ML17059B749

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Insp Repts 50-220/97-80 & 50-410/97-80 on 970804-22. Violations Noted.Major Areas Inspected:Operation,Maint & Engineering
ML17059B749
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 10/17/1997
From: Doerflein L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17059B747 List:
References
50-220-97-80, 50-410-97-80, NUDOCS 9711030003
Download: ML17059B749 (82)


See also: IR 05000220/1997080

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION

I

Docket Nos.:

50-220; 50-410

Report No.:

97-80; 97-80

Licensee:

Niagara Mohawk Power Corporation

Facility:

Nine Mile Point

Location:

Oswego, New York

Dates:

August 4 - 22, 1997

Inspectors:

G. K. Hunegs, Senior Resident Inspector

G. S. Galletti, Human Factors Branch, NRR

C. W. Smith, Project Manager,

NRR

E. C. Knutson, Resident Inspector

R. A..Skokowski, Resident Inspector

Approved by:

~&et+>" ~

. l'~..~.

~~l<~~~~

Lawrence T. Doerflein, Chi f

Projects Branch

1

Division 'of Reactor Projects

97ii030003 9'7i024

PDR

ADOCK 05000220

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pDR

ah

TABLE OF CONTENTS

TABLE OF CONTENTS

EXECUTIVE SUMMARY

IV

I ~ OPERATIONS

03

07

08

08.3

Operations

Procedures

and Documentation

03.1

Corrective Action Program Procedures.....

03.2

Operability Determination Procedures

Quality Assurance

in Operations

.

07.'I

Review of Deviation/Event Reports

07.2

Root Cause Analysis

07.3

Deviation/Event Report Program Summary Trend Report ..

~ ..

07.4

Corrective Action Program Quality Assurance Audits

07.5

Operating Experience Review Process

. ~....,

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07.6

Adverse Trend Identification .. ~.....

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07.7

Independent

Safety Engineering Group (ISEG)

07.8

Self Assessment

Program

~ ..

~

.

07.9

Corrective Action Program Related to Human Performance

Miscellaneous Operating Issues

08.1

Unresolved Item 50-410/95-25-03:

DERs Extended Without

Justification

08.2

(Closed) Inspector Follow Item 50-410/96-07-12:

Weaknesses

in the DER Process

(Closed) Inspector Followup Item (IFI) 50-410/96-07-13:

ISEG

Review of NRC Documents....

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1

1

1

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2

3

3

5

7

8

10

11

13

14

14

16

16

17

17

II. MAINTENANCE

M3

M8

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Conduct of Maintenance

M1.1

Emergent Maintenance

Maintenance

and Material Condition of Facilities and Equipment

M2.1

Material Condition Observations

M2.2

Unit 2 Drywell Cleanliness Controls...

~

M2.3

Unit 2 Residual Heat Removal System Flow Control Valve

Problem

M2.4

Unit 2 Steam Tunnel Door Seal

.

Maintenance

Procedures

and Documentation

~ .

M3.1

Problem Identification and Work Control Process

M3.2

Operator Work Arounds

Miscellaneous Maintenance

Issues

M8.1

(Closed) Unresolved Item 50-410/95-25-02:

Extended

Inoperability of the Unit 2 Loose Parts Monitor...........

M8.2

(Closed) Inspector Followup Items 50-220/96-07-17

and 50-

4'IO/96-07-17:

Extended Installation Period for a Service

Water System Temporary Modification

18

18

18

20

20

22

24

26

27

27

28

30

30

31

a5

Table of Contents (cont'd)

III~ ENGINEERING

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E7

Quality Assurance

in Engineering Activities

E7.1

50.59 Program Review

E8

Miscellaneous

Engineering

Issues

E8.1

IFI 50-220 5 410/96-07-14:

Weaknesses

Program

I

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0

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in the 50.59

31

31

31

32

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32

V. MANAGEMENTMEETINGS

X1

Exit Meeting Summary...

~ .

X2

Review of UFSAR Commitments...

~

33

33

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33

ATTACHMENT

Attachment

1 - Partial List of Persons

Contacted

- Inspection Procedures

Used

- Items Opened,

Closed, and Discussed

- List of Acronyms Used

EXECUTIVE SUMMARY

Nine Mile Point Units

1 and 2

NRC Inspection Report Nos. 50-220; 50-410/97-80

~Oerations

The procedures

for implementing the corrective action program and operability

determination were generally good with some shortcomings

noted.

The use of the

validation test for root cause

and corrective actions was considered

a good aid for

verifying the quality of proposed corrective actions.

In general, the licensee analyzed and resolved problems.

However, shortcomings

were identified With the quality of root cause determinations,

corrective actions and

documentation.

Root causes

and apparent root causes

were generally good at

identifying the first level, technical causes

but tended to stop and not go to a

greater depth.

Therefore what was necessary

to prevent recurrence was not

always fully developed.

Several weaknesses

in the programs to identify and

address

human performance

issues were apparent.

Self assessment

and quality

assurance

activities were generally effective and improvement in these areas was

noted.

A violation was identified concerning the failure to justify the extension of

deviation/event

report (DER) due dates.

Furthermore,

the licensee's corrective

actions to prevent recurrence of this previously identified concern were ineffective.

Maintenance

The licensee was effective in resolving emergent maintenance

issues including the

Unit 2 reactor coolant system flexible hose failure, the Unit 2 service water makeup

control valve to the circulating water system malfunction, and the Unit 2 emergency

diesel generator

DC control power annunciator failure. The operations department

made significant contributions both to the identification of problems and control of

'plant conditions to support maintenance.

An inspector followup item concerning

the failed flex hose was documented

in a separate

NRC inspection report No. 50-

41 0/97-06.

The overall material condition of Unit 2 was good; however, inspector identification

of several material problems in the reactor building indicated that additional material

inspections

by the licensee could be productive.

The material condition of the

steam tunnel was assessed

to be poor.

Based on the material deficiencies that

were identified by the inspectors

in this area, it did not appear that the licensee was

taking full advantage

of the forced outage to inspect normally inaccessible

areas of

the plant for emergent material problems.

Drywell cleanliness was generally good; however, cleanliness requirements for the

drywell are not clearly established

in the governing procedure

especially with

respect to control of downcomer foreign material exclusion covers.

Executive Summary (cont'd)

Given the safety significant functions performed by the "B" residual heat removal

system full flow test valve, licensee investigation of the reported degraded

condition of the valve was slow. Additionally, the decision to start the 72 hr LCO

at 11:00 a.m. on August 19, rather than on the afternoon of August 18, when the

condition was reported, was not conservative.

The intermediate valve position

indication that occurred'n June 1997 was apparently

a missed opportunity to

identify the loose stem lock nut.

The temporary modification that installed a urethane

seal on the Unit 2 inner steam

tunnel door in 1992 was inadequate,

in that it failed to account for environmental

temperatures

that exceeded

the design temperature

of the seal material.

After seal

degradation

was identified, corrective actions were appropriate.

Use of the

~ inappropriate

seal material from 1992 until 1996 had the potential to cause

a failure

of secondary containment; however this did not occur, and the degraded

condition

,did not constitute

a violation of any other specific regulatory requirements.

Operability of the door as a fire barrier was not affected by the degraded

seal.

The problem identification (PID) system procedures

established

adequate

guidance

for work control.

However, the PID process

does not procedurally ensure the same

level of review and evaluation

as does the DER entry mechanism for the corrective

action program.

Adequate procedures

and processes

are in place for identification and correction of

operator work arounds.

Unit 2 has been effective in reducing the number of

operator work arounds

and longstanding tagouts.

Some items being carried on the

Unit 2 operator work around list apparently have no recourse remaining, and could

lessen the credibility of this corrective action mechanism.

~ncnineering

The quality of safety evaluations reviewed was good.

The improvement in quality

was attributed in part to good senior management

oversight of the program.

In

'

contrast to the quality of the safety evaluations,

the quality of applicability reviews

was mixed primarily due to the level of documentation.

In some cases,

documentation

was not sufficient to support the conclusions

reached.

Overview

Through the review of several licensee programs, performance indicators, material

condition deficiencies and discussions

with licensee personnel,

the inspectors evaluated

the effectiveness

of the licensee's controls for identifying, resolving, and preventing issues

that degrade the quality of plant operations

and safety.

The objective of the inspection

was to determine if the licensee's corrective action program resulted in problems getting

resolved.

I. OPERATIONS

03

Operations Procedures

and Documentation

03.1

Corrective Action Program Procedures

a.

Ins ection Sco

e

The team assessed

the licensee's corrective action program procedures to

determine whether adequate

controls are in place to facilitate an effective program.

Findin s and Observations

Niagara Mohawk Power Corporation's

(NMPC's) corrective action program was

controlled by Procedure

NIP-ECA-01, "Deviation/Event Report," Revision 11, with

additional guidance for deviation/event report (DER) dispositioning provided in

Procedure,

S-GUI-ECA-0101, "Guidelines for DER Disposition," Revision 00.

Although some shortcomings were noted, the implementing procedures

for the

corrective action program were generally good.

Particularly noteworthy was the

validation test to verify the quality of proposed corrective actions.

Furthermore, the

team noted that improved guidance regarding

10 Code of Federal Regulations

(CFR)

Part 21 reviews was incorporated

in Procedure

NIP-ECA-01 subsequent

to a

weakness

identified in this area in NRC Inspection Report (IR) 50-410/97-01.

The most significant shortcoming with the licensee's corrective action procedures

was that an acceptable

length of time to route a DER to the station shift supervisor

(SSS) was not specified.

Since the initiator may not be fully aware of the impact of

a concern with respect to plant conditions, and since the SSS is responsible for

making equipment operability determinations,

timely routing of DERs to the SSS is

critical.

Additional shortcomings with the DER procedures

included a lack of guidance on

evaluating the extent of the problem, such as verifying other susceptible

locations

for similar problems.

Nominal guidance was provided regarding specific reviews for

repeat failure and for the identification of adverse trends.

No guidance was

provided describing management's

expectations

regarding the branch managers

review of the quarterly'DER Trend Report.

Further details regarding these

shortcomings

are provided within the applicable sections of this report.

)

Conclusions

The procedures

for implementing the corrective action program were generally good

with some shortcomings

noted.

The use of the validation test for root cause and

corrective actions was considered

a good aid for verifying the quality of proposed

corrective actions.

03.2

Operability Determination Procedures

Ins ection Sco

e

The station shift supervisor

is responsible

for making decisions concerning

operability and may request that the NMPC engineering department provide an

analysis to provide technical justification for the decision.

The team assessed

the

.adequacy

of the licensee's

procedures

associated

with operability determinations

by

comparing the procedures

to the guidance provided in NRC Inspection Manual

Sections on Resolution of Degraded

and Nonconforming'Conditions

and Operability

as referred to by Generic Letter 91-18.

b.

