ML15118A318

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Insp Repts 50-269/98-08,50-270/98-08 & 50-287/98-08 on 980726-0905.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support
ML15118A318
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 10/05/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A316 List:
References
50-269-98-08, 50-269-98-8, 50-270-98-08, 50-270-98-8, 50-287-98-08, 50-287-98-8, NUDOCS 9810290275
Download: ML15118A318 (61)


See also: IR 05000269/1998008

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270, 50-287, 72-04

License Nos:

DPR-38, DPR-47, DPR-55. SNM-2503

Report No:

50-269/98-08, 50-270/98-08, 50-287/98-08

Licensee:

Duke Energy Corporation

Facility:

Oconee Nuclear Station, Units 1,

2,. and 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

July 26 -September 5, 1998

Inspectors:

M. Scott. Senior Resident Inspector

D. Billings, Resident Inspector

E. Christnot, Resident Inspector

S. Freeman, Resident Inspector

K. Kennedy, Senior Resident Inspector. Region IV.

(Section M8.3)

J. Blake, Regional Inspector (Sections M3.1. M8.1.

8.2)

R. Chou, Regional Inspector (Sections E8.6, E8.7)

D. Forbes: Regional Inspector (Sections R1.1, R1.2,

R2.1. and R2.2)

F. Jape, Regional Inspector (Sections 08.2, 08.3.

08.4, 08.5. 08.6. 08.7, and E8.4)

R. Moore, Regional Inspector (Sections E1.1, E1.4.

E2.1. E7.1. E7.2. E8.1, E8.2. E8.3)

B. Schin, Regional Inspector (Sections E1.1; E1.4,

E2.1, E7.1, E7.2, E8.1, E8.2, E8.3)

M. Thomas. Regional Inspector (Sections E1.1. E1.4,

E2.1, E7.1, E7.2. E8.1, E8.2, E8.3)

Approved by:

C. Ogle, Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9810290275 981005

PDR ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1. 2. and 3

NRC Inspection Report 50-269/98-08.

50-270/98-08, and 50-287/98-08

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection, as well as the results of announced inspections

by seven Region based inspectors. [Applicable template codes and the

assessment for items inspected are provided below.]

Operations

The Unit 1 shutdown was performed in a controlled fashion with good

command and control.

(Section 01.3, [1A. 3B - Good])

-The engineering evaluation to support the return to service of the Unit

3 auxiliary fan coolers was adequate (Recovery Plan Item DB8).

(Section

01.4, [4B, 5C - Adequate])

Pre-job briefs to support return to service of the Unit 3 auxiliary fan

coolers were good in that they contained appropriate -detail and stressed

procedure adherence (Recovery Plan Item DB8).

(Section 01.4, [1A,

3B - Good])

The evaluation and followup actions established by the licensee in

response to lack of oil in a reactor building spray pump were adequate.

(Section 01.5, [4B, SB, SC - Adequate])

The compensatory actions established in response to the licensee's

identification of another water hammer scenario identified during a

Generic Letter 96-06 review were adequate (Recovery Plan Item DB8).

(Section 01.5, [4B, SA - Adequate])

The inoperability of both trains of the essential siphon vacuum system

on Unit 2 was due to a procedure weakness that resulted in a

mispositioned valve (Recovery Plan Item DB4).

(Section 01.5,

[2B - Poor])

Once the potential inoperability of the essential siphon vacuum system

was recognized, the licensee took rapid action to return the system to

readiness and made appropriate notifications to the.NRC (Recovery Plan

Item DB4).

(Section 01.5, [5A. SB, SC - Adequate])

During the Unit 1 return to power operations, the licensee adequately

responded to a condensate air ejector radiation monitor alarm. This

showed a marked improvement over a past occurrence, which resulted in a

non-cited violation. (Section 01.6. [1B - Adequate])

The Unit 1 startup from a forced outage was performed effectively. The

operators' responses to annunciators, monitoring of parameters,

supervisor control, the use of procedures, communications, and

2

management oversight were good. (Section 01.6. [1A. 3B - Good])

Poor communications between operations and material condition personnel

resulted in tape remaining on the stem of an operable safety-related low

pressure injection valve for three days. This was considered a weakness

in communications between site organizations. (Section 04.1, [1A. 3A

Poor])

The licensee's activities involving the Technical Specification change

and administrative controls i.n place to require three high pressure

injection pumps to be operable above 350 degrees F were adequate.

(Section 08.1, [4C - Adequate])

The analysis performed to ascertain reactor building sump operability,

causes of discovery, and resolution were timely and complete. (Section

08.2. [5B. SC - Adequate])

The discovery and subsequent corrective actions for a failure to perform

a low pressure injection flow instrument surveillance were timely and

thorough.

(Section 08.3, [5B. 5C - Adequate])

Following the inspection and recognition of the significance of the

failure to install cotter pins on main steam safety valves, the licensee

took prompt and thorough corrective measures. (Section 08.4. [5B, SC

Good])

The recognition and response by the operators to a failure '

of main

feedwater while shutdown, and the resolution were considered timely and

thorough. (Section 08.5. [lA, SA, SC - Good])

The resolution and corrective action in response to an inadequate

procedure for voltage regulator adjustment were timely and thorough.

