IR 05000324/2015003

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IR 05000324/2015003 and 05000325/2015003; July 1, 2015 Through September 30, 2015; Brunswick Steam Electric Plant; NRC Integrated Inspection Report and Exercise of Enforcement Discretion
ML15310A162
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 11/06/2015
From: Hopper G
NRC/RGN-II/DRP/RPB4
To: William Gideon
Duke Energy Progress
References
EA-15-234 IR 2015003
Download: ML15310A162 (30)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ber 6, 2015

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2015003 AND 05000324/2015003 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Gideon:

On September 30, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Brunswick Unit 1 and 2 facilities. The enclosed integrated inspection report documents the inspection findings, which were discussed on October 20, 2015, with you and other members of your staff.

No NRC-identified or self-revealing findings were identified during this inspection. However, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as non-cited violation NCV consistent with Section 2.3.2.a of the Enforcement Policy.

In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

George T. Hopper, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62

Enclosure:

IR 05000325, 324/2015003 w/Attachment: Supplementary Information

REGION II==

Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62 Report No.: 05000325/2015003, 05000324/2015003 Licensee: Duke Energy Progress, Inc.

Facility: Brunswick Steam Electric Plant, Units 1 & 2 Location: Southport, NC Dates: July 1, 2015 through September 30, 2015 Inspectors: M. Catts, Senior Resident Inspector L. Pressley, Acting Senior Resident Inspector M. Orr, Acting Resident Inspector M. Schwieg, Resident Inspector J. Austin, Senior Resident Inspector (1R18)

A. Ruh, Resident Inspector (1R04/1R05)

A. Sengupta, RII Reactor Inspector (1R07)

S. Sanchez, Senior Emergency Preparedness Inspector (1EP2, 1EP3, 1EP4, 1EP5, 4OA1, 4OA6)

C. Fontana, Emergency Preparedness Inspector (1EP2, 1EP3, 1EP4, IEP5, 4OA1, 4OA6)

Approved by: George T. Hopper, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure

SUMMARY

IR 05000325/2015003, 05000324/2015003; 07/01/15 - 09/30/15; Duke Energy Progress, Inc.,

Brunswick Steam Electric Plant, Units 1 and 2.

This report covers a three-month period of inspection by resident and regional inspectors.

There are no NRC-identified violations documented in this report. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP) dated April 29, 2015. The cross-cutting aspects are determined using IMC 0310,

Aspects within the Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy dated February 4, 2015. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014.

Licensee-Identified Violation One violation of very low safety significance that was identified by the licensee has been reviewed by the inspectors. Corrective actions planned or taken by the licensee have been entered into the corrective action program (CAP). This violation is listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at rated thermal power (RTP). On August 29, 2015, the unit was down powered to 70 percent for a scheduled control rod sequence exchange. The unit was returned to RTP on August 30, 2015. On September 1, 2015, the unit was down powered to 83 percent for a scheduled control rod pattern adjustment. The unit was returned to RTP on September 2, 2015 and remained at or near RTP for the remainder of the inspection period.

Unit 2 began the inspection period at RTP. On September 18, 2015, the unit was down powered to 70 percent for a scheduled control rod sequence exchange. The unit was returned to RTP on September 19, 2015. On September 21, 2015, the unit was down powered to 70 percent for a scheduled control rod improvement. The unit was returned to RTP on September 22, 2015. On September 23, 2015, the unit was down powered to 75 percent for a scheduled control rod improvement. The unit was returned to RTP on September 24, 2015 and remained at or near RTP for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness to Cope with External Flooding

a. Inspection Scope

The inspectors evaluated the licensees implementation of flood protection procedures and compensatory measures during impending conditions of flooding or heavy rains.

The inspectors reviewed the updated final safety analysis report and related flood analysis documents to identify those areas containing safety related equipment that could be affected by external flooding and their design flood levels. The inspectors walked down flood protection barriers, reviewed procedures for coping with external flooding, and reviewed corrective actions for past flooding events. The inspectors verified that the procedures for coping with flooding could reasonably be used to achieve the desired results. For those areas where operator actions are credited, the inspectors assessed whether the flooding event could limit or preclude the required actions.

Documents reviewed are listed in the attachment.