Findin s and Observations

0 erabilit

Determinations

I

The Nine Mile Point Unit

1 (Unit 1) Procedure

N1-ODP-OPS-0103,

"Equipment

Operability Determinations,"

Revision 00, and Nine Mile Point Unit 2 (Unit 2)

Procedure

N2-ODP-OPS-0001,

"Conduct of Operations,"

Revision 8, are associated

with operability determinations.

The procedures

were found to be consistent with

each other and with the guidance provided in Generic Letter 91-18.

The procedures

provided the station shift supervision with a checklist to aid in operability

determinations

and guidance

in whether requesting

an engineering support analysis

(ESA) would be necessary.

During the team's review of DERs, no examples of improper operability

'determinations

were identified.

However, as described

above, the team noted that

the DER procedure

lacked positive controls to ensure that DERs would be routed to

the station shift supervisor in a timely manner.

The team identified one DER (1-97-

0002) associated

with core spray system design pressure

inaccuracies

in the

UFSAR that took six days from initiation until it reached the SSS.

Although the SSS

determined that the discrepancy

associated

with DER 1-97-0002 did not adversely

impact system operability, the excessive time for the DER to reach shift supervision

failed to meet licensee managemeiir, expectations.

En ineerin

Su

ortin

Anal sis

The team reviewed NMPC's Engineering

Guidelines entitled "Engineering Supporting

Analysis," NEG-1E-0006 and NEG-2S-010 for Units

1 and 2 respectively.

Both

procedures

contained essentially the same information and were consistent with

Generic Letter 91-18.

However, the team noted that the Unit 2 guidelines lacked

information regarding the level of supervision required for approval of ESAs.

Discussion with the Unit 2 Engineering Department Manager indicated that the first

level supervisor was responsible for ESA approval.

The team found this consistent

with the guidance for Unit

1 ESA approvals

and with the Unit 2 ESAs reviewed.

The team found the procedural guidance regarding ESAs appropriate.

C.

Conclusions

The procedural guidance regarding operability determinations

and ESAs were

consistent with the guidance provided in Generic Letter 91-18, and considered

appropriate.

07

Quality Assurance

in Operations

07.1

Review of Deviation/Event Reports

a

~

Ins ection Sco

e

The team reviewed selected

DERs for both units to assess

implementation adequacy

and technical quality.

b.

Findin

s and Observations

Im lementation Ade uac

Some minor implementation discrepancies

were noted.

These discrepancies

were

normally administrative in nature and did not impact the quality of the DER.

However, the team noted that a relatively large number of DERs were past the due

date without procedurally required extension requests,

this concern is described

in

detail in Section 08.1, "Unresolved.Item 95-25-03:

DERs Extended without

Justification."

The DER procedure

(NIP-ECA-01) requires the plant managers

to categorize

DERs

with respect to significance.

This allows issues of higher significance to receive

more stringent evaluation and quicker disposition.

The procedures

provided

a list of

examples to aid in determining the appropriate

DER category.

The team noted at

least six cases where DER categorization was questionable.

Although the category

determined for each case fit examples provided, the team considered

the DERs to

be better suited to the examples provided for the next higher category.

The questionable

categorization was common to two areas.

First, DERs associated

with potential common mode failure issues (for example DERs 1-97-0565 and 1-97-

1482 associated

with equipment response

to high energy line breaks, and DERs 2-

97-0498 and 2-97-1560, associated

with recurring failures of a component within

the Riley temperature switches as described

in Section 07.6), were category 2.

The team considered

category

1 to be more suitable for these

DERs since "common

mode failure" was specifically provided in the DER procedure

as an example of a

category

1 DER.

Second,

DERs associated

with adverse trend (for example

DER 2-

P

97-0203 regarding recurring Unit 2 Operations Department failure to comply with

administrative procedures

as described

in Section 07.6) were category 3; the team

considered

category 2 to be more suitable based

on the extensive nature of the

concerns.

Technical Qualit

The team reviewed

a representative

sample of DERs for technical quality, and

generally found that problems were analyzed and resolved.

However, some

shortcomings

were identified regarding root cause determination

and corrective

actions.

Concerns associated

with root cause analysis are included in Section

07.2.

The issues associated

with corrective actions include ineffective corrective

actions, corrective actions not addressing

the root cause, narrowly focused

corrective actions, and poorly documented

DER dispositions.

Examples of DERs with corrective actions that did not address

the root cause

included DER 2-96-2155, "QVSA - Adverse Trend 'Chemical Control'iolations of

NIP-CHE-01," which is described

in Section 07 .6, "Adverse Trend Identification."

Also, DER 1-97-1439 associated

with feedwater low flow control valve leakage

illustrated corrective actions not associated

with the root cause.

Although the

licensee determined the leakage not to be excess'ive,

the root cause of the leakage

was determined to be component

aging; however, no corrective actions were taken

to address the aging concern.

Furthermore, the closure summary of this DER

included

a recommendation

to reduce the differential pressure

across the valve to

minimize leakage; but, no means were in place to track this recommendation.

Narrowly focused corrective actions were noted in DERs 2-97-0203, 2-97-0201

and

1-97-1850.

DER 2-97-0203:

Adverse Trend in Operations Abilityto Implement

Administrative Requirements,

as described

in Section 07.6, "Averse Trend

Identification," in which the corrective actions only addressed

Unit 2 Operations

Department, when all departments

on site were susceptible to this problem.

The

corrective actions for DER 2-97-0201 associated

with a high frequency of valves

found out of position, only addressed

Unit 2, when the potential for similar concerns

existed at Unit 1.

DER 1-97-1850 associated

with a control room vent chiller

failure, as described

in Section 07.2, "Root Cause Analysis," determined the cause

of the failure to be the deferral of system periodic preventive maintenance.

However, the corrective actions only focused on the chiller that failed, no indication

was provided regarding the status of the preventive maintenance

for the other

division chiller, nor was an evaluation of the impact of deferred preventive

maintenance

for other equipment available.

In general, the team considered

the quality of the documentation

associated

with

DER dispositions to be acceptable.

Some of the better documented

dispositions

provided written answers to the root cause and corrective action validation test

described

by the licensee's

procedure.

However, the team considered

the

documentation oi some DERs to be poor.

In particular, the disposition for DER 1-

97-0697 regarding degraded

wiring in an emergency diesel generator

(EDG) relay

target coil was poor due to the limited information provided.

The team discussed

P

the issues with the relay and controls supervisor,

and obtained pertinent information

that was not provided within DER disposition.

Information, such as, that the similar

relays for the EDG were verified not to be degraded,

and the programmatic controls

in place to allow the licensee to identify similar problems with other relays.

Conclusions

ln general, the licensee analyzed and resolved problems.

Howe'ver, based on the

DERs reviewed, shortcomings

were identified in the following areas:

4quality of root cause determinations;

oeffectiveness

of corrective actions;

oadequacy

of corrective actions to address the root cause;

oscope of corrective actions;

odocumentation

of DER disposition;

ocategorization of DERs; and

oextension of DERs without required justification.

Root Cause Analysis

Ins ection Sco

e

The team reviewed recent root cause evaluations conducted

by the licensee.

In

accordance

with station procedures,

root cause evaluations

are required to be

performed on all Category

1 DERs and for other events meeting a licensee

established

threshold.

The team used these reviews to assess

the licensee's

capability to determine the root cause of events and the effectiveness

of the

preventive actions assigned

to the identified causes

at preventing

a recurrence.

The team reviewed recent root cause evaluations conducted at each unit.

Unit

1

1-97-1489

- sodium hypochlorite not being injected into waste water

1-97-150'I - failure to write a DER on a non-conforming condition

1-97-1647 - tom screen on condensate

demineralizer strainer basket,

1-97-1830 - failure of drywell drain isolation valve resulting in plant shut down

1-97-1850 - control room vent chiller failure

'I-97-2207 - discrepancy with dose rates for off site shipment

Unit 2

2-97-1570 - blown control power fuses

2-97-1696 - loss of electric power during control room fire

2-97-1698 - primary containment circuit breaker found out of position

2-97-1773 - inadvertent isolation of RWCU system

2-97-1960 - reverse flow failure of check valve 2CSH "V16

In addition, the team interviewed several qualified root cause evaluators

and

representatives

from the quality assurance

and training departments.

I

Findin s and Observations

The team found that the root cause evaluations

in most cases were adequate

at

determining the higher level, technical causes for an event but did not go into

sufficient depth to explore the potential for human error.

In some cases,

this led the

licensee to assigning preventive actions that provided additional procedural or

physical barriers to prevent recurrence rather than correcting the underlying human

performance

issues.

An example is the event and root cause determination, documented

in DER 1-97-

1830.

This event led to a plant shutdown

as a result of debris found in the seat of

a drywell isolation valve.

The root cause assigned

was failure to maintain adequate

foreign material exclusion.

The preventive actions assigned

included the use of

temporary screens

during future maintenance

activities, increased inspections of

floor drain sumps, awareness

training, and a revision to the procedure to consider

potential impacts of foreign material.

The root cause does not discuss why the,

existing procedural guidance on foreign materials control was inadequate

to prevent

this event.. There is no evidence that any personnel interviews were conducted to

determine why the individuals involved in planning and executing the precipitating

work activity did not consider the consequences

of their actions.

DER 1-97-1850 was associated

with a control room vent chiller. The licensee

determined the root cause to be the deferral of periodic preventive maintenance

on

the system.

The root cause evaluation was not thorough,

in that information was

not provided regarding the adequacy of the deferral decision, or the adequacy of the

preventive maintenance

deferral process.

Furthermore, the licensee's corrective

actions were narrowly focused in that an evaluation of the acceptability of the

preventive maintenance

for the other division chiller was not provided, nor was an

evaluation of the impact of deferred preventive maintenance

for other equipment

completed.

DER 2-95-1850 was associated

with a delay in Unit 2 plant startup due to a

significant number of non-safety related air-operated

valve failures within the

condensate

demineralizer system.

The licensee identified three different types of

-failures during their review.

The team's review of the DER concluded that the

licensee failed to identify the underlying cause of the problem, and that the

corrective actions were narrowly focused.

For example, the licensee determined

that a lack of periodic preventive maintenance

was a cause, but no reason for the

lack of periodic preventive maintenance

was provided.

Also, the corrective actions

were limited to incorporating preventive maintenance

for the valves in question, but

no consideration was given for the potential for a lack of periodic preventive

maintenance

on other equipment.

The licensee has self-identified similar inadequacies

with the quality of root cause

evaluations.

These are documented

in the Nuclear Quality Assurance department's

most recent audit of the corrective action program, NQA Audit 97004, Corrective

Action Program.