(Section 08.6, [5B, SC - Adequate])

The licensee's analysis and resolution of the issues related to the May

3, 1997. Unit 3 high pressure injection event were timely and thorough.

(Section 08.7 [5B. SC - Good])

Maintenance

The maintenance activities observed were, in general, completed

thoroughly and professionally. (Section M1.1, [3A, 3B - Adequate])

Due to potential procedural and work control problems. packing practices

on the safety-related station auxiliary service water pump showed a lack

of attention to detail.

This item was left unresolved pending

additional NRC review of pump packing procedures, material controls, and

work control requirements. (Section M1.2, [2B - URI])

The licensee's plans for inservice inspection and steam generator

examinations during the Fall 1998, Unit 3 refueling outage were

comprehensive (Recovery Plan Item SE8).

(Section M3.1, [2B - Good])

3

Engineering

The Oconee Safety-Related Designation Clarification Program was two

years behind its original completion schedule of January, 1997. The

licensee had essentially kept the program on its revised schedule during

the last 11 months of increased oversight, and overall progress on the

program during the last year was adequate (Recovery Plan Item DB3).

(Section E1.1. [4A, 5C. - Adequate])

Some of the level of detail in the partially completed Oconee Safety

Related Designation Clarification Program database of components relied

upon to mitigate accidents was good. in that related indication and

associated components were included (Recovery Plan Item DB3).

(Section

E1.1, [4C - Good])

Some equipment was notably missing from the partially completed Oconee

Safety-Related Designation Clarification Program database, such as

electrical power supplies (Recovery Plan Item DB3).

(Section E1.1, [4C

-

Poor])

The repair practice on the non-safety-related 1B1 reactor coolant pump

lower oil reservoir that had perpetuated a repetitive minor oil leak was

poor. The leak from the reservoir was the reason for the Unit 1

shutdown this period. (Section E1.2, [2A. 3A. 5B - Poor])

Engineering analysis of the current self-disclosing 1B1 reactor coolant

pump reservoir leak was good. (Section E1.2. [4B. 5B - Good])

.Engineering

analysis of the self-disclosing 1A2 reactor coolant pump

seal problem was good. (Section E1.2, [5B - Good])

The use of the problem investigation process to track to closure

corrective actions for NRC open items and commitments involvingthe

emergency power system and the quality of this process were good

(Recovery Plan Item DB7).

(Section E1.3. [5C *- Good])

The use of the failure investigation process reports, at management

direction when necessary, by engineering to address significant issues

involving the emergency power system and the quality of the failure

reports was excellent (Recovery Plan Item DB7).

(Section E1.3, [4B

Excellent])

The onsite engineering group was addressing the NRC open items and

commitments involving the emergency power system in a sound technical

manner, with appropriate resources, using approved methods, and with

management and supervisory oversight (Recovery Plan Item DB7 - Closed).

(Section E1.3, [4B, 5B, SC - Good])

A violation was identified for an inadequate 50.59 safety evaluation,

for a 1996 Final Safety Analysis Report revision, which failed to

identify an unreviewed safety question related to the net positive

suction head for the reactor building spray pumps. (Section E1.4, [4A,

4B - Poor])

4

Although the licensee failed to adequately identify the licensing basis

related to reactor building spray pump net positive suction head

assumptions; they performed .appropriate, timely analysis to assure

operability of the pumps.

(Section E1.4. [5B - Adequate])

Screening of Problem Investigation Process reports was generally good in

that the significance level was appropriately identified. Downgrading

of Problem Investigation Process reports was adequately controlled

(Recovery Plan Item SA2).

(Section E2.1, [5B - Good])

Operability evaluations of Problem Investigation Process report

identified problems were adequate (Recovery Plan Item SA2).

(Section

E2.1. [5B - Adequate])

S*

Problem Investigation Process report cause determinations and assigned

corrective actions were adequate (Recovery Plan Item SA2).

(Section

E2.1, [5B. 5C - Adequate])

The Problem Investigation Process corrective action backlog, as stated

in the Oconee Recovery Plan, provided an inaccurate and unclear

assessment of the overall Problem Investigation Process corrective

action backlog. Specifically, the recovery plan stated that there were

232 open Problem Investigation Process corrective actions greater than

six months old, while other performance indicators showed the actual

number was approximately 660 (which included 428 management exception

items) open Problem Investigation Process corrective actions (Recovery

Plan Item SA1).

(Section E2.1, [5C - Poor])

The Problem Investigation Process quality reviews performed by the

Safety Review Group were effective in identifying areas for improvement

in the Problem Investigation Process (Recovery Plan Item SA2).

(Section

E7.1. [5A.- Good])

The in-plant reviews of the Oconee Recovery Plan were being performed in

accordance with established schedules. However, programs and directives

under which the Independent Nuclear Oversight Team will function were

still in the process of being revised to reflect the Safety Review Group

organization (including the Independent Nuclear Oversight Team roles and

responsibilities) (Recovery Plan Item SA4).

