose handwheel found lying on deck grating in HPCI pipe routing area;
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Mirror insulation clips unclipped and misaligned on HV155F066 HPCI turbine
exhaust valve to suppression
pool;
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Webbed sling and "C" clamp in overhead
area of HPCI pipe routing area;
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OPI-PSHIN012A HPCI turbine exhaust rupture disk pressure switch isolation
valve
not properly lockwired;
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Cap downstream of HPCI lube oil sample valve 156020 is leaking oil;
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Several lights burned out in the HPCI pump room elevation 645'.
The following valves had insufficient packing gland stud thread engagement:
HV-155-F001, HPCI turbine steam supply;
1RV LSH 1N018, HPCI turbine exhaust line drain pot level switch root valve;
2RV LSH 1N018, HPCI turbine exhaust line drain pot level switch root valve;
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RV PT1N06/PI1R005 HPCI exhaust pressure instrument root valve;
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DRN LSH1N014 HPCI steam valve drain line level switch drain valve;
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155F001 HPCI steam line drain pot inboard drain valve.
The inspector notified the licensee that valve 155FO92 was not locked immediately following
discovery.
Operations promptly locked the valve.
The licensee documented
the problem in
Significant Operating Occurrence Report (SOOR)93-130.
Operations Department initiated
the HPCI system checklists for both units and formed a Status Control Occurrence Review
Team.
Nuclear System Engineering (NSE) initiated a Work Authorization to document the HPCI
steam admission valve seat leak.
The licensee is evaluating valve repair for the June 1993
quarterly work window.
NSE will closely monitor for any increase in the seat leak rate.
Additionally, lube oil samples were obtained to check for the presence of water resulting
from the leak.
Sampling confirmed minor water contamination, however, the system
engineer determined
the system was operable.
NSE initiated a WA to perform a feed and
bleed on the HPCI lube oil sump to reduce the moisture contamination.
NSE directed that
lube oil sampling frequency be increased
from quarterly to weekly until the valve is repaired.
NSE initiated Engineering Work Request (EWR) M30323 to evaluate the packing gland
thread engagement
issue for the valves identified.
Maintenance is also evaluating the need to
proceduralize the thread engagement
requirements.
Currently, the licensee's procedures only
address packing gland torque and do not specify minimum thread engagement for valve
packing gland studs.
The inspector found the system capable of performing its intended safety function. The
inspector verified risk significant components included on the system walkdown checklist to
be in the proper position.
However, the system was not properly aligned in accordance with
the system checklistCL-152-0012, Unit 1 HPCI System-Mechanical.
The HPCI turbine
exhaust vacuum breaker test valve (155FO92) is required to be closed, capped, containment
tagged and locked.
Additionally, the CL requires independent verification of the position of
this valve.
The inspector discovered the valve to be closed, but unlocked while performing
independent verification of the HPCI system lineup.
The valve is a containment boundary
valve and is required to be closed, capped, containment tagged and locked.
The valve has
primary containment atmosphere
on the containment penetration side of the valve.
The last
documented
system CL was performed was May 9, 1992 during an outage,
The licensee
could not positively determine the cause of the valve being unlocked.
The Status Control
Review Team could not locate any documentation that revealed subsequent
authorized
operation of the valve since the checklist was last completed.
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The inspector considered
the NSE response,
once identified, to the steam admission valve
seat leak a strength.
However, the condition went undetected for some period of time; Both
units have a history of the HPCI steam admission valve exhibiting seat leakage.
NSE had
the responsibility of monitoring these valves for leakage.
The system engineer, recently
assigned to the system, was aware of the need to monitor for leakage.
However, since no
specific formal monitoring frequency was established,
the problem went undetected.
The
system was last operated
on March 18, 1993 for HPCI quarterly flow verification and no
evidence of seat leakage existed.
NSE has committed to monitor the HPCI steam admission
valve for leakage on both units on a weekly basis.
The other minor deficiencies, although not significant, indicate the need for greater attention
to detail to the material condition of the system.
PPEcL took or planned corrective action for
the inspector identified deficiencies at the conclusion of the inspection period.
Licensee
housekeeping
and combustible material controls for the affected areas
was adequate,
System
labeling was excellent.
The inspector concluded there was no actual safety impact caused by the HPCI vacuum
breaker test valve not being locked.
However, the containment boundary valve not being in
the condition required by the CL was a weakness.
This is a violation of Technical Specification 6.8.1 which requires appropriate administrative controls for locked valves.
(VIO 50-387/93-07-01).
2.2.2
Safety Related Pump Motor Bearing Oil Levels
During a routine tour, the inspector identified that oil level was below the standstill level on
10 of 16 safety related pump motor bearings in the Engineered
Safeguards
(ESSW) pumphouse.
The ESSW pumphouse contains four Emergency Service Water (ESW)
pumps and four Residual Heat Removal Service Water (RHRSW) pumps.
Each pump motor
has an upper and lower bearing.