DER C-97-1538 was written based

on the audit report finding of a

failure to provide complete root cause evaluations for five of six Category

1 DERs

written from February 12, 1997 through May 12, 1997.

c.

Conclusion

Root causes

and apparent root causes were generally good at identifying the first

level, technical causes

but tended to stop and not go to a greater depth.

Therefore

what is necessary

to prevent recurrence

is not always fully developed.

07.3

Deviation/Event Report Program Summary Trend Report

a.

Ins ection Sco

e

The team reviewed the last four quarterly DER Program Trend Summary Reports to

-evaluate the usefulness

of the reports in assessing

the types of problems occurring

at the Nine Mile Point (NMP) station, and in the identification of adverse trends at

the station.

The team discussed

the use of the trend reports with the plant

managers,

and selected branch managers.

Also, the team evaluated the accuracy

of the information contained within the trend report by comparing

DER data to the

information provided within the reports.

b.

Findin s and Observations

The team found the quarterly DER Program Trend Reports contained

a large amount

of raw data, including, number of DERs sorted by department,

cause code and

system, number of adverse trend DERS initiated, number of DERs open greater than

one and two years, and the number of DER implementation due date extensions

sorted by department.

The report also included information regarding personnel

error rate for each department,

in which the error rate was based on work practice

cause code per 10,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> worked.

Although the team considered

the amount of

information provided within the Trend Report to be significant, no information

regarding repeat failures was provided." Furthermore,

no assessment

of the

information was provided.

Through discussion with members of the licensee's

senior management,

the team

ascertained

that the licensee's

senior management

reviewed the Trend Report, and

that each branch manager was responsible to review the Trend Report for

information pertaining to their respective branch.

Since there was no procedural-

guidance prescribing NMPC's expectation for branch manager review of the Trend

Report, the team discussed

the assessment

of the Trend Report with branch

managers

from both units.

The team noted that the methodology used to assess

the Trend Report varied for each branch manager,

and that no documented

assessment

of the Trend Report was required.

In general, the branch managers

interviewed had reviewed the Trend Reports to determine if their branch was an

outlier with respect to the rest of the site.

Additionally, all branch managers

interviewed noted that the personnel error rate was a valuable indicator of branch

performance.

The team concluded that although the DER Program Trend Report

was reviewed by licensee management,

the quality and methodology of the

8

reviewed varied, and that documented

assessment

of the data from the DER

Program Trend Report was lacking.

The team noted that approximately two percent of all DERs listed in the licensee's

database

were not assigned

the correct category due to data entry errors.

Additionally, the team noted that only adverse trend DERs that include the words

"Adverse Trend" in the title were included within the DER Program Trend Report.

The team discussed

this discrepancy with QA and the Plant Managers.

Based on

these discussions,

the team concluded that there was a lack of communication

between QA and the plarits regarding the adverse trend documentation

and

trending.

Discrepancies with the DER database

were noted previously by QA in

DER C-97-1611, the specific issues identified by the team were noted by the

licensee in DER C-97-2494.

C.

.Conclusions

The amount of raw data provided within the quarterly DER Program Trend Report

was significant; however, no information regarding repeat, failures was provided.

Although the DER Program Trend Report was reviewed by licensee management,

the review varied, and that documented

assessment

of the data from the DER

Program Trend Report was lacking.

Data-entry errors associated

with DER category

were identified.

Furthermore,

a lack of communications

between QA and the units

resulted in a failure to trend all adverse trend DERs in the DER Program Trend

Report.

07.4

Corrective Action Program Quality Assurance Audits

a 0

Ins ection Sco

e

The team reviewed the last three corrective action program audits performed by

Quality Assurance

(QA) to assess

the quality of the findings and the effectiveness

of the licensee's

actions taken to address

identified discrepancies.

b.

Findin s and Observations

The Unit

1 and Unit 2 Technical Specifications

(TS) required that an audit of the

corrective action program be performed every six months.

The team verified that

the last three corrective action program audits were completed according to the TS

requirement.

QA Audit 96008 was completed

in May 1996 and concluded that the corrective

action program was overall satisfactory with some areas in need of improvement

noted.

The areas in need of improvement were addressed

in two existing DERs (C-

94-2560 and C-96-0600); therefore, no additional DERs were generated

as a result

of the QA audit.

The NRC considered that QA Audit 96008 emphasized

the

findings of previous assessments

and provided little independent

evaluation.

QA's

review of corrective action program effectiveness

indicated the corrective actions

were effective, however, the team considered

the sample size to be too small and

narrowly focused on QA identified issues to provide and accurate assessment.

QA Audit 96020 was completed November 1996 and focused on the effectiveness

of management's

efforts to address

previously identified discrepancies

related to the

corrective action program.

Particularly, QA reviewed the effectiveness of the

corrective actions taken through DERs C-94-2560 and C-96-0600.

In addition, QA

reviewed

a sample of DERs for compliance and effectiveness

of corrective actions.

Assessments

of the operating experience

(OE) process

and Branch self-assessments

were also included in the audit.

QA concluded that the corrective action program

was being effectively implemented with some exceptions.

The team found QA Audit 96020 to be more thorough than the previous audit, in

that it contained more independent

review.

However, shortcomings

were noted by

,the team; in particular, QA reviewed 29 significant DERs for compliance with the

controlling procedure,

but only 3 DERs (C-94-2560, C-96-0600 and 2-95-3187)

were reviewed for effectiveness of corrective actions and discrepancies

were noted

in each case.

The team considered

the number of items reviewed for effectiveness

of corrective actions to be small and the scope of the audit was not increased

even

though the results indicated that the corrective actions were not completely

effective.

The team also noted that the executive summary and the conclusion section of QA

Audit 96020 did not reflect the shortcomings

described within the details of the

audit.

This concern was discussed

with the QA manager and the Chief Nuclear

Officer (CNO) and it was ascertained

that the licensee

had recognized this and

expressed

the concern to QA management.

QA Audit 97004 was completed in May 1997 and focused on a review of DERs for

administrative and fundamental soundness.

Of the 61 DERs reviewed, QA

concluded that 62% acceptably implemented the program requirements

and that

75% acceptably identified and corrected the underlying cause.

The QA audit team

concluded that the overall effectiveness

and implementation of the CA program was

marginally acceptable

and that problems existed with DER procedure

adherence

and

root cause determination.

As a result of the audit, QA initiated five DERs to

address

specific concerns,

most notable was DER C-97-1680, "Audit 97004:

Results of Corrective Actions to Improve Quality of DER Dispositions not in

Accordance with Managements'xpectations."

The team considered Audit 97004 to be critical. The review of DERs included

a

sufficient sample size to provide a credible indication of the overall program status.

The checklist used by the QA auditors to evaluate the DERs was found to be good.

The separation of the fundamental

and administrative soundness,

provides the

licensee's

management

the nature and extent of the discrepancies.

The actions taken by the licensee to address

concerns identified with the corrective

actions program have not been completely effective as evidenced

by the recurrent

failures to implement DERs in accordance

with the procedure,

and failures to

10

adequately identify the underlying cause of problems noted by QA Audits and the

NRC team's review of DERs as described

in Section 07.1, "Review of

Deviation/Event Reports," and Section 07.2, "Root Cause Analysis."

C.

Conclusions

Weaknesses

were identified in both QA Audits of the corrective action program

completed

in 1996.

The weaknesses

included:

limited independent

assessment,

small and narrowly focused samples,

and not clearly representing

audit findings in

the executive summary.

Significant improvement in all areas was noted within the

latest QA audit, w'hich included a critical assessment

of licensee's corrective action

program.

However, the licensee's corrective actions to address

previously identified

QA audit weaknesses

had not been completely effective as evidenced

by recurring

discrepancies

in implementing the corrective action program and in determining the

underlying cause of problems.

07.5

Operating Experience

Review Process

a.

Ins ection Sco

e

The team assessed

the licensee's

process for evaluating operating experience

(OE)

information including a review of the controlling procedures,

and selected

OE

information.

b.

Findin

s and Observations

NMPC controlled their review of OE through Procedure

NIP-ECA-01, "Deviation

/Event Report," Revision 11.

The procedure

allowed for QA, Licensing, and

Engineering Departments to determine the applicability of incoming OE information.

The responsible

departments

were required to maintain a record of OE documents

received, and to review and document the applicability of the OE information to the

NMP station.

For OE information found to be applicable to the NMP station,

a DER

would be initiated for review by the appropriate department.

The team considered

the licensee's controls for evaluating

OE information to be appropriate.

The team reviewed the NMPC Licensing Department records for OE items received

in 1997, and the associated

statements

of applicability.

The items were

appropriately reviewed and documented.

The team also reviewed selected

DERs for

both units pertaining to NRC Information Notices (INs), General Electric Service

Information Letters (SILs), and Title 10 of the Code of Federal Regulations

Part 21

notifications, and determined them to be acceptable.

C.

Conclusions

The licensee's controls for evaluating

OE information were appropriate.

The OE-

related DERs reviewed were found to be acceptable.

11

07.6

Adverse Trend Identification

'ns

ection Sco

e

The team assessed

the licensee's

process and effectiveness for identifying adverse

trends.

Applicable portions of the licensee's

procedures,

trending information

regarding adverse trend DERs and selected adverse trend DERs were reviewed.

In

addition, the team reviewed the DER history for selected

areas in which the

potential for an adverse trend existed to determine if adverse trends were properly

identified by the licensee.

Findin

s and Observations

Although no guidance

is provided within the licensee's

procedure controlling the

DER process

(NIP-ECA-01), the licensee has been initiating DERs for situations

where adverse trends were identified. Additionally, a listing of 'adverse trend DERs

was provided in the quarterly DER Program Trend Summary Report.

Discussions

with the QA manager indicated that the concept of adverse trend DERs as used at

the NMP Station is approximately one year. old. A review of the trend report

indicated that the use of adverse trend DERs had increased

over the last year and

that most departments

were currently involved in the identification of adverse trend

DERs.

The team reviewed

a list of the adverse trend DERs from July 1, 1996, through

August 1, 1997.

During that period the licensee initiated approximately 45 adverse

trend DERS.

The types of issues described

by the adverse trend DERS included:

equipment issues (13), training issues

(5), foreign material exclusion (FME) control

issues (2), procedural noncompliance

issues (14), DER timeliness and quality-related

issues (5), and miscellaneous

issues (5).

The team reviewed the thirteen adverse trend DERs associated

with equipment

issues and noted that five of the DERs were with non-safety-related

equipment.

Another five DERs were associated

with the Unit 2 safety-related unit coolers

performance test problems.

The five adverse trend DERs associated

with the

coolers were reviewed by the team and considered to be technically sound with

good justifications to support adequacy of the root cause

and proposed corrective

actions as provided in the form of validation test questions described

in the DER

procedure.

However, three of the five DERs were approximately one month late for

disposition without an extension.