(Section.E7.1, [5A

Adequate])

A non-cited violation of the maintenance rule was identified by the

inspectors for a failure to monitor the performance of manual caustic

injection valves. (Section E8.1. [3A, 2B - Poor])

The licensee promptly responded to the maintenance rule violation,

including cycling the caustic injection valves to assure that they were

capable of fulfilling their intended function and revising a procedure

to include cycling the valves annually. (Section E8.1, [5C - Good])

The inspectors identified a poor design condition for both timely access

to equipment and personnel safety in that operator access to the

5

handwheel of Unit 3 emergency feedwater flow control valve FDW-316

involved walking on a horizontal.pipe about 15 feet above the floor.

This condition had existed for many years without licensee

identification and corrective action (Recovery Plan Item DB9).

(Section

E8.1, [4A, 5A - Poor])

The recent leak sealing in the Unit 3 control room ventilation system

outside the control room was very thorough and professional. This leak

sealing resulted in a substantial improvement in the attainable pressure

in the Unit 3 control room (Recovery Plan Item NRC3).

(Section E8.2.

[4B. SC - Good])

The licensee's procedures, oversight, and performance of a surveillance

test of the Unit 2B penetration room ventilation system air flow, using

a pitot tube, were good (Recovery Plan Item NRC3).

(Section E8.3. [2B,

4B, 5C - Good])

The licensee's review of the history and causal factors associated with

an issue involving fuses in the reactor trip confirm circuit was

thorough and timely. (Section E8.4, [4A, 5B. SC - Good])

  • -A non-cited violation was identified for improper design basis.

assumptions regarding the high pressure injection system injection and

crossover valves.

(Section E8.5. [4A - Poor])

The identification, analysis, and resolution of the design basis

concerns related to the failure of Valve 1HP-27 to close were adequate.

(Section E8.5, [5A, 5B. SC - Adequate])

Based on the sample reviewed, the licensee exhibited good progress in

the evaluation and resolution of the outliers for the Seismic

Qualification Utility Group program. Most outliers resolved to date

have been through analyses or documentation review. More complex

outliers remain to be resolved by repairs. modifications, or refined

analyses (Recovery Plan Item DB6 - Closed).

(Section E8.6, [4B, 5B.5C

- Good])

Inspector identified deficiencies found in the seismic mounting of the

nitrogen supply lines for all three units degraded the emergency

feedwater systems and indicated a weakness in maintaining the nitrogen

supply line supports (Recovery Plan Item DB6).

(Section E8.7, [2A,

SA - Poor])

Plant Suport

The licensee was effectively.maintaining controls for radioactive

material storage and radioactive waste processing. Work practices

observed during radioactive waste processing were good. (Section R1.1,

[1C. 3A - Good])

  • .

The licensee's water chemistry control program for monitoring primary

and secondary water quality had been effectively implemented in

6

accordance With the Technical Specification requirements and the Station

Chemistry Manual for water chemistry. .The collection of the samples was

performed in accordance with the licensee's chemistry sampling

procedure. (Section R1.2, [1C, 3A - Good])

The inspectors concluded radiation and process effluent and

environmental monitors were .being maintained in an operational condition

to comply with Technical Specification requirements and Updated Final

Safety Analysis Report commitments. (Section R2.1, [2A - Adequate])

The meteorological instrumentation had been adequately maintained and

the meteorological monitoring program had been adequately implemented.

(Section R2.2, [2A, 1C - Adequate])

Report Details

Summary of Plant Status

Unit 1 began the period at 100 percent power. On August 8, 1998, the unit was

shutdown due to reactor coolant pump motor lube oil and pump seal problems.

On August 27, 1998, the unit was returned to and ended the period at 100

percent power.

Unit 2 began and ended the period at 100 percent power.

Unit 3 began the period at 100 percent power. On August 25, 1998, the unit

began an end-of-cycle power reduction and ended the period at 91 percent

power.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection .Procedure (IP)

71707. the inspectors conducted frequent

reviews of ongoing plant operations. In general the conduct of

operations was professional and safety-conscious: specific events'and

noteworthy observations are detailed in the sections below.

01.2 Operations Clearances (71707)

The inspectors reviewed the following clearances during the inspection

period:

98-2910

1MS-87 Air Actuator Preventive Maintenance

98-2816

Perform MPM Test of 1MS-84

The inspectors observed that the clearances were properly prepared and

authorized and that the tagged components were in the required positions

with the appropriate tags in place.

01.3 Unit 1 Reactor Coolant Pump (RCP) Problems and Forced Shutdown

a. Inspection Scope (71707,93702)

On August 8. 1998. Unit 1 was shutdown (SD) due to several RCP problems.

The inspectors observed pump operations, plant conditions, operator.

actions, and observed management interactions during the shutdown.

b. Observations and Findings

On August 7. 1998, at 5:00 a.m., Unit 1 received a RCP 1A2 Seal Outlet

Flow Hi/Low alarm due to number 2 shaft seal leakage above 4.0 gallons

per minut'e (gpm). In accordance with licensee procedures, if leakage

exceeded 4.5 gpm, the unit would require SD due to the inability of the

standby shutdown facility (SSF) to provide adequate emergency seal flow.