The inspectors conducted walkdowns of the following plant areas containing risk-significant structures, systems, and components that are below flood levels or otherwise susceptible to flooding:

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial Walkdown (71111.04 - 4 samples)

a. Inspection Scope

The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. The inspectors observed whether there was indication of degradation, and if so, verified degradation was being appropriately managed in accordance with an aging management program, if applicable, and it had been entered into the licensees CAP at the appropriate threshold. Documents reviewed are listed in the Attachment.

The inspectors selected the following four systems or trains to inspect:

  • Unit 1 and Unit 2 nuclear service water (NSW) pumps and Unit 2 conventional service water (CSW) pumps with 2B NSW pump out of service due to planned maintenance on August 19, 2015
  • Unit 1 HPCI during increased activity associated with the dehydration skid on September 3, 2015

b. Findings

No findings were identified.

1R05 Fire Protection

Quarterly Inspection (71111.05Q - 5 samples)

a. Inspection Scope

The inspectors evaluated the adequacy of selected pre-fire plans and fire protection procedures by comparing the pre-fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the pre-fire plans, the inspectors assessed the following items:

  • control of transient combustibles and ignition sources
  • fire detection systems
  • water-based fire suppression systems
  • gaseous fire suppression systems
  • manual firefighting equipment and capability
  • passive fire protection features
  • compensatory measures and fire watches
  • issues related to fire protection contained in the licensees CAP The inspectors toured the following fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the

.

  • 2PFP-RB2-1g, Unit 2, Reactor Building, 20 foot elevation North and South
  • 1PFP-TB1-01A/B and 1PFP-TB1-10, Unit 1 Turbine Building Breezeway 20 foot elevation and Exhaust Fan Room 45 foot elevation
  • 1PFP-RB, Unit 1, Reactor Building, -17 foot elevation, HPCI Room

b. Findings

No findings were identified.

1R07 Heat Sink Performance

Triennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors reviewed, where applicable, vendor manual information, associated calculations, performance test results, and inspection results for the RHR heat exchanger 1A and 2B, EDG jacket water cooler-1 heat exchanger, 1C reactor building component cooling water (RBCCW) heat exchanger, and 2B control rod drive pump lube oil cooler heat exchanger.

These heat exchangers were chosen based on their risk significance in the licensees probabilistic safety analysis, and their important safety-related mitigating system support functions.

The inspectors determined, where applicable, whether the testing, inspection, maintenance, and monitoring of biotic fouling and macrofouling programs for the selected heat exchangers were adequate, to ensure proper heat transfer. This was accomplished by determining whether the test method used was consistent with accepted industry practices, or equivalent; the test conditions were consistent with the selected methodology; the test acceptance criteria were consistent with the design basis values; and reviewing results of heat exchanger performance testing. The inspectors also determined whether the test results appropriately considered differences between testing conditions and design conditions; the frequency of testing based on trending of test results was sufficient to detect degradation prior to loss of heat removal capabilities below design basis values; and the test results considered test instrument inaccuracies and differences.

For the heat exchangers selected, the inspectors reviewed the methods and results of heat exchanger performance inspections. The inspectors determined whether the methods used to inspect and clean heat exchangers were consistent with the as-found conditions identified, expected degradation trends, and industry standards. The inspectors also verified that the licensees inspection and cleaning activities had established acceptance criteria consistent with industry standards, and the as-found results were recorded, evaluated, and appropriately dispositioned so that the as-left condition was acceptable.

In addition, the inspectors determined whether the condition and operation of the heat exchangers selected were consistent with design assumptions in heat transfer calculations, and as described in the Final Safety Analysis Report. This included determining whether the number of plugged tubes were within pre-established limits based on capacity and heat transfer assumptions. In addition, eddy current test reports and visual inspection records were reviewed for the RHR heat exchanger 1A and 2B, EDG jacket water cooler-1, and the 1C RBCCW to determine the structural integrity of the heat exchangers.

The inspectors determined whether the performance of ultimate heat sinks (UHS), and their subcomponents such as piping, intake screens, pumps, valves, etc., were appropriately evaluated by tests or other equivalent methods, to ensure availability and accessibility to the in-plant cooling water systems.

The inspectors determined whether the licensees inspection of the UHS was thorough, and of sufficient depth to identify degradation of the shoreline protection, or loss of structural integrity. This included determination whether vegetation present along the slopes were trimmed, maintained, and were not adversely impacted by the embankment.