Further discussion

regarding

DER extensions

is

provided in Section 08.1 of this report.

The team reviewed two of the fourteen adverse trend DERs associated

with

procedural noncompliance.

DER 2-97-0203, "Adverse Trend in Operations Ability

to Implement Administrative Requirements,"

was generated

as a result of a Unit 2

Operations Department'self-assessment.

Although no formal root cause analysis of

the issue was completed, the team considered the apparent cause determination to

be thorough,

and the proposed

corrective actions to be sound.

However, the

licensee's

review and proposed

corrective actions focused only on Unit 2

tf

12

Operations Department.

The team considered this to be narrowly focused,

as

evidenced

by the significant number of other adverse trend DERs associated

with

, procedural noncompliance

issues.

The second procedure noncompliance-related

adverse trend DER the team reviewed

was DER 2-96-2155, "QVSA - Adverse Trend 'Chemical Control'iolations of NIP-

CHE-01." This DER noted nine DERs from April 4, through September

10, 1996,

associated

with Unit 2 failures to implemented Procedure

NIP-CHE-01, "Chemistry

Control Program."

The teams's review of DER 2-96-2155 noted that the root cause

of inadequate

corrective actions to previously identified problems was not

addressed

as part of the corrective actions.

Furthermore,

based

on the limited

information provided within the DER, the team was unable to assess

the proposed

corrective actions.

The team reviewed the DER history of selected

areas in which the potential for an

adverse trend existed to assess

the licensee's performance

in identifying adverse

trend conditions.

The areas selected were FME, unexpected

half scrams,

and Riley

temperature

switches.

For FME issues, the licensee had generated two adverse

trend DERs, for unexpected

half scrams, the team noted eight Unit 1 DERs

associated

with unexpected

half scrams within the last year.

Discussions with the

Unit

1 system engineering staff indicated that the causes of the half scrams were

generally unrelated that no adverse trend could be established.

Based on the

discussion with system engineering

and

a review of applicable DERs the team found

the licensee's conclusion acceptable.

With respect to Riley temperature

switches, the team noted eight DERs related to

Riley Temperature switch failure at Unit 2 over the last three years.

Discussion with

members of the Unit 2 Instrumentation

and Controls (IS.C) Department and a review

of the applicable DERs indicated that the trend associated

with the temperature

switch failures was being addressed.

Although some minor implementation issues

were noted, the team considered

the licensee's

evaluation of the issue as provided

in DERs 2-97-0498 and 2-97-1560 to be technically sound.

The licensee classified

these

DERs as category 2, but the team considered

the potential for the problem to

be a common failure made them more suitable to be classified as category

1.

Based on the teams review, the licensee,

appears to identify and evaluate adverse

trend conditions.

However, during the review of these and other DERs, the team

noted

a not all DERs associated

with adverse trends were included in the quarterly

DER Program Summary Report, this observation was described

in Section 07.3,

"Deviation/Event Report Program Summary Trend Report."

Conclusions

Although no procedural guidance was provided for reporting adverse trends, the

licensee appeared to be identifying and evaluating adverse trend conditions.

Based

on the team's review of the procedural noncompliance-related

adverse trend DERs,

the team considered

the corrective actions taken to address

human performance

issues to be narrowly focused and not completely effective as evidenced

by the

13

significant number of adverse trend DERs associated

with procedural noncompliance

issues.

Independent

Safety Engineering

Group (ISEG)

Ins ection Sco

e

Technical Specification 6.2.3 defines the function, composition,

and responsibility

of ISEG.

This technical specification is only applicable to Unit 2. The technical

specification states

in part that ISEG shall function to examine unit operating

characteristics,

NRC issuances,

industry advisories,

license event reports and other

sources of operating experience

and make detailed recommendations

for improving

unit safety to the Vice President

- Nuclear Safety Assessment

and Support.

The

team evaluated

ISEG's performance

in carrying out these responsibilities.

The team interviewed the ISEG Director, ISEG members,

and personnel from the

plant staff to assess

ISEG's performance

in carrying out its responsibilities.

The

team also reviewed ISEG activity reports for the last twelve months and the two

most recent self assessments

prepared

by the ISEG Director.

Findin s and Observations

Overall, the team found that ISEG was functioning adequately to carry out its

responsibilities

as defined in Technical Specification 6.2.3.

The team noted

improvement over the last several months in ISEG's use of industry operating

experience

and NRC issuances

for assessment

planning.

In the past, ISEG was

more focused on providing follow-up assessments

to site specific events rather than

taking a more proactive approach utilizing industry operating experience.

ISEG has

also recently begun to perform broader range programmatic assessments

rather than

focussing on isolated issues

and events.

These are both positive trends that need

to continue for ISEG to have a greater impact on improving safety.

The self assessments

prepared

by the ISEG Director identified areas for

improvement that have not been followed through on.

A self assessment

recommendation

was made in June 1996 and again in December 1996 for ISEG to

perform team assessments

on a pre-planned

list of topics to provide broader

oversights of functional areas including Operations,

Engineering,

Maintenance,

and

Technical Support.

The team found no evidence that this recommendation

had

been implemented.

Additionally, the December 1996 self assessment

repeated the

assessment

results and program enhancements

made in the previous self

assessment

completed in June 1996.

One of the ISEG responsibilities listed in the Technical Specifications is to examine

unit operating characteristics.

ISEG currently carries out this function through daily

reviews of operating logs and plant parameters.

There was no evidence of ISEG

performing, or being provided with, any long term trends of unit operating

characteristics to allow for a more thorough review and assessment

of safety

significant parameters.

c.

Conclusions

Overall, ISEG was functioning adequately to carry out its responsibilities

as defined

in Technical Specifications.

Although ISEG had performed self assessments

and

identified areas for imp'rovement, follow through on the recommendations

for

~ improvement has been limited.

07.8

Self Assessment

Program

a.

Ins ection Sco

e

The team reviewed the licensee's

self-assessment

(SA) program including

procedures,

interviewed licensee personnel

and evaluated selected self assessments

from engineering,

operations,

and maintenance.

b.

Observations

and Findin s

Administrative procedure

NIP-ECA-05, "Self-Assessment,"

Revision 00, provided

adequate

guidance for the self assessment

program.

A sample of SA reports were

reviewed and it was determined that the level of detail with respect to identifying

performance

weaknesses

and planned or implemented corrective actions varied

greatly between reports.

Specific SA weaknesses

included: (1) SAs which lacked

specific criterion against which performance was judged, (2) Some SAs were

essentially

a summary of documents

reviewed (e.g., tabulation of DERs, NRC

reports, and QA assessments),

(3) Some branches

do not have

a method for

capturing routine performance observations

for inclusion in the SA programs,

and

(4) Some SAs either lacked specific recommendations

or did not provide a

mechanism to formally track what was being done with recommendations.

In

addition, management

expectations with respect to developing

a two-year schedule

of branch SAs, maintaining the timeliness of SAs (i.e., at least one within a six

month period), and including a section within the SAs which assesses

the

adequacy'f

past corrective actions, have not been met by various branch organizations.

Conclusions

Overall the licensee had an adequate

program for self-assessment

activities.

However, several weaknesses

with the program implementation limit the

effectiveness of the overall SA program, and may lead to missed opportunities to

implement useful recommendations

in a timely manner.

07.9

Corrective Action Program Related to Human Performance

a.

Ins ection Sco

e

The team reviewed aspects of the licensee's

corrective action programs and

conducted

personnel interviews to determine if the licensee's

programs were

adequately

identifying and addressing

human performance

issues.

15

Findin

s and Observations

The primary method for identifying, tracking and dispositioning human performance

issues

is through the DER process.

DER data is tabulated quarterly by the Quality

Assurance

(QA) department

and provided as a report to each branch for further

evaluation and corrective action.

The team reviewed the QA DER Program Trend

Summary Report for the second quarter of 1997 and a QA report to the Senior

Management

Team which characterized

the 1997 significant DERS attributed to

personnel

errors, dated August 8, 1997, to determine what performance

weaknesses

were being identified.

The licensee reports indicated that significant

contributors to performance weaknesses

appear to be concentrated

in the areas of

self-checking, required verifications not performed, and procedures

not followed

correctly.

Results of these performance weaknesses

have manifested themselves

as plant equipment found out of expected position, work performed on plant

equipment using inappropriate materials or equipment,

and inadequate

operability

determination calculations.

In response

to the human performance

issues identified in the DERs, the licensee

often counseled

the individuals involved in the event and made changes to

administrative or plant procedures.

While these actions appear to be effective in

minimizing the possibility of a repeat of a particular incident, the continued

observation of personnel

errors is indicative of the need to evaluate the underlying

causes of these errors more broadly.

The team also reviewed

a sample of DERs, recent RCAs, self-assessments,

and

various branch performance observation forms to determine if human performance

issues were being identified.

In most cases,

these reporting methods did identify

human performance

issues contributing to events, but the team did note some

exceptions.

In at least one case, the licensee identified a lack of human

performance contributors as a r'esult of a DER review and initiated a second

DER to

address

the human performance

issues.

A recent Quality Assurance

Branch

assessment

of significant personnel

errors noted that recent root cause analyses

do

not adequately

evaluate the contribution of human performance to the events being

analyzed,

and DER C-97-1538 was written to address

the issue.

The team noted some positive initiatives such as the Unit 2 Operations observation

card system which contain performance observations

generated

by operations

supervision of their respective crews.

The observations

are entered into a database

which can be sorted on a variety of evaluation criteria and used as input into the

self-assessment

process.

However, the team noted that some other branches

did

not have any method for capturing performance

observations

and in some cases,

other branches

had apparently stopped

using existing observation processes

contrary to management

expectations.

The licensee appears to recognize that human performance weaknesses

persist and

has implemented initiatives to address the situations'ncluding:

delineating

management

expectations

for error free performance,

increased

supervisory

0

16

oversight of activities, increased

emphasis

on peer-checking,

and performance.

reinforcement during training.

C.

Conclusions

Overall, the licensee had an adequate

program for identifying human performance

errors.

However several weaknesses

in the programs to identify and address

human performance

issues were apparent.

08

Miscellaneous Operating Issues

08.1

Unresolved Item 50-410/95-25-03:

DERs Extended Without Justification

Ins ection Sco

e

During NRC Inspection 50-410/95-25

NRC inspectors identified examples of Unit 2

DERs assigned to both engineering

and technical support departments that failed to

contain justification for the extension of implementation

as required by Procedure

NIP-ECA-01. Additionally, the inspectors noted that documentation

of extension

requests

varied widely. The team reviewed the licensee's

actions taken in response

to this concern, including the DER written to address

the issue,

a QA surveillance

performed by the licensee to determine the extent of the problem, and resulting

changes

made to the DER procedure.