The licensee appropriately established an administrative limit on the

pump shaft seal leakage to ensure that this value would not be exceeded

and made plans for an outage on August 14. 1998.

On August 8, 1998, at 3:50 a.m., Unit 1 received a RCP Motor iB1 Oil Pot

Low Level alarm. Operators verified the leakage and noted that RCP 1BI

lower motor bearing reservoir level had dropped about 0.4 inches over a

short period. The operators also observed increasing bearing

temperatures. The oil loss had begun on August 3. 1998. but the leakage

rate had not increased until August 8. 1998, (total drop of 0.8 inches).

These oil levels are not normally trended.

At 4:30 a.m., operations began a controlled plant power reduction. At

approximately 69 percent power, the 181 pump was SD. After consultation

with management, power was further reduced to take the plant off line.

The inspectors observed the shutdown.

c. Conclusions

The SD was performed in a controlled fashion with good command and

control of the plant.

01.4 Return to Service of the Unit 3 Auxiliary Fan Coolers (AFC)

a. Inspection Scope (71707)

The inspectors followed the return to service of the Unit 3 AFCs

following engineering evaluation to resolve Generic Letter (GL) 96-06

water hammer concerns.

b. Observations and Findings

The removal of the Unit 3 AFCs was originally discussed in Inspection

Report (IR)

50-267.270.287/96-20 and Licensee Event Report (LER) 50

269/97-02. Prior to the return-to-service, the inspectors reviewed the

engineering evaluations and 10 CFR 50.59 review. The inspectors noted

that the engineering evaluations were thorough and complete.

Utilizing OP/3/A/1104/10. Revision 58. Enclosure 3.23. Filling Reactor

Building Auxiliary Fan Coolers, the licensee satisfactorily returned the

Unit 3 AFCs to service. This return to service was based on the

licensee's satisfactory completion of an evaluation which demonstrated

that despite the existence of potential water hammer concerns, the Unit

3 low pressure service water (LPSW) system would perform its safety.

function during normal and accident conditions.

3

The inspectors were present for the pre-job briefs and observed low

pressure service water (LPSW)

and reactor building (RB)

responses to the

flow changes. The pre-job briefs contained appropriate detail and

stressed proper procedure implementation. The procedure was carried out

as written and plant response was appropriate. The return-to-service

did not perturb LPSW flow to the reactor building cooling units (RBCUs).

but did reduce RB temperatures significantly. The licensee

appropriately verified, through inspection and normal sump changes, that

the AFCs did not leak.

The licensee indicated that the remaining units'.AFCs will be returned

to service as the supporting analysis is completed on each unit.

Additional NRC review of this issue will occur during the review of LER

50-269/97-02.

c. Conclusions

The engineering evaluation to support the return to service of the Unit

3 auxiliary fan coolers was adequate.

Pre-job briefs to support return

to service of the Unit 3 auxiliary fan coolers were good in that they'

contained appropriate detail and stressed procedure adherence.

01.5 Licensee 10 CFR 50.72 Notifications

a. Inspection Scope (92712, 71707)

The inspectors reviewed the following licensee notifications to the NRC:

On June 30, 1998. the licensee completed a notification for both

trains of the reactor building spray (RBS) system being out-of

service. On July 30. 1998, following completion of an engineering

evaluation, the licensee retracted the notification.

On August 13, 1998, a notification was made for a potential GL 96

06 scenario involving a water hammer in the LPSW pipe within

containment.

On August 31, 1998, the licensee completed a notification for both

trains of the essential siphon vacuum (ESV) system being out of

service.

The inspectors reviewed the notification issues and the corrective

actions taken.

b. Observations and Findings

The inspectors made the following observations:

On July 30, 1998, following completion of an engineering

evaluation, the licensee retracted the June 30, 1998, notification

  • regarding a low oil reservoir level on the 1A RBS pump. The

licensee's evaluation determined that the oil remaining in the

4

pump was sufficient to lubricate its bearings. Engineering also

determined that the leak mechanism was self-limiting and therefore

could not cause the pump to.be inoperable. Based on their review

of the evaluation and discussion with the licensee, the inspectors

agree with this assessment. Duke also no longer plans to submit

an LER on this event. This issue was initially addressed in IR

50-269.270.287/98-07.

On January 24, 1997. Oconee Nuclear Station completed a GL 96-06

notification to report .that analysis performed pursuant to GL 96

06 had predicted water hammer in portions of the LPSW piping.

LER 50-269/97-02, Revision 1. submitted July 31, 1997, addressed

that analysis, and the corrective actions. On August 13. 1998,

the licensee identified another scenario that was predicted to

result in severe water hammers in the LPSW piping inside

containment. This scenario involves having LPSW isolated or

reduced below 420 gpm, when a loss of coolant accident (LOCA) or

main steam line break occurs. The analysis indicates that a water

hammer may occur that could breach the piping. All RBCUs

currently are in service with greater than 420 gpm flow. An

administrative limit of 550 gallons per minute (gpm) has been set

to ensure containment integrity is maintained.- Historically, the

RBCU outlet valves have been tested on a quarterly basis which

does decrease flow to less than 420 gpm during the test. The

licensee indicate that this will be addressed in a supplement to

LER 50-269/97-02. The inspectors verified that all nine RBCUs had

flow greater than 420 gpm and that the operators were aware of the

new minimum flow criteria (operator guidance had been issued).