In addition, the inspectors determined whether the licensee ensured sufficient reservoir capacity by trending, and removing debris or sediment buildup, in the UHS.

The inspectors reviewed the licensees operation of the service water (SW) system and UHS. This included a review of licensees procedures for a loss of the SW system or UHS, and the verification that instrumentation, which is relied upon for decision-making, was available and functional. In addition, the inspectors determined whether macrofouling was adequately monitored, trended, and controlled by the licensee to prevent clogging. The inspectors determined whether the licensees biocide treatments for biotic control were adequately conducted, and whether the results were adequately monitored, trended, and evaluated. The inspectors also reviewed strong pump-weak pump interaction, and design changes, to the SW system and the UHS.

The inspector performed a system walkdown of the SW intake structure to determine whether the licensees assessment of structural integrity, and component functionality, was adequate, and that the licensee ensured proper functioning of traveling screens and strainers, and structural integrity of component mounts. In addition, the inspectors determined whether SW pump bay silt accumulation was monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments were functional and routinely monitored. The inspectors also determined whether the licensees ability to ensure functionality during adverse weather conditions was adequate.

In addition, the inspectors reviewed condition reports (CRs) related to the heat exchangers, and heat sink performance issues, to determine whether the licensee had an appropriate threshold for identifying issues, and to evaluate the effectiveness of the corrective actions. Documents reviewed are listed in the Attachment.

These inspection activities constituted five heat sink inspection samples as defined in inspection procedure 71111.07-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11 - 1

sample)

a. Inspection Scope

On August 11, 2015, the inspectors observed simulator scenario LORX-202 conducted for training of an operating crew. The scenario included a loss of offsite power and a small break loss of coolant accident.

The inspectors assessed the following:

  • licensed operator performance
  • the ability of the licensee to administer the scenario and evaluate the operators
  • the quality of the post-scenario critique
  • simulator performance Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual

Plant/Main Control Room (71111.11 - 1 sample)

a. Inspection Scope

The inspectors observed licensed operator performance in the main control room on August 29, 2015 during a Unit 1 downpower reactivity manipulation to 70% rated thermal power to support a control rod sequence exchange and various testing activities.

The inspectors assessed the following:

  • use of plant procedures
  • control board manipulations
  • communications between crew members
  • use and interpretation of instruments, indications, and alarms
  • use of human error prevention techniques
  • documentation of activities
  • management and supervision Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors assessed the licensees treatment of the issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. The inspectors also interviewed system engineers to assess the accuracy of performance deficiencies and extent of condition. Documents reviewed are listed in the

.

  • Elevated moisture content in Unit 1 HPCI oil system
  • Service water strainer shear pin failure maintenance rule evaluation

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk mitigation assessments. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the CAP. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities. Documents reviewed are listed in the Attachment.

  • Yellow risk condition due to Unit 1 RHR time delay relay channel calibration on B Loop, 1MST-RHR28BR
  • Yellow risk condition due to Unit 1 RHR and RHRSW outage on B Loop
  • Orange risk condition due to unplanned trip of Unit 1 480 V feeder breaker to motor control center 1CB
  • Elevated risk condition due to Unit 1 1B CSW and RCIC outage

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

Operability and Functionality Review (71111.15 - 6 samples)

a. Inspection Scope

The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that Technical Specification (TS) operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the TS and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.

Documents reviewed are listed in the Attachment.

  • Unit 1, HPCI operable with pump casing leaking, August 12, 2015
  • Unit 1, nitrogen backup pressure drop, August 20, 2015
  • Unit 2, 2A-2 station battery cell 6 low voltage, August 25, 2015
  • Unit 1, 1C RHRSW booster pump oil condition, August 25, 2015
  • Unit 1, reactor water clean-up (RWCU) inlet inboard isolation valve, (1-G31-F001)containment isolation function given dual indication and over thrust event, September 9, 2015

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors verified that the plant modification listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors either observed post-maintenance testing or reviewed the test results for the maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.