The team also reviewed selected

DERs to

assess

the effectiveness of the licensee's corrective actions to remedy the problem.

Findin s and Observations

NMPC generated

DER 2-96-0211 to address the concern related to DER extensions.

As part of the disposition, QA completed

a surveillance of the justifications provided

for DER extensions.

The results of the QA surveillance (Report 96-0039-C)

identified that the only group to consistently justify DER extensions was Unit 1

Engineering Department.

The licensee identified the root cause to be ineffective

change management

for Revision 8 to NIP-ECA-01, which incorporated the

requirement for justifying DER extensions.

Corrective actions included informing all

branch managers

through a memorandum

of the requirements to justify DER

extensions,

and training on DER extensions

was to be included for "DER

coordinator" training.

In addition, the DER procedure was enhanced

to clarify the

requirements for justifying and documenting

DER extensions.

The team reviewed the licensee's corrective actions.

The team considered that the

procedure

changes facilitate the use of DER extension requests.

The team

considered

this enhancement

to be good, and the DER extension requests reviewed

by the team consistently used the extension forms and assessed

the impact on

safety.

Although the procedure

changes

were considered to be good, the process

was not consistently being used.

There were currently 687 DERs open for

disposition with 165 greater than ten days overdue without an extension request

(51 were greater than 50 days overdue,

and 16 were greater than 100 days

overdue).

With respect to implementation of the DER corrective actions, 1622

17

DERs were open with 72 DERs greater than ten days overdue without an extension

request (29 were greater than 50 days overdue,

and five were greater than 100

days overdue).

The failure to justify the extension of DER disposition and

implementation due dates was not in compliance with licensee Procedure

NIP-ECA-

01, and was considered

a violation of TS 6.8.1.

(VIO 50-220/97-80-01

and 50-

410/97-80-01)

Furthermore,

based on the numbers

DERs currently overdue without

justification, the team considered

the licensee's

actions described

in DER 2-96-0211

ineffective to prevent recurrence.

Based on this violation, Unresolved Item (URI)

50-410/95-25-03

is closed.

Conclusions

The continuing failure to justify the extension of DER due dates

as required by

licensee procedure was a violation of TS 6.8.1.

Furthermore, the licensee's

corrective actions to prevent recurrence of this previously identified concern were

ineffective.

(Closed) Inspector Follow Item 50-410/96-07-12:

Weaknesses

in the DER Process

This item was opened

in response

to a finding during the 1996 Integrated

Performance Assessment

Process

(IPAP) team inspection (NRC IR 50-220/96-201

and 50-410/96-201),

in which weaknesses

were identified within the DER process.

The particular concerns were in the areas of trending, root cause analysis, adequacy

of corrective actions to prevent recurrence,

and root cause analysis training.

Also,

the implementation of corrective actions associated

with self-assessments,

ISEG,

and QA recommendations

were not verified sufficiently to assure that the required

actions were effective.

During the course of this inspection, the team assessed

all the areas of concerns

identified within this Inspector Follow Item (IFI). The team's assessments

were

included in the applicable sections of this inspection report, and any continuing

weaknesses

requiring follow up were noted as such.

In addition, subsequent

to

issuing

IFI 96-07-12, Notice of Violations (NOVs) associated

with the corrective

action program were issued,

as described

in Escalated

Enforcement Letter dated

April 10, 1997; any continuing weaknesses

oertaining to the corrective action

program will be review as part of the NOV closures.

Therefore,

IFI 96-07-12 is

administratively closed.

(Closed) Inspector Followup Item (IFI) 50-410/96-07-13:

ISEG Review of NRC

Documents

The May 1996 IPAP report noted that ISEG was not carrying out its responsibility to

review NRC issuances.

This function was being performed by different branches

other than ISEG.

ISEG has taken actions to correct this situation and the team

reviewed ISEG's functions with respect to this issue.

A member of ISEG routinely

reviews a complete listing of NRC issuances

for applicability and safety significance.

Selected items are flagged for a follow-up assessment

by ISEG to determine if the

issue is being properly addressed.

The team reviewed ISEG activity reports for the

18

last twelve months and found evidence of these actions being taken and that

meaningful feedback was being supplied by ISEG to responsible

plant organizations.

II. MAINTENANCE

M1

Conduct of Maintenance

M1.1

Emergent Maintenance

a.

Ins ection Sco

e

The inspector observed

various aspects

of the licensee's

response

to emergent

conditions that required corrective maintenance.

b.

Findin s and Observations

Unit 2 Reactor Coolant S stem Flexible Hose Failure

On August 4, 1997 Unit 2 was shutdown

in response

to an elevated drywell floor

drain leak rate.

The source of the leakage was a 3/4 inch flexible metallic hose,

2RCS" HOSE40, connected to the drain line of the B recirculation loop flow control

valve, 2RCS" HYV17B. The leak was at the bottom of the flexible hose where the

stainless steel braid is connected

to the end ferrule.

The team followed the

licensee's

response

to the event as it related to implementation of the plant's

corrective action program.

This was the second occurrence of a failed flex hose at Unit 2.

On March 30, 1991

a flexible hose of similar design in the reactor coolant sample system failed, also

resulting in a plant shut down.

In response

to the previous event, the licensee sent

the failed flex hose off site for failure analysis.

The cause of the failure was

determined to be pitting attack and subsequent

fatigue failure as a result of

exposure to an aggressive

environment prior to the hose being placed in service.

The source and characterization

of the aggressive

environment were never

established.

The Licensee Event Report (LER) 91-01 submitted in response to this

event committed to evaluating flex hoses removed

in future outages for signs of

metal fatigue.

Only one of twelve flex hoses removed in the next refueling outage

was subsequently

examined.

No evidence of metal fatigue was found in the sole

flex hose that was examined.

The team does not consider the examination of only

one additional flex hose to have met the intent of the LER commitment to determine

the extent of the failure mechanism.

The team determined that the licensee did not

have a sufficient enough understanding

of the failure mechanism

and contributing

environment for the flex hose that failed in March 1991 to consider the failure to be

an isolated event with no generic implications as stated in the LER.

The team assessed

the licensee's

response

to the most recent flex hose failure.

The team observed

meetings of the root cause evaluation team, routine outage

planning meetings,

SORC meetings, interviewed personnel

involved with responding

19

to the event, and walked down the location of the failed flex hose in the dry well ~

The team found the lice'nsee's

response

to the event to be appropriate.

The

licensee removed the failed flex hose from the valve body and capped

and seal

welded the connections.

Visual inspections were conducted

on the remaining flex

hoses.

The licensee recognized the limitations of the visual inspections at

identifying fatigued hoses prior to failure and made an appropriate safety

assessment

justifying plant restart.

The licensee's

preventive actions for the most recent flex hose failure include

prioritizing a list of flex hoses most susceptible to failure; identifying flex hoses for

replacement,

modification, or inspection in the next scheduled

refueling outage; and

performing a failure analysis on the failed flex hose and other selected flex hoses to

establish

a failure mechanism.

The team considered

the March 30, 1991 event a

missed opportunity for the licensee to pursue the cause of the failed flex hose and

establish appropriate corrective actions to prevent recurrence.

The licensee

considered

several preventive actions in response

to the March 1991 flex hose

failure, but did not follow through on them.

An inspector follow item, 50-410/97-

06-02, was established

to track the resolution of the most recent event.

Failure of Unit 2 Service Water Makeu

Control Valve to the

Circulatin

On August 18, while conducting activities involving the service water (SW) system,

an operator noted that the hydraulic positioning unit for the SW loop B makeup

control valve to the cooling tower was malfunctioning.

Specifically, the hydraulic

pump was running continuously; normally, it operates

only as necessary

to support

valve operations

and to maintain an accumulator full. The accumulator serves as a

backup power source to the hydraulic pump, to allow the valve to isolate the non

safety-related

cooling tower from the safety related portions of the SW system.

Continuous pump operation with no corresponding

valve operations indicated that

the accumulator was not holding pressure,

and therefore could not be relied on to

perform its safety function.

As a result, SW loop B was declared inoperable, which

placed the Unit 2 in a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> shutdown action statement.

Due to the malfunction, switching SW loops for makeup to the cooling tower by the

existing procedure would have temporarily resulted in two loops of SW being

inoperable.

To avoid this, a one-time use procedure

change was prepared.

The

inspector observed preparations

in the control room to perform this procedure.

Following individual review of the change,

operators discussed

problems that could

be encountered

during the shift.

Based on the sequence

of procedural actions,

parameters

were established

that would give early indications of a problem, as well

as actions to be taken if problems did develop.

However, due to the lateness of the

shift and other required activities, the decision was made to defer conduct of the

operation to the oncoming shift.

Based on turnover discussions

of the procedure,

the oncoming operations shift

discussed

the evolution in overview during the turnover brief. The pre-job brief was

deferred until after completion of normal shiftly rounds and to allow the control

0

20

room operators to thoroughly review the procedure

change.

The inspector observed

the shift turnover brief and noted that the auxiliary operators were active and

'nowledgeable

participants

in discussion of the upcoming SW evolution.

Unit 2 Emer enc

Diesel Generator

DC Control Power Annunciator Failure

On August 18, operators

received an alarm on main control board annunciator 319,

"EDG2 DC Control Power Failure."

Loss of DC control power for an emergency

diesel generator

(EDG) renders that EDG inoperable.

Loss of EDG2 at that time

would have been particularly significant, in that scheduled

LCO maintenance

on

division

1 equipment was in progress.

An operator was dispatched to investigate

the condition and, from local indications, it was determined that the EDG2 DC

control power was still operable.

As an interim measure,

an individual was

stationed to monitor local indications while maintaining communication v ".h the

.control room.

Troubleshooting

revealed that the cause of the alarm was a failed

relay in the annunciator circuit. The relay was replaced and the annunciator was

returned to service later the same day.

The inspector observed activities associated

with the annunciator circuit relay

replacement from the control room.

The maintenance

activity was thoroughly

discussed,

including expected

alarms, prior to commencing work. Post maintenance

testing was technically appropriate

and was well controlled.

Following restoration

of the annunciator circuit and approval by the operations supervisor, the local watch

was secured.

The inspector concluded that use of a watchstander

for this function

had been acceptable,

given that the affected circuit provided no functions other

.

than alarm.

C.

Conclusions

The licensee effectively dealt with these emergent maintenance

issues.

The

operations department

made significant contributions both to the identification of

problems and control of plant conditions to support maintenance.

An IFI concerning

the failed flex hose was documented

in a separate

NRC inspection report 50-

41 0/97-06-02.

IVI2

Maintenance and IVlaterial Condition of Facilities and Equipment

M2.1

Material Condition Observations

Ins ection Sco

e

The inspector toured portions of the plants to assess

the effectiveness of the

corrective action process with respect to identifying and correcting material

discrepancies.