On August 28, 1998, ESV train 2A was removed from service for

testing by procedure PT/2/A/0261/010. Revision 010. A 72-hour TS

3.19 LCO was entered for ESV 2A train. Testing was completed, the

ESV 2A train was placed back in service, and the LCO was exited on

August 28. 1998. On August 31, 1998, ESV 2B train was removed

from service .for testing and TS 3.19 was entered. During the

conduct of testing on the Train B equipmeht, test personnel

realized that the procedure for the Train B testing did not re

open the suction block valve for the Train B equipment. Licensee

personnel then determined that the ESV 2A suction block valve was

still closed from the previous testing. As a result of this

procedure error, ESV 2A train was inoperable while the ESV 2B

train was also inoperable for testing. This placed Unit 2 in a TS

3.0, a 12-hour LCO for having both trains of ESV inoperable. It

appears that both trains were inoperable for approximately 3

hours, from 11:00 a.m to 2:00 p.m. Following the discovery of the

mispositioned valve, the licensee reopened the ESV 2A suction

block valve, completed a procedure change to the ESV test

procedure to open the ESV 2B suction block valve prior to exiting

the LCO, initiated PIP 2-098-4153. and initiated a 10 CFR 50.72

notification to the NRC. The inspectors verified that the valves

were returned to their correct position and that the procedure had

0II

5

been corrected. This event will be followed by the NRC through

LER 50-270/98-06.

c. Conclusions

The evaluation and followup actions established by the licensee in

response to lack of oil in a reactor building spray pump were adequate.

The compensatory actions established in response to the licensee's

identification of another water hammer scenario identified during a GL

96-06 review were adequate.

The inoperability of both trains of the essential siphon vacuum system

on Unit 2 was due to a procedure weakness which resulted in a

mispositioned valve. Once the potential inoperability of the essential

siphon vacuum system was recognized, the licensee took rapid action to

return the system to.readiness and made appropriate notification to the

NRC.

01.6 Unit 1 Startup Observations

a. Inspection Scope (71707)

Unit 1 was started on August 27. 1998, after a forced outage due to RCP

problems. The inspectors observed the startup.

b. Observations and Findings

During the return to power. the condensate air ejector radiation

monitor, RIA-40. alarmed. This was an expected occurrence due to

chemistry changes which occurred in the secondary system. The

operators, health physics personnel, and chemist took appropriate action

to understand the alarm and followup through successive shifts. This

was marked improvement in RIA-40 interface performance as compared to

that indicated i.n Inspection Report 50-269,270.287/97-18, Section 01.3,

where the licensee's procedure problems were identified during a steam

generator tube leak event. The current alarm had no significance but

was important in that the licensee showed increased understanding in

this area.

.During the return to power operations, the inspectors observed the

.operators' responses to annunciators, monitoring of parameters,

sup ervisor control, communications..the use of procedures, and

management oversight. Access to the control room was restricted to

necessary personnel only. Shift turnovers were well planned and

controlled.

c. Conclusions

During the Unit 1 return to power operations, the licensee adequately

responded to a condensate air ejector radiation monitor.alarm. This

showed a marked improvement over a past occurrence which resulted in a

6

non-cited violation (NCV).

The Unit 1 startup from a forced outage was performed effectively. The

operators' responses to annunciators, monitoring of parameters,

supervisor control; communications, the use of procedures, and

management oversight were good.

02

Operational Status of Facilities and Equipment

02.1 Engineered Safety Feature (ESF) System Walkdowns (71707)

The inspectors used IP 71707 to walkdown accessible portions of the

following ESF systems:

Si.phon Seal Water (Unit 2)

Essential Siphon Vacuum (Unit 2)

Emergency Feedwater (Unit 3)

Equipment operability, material condition, and housekeeping were

acceptable in all cases. Several minor discrepancies were brought to

the licensee's attention and were corrected.

.

02.2 Containment Isolation Lineup (71707)

The inspectors reviewed the following portions of the containment

isolation lineup during the inspection period:

Unit 3 South Low Pressure Injection (LPI) Room

The inspectors observed that the lineup was in accordance with plant

operating procedures and the Updated Final Safety Analysis Report

(UFSAR).

04

Operator Knowledge and Performance

04.1 Tape Found on Stem of Valve 3LP-22

a. Inspection Scooe (71707)

On September 2. 1998. during routine tours of the Unit 3 auxiliary

building, the inspectors found masking tape on the stem and parts of the

motor operator for borated water storage tank (BWST) suction valve 3LP

22. The inspectors questioned the operability of the LPI system and

discussed the issue with the appropriate operations, maintenance, and

management personnel.

b. Observations and Findings

The inspectors determined that valve 3LP-22. which is in the line from

the BWST to the 3B LPI pump, was to be painted as part of the material

condition upgrade for all units. Material condition upgrade personnel

7

had placed the tape in preparation for painting the motor operator but

were moved to other work before actually completing the painting.