The inspector had to climb to an elevated position to
clearly determine the upper bearing oil levels.
From the fioor, the inspector noted the levels
appeared
to be satisfactory.
The inspector questioned
the Auxiliary System Operator (ASO) on how he checked oil levels.
The ASO responded
he checked oil levels visually during rounds from the floor. He
considered
a level above the minimum level acceptable.
The particular individual did not
realize that there was a standstill level indication and that his check was ensure the oil level
was above the minimum level.
The individual stated this type of level marking was not
specifically covered in his non-licensed operator training.
The oil levels are not specifically
recorded on the logs but are expected to be checked during rounds.
For the bearings in
question, a sight glass exists with an operating range with minimum and maximum level and
the standstill level markings.
The standstill level mark indicates the proper oil level with the
pump secured.
This ensures proper oil level with the motor running.
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The inspector reviewed OP-PM-002, Good Lubrication Practices.
Section 4.1.1 of the
procedure requires oil levels be checked while the pump is running unless there is a static
mark (standstill level) ~
Furthermore the procedure
states ifno mark exists,
1/3 level oil
level should be maintained.
Electrical maintenance indicated the intent of the standstill level
is a reference level to ensure level remains above min and below max during pump
operation.
Electrical maintenance
stated an acceptable standstill level as a level 'close to the
standstill level.
The standstill level is a single line with no tolerance.
The inspector
concluded there was no safety significance of the condition since the oil levels were
acceptable.
However, the inspector considered
the knowledge deficiency a weakness.
In
response,
the licensee will upgrade non-licensed operator training to assure proper
performance of all level checks.
The inspector had no further questions,
3.
RADIOLOGICALCONTROLS
3.1
Inspection Activities
PP&L's compliance with the radiological protection program was verified on a periodic
basis.
These inspection activities were conducted in accordance
with NRC inspection
procedure 71707.
3.2
Inspection Findings
Observations of radiological controls during maintenance activities and plant tours indicated
that workers generally obeyed postings and Radiation Work Permit requirements.
4.
MAINTENANCE/SURVEILLANCE
4.1
Maintenance and Surveillance Inspection Activity
On a sampling basis, the inspector observed and/or reviewed selected surveillance and
maintenance activities to ensure that specific programmatic elements described below were
being met.
Details of this review are documented in the following sections.
4.2
Maintenance Observations
- The inspector observed and/or reviewed selected
maintenanc'e activities to determine that the
work was conducted in accordance with approved procedures,
regulatory guides, Technical
Specifications, and industry codes or standards.
The following items were considered,
as
applicable, during this review:
Limiting Conditions for Operation were met while
components or systems were removed from service; required administrative approvals were
obtained prior to initiating the work; activities were accomplished
using approved procedures
and quality control hold points were established
where required; functional testing was
performed prior to declaring the involved component(s) operable; activities were
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accomplished by qualified personnel; radiological controls were implemented; fire protection
controls were implemented; and the equipment was verified to be properly returned to
service.
These observations and/or reviews included:
WA 21481, Replace MDR Relay 42X-527022 for RHRSW Pump "1B" Supply Fan
1V506B, dated April 8.
WA 30114, Repair Thermo-Lag in Unit 1 Remote Shutdown Panel in accordance with
NCR 93-005 disposition, dated April 13.
WA 15336, C Emergency Service Water Pump Disassembly for Five Year Inspection,
dated April 15.
WA 30350, Replace HFA relay B21H-K51 in panel 1C622 for MSIV B/D isolation
logic, dated April 23.
4.3
Surveillance Observations
The inspector observed and/or reviewed the following surveillance tests to determine that the
following criteria, ifapplicable to the specific test, were met:
the test conformed to
Technical Specification requirements;
administrative approvals and tagouts were obtained
before initiating the surveillance; testing was accomplished by qualified personnel in
accordance with an approved procedure;
test instrumentation was calibrated; Limiting
Conditions for Operations were met; test data was accurate and complete; removal and
restoration of the affected components was properly accomplished;
test results met Technical
Specification and procedural requirements;
deficiencies noted were reviewed and
appropriately resolved; and the surveillance was completed at the required frequency.
These observations and/or reviews included:
SI-280-308,
18 Month Calibration of RWCU/MSIV System Isolation Reactor Water
Levels
1 and 2, dated April 6.
SI-180-203, Monthly Functional Test of Reactor Water Level LIS-B2-IN031A, B, C,
D, dated April 9.
SI-180-206, Monthly Functional Test of RWCU/MSIV Isolation Reactor Water Levels
1 and 2.
4.4
Inspection Findings
The inspector reviewed the listed maintenance
and surveillance activities.
The review noted
that work was properly released before its commencement,
systems and components were
properly tested before being returned to service, and that surveillance and maintenance
activities were conducted properly by qualified personnel.
Where questionable issues arose,
the inspector verified that the licensee took the appropriate action before system/component
'perability was declared.