21

Findin

s and Observations

Unit 2 Material Condition

During the first week of onsite inspection (August 4), unit 2 was shut down due to

a reactor coolant leak from a flexible hose in the drywell. As a result, the

inspectors were able to tour areas that are normally inaccessible

during power

operations.

~Dr well

The main steam isolation valves appeared

to be in g'ood material condition; nitrogen

flexible hoses were not crimped and actuator venting was not obstructed.

No

problems were noted with the mounting of piping and electrical conduit runs, nor

.with seismic restraints.

No temporary storage of equipment or materials was noted,

and no temporary postings were observed.

Drywell coatings appeared to be in

good condition, and no peeling was noted.

Overall, the inspectors considered that

the material condition of the drywell was good; drywell cleanliness

is discussed

in

section M2.2 below.

Steam Tunnel

The inspectors

noted several previously unidentified deficiencies that had occurred

during'the preceding plant operations.

For example,

a valve packing leak had

developed which created

a puddle of water on top of one of the room coolers.

Also, a flange leak on a steam pipe had melted the surrounding insulation.

In

addition, the inspectors noted several maintenance-related

material deficiencies.

Examples included:

the inlet screens/filters were not in place on one of the room

coolers; one of four baseplate

fasteners was not made up for a seismic strut;

frayed, crumpled fire wrap material; and a long ladder that was being stored upright

without adequate

restraint.

Overall, the inspectors

assessed

the material condition

of the steam tunnel to be poor.

A-Feedwater Heater Ba

No significant problems were noted, overall material condition and housekeeping

appeared

to be good.

Unit 2 Reactor Buildin

The inspectors

also toured the reactor building during the course of the inspection,

and made the following observations:

Control rod drive system relief valve 2RDS" RV1B (RDS pump 1B suction relief) had

an open threaded

port on the valve bonnet; the inspector noted that this port for the

1A RDS pump suction relief valve was plugged and lockwired. The licensee

initiated a DER (2-97-2455) to investigate this inconsistency.

The licensee

determined that the plug was supposed

to be installed, but that it did not affect

22

valve operability; the bonnet is vented to the valve discharge

side by an internal

passage,

and the valve relieves to atmospheric

pressure.

A plug was promptly

installed in 2RDS "RV18.

Gas treatment system valve GTS-PV104 (AOV-101 bypass line pressure

controller)

position switch actuator on the valve stem was rotated so that it was out of

alignment and made minimal contact with the limit switches.

The licensee initiated

a problem identification report to correct the problem.

The discharge flexible coupling for reactor building closed loop cooling pump CCP-

P1A had several radial tears in the outer covering.

As compared to the other pumps

in the system, the coupling appeared

to be slightly deformed, suggesting

that the

cause of the tears was an inadequate fit. Although a work order existed to replace

this flexible coupling, the reason for the work order was listed as preventive

maintenance,

indicating that the tears apparently had not been previously identified.

c.

Conclusions

The overall material condition of Unit 2 was good; however, inspector identification

of several material problems in the reactor building indicated that additional material

inspections

by the licensee could be productive.

The material condition of the

steam tunnel was assessed

to be poor.

Based on the material deficiencies that

were identified by the inspectors

in this area, it did not appear that the licensee was

taking full advantage

of the forced outage to inspect normally inaccessible

areas of

the plant for emergent material problems.

M2.2

Unit 2 Drywell Cleanliness Controls

a.

Ins ection Sco

e

During an inspection of the Unit 2 drywell, the inspectors identified some foreign

materials in out-of-the-way locations.

As a result, the inspectors reviewed the

licensee's

cleanliness control requirements for the drywell.

Findin

s and Observations

The Unit 2 drywell was opened

during the forced outage to support repair of the

failed reactor coolant system flexible hose, but w'as not open for general access.

In

discussions

with plant personnel

during entry preparations,

the inspectors were

informed that the drywell was a I~vel 3 cleanliness

area, and that foreign material

exclusion (FME) requirements

were in effect.

The general standard for area

cleanliness

requirements

is ANSI N45.2.3, "Housekeeping

During the Construction

Phase of Nuclear Power Plants," and the requirements

for level 3 cleanliness

as

specified in this ANSI standard

are relatively stringent.

Area cleanliness

classifications for Unit 2 are established

by procedure

GAP-HSC-02, "Local Work

Zones and System Cleanliness Controls," and basically parallel the requirements of

ANSI N45.2.3.

23

During inspection of drywell, the inspectors noted that the overall cleanliness of the

drywell was good.

However, the inspectors observed that numerous

open-ended

square steel structural braces were collecting points for debris (for example, tie

wraps, wire, and contamination swipes), as well as some tools (the inspectors

found two pens and two screwdrivers).

The inspectors considered that these

conditions were not consistent with level 3 cleanliness requirements.

However, in

reviewing GAP-HSC-02, the inspector noted 'that the cleanliness

level of the drywell

was not specified.

The procedure

does discuss the use of FME controls (material

accountability log and capturing of loose items) for the drywell; since FME controls

are normally established

for systems requiring a high degree of cleanliness

(level 1,

2, or 3), this could imply that the drywell was a level 3 area.

However, in this case,

the use of FME controls is to maintain drywell cleanliness at the level established

during the previous closeout inspection and thereby preclude the need for a drywell

closeout inspection following a short duration outage.

In addition, the inspector was informed that heavy fabric cleanliness covers were

used to maintain FME control of the drywell-to-suppression

pool downcomers.

While this is an effective mechanism for maintaining cleanliness,

the inspector was

concerned that, were they to be inadvertently left in place while primary

containment was required, they would have

a significant effect on the ability of the

containment to perform its design functions; specifically, while in place, they

defeated the steam quenching function of the suppression

pool, and if dislodged,

could produce significant blockage of water to the ECCS pumps.

The inspector was

informed that the downcomer covers were used as deemed

necessary

by the

drywell coordinator,

and that installation and removal was documented

by the

material accountability log. The inspector considered

that more stringent controls

over installation and removal of these covers would be appropriate,

due to the major

impact they could have on containment operability.

'I

The requirement to perform a drywell closeout inspection prior to plant startup is

established

by procedure

N2-OP-101A, "Plant Startup."

As a prerequisite to the

procedure,

either the master or short form startup checklist (Attachments

1 and 2)

must be completed,

and both require that a drywell inspection be performed if a

drywell entry had been made.

However, GAP-HSC-02 specifies that, for short

outages,

FME controls may be used in lieu of a final inspection.

It was not clear

how this provision is intended to be implemented.

The inspector was concerned,

because

the N2-OP-101A drywell closeout checklist is the source of the

requirement for final verification that the downcomer covers have been removed;

were it to be interpreted

as not being required, then this final verification would not

be performed.

The inspector noted that GAP-HSC-02 specifies that installation and removal of the

downcomer covers is to be performed under work order control.

The inspector

considered

this to be an appropriate

level of administrative control for use of the

downcomer covers.

The inspector verified that a work order (97-00852-03) had

been used to control use of the downcomer covers during the August 4 forced

outage; however, it was a general work order for drywell FME control, titled, "FME

Control Accountability of Material in the Drywell During Forced Outage," rather than

24

a work order specifically for the installation and removal of downcomer FME covers.

Additionally, the work order did not specify which downcomers were to be covered,

but rather, had blanks for the worker to record the identification numbers of the

affected downcomers.

The inspector noted that the completed work permit did not

provide rigorous accountability for pfacem'ent of the covers.

For example, removal

of four covers was documented

by having lined out the numbers that had been

recorded

in the "installation" section, with a note that they were removed and

reinstalled at the locations listed on the next line; this removal had not been

recorded

in the "removal" section of the work permit.

In the same example, one of

the downcomers

listed as having its cover removed is also listed on the next line as

having a cover installed.

Finally, in the "removal" section, it would not be possible

to determine whether one of the numbers was "6" or "8" (due to a write-over)

without referring to the "installation" section to find out which it should be.

Conclusions

Drywell cleanliness

was generally good, however, cleanliness requirements for the

drywell are not clearly established

in the governing procedure,

GAP-HSC-02.

Given

that this procedure provides allowance for not performing a drywell inspection prior

to plant startup, and that the plant startup procedure,

N2-OP-101A, does not

address

how this allowance is to be implemented, interpretation could result in

omission of the final verification that the downcomer FME covers have been

removed.

Work order control of installation and removal of the downcomer FME

covers is appropriate, given the significant impact they could have on containment

operability if inadvertently left in place.

However, the work order used to

accomplish this during the August 4 forced outage was general in nature and did

not provide rigorous accountability for installation and removal of these covers.

Unit 2 Residual Heat Removal System Flow Control Valve Problem

Ins ection Sco

e

The inspector noted

a mechanical problem with a residual heat removal (RHR)

system valve, and observed the licensee's

actions to disposition the deficiency.

Findin s and Observations

During an inspection of the Unit 2 reactor building, the inspector noted that a

split ring lock washer between

a nut and the anti-rotation device on the stem of

valve RHS" FV388 ("8" RHR full flow test) was not compressed.

The inspector

reported this condition to the station shift supervisor

(SSS) late in the afternoon of

August 18.

Licensee investigation of the condition the following day identified the

valve as having a two piece stern, and that the nut and lock washer in question

were the mechanical fasteners that locked the two threaded stem pieces together.

The condition of the valve was assessed

to be indeterminate.

At 11:00 a.m. on

August 19, the valve was declared inoperable,

along with the associated

loop of the

RHR system.

This placed the licensee in a 72-hour shutdown action statement

per

25

technical specification 3.6.2.3.

DER 2-97-2451 was initiated to document the

condition in the corrective action program and initiate corrective action.

The condition of valve RHS "FV38B was evaluated

by an engineering

supporting

analysis (ESB2M970760).

The analysis indicated that the functions of the valve

included initiating and terminating suppression

pool cooling during normal plant

operations

and accident conditions,

and as an RHR pump minimum flow valve

operated

from the remote shutdown panel in case of control room evacuation

due to

fire. The evaluation concluded that the valve position was currently known, but

that, with continued operation, the lower stem could loosen and back out of its

connection with the upper stem, resulting in inability to open the valve.

Licensee review revealed that there had been

a problem had with valve

RHS "FV38B

in June 1997.

Specifically, the valve position indication had been intermediate

when the valve was fully closed.

This condition was corrected with a minor

adjustment of the valve position limit switch. At the time, the problem was

believed to be due to the switch having been set too close to the maximum closed

tolerance.

However, in light of the loose lock nut, it was considered

likely that the

intermediate position indication had been due to increased

stem length, as a result

of the lower stem beginning to back out of the upper stem.

Repair of valve RHS" FV38B was performed under work order 97-12724-00,

and

consisted of tightening the loose nut.