  • Unit 1, Work Order ( WO) 13432010, July 16, 2015, HPCI maintenance outage
  • Unit 2, WO 13316882, July 24, 2015, No. 4 diesel generator maintenance outage
  • Unit 2, WO 20012340, August 22, 2015, RCIC following failure of steam trip and throttle valve to close during overspeed test
  • Unit 1, WO 11842952, September 24, 2015, 1B CSW pump strainer replacement
  • Unit 1, WO 12287726, September 28, 2015, RCIC actuator inspection The inspectors evaluated these activities for the following:
  • acceptance criteria were clear and demonstrated operational readiness
  • effects of testing on the plant were adequately addressed
  • test instrumentation was appropriate
  • tests were performed in accordance with approved procedures
  • equipment was returned to its operational status following testing
  • test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the attachment.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the surveillance tests listed below and either observed the test or reviewed test results to verify testing adequately demonstrated equipment operability and met TS and licensee procedural requirements. The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance. Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the attachment.

Routine Surveillance Tests (71111.22 - 2 samples)

  • 1MST-RHR28BR, RHR B Loop Time Delay Relay Channel Calibration, August 4, 2015
  • 0PT-12.2C, No. 3 Diesel Generator Monthly Load Test, August 9, 2015 In-Service Tests (71111.22 - 1 sample)
  • 2OI-03.2, Reactor Operator Daily Surveillance Report, Attachment 1, Drywell Leakage Calculation

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Evaluation

a. Inspection Scope

The inspectors evaluated the adequacy of the licensees methods for testing and maintaining the alert and notification system in accordance with NRC Inspection Procedure 71114, Attachment 02, Alert and Notification System Evaluation. The applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section IV.D requirements were used as reference criteria. The criteria contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, were also used as a reference.

The inspectors reviewed various documents which are listed in the Attachment, interviewed personnel responsible for system performance, and observed aspects of periodic siren maintenance and testing. This inspection activity satisfied one inspection sample for the alert and notification system on a biennial basis.

b. Findings

No findings were identified.

1EP3 Emergency Response Organization Staffing and Augmentation System

a. Inspection Scope

The inspectors reviewed the licensees Emergency Response Organization (ERO)augmentation staffing requirements and process for notifying the ERO to ensure the readiness of key staff for responding to an event and timely facility activation. The qualification records of key position ERO personnel were reviewed to ensure all ERO qualifications were current. A sample of problems identified from augmentation drills or system tests performed since the last inspection was reviewed to assess the effectiveness of corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114, 03, Emergency Response Organization Staffing and Augmentation System.

The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50, Appendix E requirements were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the ERO staffing and augmentation system on a biennial basis.

b. Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

Since the last NRC inspection of this program area, several changes were made to the Radiological Emergency Plan, along with changes to several implementing procedures.

The licensee determined that, in accordance with 10 CFR 50.54(q), the Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors reviewed these changes to evaluate for potential reductions in the effectiveness of the Plan. However, this review was not documented in a Safety Evaluation Report and does not constitute formal NRC approval of the changes.

Therefore, these changes remain subject to future NRC inspection in their entirety.

The inspection was conducted in accordance with NRC Inspection Procedure 71114, 04, Emergency Action Level and Emergency Plan Changes. The applicable planning standards of 10 CFR 50.47(b), and its related requirements in 10 CFR 50, Appendix E, were used as reference criteria.

The inspectors reviewed various documents that are listed in the Attachment to this report. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis.

b. Findings

No findings were identified.

1EP5 Maintenance of Emergency Preparedness

a. Inspection Scope

The inspectors reviewed the corrective actions identified through the Emergency Preparedness program to determine the significance of the issues, the completeness and effectiveness of corrective actions, and to determine if issues were recurring. The licensees post-event after action reports, self-assessments, and audits were reviewed to assess the licensees ability to be self-critical, thus avoiding complacency and degradation of their emergency preparedness program. Inspectors reviewed the licensees 10 CFR 50.54(q) change process, personnel training, and selected screenings and evaluations to assess adequacy. The inspectors toured facilities and reviewed equipment and facility maintenance records to assess licensees adequacy in maintaining them. The inspectors evaluated the capabilities of selected radiation monitoring instrumentation to adequately support Emergency Action Level (EAL)declarations.

The inspection was conducted in accordance with NRC Inspection Procedure 71114, 05, Maintenance of Emergency Preparedness. The applicable planning standards, related 10 CFR 50, Appendix E requirements, and 10 CFR 50.54(q) and (t)were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the maintenance of emergency preparedness on a biennial basis.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the emergency preparedness drill conducted on September 9, 2015. The inspectors observed licensee activities in the simulator and technical support center to evaluate implementation of the emergency plan, including event classification, notification, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures.

Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the CAP. Documents reviewed are listed in the

.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between July 1, 2014, through June 30, 2015. to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.

In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. Documents reviewed are listed in the Attachment.

Cornerstone: Mitigating Systems

Cornerstone: Barrier Integrity

  • RCS specific activity

Cornerstone: Emergency Preparedness

  • Drill/Exercise Performance (DEP)
  • Emergency Response Organization Drill Participation (ERO)
  • Alert and Notification System Reliability (ANS)

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

The inspectors screened items entered into the licensees CAP to identify repetitive equipment failures or specific human performance issues for follow-up. The inspectors reviewed CRs, attended screening meetings, or accessed the licensees computerized corrective action database.

.2 Annual Follow-up of Selected Issues (71152 - 3 annual samples)

a. Inspection Scope

The inspectors conducted a detailed review of the following three CRs:

  • CR 758254, Unplanned TS entry for 2A CSW high strainer differential pressure
  • CR 752720, Unit1 1A RHRSW booster pump maintenance causing secondary containment inoperability The inspectors evaluated the following attributes of the licensees actions:
  • complete and accurate identification of the problem in a timely manner
  • evaluation and disposition of operability and reportability issues
  • consideration of extent of condition, generic implications, common cause, and previous occurrences
  • classification and prioritization of the problem
  • identification of root and contributing causes of the problem
  • identification of any additional CRs
  • completion of corrective actions in a timely manner Documents reviewed are listed in the Attachment.

b. Findings

A licensee identified violation was identified on the 1A RHRSW booster pump maintenance. This violation is documented in Section 4OA7.

4OA3 Follow-up of Events

.1 (Closed) Licensee Event Report (LER) 05000324/2015-001-00, Implementation of

Enforcement Guidance Memorandum (EGM) 11-003, Revision 2

a. Inspection Scope

On February 26, 2015, Unit 2 implemented the guidance of EGM 11-003, Revision 2, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with TS Containment Requirements During Operations with a Potential for Draining the Reactor Vessel. Consistent with this EGM, secondary containment operability was not maintained during operations with the potential for draining the reactor vessel (OPDRV) activities. The EGM guidance was implemented four additional times during the Unit 2 refueling outage. The activities are discussed in Section 4OA5.

Inspectors verified compliance with the guidelines of EGM 11-003 prior to and during these activities. The licensee plans to submit a license amendment request to adopt Technical Specification Task Force traveler associated with generic resolution of this issue within 12 months after the issuance of the Notice of Availability. The licensee entered this issue into the CAP as CR 734902.

b. Findings

The enforcement actions associated with this LER are documented in Sections 4OA5.

No findings were identified during the review of this LER. This LER is closed.

.2 (Closed) LER 05000324/2015-002-00 and LER 05000324/2015-002-01, Setpoint Drift in

Main Steam Line Safety/Relief Valves Results in Three Valves Inoperable

a. Inspection Scope

On March 10, 2015, the licensee received the results of testing of eleven main steam line SRVs removed from Unit 1 during the spring refueling outage. Three of the eleven SRVs were found to have as-found lift setpoints outside the +/- 3% tolerance required by TS 3.4.3. One SRV was 3.2% high; one SRV was 3.6% high, and one SRV was 4%

low. The root cause for the high setpoints was determined to be micro-cracking on the pilot disc surface which allowed localized loss of the platinum coating, resulting in corrosion bonding and raising the breakaway force. The low setpoint cause was not determined. Although the SRV setpoints limits were exceeded, the plant condition was bounded by the Brunswick Unit 1 Cycle 21 Reload Safety Analysis, demonstrating that the SRVs could have performed their safety function of limiting reactor vessel overpressure. The inspectors determined the root cause was different from previous SRV failures and, therefore, the issue was not within the licensees ability to foresee and correct.. The licensee entered this issue into the CAP as NCR 737292 and is taking corrective actions to reduce micro-cracking in future SRV pilot rebuilds.

b. Findings

No findings were identified during the review of these LERs. These LERs are closed.