Except as noted below, the inspectors had no further questions on
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the listed activities.
4.4.1
Class 1E Isolation Capability of the Bailey 740 MllivoltConverter
The inspector reviewed the class 1E isolator design of the Bailey type 740 millivolt
converter, specifically, relative to its use in isolating, class 1E analog inputs from computer
and annunciator systems.
This review was to determine the following: 1) whether the
licensee was bypassing the isolation capability of the converter through internal wire jumper
changes
and, 2) the possibility of inadequate documentation of changes
to the module
schematics
which, over time, could have resulted in the bypass of isolation features of
replacement converters.
The Bailey type 740 millivolt(mv) converter is designed to convert a millivoltor resistance
input signal to a 1-5 Vdc or 4-20 milliamperes output signal.
These converters provide
signal and power isolations between class 1E systems and the balance of plant (BOP) inputs.
There are two types of Bailey 740 millivoltconverters used at Susquehanna.
Types 7401 and
7403 are used with thermocouples
and resistance
temperature detectors,
respectively.
The inspector determined that twenty seven 740 mv converters were installed as isolators in
each unit. Of these, 25 were used for isolating non-1E computer/annunciator
inputs from
class 1E inputs and the remaining two were used for class 1E division isolations.
The
inspector noted that this converter had been previously tested and found to be acceptable for
use as an isolation device.
The inspector reviewed General Electric (GE) elementary diagrams, PP&L instrumentation
diagrams and vendor instruction manuals for several instrument loops which used Bailey 740
mv converters.
The inspector noted that the correct information was transferred from the GE
drawings as evidenced by the proper signal, power pin arrangements,
and wiring
configurations on the loop drawings.
The vendor instruction manual in the licensee's
document control system was appropriate for the applications at Susquehanna.
The inspector
also reviewed procurement documents and randomly inspected the Bailey 740 mv converters
in the warehouse
and found that they were properly identified and purchased
in accordance
with design requirements.
Thus, the inspector determined that the information provided in
the design documents
appeared
suitable for,the Bailey 740 mv converter applications.
10
Several (I&C) technicians were interviewed to determine their knowledge of the Bailey 740
mv converters installation and calibration.
Calibration'nformation was described in
procedure IC-DC-100, Revision 8, and vendor instruction manual 4574 K10-100.
The I&C
technicians were found to be adequately trained in the maintenance
and calibration of Bailey
740 mv converters and were familiar with its installation and operation.
The inspector also
visually verified a sample of converters installed in the diesel generator circuits.
Based on
this external inspection, the converters were found to be appropriate for their application.
Since both units were o'perating at power, the inspector was not able to verify the as-built
internal wiring of these converters.
To compensate for this, the licensee committed to verify
the wiring of a representative
sample of the mv converters during the-next periodic
calibration to assure that their isolation capability agrees with the design requirements.
If
any discrepancies
are identified the NRC Region
1 inspectors willbe informed.
The inspector questioned
the licensee regarding the possible installation of converters with
the incorrect jumper configuration.
This configuration could disable isolation features
without any accompanying external indication.
The inspector noted this as a credible
problem since certain Bailey multifunction 740 mv converters could be procured for general
applications and could be modified by the licensee to meet the class 1E isolation criteria.
In
response,
the licensee stated that all converters are tested and calibrated after any jumper
changes are made.
These changes would be noticed as anomalies during the calibration
process.
The licensee also stated that the mv converters were originally procured to meet
class lE isolation design and needed no further wiring or internal jumper changes during
initial installation.
In addition, periodic calibrations do not require any jumper changes or
wiring changes.
Any incorrect jumper or wiring changes
that c'ould bypass the converters
isolation function would be detected during the calibration as evidenced by incorrect
input/output response.
The manufacturer (Bailey), agreed with this assertion.
Work
documents were searched
to determine ifany=of the originally installed converters could have
been replaced with possible jumper or wiring changes present.
No converters have been
replaced.
Quality Control was found to be effectively monitoring calibration activities.
Based on the above, the inspector concluded that the licensee was currently providing
adequate jumper control for Bailey 740 mv converters and found no evidence of inadvertent
or improper bypassing of their isolation features.
One minor weakness
was noted in data
recording.
The inspector noted that the licensee was not documenting the calibration details
as shown in the vendor instruction manual in their calibration data sheets.
In response,
the
licensee agreed to review the calibration procedure (IC-DC-100) to determine whether there
is a need for additional instructions to avoid any possible errors.
4.4.2
Thermo-Lag Repair Unit 1 Remote Shutdown Panel
During the inspection period, the inspector observed portions of the Thermo-Lag repair in
'he
Unit 1 remote shutdown panel in accordance with NCR 93-005 disposition.
11
The inspector noted the following weaknesses:
. ~
Personnel did not cover floor/equipment as required by the work plan.
~
Yellow copy of signed ERF was not in work package
as required by NDAP-QA-306.
~
Personnel did not fully understand
respiratory safety precautions regarding use of the
trowel grade Thermo-Lag 330-1.