The

use of this tape was not evaluated as part of the valve configuration

nor did the painters specifically notify operations of this taping.

The

tape had been on the valve for three days before discovery by the

inspectors.

The licensee stated that the work order controlling the painting had

been signed by operations giving permission for the work to begin.

However, shift operations personnel in Unit 3 were not aware of the work

on 3LP-22 and the potential to affect its operability. Additionally,

while the valve was located in a relatively open area with moderate

traffic, no one reported the tape.

The licensee immediately removed the tape and initiated PIP 3-098-4178.

Material condition upgrade personnel were instructed to discuss their

work with operations on a daily basis. Prior to this they would only

update operations on work status weekly. Operations management also

issued a memo to shift personnel reminding them-of the importance of

moni'toring the plant. The licensee's review of past operability on

valve 3LP-22 indicated that there was enough thrust margin available for

the valveto open or close with tape on the stem. The inspectors agreed

with this analysis.

c. Conclusions

'Poor communications between operations and material condition personnel

resulted in tape remaining on the stem of an operable safety-related low

pressure injection valve for three days. This was considered a weakness

in communications between site organizations.

08

Miscellaneous Operations Issues (92901.92700)

08.1 (Closed) Inspector Followup Item (IFI) 50-269.270.287/95-03-01:

Clarification of TS 3.3.1

(Closed) LER 50-269/90-15: Unit Operation In an Unanalyzed Condition

Due to Design Deficiency, Design Oversight

This issue was originally described in IR 50-269,270.287/90-30.

TS

3.3.1 requires only two HPI pumps to be operable below 60 percent power

and three HPI pumps to be operable above 60 percent power. The licensee

identified that under some accident scenarios below 60 percent power

with a single failure, there could be insufficient flow with only two

HPI pumps. The licensee reported this condition in LER 50-269/90-15 and

established administrative controls to require three HPI pumps to be

operable above 350 degrees F. This was left as Unresolved Item (URI)

50-269,270,287/90-30-01, Clarification of TS 3.3.1 pending completion of

a TS change to revise TS 3.3.1 to clarify HPI system operability

requirements.

8

In IR 50-269,270,287/90-34-, the URI was dispositioned as a NCV with the

URI remaining open. In IR 50-269,270.287/95-03. since the enforcement

had occurred previously, the.URI was closed and.IFI 50-269,270.287/95

03-01 was opened. A TS submittal containing the administrative details

was transmitted to NRC on March 31, 1997. Due to events involving the

failure of the HPI pumps in April of 1997. the licensee committed to

complete a reliability study for the HPI system. This study was to be

completed by December 31. 1997. The NRC has requested additiQnal

information from the licensee and these efforts are being tracked

through Technical Assignment Control (TAC) numbers: M98296, M98297. and

M98298. The inspectors reviewed the documentation cited above and

discussed the issue with NRC management.

Based on the licensee's submittal of the TS change, the tracking and.

review of the submittal by NRR. and the administrative controls in place

to require three HPI pumps to be operable above 350 degrees F. this IFI

and associated LER are closed.

The licensee's activities involving the TS change and.administrative

controls in place to require three HPI pumps to be operable above 350

degrees Fahrenheit (F)

were considered adequate.

08.2 (Closed) Violation (VIO) 50-269,270,287/97-05-02:Failure to Maintain

Configuration Control

The bolts for the RB emergency sump covers, for all three units were

found missing. The licensee's root cause analysis, discussed in PIP 0

097-0146, determined the cause to be a lack of guidance regarding the

bolts in the maintenance procedure. Also, it was determined that a lack

of all bolts did not make the screen inoperable.. Maintenance procedure.

MP10A/1800/105, Revision 08. Reactor Building Emergency Sump LPI Suction

Line Flange - Installation, Removal., and Screen Inspection, was

clarified. The procedure was changed to require at least 4 bolts to be

installed and tightened in a diagonal pattern. The analysis performed

to. ascertain operability, causes of discovery and resolution were timely

and complete.

The corrective actions presented in the licensee's response, dated

August 18. 1997, were verified by the inspectors. This violation is

closed.

08.3 (Closed) VIO 50-269,287/97-15-01: Failure to Complete Required TS

Surveillance on LPI Flow Instruments

(Closed) LER 269/97-09-00: LPI Flow Instrument TS Surveillance Interval

Exceeded Due to Deficient Work Practices

On October 10, 1997. the licensee discovered that the last time the LPI

flow instrument surveillance, required by TS Table 4.1-1 was performed,

the flow transmitters were omitted from the surveillance. The

surveillance was immediately performed which restored operability and

met the TS. The licensee issued LER 269/97-09-00 on November 11. 1997,

9

and the NRC issued VIO 50-269.287/97-15-01. on December 15. 1997.