Acceptance testing was to stroke time the

valve and verify proper valve position indication.

During this testing, the valve

again exhibited dual indication, indicating that the stem had continued to back out

since June.

The problem was again corrected by minor adjustment of the valve

position limit switch, and valve stroke time was demonstrated

to be satisfactory.

Valve RHS" FV38B and RHR system loop B were declared operable on August 20.

Additionally, the licensee verified that similarly designed

valves in safety systems

did not exhibit the same problem.

Conclusions

Given the safety significant functions performed by valve

RHS "FV38B, licensee

investigation of the reported degraded

condition of the valve was slow.

Additionally, the decision to start the 72 hr LCO at 11:00 a.m. on August 19, rather

than on the afternoon of August 18 (when the condition was reported to the SSS)

was not conservative.

The intermediate valve position indication that occurred in

June 1997 was apparently

a missed opportunity to identify the loose stem lock nut.

Pending engineering evaluation of the as-left, partially unthreaded

condition of the

lower valve stem and review of the completed

DER, this-item remains open. (IFI 50-

410/97-80-02)

26

M2.4

Unit 2 Steam Tunnel Door Seal

a o

Ins ection Sco

e

The inspectors reviewed the adequacy of a temporary modification of the Unit 2

steam tunnel door seal that was in place from 1992 to 1996.

b.

Findin s and Observations

The entrance to the Unit 2 steam tunnel consists of two doors, separated

by a short

passage

way.

The outer door is a single latch security door, and the inner door is a

multiple latched metal door with an elastomer seal around the edge; together, the

doors form a portion of the secondary containment boundary.

During an inspection

of the steam tunnel, the inspectors noted

a puddle of sticky liquid on the floor of

-the passage

way between the two doors.

The licensee determined that the material

was elastomer door seal material

~ The inner door seal had been replaced during the

1996 refueling outage; some of the old seal material had been inadvertently left in

the passage

way and had decomposed.

The inspector was concerned that the

elastomer might not be appropriate for use as a steam tunnel door seal.

The inspector determined that a DER (2-96-0836) had been written on March 29,

1996 concerning degradation

of the inner steam tunnel door seal.

The DER

indicated that the door seal was melting, that there were puddles of seal material on

the floor, and that air was bubbling through the seal area.

The problem had

previously been documented

in a problem identification report (11716) on

February 18, 1996.

The DER also indicated that the problem had happened

before

and that the seal had last been replaced

in March 1992.

The resolution to DER 2-96-0836 provided

a history of problems with the inner

steam tunnel door seal

~ Melting of the seal was first noted in 1991 and

documented

in DER 2-91-Q-0755.

The condition was evaluated

as being due to

use of an incompatible cleaning solvent.

Corrective action was to replace the

existing neoprene

seal with an urethane

seal.

This was performed as a temporary

modification (91-068) in 1992.

The urethane

seal had a five year life, but a design

temperature

of only 90 degrees

Fahrenheit

(

F); the actual environmental

temperature

can be as high as 130~F.

As a result, the seal was deteriorating

(melting) after four years of service.

DER 2-96-0836 concluded that the door was

operable

in its degraded

condition, because

it was still able to hold a seal.

The root

cause of the door seal degradation

was an inadequate

design evaluation of the

urethane

seal material for environmental conditions.

The cause of the inadequate

design evaluation was indeterminate.

As corrective action, an engineering

design change (2F00373A) was developed to

replace the urethane

seal with a more suitable material.. An interim corrective

action, to install a new seal of the same material during a forced outage, was never

performed because

there were no forced outages prior to shutdown for refueling.

The design change was implemented during the ".996 refueling outage,

and installed

a seal composed

of E401

EPDM compound.

'

27

One of the functions of the inner steam tunnel door is to act as a portion of the

secondary containment boundary.

Per technical specification 3/4.6.5.1, secondary

containment integrity is demonstrated

by the ability to maintain at least 0.25 inches

of vacuum (water gauge) within the secondary containment; there are no

requirements for leak tightness of individual boundaries.

Given that the required

vacuum was maintained from the time the degraded

condition was identified until

the plant was shutdown for refueling outage, the inspector concluded that the inner

steam tunnel door seal was adequate

to perform its secondary containment

function, even though it was progressively degrading.

DER 2-96-0836 states that the inner steam tunnel door is also a class C (thr'ee hour)

fire door.

The DER indicates that engineering determined that the urethane

seal

does not sustain

a fire and is a proper door material to have in a fire boundary to

maintain a three hour fire rating.

The inspector was concerned that this

determination suggested

that there was a requirement for the seal to function as a

portion of the fire barrier.

However, in discussions

on this matter, the licensee

indicated that the seal served no fire protection function, and that the recess for the

seal formed a baffle which directed fire away from the gap between the door and

the frame.

Therefore, the inspector concluded that the fire protection function of

the door had not been degraded

by the inadequate

door seal.

Conclusions

The temporary modification that installed a urethane

seal on the inner steam tunnel

door in 1992 was inadequate,

in that it failed to account for environmental

temperatures

that exceeded

the design temperature

of the seal material.

After seal

degradation

was identified, corrective actions were appropriate.

Use of the

inappropriate

seal material from 1992 until 1996 had the potential to cause

a failure

of secondary containment; however this did not occur, and the degraded

condition

did not constitute

a violation of any other specific regulatory requirements.

Operability of the door as a fire barrier was not affected by the degraded

seal

~

'3

Maintenance Procedures

and Documentation

M3.1

Problem Identification and Work Control Process

a 0

Ins ection Sco

e

Applicable work control procedures

were reviewed to determine the effectiveness

of

problem identification processes.

b.

Findin s and Observations

Procedure

GAP-PSH-01, "Work Control" establishes

the procedure for entering

equipment/material

problems into the corrective action program.

Problems are

entered into the program by the identifying individual using a problem identification

(PID) report.

PIDs that involve plant equipment or operations

are initially reviewed

28

by the SSS for operability/reportability.

A PID ultimately causes

a work order to be

generated

to correct the identified problem.

In reviewing GAP-PSH-01, the inspector noted that it did not provide guidance

concerning equipment problems that should also be reported under the DER system.

On the other hand, procedure

NIP-EAC-01, "Deviation/Event Report," does refer to

'he use of PIDs in parallel with DERs.

The inspector considered that material

problems identified by a PID might not receive the same level of management

attention and evaluation (for example, root cause evaluation) as if a DER had been

used.

Also, the inspector noted that newly submitted

PIDs are reviewed by the SSS

every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The inspector considered that this could delay operability issues.

from being recognized,

although no instances

of this were noted.

Finally, the

inspector noted that GAP-PSH-01 discusses

the use of deficiency tags, however

none were observed

to be posted during plant tours.

The licensee acknow'~aged

.the inspector's observations

but indicated that the approach of using the computer

data base to enter and track PIDs in lieu of using deficiency tags meets

management

expectations.

Conclusions

The problem identification system procedures

established

adequate

guidance for

work control.

However, the PID process does not procedurally ensure the same

level of review and evaluation as does the DER entry mechanism for the corrective

action program.

M3.2 Operator Work Arounds

Ins ection Sco

e

The inspector reviewed licensee processes

for identifying, tracking, and correcting

operator work around items.

Findin s and Observations

The governing procedure for tracking control room deficiencies at Unit 1 is N1-ODG-

04, "Control Room Deficiencies Guideline."

The procedure

establishes

basic

classifications of deficiencies, including corrective maintenance

deficiencies,

defeated annunciators,

extended

markups and holdouts, configuration control

holdouts, longstanding

control room operator aids, and invalid and nuisance

alarms.

The control room deficiency log is maintained by the shift technical advisor and is

reviewed monthly by the operations manager.

At the time of this inspection, the

Unit 1 control room deficiency list contained 20 items.

Control room deficiencies at Unit 2 are tracked in accordance

with N2-ODP-0001,

"Conduct of Operations," section 3.3.8.

Other than markups, control room

deficiencies are documented

by PIDs. At the time of this inspection, the Unit 2

control room deficiency list contained 35 items.

v

0

29

Operator work arounds at Unit 2 are tracked in accordance

with procedure N2-ODI-

5.70, "Work Arounds and Longstanding Tagouts."

Items are identified as operator

work arounds using a Work Around Tracking Form, and tagouts greater than six

month old are designated

as longstanding.

Based on two year trending presented

by the licensee, this procedure

appears to be effective; work arounds have been

reduced from about 40 in mid-1995 to 19 at the time of this inspection, and

longstanding

tagouts have been reduced'from about 100 to about 30.

In reviewing the work around list, the inspector noted that some items that had

been examined

and were apparently resolved, were still being carried on the list.

For example, the requirement for operators to open specific circuit breakers for

some Appendix R fire scenarios was listed as a work around in January 1996.

However, the issue was addressed

in DER 2-94-0202, and as a result, the

requirements

have been incorporated into the appropriate

procedures,

and the FSAR

.has been updated to indicate this strategy.

In another example, operator action to

run emergency fans during the summer to maintain EDG room temperatures

less

than 95'F was added in July 1996.

However, in discussions

with system

engineering,

the inspector was informed that the emergency fans start automatically

when the associated

EDGs start, and that there were no room temperature

issues

that affected EDG operability; the identified work around was considered to be a

habitability issue and no action was being taken to address

it. The inspector

considered that continuing to carry such item could lessen the credibility of the

operator work around list.

The inspector reviewed the operator work around list for Unit 1 and noted that it

included five items.

From discussions

with the coordinator of the operator work

around list, the inspector determined that a procedure was being developed to

incorporate enhancements

such as prioritization of corrective actions.

Improving

the effectiveness of the operator work around list appeared

to have significant

management

attention.

Conclusions

Adequate procedures

and processes

are in place for identification and.correction of

operator work arounds.

Unit 2 has been effective in reducing the number of

operator work arounds

and longstanding tagouts.

Some items being carried on the

Unit 2 operator work around list apparently have no recourse remaining, and could

lessen the credibility of this corrective action mechanism.

30

Miscellaneous Maintenance Issues

(Closed) Unresolved Item 50-410/95-25-02:

Extended Inoperability of the Unit 2

Loose Parts Monitor

~Back round

This item concerned

the inoperability of the loose parts monitor (LPM) from July

1991 until it was noted by the NRC resident inspector in December 1995.

As

discussed

in inspection report 50-410/95-25, the inspectors were concerned with

the weak organizational attention that had allowed the LPM to be inoperable for so

long.

The licensee initiated DER 2-95-3455 to investigate this situation.

Findin s and Observations

The inspector reviewed DER 2-95-3455, "Timeliness of restoration and reporting for

LPM system inoperability."

The DER indicated that the long'standing system

inoperability was the result of repeated

attempts to correct system lockups that

occurred during plant 'operations at less than full power.