Additionally, the job planner did not include actual
safety precautions in the work package.
The work plan referenced
safety precautions
contained in other documents.
However, they were not available at thejob site.
The actual work was done in an acceptable manner consistent with the work plan.
However,
the above weaknesses
indicate inattention to detail regarding adherence
to specific work
procedure requirements
and a lack of thorough and complete knowledge regarding safe use of
the trowel grade Thermo-Lag 330-1.
The inspector discussed
the situation with both the
work group foreman and SSES Safety group.
The licensee agreed to include the material
safety data sheet (MSDS) in the work package where appropriate.
The MSDS provides
information concerning safe use of products used at the site.
The licensee plans to place a
Hazard Communications Center in a centrally located area of the plant.
The MSDS willbe
available to plant personnel at this more readily accessible
location.
The inspector
considered this a positive initiative.
~
~
~
5.
5.1
Inspection Activity
The inspector reviewed licensee event notifications and reporting requirements for events that
could have required entry into the emergency plan.
5.2
Inspection Findings
No events were identified that required emergency plan entry.
6.
SECURITY
6.1
Inspection Activity
PPEcL's implementation of the physical security program was verified on a periodic basis,
including the adequacy of staffing, entry control, alarm stations, and physical boundaries.
These inspection activities were conducted in accordance with NRC inspection procedure
71707.
12
6.2
Inspection Findings
The inspector reviewed access
and egress controls throughout the period.
No significant
observations were made.
7.
ENGINEERING/TECHNICALSUPPORT
7.1
Inspection Activity
The inspector periodically reviewed engineering and technical support activities during this
inspection period.
The on-site Nuclear Systems Engineering (NSE) organization, along with
Nuclear Technology in Allentown, provided engineering resolution for problems during the
inspection period.
NSE generally addressed
the short term resolution of engineering
problems; and interfaced with the Nuclear Modifications organization to schedule
modifications and design changes,
as appropriate,
to provide long term corrective action.
The inspector verified that problem resolutions were thorough and directed at preventing
recurrence.
In addition, the inspector reviewed short term actions to ensure that they
provided reasonable
assurance
that safe operation could be maintained.
7.2
Inspection Findings
7.2.1
Reactor Protection System Overvoltage Setpoint
During an ongoing review of reactor protection system (RPS) performance,
the. inspector
discovered
a potential concern with original establishment of the overvoltage setpoint for the
Unit 1 "B" RPS power supply.
Specifically, based on a March 1, 1993 letter on Design
Change Package (DCP) 92-3023, the Main Steam Isolation Valve (MSIV) solenoids are
designed to operate between
105 vac and 125 vac.
Other safety-related components powered
by the RPS busses
are designed to operate between
108 vac and 132 vac.
The current
overvoltage setpoint (129.5 vac) could potentially allow voltages above design to exist at the
MSIV solenoids.
This could result in excessive internal heating and shorten their qualified
life. The finding also implies a weakness in the licensee's
1982 efforts to determine and
document the associated
overvoltage setpoints.
The inspector questioned
the licensee on the establishment of RPS voltage setpoints provided
in Technical Specification (TS) 3.8.4.3.
These setpoints were determined prior to initial
licensing for each unit. Work Authorization (WA) U21180 (completed March 11, 1982)
measured
actual voltage drops along the power cable that supplied RPS components.
These
voltage drops were then added to the minimum and maximum design voltages for each RPS
component.
The most limiting voltage at any given component was then used to establish the
over and under voltage setpoints.
This WA showed that the most limiting voltage for the
MSIV AC solenoids was 126.1 vac, as compared to the current TS setpoint of 129.5 vac.
Thus, the current overvoltage setpoint could potentially allow voltage above design (125 vac)
at the MSIV solenoid valves.
I
13
The licensee provided a June 28, 1988 letter from the solenoid supplier that lists the
maximum acceptable voltage as 132 vac, and indicates that the current setpoint is acceptable.
However, this did not justify operation from 1982 to 1988 with the current setpoint.
The
licensee suggested
that General Electric (GE) verbally approved the operation of MSIV AC
solenoids up to 132 vac during initial construction.
WA U21180 showed that the MSIV AC
solenoids for the "A" RPS were inaccessible
and GE startup approved the omission.
In
addition, WA U21180 Step 5.b. excluded the MSIV AC solenoids from the overvoltage
setpoint determination.
This provided some limited justification for the licensee's position.
The inspector reviewed the licensee's justifications and noted that records loosely support
their assertion.
However, the licensee apparently operated for six years without appropriate
documentation for their RPS overvoltage setpoints.
Since the June 28, 1988 letter clarifies
the MSIV AC solenoid voltage requirements,
this concern is more administrative than
technical in nature.
Thus, although this apparent noncompliance was identified by the
inspector, it will not be cited because
the criteria in Section VII.B. of the enforcement policy
were satisfied.