4OA5 Other Activities

.1 Implementation of EGM 11-003, Revision 2, Enforcement Guidance Memorandum on

Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel

a. Inspection Scope

The inspectors reviewed the plants implementation of NRC EGM 11-003, Revision 2, during Unit 2 maintenance activities which had the potential to drain the reactor vessel during the Unit 2 refueling outage. The activities included:

  • February 26, 2015: 398 gallons per minute leakage for establishing a clearance for RWCU vent and drain valve maintenance
  • March 14, 2015: 85 gallons per minute leakage for RWCU maintenance activities and excess flow check valve testing through test valve 2-B32-V85
  • March 17, 2015, 0411: 1 gallon per minute leakage for RWCU isolation valve leak
  • March 17, 2015, 1300: 1 gallon per minute leakage for RWCU isolation valve leak
  • March 18, 2015: 1 gallon per minute leakage for RWCU isolation valve leak, leak stopped when the 2A RWCU pump was put under clearance These activities took place without secondary containment being operable. Inspectors verified compliance with the guidelines of EGM 11-003 prior to and during these activities. Additionally, inspectors verified that, for all dates, all other TSs were met during OPDRVs with secondary containment inoperable.

b. Findings

TS 3.6.4.1, Secondary Containment requires that secondary containment be operable and is applicable during OPDRVs. The required action if secondary containment is inoperable in this condition is to initiate actions to suspend OPDRVs immediately.

Contrary to the above, on February 26, 2015, March 14, 2015, twice on March 17, 2015, and March 18, 2015, the licensee failed to maintain secondary containment operable while performing OPDRVs.

However, because the violations were identified during the discretion period described in EGM 11-003, Revision 2, the NRC is exercising enforcement discretion for the dates of February 26, 2015, March 14, 2015, twice on March 17, 2015, and March 18, 2015, in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation, subject to a timely license amendment request being submitted.

.2 Temporary Instruction 2515/190 - Inspection of the Proposed Interim Actions Associated

with Near-Term Task Force Recommendation 2.1 Flooding Hazard Evaluations

a. Inspection Scope

The inspectors independently verified that the licensees proposed interim actions would perform their intended function for flooding mitigation.

  • Visual inspection of the flood protection feature was performed if the flood protection feature was relevant. External visual inspection for indications of degradation that would prevent its credited function from being performed was performed.
  • Flood protection feature functionality was determined using either visual observation or by review of other documents.

The inspectors verified that issues identified were entered into the licensee's CAP.

b. Findings

No findings were identified.

The inspectors identified the following minor issues and observations:

  • The inspectors performed a walk down of the flooding cliff edge barriers. During the walk down, the inspectors identified that the beyond design basis cliff edge barriers for the Unit 1 and Unit 2 Control Building double doors, doors 1-CTB-DR-EL023-104A/B and 2-CTB-DR-EL023-101A/B, could not be found. The licensee entered this issue in the CAP as NCR 758759. The licensee fabricated new cliff edge barriers for these doors. This is an observation since these cliff edge barriers are for beyond design basis events.
  • During the walk down of the EDG building North door, door 114, the inspectors identified a gap in the watertight door seal of approximately 2 inches by 1 inch, 2 inches off of the ground. The identified gap is below the design basis still water flood level of 22 feet. The licensee entered this issue in the CAP as NCR 758454.

This is a minor issue since a second watertight door with no gaps exists inside of door 114.

  • During the walk down of the EDG building fuel oil transfer chamber South door, the inspectors identified the watertight door would not fully close. The licensee determined the door hinges were misaligned which prevented the watertight door from closing fully. This allowed a gap the entire length of the left side of the door.

The licensee entered this issue into the CAP as NCR 756971 and performed an evaluation of water intrusion during the probable maximum hurricane. This is a minor issue since inleakage due to the gap would not have exceeded the allowed design basis of 5 gallons per minute.

  • The inspectors reviewed Procedure 0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings, Attachment 21, which requires the cliff edge barriers to be installed at least 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> prior to the predicted storm surge of 20 feet or greater on site. Attachment 22 requires the use of a mobile crane to move the EDG rollup door platform to install the flood barrier. The inspectors identified that Procedure 0AI-68 did not include a step to receive notification of the storm surge 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> prior the storm surge being onsite so that the cliff edge barriers could be installed. The licensee entered this issue in the CAP as procedure revision request 758399 and NCR 758338. This is a minor issue since the licensee would be monitoring the path and severity of the storm in the emergency operations facilities.