The system lockups were

due to alarms, caused

by increased

background

noise, from the LPM channels that

monitored the recirculation loops.

The licensee addressed

this hardware issue by

transferring it to another

DER, 2-95-2128, while DER 2-95-3455 went on to

address

additional reportability requirements

and the lack of timely corrective action.

The root cause evaluation concluded that the cause of this event was managerial

methods,

based

on the repetitive problems and that managements

response

to the

problems were untimely and ineffective.

However, the evaluation proposed

no

corrective actions.

The root cause verification noted that the problem would

not'ecur

if the root cause was eliminated, because,

"appropriate management

oversight

on long standing hardware issues will prevent similar occurrences

in the future."

However, the mechanism

by which this is supposed

to occur is not identified.

The

evaluation went on to indicate that a system engineer has been assigned to the LPM

system, which the inspector considered

to be a substantive

'measure to prevent

recurrence.

The hardware problem with the LPM system was corrected by disabling the alarm

function for the recirculation loop detectors

(four of the 10 channels

in the system).

The technical acceptability of thas approach

is discussed

in safety evaluation 96-

089.

The system modification was completed during the 1996 refueling outage and

was reported to the NRC in a letter from the licensee,

NMP2L 1678, dated

December 6, 1996.

As of this inspection, the LPM system remained operable.

Conclusions

The extended

inoperability of the LPM system was due to ineffective management

oversight of efforts to resolve

a technical issue.

The licensee's root cause

evaluation did not specify corrective actions, and the mechanism

by which

increased management

oversight will be maintained was not clear.

However, given

0

31

that the longstanding

hardware problems with the LPM system have been

addressed

and that the system has been returped to service, this item is closed.

M8.2

(Closed) Inspector Followup Items 50-220/96-07-17

and 50-410/96-07-17:

Extended

Installation Period for a Service Water System Temporary Modification

This item concerned

temporary modification 91-107, which installed a corrosion

monitoring station for the Unit 2 service water system.

The modification consisted

of rack mounted corrosion coupons which were used to assess

the effectiveness

of

biocides at controlling microbiologically induced corrosion and biofouling.

Per

discussions'with the licensee, the long installation period was required to develop

and verify the long term effectiveness

of what would become

a permanent chemical

treatment system.

This temporary modification was subsequently

incorporated

as

part of a permanent modification (design change N2-94-007) which installed the

service water chemical treatment system.

Design change N2-94-007 was

completed on August 8, 1997, therefore, this item is closed.

III. ENGINEERING

E7

Quality Assurance in Engineering Activities

E7.1

50.59 Program Review

a.

Ins ection Sco

e

The team reviewed safety evaluations

and applicability reviews prepared

by the

licensee in support of changes,

tests, and experiments

made in accordance

with

10 CFR 50.59.

The licensee uses applicability reviews -:or a preliminary screening

to determine if 10 CFR 50.59 is applicable to the proposed

change.

The team

measured

the licensee's

performance

by the quality of the safety evaluations

and

applicability reviews.

The team reviewed the following safety evaluations

prepared for each unit.

Unit 1

97-021, Draft E, Rev. 0

97-024, Draft C, Rev. 0

97-108, Draft A, Rev.

1

97-119, Draft A, Rev. 0

97-114, Draft B, Rev. 0

Unit 2

97-046, Draft C, Rev. 0

97-050, Draft A, Rev. 0

97-057, Draft A, Rev. 0

97-060, Draft A, Rev. 2

97-062, Draft A, Rev. 0

97-070, Draft A,'Rev. 0

In addition, the team reviewed 26 applicability reviews conducted at Unit 1 and 16

applicability reviews conducted at Unit 2. The team reviewed SORC and SRAB

meeting minutes for the past six months to assess

the management

oversight of the

50.59 program and also interviewed qualified preparers of safety evaluations

and

applicability reviews.

\\

Oi~

V

32

b.

Findin s and Observations

The team found the quality of the safety evaluations to be good.

The increased

quality of the safety evaluations

can be attributed, in part, to good senior

management

oversight of the program.

The SORC and SRAB meeting minutes

show evidence of detailed reviews of safety evaluations

by senior management.

Good feedback was provided to the preparers of safety evaluations.

The team found the quality of applicability reviews to be mixed.

The applicability

reviews prepared

by individuals experienced

in the 50.59 process were of good

quality.

Applicability reviews prepared

by individuals less experienced

in the 50.59

process were of lesser quality.

The team had comments concerning the amount of

detail provided in the description of the proposed

change for 6 of the 26 Unit 1

applicability reviews and 6 of the 16 Unit 2 applicability reviews that were

presented.

In some cases the written responses

provided for justification of the

answers to the five screening questions were not of sufficient detail to support the

preparer's

conclusions.

In no case did the team find the applicability review

conclusion to be incorrect.

The team noted that the licensee's

procedures

do not

require supervisory approval of completed applicability reviews, and there was no

evidence provided that any site organization conducted

routine periodic reviews of

completed applicability reviews for adherence

to plant procedures.

C.

Conclusions

The quality of safety evaluations were good and could be attributed in part to good

. senior management

oversight of the program.

In contrast to the quality of the

safety evaluations,

the quality of applicability reviews was mixed primarily due to

the level of documentation.

In some cases,

documentation

was not sufficient to

support the conclusions.

E8

IVllscellaneous Engineering Issues

E8.1

IFI 50-220 5 410/96-07-14:

Weaknesses

in the 50.59 Program

The May 1996 IPAP report noted that the quality of safety evaluations

and

applicability reviews prepared

by plant personnel

needed improvement.

This

comment was made in part based

on the number of safety evaluations that were

being rejected by the two management

review committees.

Since the IPAP report was published, plant management

has made a significant

effort to improve the quality of safety evaluations.

A review of recent SRAB and

SORC meeting minutes indicate that the rejection rate is near zero and the

committee members have continued to ask challenging questions of the preparers.

The team independently

review'ed the five most recent safety evaluations completed

at both units and found the quality to be good.

33

V. MANAGEMENTIVIEETINGS

X1

Exit lVleeting Summary

The inspectors

presented

the inspection results to members of the licensee

management

at the conclusion of the inspection on August 22, 1997.

The licensee

acknowledged

the findings presented.

The inspectors

asked the licensee whether

any materials examined during the inspection should be considered

proprietary.

No

proprietary information was identified.

X2

Review of UFSAR Commitments

A recerit discovery of a licensee operating their facility in a manner contrary to the

Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a

special focused review that compares plant practices, procedures

and/or parameters

to the UFSAR description.

While performing the inspections discussed

in this

report, the inspector reviewed the applicable portions of the UFSAR that related to

the areas inspected.

The inspector verified that the UFSAR wording was consistent

with the observed plant practices, procedure,and/or

parameters.

ATTACHMENT1

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Abbott, Unit

1 Plant Manager

D. Baker, Licensing Supervisor

C. Beckham, Manager, Quality Assurance

J. Burton, Director, ISEG

W. Connolly, QA Audit Supervisor

J. Conway, V.P. Nuclear Engineering

G. Corell, Mgr., Chemistry-U1

R. Dean, Manager, Unit 2 Engineering

A. DeGracia, Mgr., WC/Outage-U1

M. Dooley, Operations Support Unit 1

S. Doty, Maintenance

Manager-U1

J. Dryfuss, General Supervisor Operations Support

T. Fiorenza, Technical Support

J. Forderkonz,

Refueling Floor Coordinator Unit

1

D. Goodney, Electrical Engr. Supv.-U1

G. Gresock, Licensing Engineer

R. Hall, Director HRD

G. Helker, Unit 2 WC/OMG

B. Holloway, NMPC U1-Chemistry

K. Johnson,

Engineer

A. Jolka, Supervisor,

Unit 2 Electrical Engineering

M. Kalsi, Unit 2 Electrical Engineering

G. Kahn, ISEG-U2

D. Lundeen, Maintenance

Support Unit

1

J. Mancuso, Operations Support

P. Mazzaferro, Mgr., Tech Support-U1

R. McCoy, Operations Support Unit 1

B. Murtha, Operations

Manager Unit

1

D. Pike, Project Management

Unit

1

M. Pisano, Maintenance

Manager, Unit 2

N. Rademacher,

Executive Staff

A. Raju, Unit 2 Electrical Engineering

B. Smith, Operations Manager Unit 1

R. Strusinski, Operations Supervisor

J. Swenszhowski,

Director, 01P

K. Sweet, Unit 1 Technical Support Manager

R. Sylvia, NMPC Exec. V.P.

R. Tessier, Training Manager

C. Terry, Vice President NSAS

A. Vierling, General Supervisor,

Fuel and Analysis

C. Wave, Chemistry Manager

G. Whitaker, Engineer,

ISEG

B. Wolken, Maintenance-U2

D. Wolniak, Manager of Licensing

Attachment

1

NRC

T. Beltz, Resident Inspector

L. Doerflein, Chief, Reactor Projects Branch

1

B. Norris, Senior Resident Inspector

INSPECTION PROCEDURES USED

40500

Effectiveness of Licensee Controls in Identifying, Resolving,

and Preveriting Problems

ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-220 5. 410/97-80-01

VIO

Failure to Justify the Extension of DER Disposition

50-410/97-80-02

Closed

50-410/95-25-02

50-410/95-25-03

IFI

Engineering

Evaluation and Corrective Actions

Concerning

Degraded

"B" RHR Full Flow Test Valve

URI

Extended Inoperability of the Unit 2 Loose Parts Monitor

URI

DERs Extended Without Justification

50-220 5 410/96-07-12

IFI

Weaknesses

in the DER Process

50-410/96-07-1 3

IFI

ISEG Review of NRC Documents

50-220 5. 410/96-07-14

IFI

Weaknesses

in the 50.59 Program

50-220 5 410/96-07-17

IFI

Extended Installation Period for a Service Water System

Temporary Modification

Discussed

None

C'

0

Attachment

1

3

LIST OF ACRONYIVIS USED

CFR

DER

EDG

ESA

FME

I&C

IFI

IN

IPAP

ISEG

NMP

NMPC

PID

QA

RHR

SA

SIL

SSS

SW

TS

UFSAR

Unit 1

Unit 2

Code of Federal Regulations

Deviation/Event Report

Emergency

Diesel Generator

Engineering Support Analysis

Foreign Material Exclusion

Instrumentation

and Controls

Inspector Followup Item

Information Notice

Integrated Performance Assessment

Process

Independent

Safety Engineering Group

Nine Mile Point

Niagara Mohawk Power Corporation

Problem Identification

Quality Assurance

Residual Heat Removal

Self-Assessment

Service Information Letter

Station Shift Supervisor

Service Water

Technical Specification

Updated Final Safety Analysis Report

Nine Mile Point Unit 1

Nine Mile Point Unit 2

0