The inspector also noted that the licensee did not have a predefined program to address
vendor initiated changes
to design information.
The June 28, 1988 letter changed
the
operating voltages to 108 vac to 132 vac. However, this information was not added to the
Susquehanna
Equipment Inventory System (SEIS) nor the equipment qualification (EQ)
database,
The lack of updates in these and other systems apparently led to the inclusion of
the old voltage band (105 vac-125 vac) in the March 1, 1993 DCP description.
Other
communications (SILs, TILs, RICSILs, etc.) are received that change or update design
information.
Although licensee programs review these communications,
there is no
requirement to update SEIS, the EQ database or other plant information systems (PMIS).
The licensee has agreed to review the need for a design input checklist or some other
mechanism to ensure that changes or clarifications to plant design information are adequately
captured in plant information systems.
8.
SAFETY ASSESSMENT/QUALITY VERIFICATION
8.1
Licensee Event Reports
The inspector reviewed LERs submitted to the NRC office to verify that details of the event
- were clearly reported, including the accuracy of the description of the cause and the
adequacy of corrective action.
The inspector determined whether further information was
required from the licensee, whether generic implications were involved, and whether the
event warranted onsite followup. The following LERs were reviewed:
93-001-00
14
ESF Actuation Due to Electrical Transient When Radwaste Electrical
Transformer Failed
On February
1, 1993 invalid ESF actuations occurred on both units as a result of load center
transformer OX340 failure.
The inboard and outboard containment isolation valves for Loop
"B" of the Containment Gas Analyzer System isolated in both units.
Additionally, the
containment instrument gas back-up storage bottle header isolation valves opened.
The
licensee determined the cause of failure was water dripping onto the transformer core and
coils." The source of water was identified as condensation
forming on the internal surface of
HVAC ductwork and subsequent
leakage from the duct low point. PAL determined warm
moist air in the duct combined with the ambient room temperature below the dewpoint
resulted in the formation of condensation.
Licensee corrective actions consist of planning
installation of a moisture barrier below the ductwork and a review of the electrical system to
assess
capability of minimizing effects of faults in non-1E components on safety related
components.
The licensee was not able to determine the root cause of the high humidity in the process air
at the time of LER submittal.
The licensee is conducting a long-term investigation.
The
inspector agreed with the licensee's reportability determination.
The inspector determined
the licensee's
short-term actions to prevent recurrence were acceptable.
The licensee is
reviewing the onsite AC power system design for enhancements
to reduce the susceptibility
'f
non-class
1E faults from affecting safety-related
class 1E systems.
This event was
documented in NRC Inspection Report 50-387/93-01.
93-002-00
Instrument Repair Leak Required Entry into LCO 3.0.3,
On January 22, the licensee entered Technical Specification (TS) Limiting Condition for
Operation (LCO) 3.0.3 at 12:55 p.m. following repair of a small leak'n the valve manifold
for reactor water level switch LIS-B21-IN031D. The licensee repaired the leak due to
heightened awareness of the effects of reference leg leaks on reactor water level (Generic Letter 92-04) ~ LIS-B21-IN031D provides initiation signals to Division Core Spray, Division
IILPCI, HPCI, ADS and RCIC. The action of TS LCO 3.3.3.b requires the associated
inoperable trip system to be placed in the tripped condition within one hour or declare the
associated
The licensee declared the associated
ECCS inoperable since
placing the trip system in the tripped condition would result in actuation of the ECCS.
TS 3.0.3 was entered when the ECCS TS 3.5.1 actions could not be met.
The licensee
repaired the leak and LCO 3.0.3 was cleared at 3:23 p.m. on January 22:
The inspector
agreed with the licensee's reportability determination.
There were no safety consequences
resulting from entry in TS LCO 3.0.3.
The inspector found the licensee's
decision to effect
the repair prudent.
15
8.2
Open Items
8.2.1
(Closed) Unresolved Item 50-387/89-21-02, RCIC and HPCI Rupture Disc NCRs
on Post Work Testing Inadequate
During inspection 50-387/89-21, the inspector noted that non-conformance reports {NCRs)
identified missed visual examinations (VT-2's) for the reactor core isolation cooling (RCIC)
and the High Pressure
Coolant Injection (HPCI) systems.
These visual exams were required
after the replacement of each turbine's exhaust rupture disc.
However, they were not done.
The inspector reviewed the work authorizations (WAs) for both HPCI and RCIC and noted
that rupture disc replacement was specified as a part of the preprinted instructions.
However, these instructions did not specify the VT-2 exam as required by administrative
procedures
and the ASME code.
The VT-2 exam requirement was later added to the
recommended
operational testing section of the RCIC WA by hand.
Following completion of
the RCIC maintenance work, four licensee groups reviewed the WA, failed to notice the
missed VT-2, and ultimately closed the WA. Although the HPCI work was similar, the VT-
2 exam was inadvertently omitted from the work documentation,
and thus, not performed.