4OA6 Meetings, Including Exit

On October 20, 2015, the inspectors presented the inspection results of the Integrated Inspection to Mr. Randy Gideon, Brunswick Nuclear Plant Site Vice President, and other members of the licensee staff. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

On August 20, 2015, the inspectors presented the inspection results of the Emergency Preparedness Baseline Inspection to Mr. Randy Gideon, Brunswick Nuclear Plant Site Vice President, and other members of the staff. The inspectors confirmed that proprietary information was not provided or reviewed during the inspection.

On July 23, 2015, the inspectors presented the inspection results of the Triennial Heat Sink Inspection to Mr. Randy Gideon, Brunswick Nuclear Plant Site President, and other members of the licensee staff. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy, for being dispositioned as a Non-Cited Violation.

  • Technical Specification 5.4.1.a requires written procedures to be established as recommended by Safety Guide 1.33, November 3, 1972.Section I.1 recommends procedures for performing maintenance of safety related equipment should be properly pre-planned and performed in accordance with documented instructions appropriate to the circumstances.

Contrary to the above, on June 3, 2015, the licensee failed to establish appropriate work instructions to properly pre-plan and perform maintenance that affected the performance of Unit 1 secondary containment. Specifically, WOs 13304512 and 13304513 failed to ensure that secondary containment was declared inoperable prior to work on the RHRSW motor coolers. The performance deficiency is more than minor, because it adversely affected the procedure quality attribute of the barrier integrity cornerstone to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, and Inspection Manual Chapter 0609, Appendix A, Exhibit 3, Barrier Integrity, the inspectors determined that the finding was of very low safety significance (Green) because it only represented a degradation of the radiological barrier function provided for the SBGT system. The licensee entered this issue into their CAP as NCR 752720 and took actions to make a late LCO entry and change the WO instruction.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

W. Gideon Vice President

C. Moser Plant Manager

K. Allen Director, Design Engineering
A. Brittain Director, Nuclear Plant Security

J. Bryant Senior Nuclear Engineer

J. Cobb Chem Control, Essential Raw Cooling Water System Engineer
K. Crocker Manager, Nuclear Emergency Preparedness

R. Davis Service Water System Engineer

M. Goddard Program Manager, Fire Protection

J Goelz Design Engineer

L. Grzeck Manager, Nuclear Regulatory Affairs
R. Heiber Superintendent, Nuclear Maintenance
J. Hicks Manager, Nuclear Training
B. Houston Manager, Maintenance
F. Jefferson Director, Nuclear Engineering
J. Johnson Manager, Nuclear Chemistry
J. Kalamaja Manager, Nuclear Operations
T. King Manager, Outage and Scheduling

W. Murray Lead Nuclear Engineer

E. Neal Acting Manager, Nuclear Rad Protection
J. Nolin General Manager, Nuclear Engineering
W. Orlando Superintendent, E/I&C
A. Padleckas Assistant Ops Manager, Shift
F. Payne Manager, Nuclear Work Management
A. Pope Director, Nuclear Operating Experience
M. Schultheis Manager, Nuclear Performance Improvement

T. Sherrill Licensing

M. Smiley Manager, Nuclear Ops Training
R. Wiemann Director, Electrical/Rx Systems
E. Williams Superintendent, Nuclear Maintenance

NRC Personnel

G. Hopper Chief, Reactor Projects Branch 4

J. Dodson Senior Project Engineer

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Closed

Temporary Instruction TI Inspection of the Proposed Interim Actions 2515/190 Associated with Near-Term Task Force Recommendation 2.1 Flooding Hazard Evaluations (Section 4OA5.2)

05000324/2015-001-00 LER Implementation of Enforcement Guidance Memorandum 11-003, Revision 2 (Section 4OA3.1)
05000324/2015-002-00 LER Setpoint Drift in Main Steam Line Safety/Relief Valves Results in Three Valves Inoperable (Section 4OA3.2)
05000324/2015-002-01 LER Setpoint Drift in Main Steam Line Safety/Relief Valves Results in Three Valves Inoperable (Section 4OA3.2)

LIST OF DOCUMENTS REVIEWED