The inspector opened this unresolved item due to weaknesses
in the licensee's control of
post-maintenance
testing.
The licensee investigated the cause of the missed VT-2's and determined that the missed VT-
2 exam on RCIC was due to an oversight by operations (the WA was closed without
performing the VT-2 exam specified in the operational testing section).
The licensee
attributed the missed VT-2 exam on HPCI to an oversight by the work planning group
(failure to specify that a VT-2 exam was required following replacement of the disk).
Reviews of the WAs for closure by the work group, quality control (QC) and operations also
failed to identify the missing requirements.
As a result, the licensee provided the following
, corrective actions:
Maintenance is to ensure that all post work testing requirements,
including visual
exams, are included on the Equipment Release Form (ERF) associated
with the work
document.
This willensure that all post work testing requirements
are entered in the
computerized system status file by the Unit Coordination Group.
Training per Hot Box 89-63 was conducted for the operation's personnel to stress the
importance of proper review and closeout of work documents.
AD-QA-482, Post Maintenance/Modification Test Program specifies the requirements for
post maintenance
testing.
The licensee attributed the failure to perform the required VT-2
exams to isolated personnel error and they are confident that the actions stated above will
prevent future similar errors.
16
In a previous update (50-387/92-20), the inspector searched
the NCR database
and identified
five cases where VT-2 visual examinations were missed; two in 1989, one in 1990, one in
1991, and one in 1992.
The cause for each instance was unique (not similar to the
aforementioned
missed VT-2's) and the inspector concluded that for each case, appropriate
corrective actions were taken to prevent recurrence.
In the current inspection, the inspector reviewed AD-QA-482 (NDAP-QA-482) and discussed
the previously missed VT-2's with the unit coordination group and shift supervision.
The
NCR database
was searched for recently missed VT-2 exams.
None were found. In
discussions with the licensee,
the inspector noted an increased
awareness of the VT-2
examination requirements.
Based on the above, this item is closed.
8.2.2
(CLOSED) Unresolved Item 50-387-90-21-01, Firewatch Rounds Not Completed
As Required
In January
1990, the licensee submitted a Licensee Event Report (LER 50-387/90-002-00)
that informed the NRC that during a three week period, four of seven roving firewatch
personnel did not complete all of their assigned rounds during midnight shifts.
The failure to.
make certain firewatch rounds was a violation of plant Technical Specifications 3.7.6 and
3.7.7.
The licensee's investigation found that the four individuals had received adequate training and
understood their responsibilities.
As a result, PP&L terminated their employment.
As
corrective actions the licensee installed a watchman key code station system to provide a
permanent,
easily-retrievable record of all firewatch rounds.
In addition, the licensee
implemented additional supervisory unannounced
backshift inspections.
The NRC opened an
unresolved item pending completion of the licensee's corrective actions.
Subsequently,
an
audit of firewatch logs and security transactions
was performed by personnel from PP&L's
Allentown office. The audit sampled security access
data and firewatch logs for eight roving
firewatch employees of all shifts during the week ending July 22, 1990.
They did not find
any skipped rounds, missed stations, or falsified times on the firewatch logs for that time
period.
The inspector independently reviewed a sample of the watchman key code system data,
official firewatch logs, and discussed
the status of the firewatch program with licensee
personnel.
No problems were identified and it appears that the licensee's corrective actions
have been effective in preventing recurrence of the problem.
The inspector reviewed a sample of the watchman key code system data, official firewatch
logs, and discussed
the status of the firewatch program with licensee personnel.
No
problems were identified and it appears
that the licensee's corrective actions have been
effective in preventing recurrence of the problem.
The missed firewatch rounds were a
violation of the TS, however, this violation meets the criteria of 10 CFR Part 2 Section
VII.Bfor non-cited violations.
The NRC's disposition of the unresolved item is based on the
17
licensee's identification of the problem, their effective corrective actions, and the apparent
severity level of the violation.
The inspector had no further questions and considered
this
unresolved item closed.
8.2.3
(Closed) Violation 50-387/91-06-01, Inservice Test Program Omission
During an inspection of the licensee's Inservice Testing {IST) program, an inspector
identified that the licensee did not include certain safety related containment instrument gas
(CIG) check valves {1-26-018, 1-26-029, Unit 1; and 2-26-018, 2-26-029, Unit 2) in their
IST program.
Consequently,
these check valves were not tested as required Section XIof
the American Society of Mechanical Engineers (ASME) Code.
During the original
inspection, the inspector found the licensee's implementation of the IST program to be
otherwise good.
The CIG check and solenoid valves provide double valve isolation between the safety related
and non-safety related portions of the CIG system.
The licensee believed that the check
valves did not function as safety related isolation valves and thus did not incorporate the
check valves into the IST program.
However, documentation (piping and instrumentation
diagrams (P&IDs), valve data lists, work authorizations, etc.) identified the check valves as
safety related isolation valves.
An inspector identified this discrepancy,
which provided the
basis for the violation. In response
to the violation, the licensee incorporated the check
valves into the next revision of the IST program.
Section XI of the ASME Code requires
testing check valves on a quarterly frequency; or ifimpractical, on a cold shutdown
frequency.
The licensee submitted a relief request to test the CIG check valves on a
refueling outage frequency as opposed to a quarterly frequency.
The NRC denied the relief
request since the relief request did not address why testing was impractical on a cold
shutdown frequency.
The NRC granted interim relief for one year, ending June 23, 1993,
allowing the licensee to test the check valves on a refueling outage frequency.
The licensee
has agreed to submit a revised relief request discussing why CIG check valve testing is
impractical on a quarterly or cold shutdown frequency.
The licensee tested the Unit 1 CIG
check valves on March 13, 1992 during the Unit 1 sixth refueling outage.
The licensee
tested the Unit 2 CIG check valves on September
14, 1992 during the Unit 2 fifth refueling
outage.
The inspector reviewed the licensee's IST program and noted that the program included the
CIG check valves and the relief request.
The inspector checked the IST valve list against the
Unit 1 P&IDs to determine the extent of valve omissions and identified no deficiencies.
The
inspector investigated testing the check valves on a cold shutdown frequency and found that
the check valves could be tested.
However, testing requires that service air be cross tied to
supply certain CIG loads, causing the containment oxygen concentration
to increase.
Technical Specifications provides limits on oxygen concentration which indicates that this
type of testing may not be feasible for short duration unplanned shutdowns.
The inspector
reviewed the CIG check valve surveillances and identified no anomalies.
Since the licensee
revised the IST program and the omission appears isolated, this item is closed.
C
e
18
8.3
Susquehanna
River Flooding
During March and April, the Susquehanna
River level rose above flood stage many times.
This flooding was the result of snow melt in upstate New York, along with repeated heavy
rain falls. The licensee took actions to cope with this condition.
The inspector evaluated the effects of the flooding on both Susquehanna
units and noted that
ON-000-002, Natural Phenomena provides guidance for high river levels. It requires that,
additional tours be made by operations and security personnel.
The inspector questioned the
licensee on their implementation of this requirement on March 30 and 31.
During the March
30 discussion,
the licensee was unable to provide the details for the increased
operational
tours even though they were implementing ON-000-002.
Discussion held the following day
indicated that shiftly rounds were changed from two to four times per shift. The licensee also
provided additional guidance to touring nuclear plant operators
and to security personnel,
thus, supporting the procedural requirement for more frequent tours.
The difference in actions on these dates was primarily attributable to the wording in Section
3.5 of ON-000-002.
Steps 3.5.2 and 3.5.4 require additional tours by both security and
operations personnel at apparently different river levels which results in unnecessary
redundancy.
Neither of these steps indicate what components or conditions (i,e., screen
clogging, river water makeup pump performance,
etc.) are to be evaluated.
Step 3.5.4
requires action prior to 382" (515'levation) without identifying a specific level.
Step 3.5.5
requires river level monitoring through the Power Control Center (PCC).
The licensee's
security organization tracked river level by contacting Luzerne County Emergency
Management Agency (LCEMA) and did not use the PCC.
The inspector noted the procedure
was general in nature and did not adequately
address
the need for action.
However, it did
not appear to adversely impact the licensee since they successfully managed activities
throughout the flooding.
Overall, the licensee's
management of the river flooding was good despite the procedural
inadequacies.
The inspector has discussed
these procedural inadequacies
with the licensee
-and the licensee has agreed to revise the procedure to address
these apparent weaknesses.
The inspector had no further questions.
8.4
(Closed) Temporary Instruction (Tl) 2515/112 - Licensee Evaluations of Changes
to the Environs Around Licensed Reactor Facilities
Background
The NRC issued Temporary Instruction (Tl) 2515/112, Licensee Evaluations of Changes to
the Environs Around Licensed Reactor Facilities.
The NRC issued the TI to determine ifthe
licensee's programs are adequate in evaluating public health and safety issues resulting from
changes in population distribution or in industrial, military, or transportation
hazards that
could arise on or near reactor sites.
t
I
19
Scope
The inspector reviewed Susquehanna
Steam Electric Station's programs relative to evaluating
public health and safety issues resulting from changes in population distribution, industrial,
military, or transportation hazards that could arise on or near Susquehanna.
The inspector
reviewed the current Final Safety Analysis Report (FSAR), NRC Safety Evaluation Report
(SER), 10 CFR 50.71, 10 CFR 100, and Generic Letter 81-06.
Licensee Evaluation of Changes in the Environs
The inspector questioned how the licensee evaluated changes to the environs with personnel
that oversee updating the FSAR.
The licensee did not have a formal program in place to
evaluate changes
to the site environs.
However, the licensee performed an evaluation and
submitted the FSAR update in response
to inspector questions that were prompted by TI 112.
The inspector considered
this a positive initiative. The FSAR has been updated to reflect
changes
to the site environs.
The update was submitted to the NRC June 30, 1992.
previously provided updates to the FSAR that refiected changes
to the site environs.
The licensee plans to implement a program that willrequire periodic evaluation of changes to
the environs.
The licensee will update Section 2.1, Geography and Demography, every 10
years coincident with issuance of the U.S. census.
This is based on the census, which is
done every 10 years.
Section 2.2, Nearby Industrial, Transportation,
and MilitaryFacilities,
willalso be updated every 10 years.
The licensee based this frequency on a history of
relatively few changes to facilities in proximity of the site.
The licensee willevaluate and
update the FSAR between scheduled revisions should a significant change to the site environs
occur.
The individual who was responsible for evaluating the changes to the environs held a
masters'egrees
in Environmental Science and Biology, was a registered Environmental Manager,
and had 22 years experience.
Organizationally, the individual worked in Nuclear
Technology in Allentown (Corporate Engineering) in the Environmental Services Section.
Geography and Demography
The licensee did not identify any significant changes in population distribution during the
- review.
The site demography data has been updated.
The general trend of population has
been decreasing.
There has been a decrease
in urban population and an increase in rural
population.
However, the overall population distribution did not exceed
those predicted in
the original FSAR.
20
Site Proximity Hazards
The licensee did not identify any significant changes in military; industrial or transportation
hazards that could affect public health and safety.
However, the FSAR had been updated
previously to reflect the addition of two natural gas pipelines in the vicinity of the site. The
licensee analyzed the hazards associated
with these changes to the site proximity. These
updates were performed on as needed basis rather than from a formal periodic review
process.
The licensee also updated this section of the FSAR 2.2 in response to the TI. The
updates did not pertain to any new hazards.
Summary
The inspector concluded that the licensee initiated response
to the TI was a strength.
The
inspector found the evaluation was performed by individuals with appropriate qualifications.
The FSAR had been previously updated to reflect the installation of the new natural gas
pipelines.
The inspector concluded this was a positive finding. However the licensee did not
have in place any formal programs to evaluate changes to the site environs and the potential
effects on public health and safety prior to issuance of the TI. Currently the licensee is in
the latter stages of developing a formal program to conduct such reviews and evaluations.
The inspector had no further questions.
This inspection closes TI-2515/112.
9.
MANAGEMENTAND EXIT MEETINGS
9.1
Resident Exit and Periodic Meetings
The inspector discussed
the findings of this inspection with station management
throughout
and at the conclusion of the inspection period.
Based on NRC Region I review of this report
and discussions
held with licensee representatives,
it was determined that this report does not
contain information subject to 10 CFR 2<<790 restrictions.
9<<2
Inspections Conducted By Region Based Inspectors
ate
4/5 - 4/8/93
~eb'eet
EOP Inspection
~lns xction
~Re ort N
.
93-06
~Re o~rtin
~Ins )ear
D. Florek
<
Ab reviati
n List
ATTACHMENTl
ANSI
CFR
CIG
CL
DX
ERT
IERP
JIO
LCO
LER
NPE
NQA
NRC
NSE
- Administrative Procedure
- Automatic Depressurization
System
-.American Nuclear Standards Institute
- American Society of Mechanical Engineers
- Containment Atmosphere Control
- Code of Federal Regulations
- Containment Instrument Gas
- Checklists
- Control Rod Drive Mechanism
- Control Room Emergency Outside AirSupply System
- Diesel Generator
- Direct Expansion
- Emergency Core Cooling System
- Engineering Discrepancy Report
- Electrical Protection Assembly
- Environmental Qualification
- Event Review Team
- Engineered
Safety Features
- Emergency Service Water
- Engineering Work Request
- Fuel Oil
- Final Safety Analysis Report
- Heating, Ventilation, and Air Conditioning
- Industry Event Review Program
- Instrumentation and Control
- Justifications for Interim Operation
- Limiting Condition for Operation
- Licensee Event Report
- Local Leak Rate Test
- Loss of Coolant Accident
- Non Conformance Report
- Nuclear Department Instruction
- Nuclear Plant Engineering
- Nuclear Plant Operator
- Nuclear Quality Assurance
- Nuclear Regulatory Commission
- Nuclear Systems Engineering
- Open Item
PC
PMR
PSID
SOOR
SPING
TS
WA
- Out-of-Service
- Protective Clothing
- Primary Containment Isolation System
- Plant Modification Request
- Plant Operations Review Committee
- Pounds Per Square Inch Differential
- Quality Assurance
- Reactor Building
- Reactor Building Closed Cooling Water
- Reactor Core Isolation Cooling
- Regulatory Guide
- Residual Heat Removal Service Water
- Standby Gas Treatment System
- Surveillance Procedure,
Instrumentation and Control
- Surveillance Procedure,
Operations
- Significant Operating Occurrence Report
- Safety Parameter Display System
- Sample Particulate, Iodine, and Noble Gas
- Technical Specifications
- Work Authorization
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