The corrective actions presented in the licensee's response to the

violation, dated January 15. 1998, and the action described in the LER

were reviewed and verified by the inspectors. The corrective actions

included a review of 615 previously completed work orders to determine

if this type of error has been made in the past. No similar errors were

detected. The licensee also clarified the wording within the model work

order used to schedule and complete these TS required calibrations. The

discovery and subsequent corrective actions for a failure to perform a

LPI flow instrument surveillance were timely and thorough. This

violation and LER are closed.

08.4 (Closed) VIO EA 96-478-01014: Failure to Properly Install Main Steam

Safety Valve (MSSV) Spindle Nut Cotter Pins

In response to an event at another nuclear power station, the licensee

conducted an inspection of the MSSVs on all three units. Results of

these inspections were reported in NRC IR 50-269.270.287/96-16. and in

LER 50-270/96-05-01. Potential Uncontrolled Release via Main Steam

Relief Valves Due to Inadequate Work Practices.

The corrective actions presented in the licensee's response, dated

January 23. 1997. and in the LER were.verified as completed. PIP 0-096

1599 was prepared to document the inspection results and PIP 0-096-2031

was written to perform root causes of the incorrectly installed cotter

pins.

After the cotter pins were correctly installed on the MSSVs, a

modification was made to remove the fork levers, spindle nuts, and

cotter pins on all relief valves. This modification was expanded to

include the primary relief valves on the pressurizer.

The modification eliminates the possibility of a relief valve failing to

reset due to. an improperly installed cotter pin. The modification was

completed on the MSSVs for all three units and has been completed on the

Unit 1 and 2 pressurizers, and the spare pressurizer relief valves. The

work is scheduled to be completed during the next outage on Unit 3.

Following the recognition of the significance of the problem, the

licensee took prompt and thorough corrective measures.

Violation EA 96-478-01014 is closed.

08.5 (Closed) LER 50-269/97-08-00: Manual Reactor Trip Due to Equipment

Failure While Shutdown

This LER describes an event whereby the operators manually tripped the

reactor protective system while the unit was at hot shutdown and sub

critical. The manual trip was required by procedure upon failure of

main feedwater.

10

The plant systems and operators responded as expected. PIP 1-097-202

was issued on July 7. 1997, to investigate and correct the failure. The

root cause was determined to be a failure of a circuit board in the main

feedwater pump turbine control system. The recognition and response by

the operators to a failure of main feedwater while shutdown, were

considered timely and thorough. This LER is closed.

08.6 (Closed) LER 50-270/97-02-00: Grid Disturbance Results in Reactor Trip

Due to Manufacturing Deficiency

On July 6, 1997, Oconee Unit 2 was operating at 100 percent power when a

system grid disturbance initiated a generator protective relay actuation

that resulted in all four reactor coolant pump monitor channels of the

reactor protective system tripping. The .operators placed the unit in

stable, hot shutdown condition. The grid disturbance was created by a

switching problem at Jocassee Hydro Station. The voltage regulator on

Unit 2 did not respond an expected. The root causes of this event were

determined to be a manufacturing deficiency and inadequate installation

instructions. Corrective action included calibration of the voltage

regulator. The resolution and corrective action in response to an

inadequate procedure for voltage regulator adjustment were timely and

thorough. Given that the voltage regulator is not subject to Appendix

B, this will not be subject to enforcement action. This LER is closed.

08.7 (Closed) VIO EA 97-298-04014: Failure to Follow Operations Procedures

Relating to Low Temperature Overpressure Protection Requirements

(Closed) VIO EA 97-298-03014: Failure to Follow Operations Procedure

During the Unit 3 Cooldown on May 3, 1997

(Closed) VIO EA 97-298-05014: Failure to Follow Maintenance Procedures

for the Installation of Tubing

(Closed) LER 50-287/97-03-00: High Pressure Injection System Inoperable

Due to Design Deficiency and Improper Work .Practices

The licensee's corrective actions for these violations were described in

a letter dated September 25, 1997. The licensee's investigation and

initial corrective actions were previously verified to have been

satisfactorily performed during an inspection documented in IR 50

269,270,287/97-08. The LER also described the event and provided

corrective actions. During this inspection, the inspectors verified

that the corrective actions for the violations listed above and the LER

had been completed. The licensee's analysis and resolution of the

issues related to the HPI event were timely and thorough. The

violations and the LER are closed.

11

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707,61726)

The inspectors observed all or portions of the following maintenance

activities:

WO 98067264

Replace AT-7 Signal Isolator for 2NI-1

IP/O/A/0301/3A-1 NI-1 Neutron Flux Instrument Calibration

(Unit 2). Revision 21

IP/O/A/0301/3S-1 Source Range and Intermediate Range Channel Test

(Unit 2). Revision 26

TT/1/A/0110/019

Penetration Room Ventilation System 1A Pitot

Tube Flow Test. Revision 0

OP/1/A/1104/019

Reactor Building Spray System, Enclosure 3.2,

Removing Reactor Building Spray From ES Standby

Mode, Revision 4

OP/1/A/1104/004

LPI System. Enclosure 3.1. RCS Cooldown Using

LPI High Pressure Mode, Revision 80

OP/0A/1106/019

Keowee Hydro Operation From Oconee. Revision 43,

Enclosure 3.1, Automatic Startup, Enclosure 3.4

Shutdown

PT/0/A/0620/009

Keowee Hydro Operation, Revision 16

IP/0/A/0250/001C Low Pressure Service Water to RCP Motor Coolers

Low Pressure Injection Decay Heat Coolers and RB

Component Coolers. Revision 7

IP/0/A/0100/001

Controlling Procedure for Electrical and I&C

Troubleshooting and Corrective Maintenance,

Revision 14

PT/2/A/0261/010

Essential Siphon Vacuum System Test, Revision

001

PT/0/A/0251/010

Auxiliary Service Water Pump Test, Revision 42

OP/3/A/1104/10

Filling Reactor Building Auxiliary Fan Coolers,

Revision 58, Enclosure 3.23

12

PT/3/A/0152/013

Low Pressure Service Water Valve Stroke Test

Revision 5

IP/0/A/0310/07C

Engineering Safeguards System Logic Test

Channel 5 (3LPSW-565), Revision 27

PT1&2/A/0110/015 Control Room Pressurization Test, Revision 11

WO 98079105-01

Check Control Rod Drive Power Supply

IP/0A/0310/08C

Engineering Safeguards System Logic Test

Channel 6 (3LPSW-565), Revision 24

b. Observations and Findings

The inspectors found the work performed under'these activities to be

professional and thorough. All work observed was performed with the

work package present and in use. Technicians were experienced and

knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present whenever required by procedure.

When applicable, appropriate radiation control measures were in place.

c. Conclusion

The inspectors concluded that, in general, the maintenance activities

listed above were completed thoroughly and professionally.

M1.2 Station Auxiliary Service Water (ASW) Pump Impeller Replacement

a. Inspection Scope (62707)

On September 3, 1998. the inspectors observed portions of the impeller

replacement and subsequent testing of the station ASW Pump.

b. Observations and Findings

In June 1998. the inspectors observed, after previous maintenance, that

the packing follower nuts on the station ASW pump were not fully

engaged. In response to inspectors questions regarding this thread

engagement, the licensee decided to replace the packing follower nuts as

part of the work order for changing the impeller. This decision was

made after the work order had been issued and the work order was not

revised to include the increased scope of work. The licensee's

mechanics indicated that they believed the instruction being used

contained sufficient direction.

On September 3, 1998, before the post-maintenance test was performed,

the inspectors observed that the packing follower was slightly cocked,

the packing follower nuts did not fully span the retaining holes in the

follower, and the studs appeared to have been backed out in order to

give the proper thread engagement on the nuts. Following questions by

13

the inspectors and observed leaks during the post-maintenance test, the

licensee decided the packing follower was not completely in the stuffing

box. They stopped the pump, removed one ring of packing, installed the

packing follower farther into the stuffing box, and added washers

underneath the packing follower nuts. They then tested the pump again

and its performance was acceptable.

Removing one ring of packing resulted in the studs being fully engaged.

The licensee later explained that the packing follower was initially

installed in the stuffing box without cocking but the follower nuts only

finger tight. They stated that, due to past problems with packing

break-in, they intended to make packing adjustments during testing. The

licensee acknowledged that the packing follower was cocked but that it

was most likely caused by static pressure against the packing when the

pump was filled for testing.

The impeller and follower nuts were replaced using procedure

MP/0/A/1300/011. Pump - Ingersoll-Rand - Auxiliary Service Water

Rotating Assembly - Removal, Repair And Replacement, Revision 14. The

inspectors reviewed this procedure and found it contained one step to

install packing, packing follower, and follower nuts. The procedure

contained no guidance about packing follower alignment, the type of nuts

and washers to use, or about thread engagement. Procedure

MP/0/A/1300/010 Pump - Packing and Adjusting Packing, Revision 14.

contained some of this guidance but only as a note dealing with how the

packing should look when finished. The inspectors reviewed the pump

vendor manual and found that it also did not contain any guidance about

packing follower alignment, the type of nuts to be used. or the need for

washers. It also did not contain any instructions on the installation

of the follower studs. The licensee stated that the missing guidance

did not affect the operability of the pump and addressed the type of

material for the follower nuts and washers in PIP 0-098-4212.

Pending NRC review of the adequacy of procedures used on the station ASW

pump, the material controls for parts used on the pump, and the work

control'requirements for the change in job scope. this item will remain

unresolved. This will tracked as URI 50-269.270.287/98-08-01:

Configuration Control of the Station ASW Pump.

c. Conclusions

Due to potential procedural and work control problems, packing practices

on the safety-related station auxiliary service water pump showed a lack

of attention to detail. This .item was left unresolved pending

additional NRC review of pump packing procedures, material controls, and

work control requirements.

14

M3

Maintenance Procedures and Documentation

M3.1 Inservice Inspection (ISI) and Steam Generator Program Review (Unit 3)

a. Inspection Scope (73753)

The inspectors reviewed the licensee's program and plans for ISI and

steam generator inspections during the Fall 1998. Unit 3 refueling

outage.

b. Observations and Findings

The Fall 1998 refueling outage will be the end of fuel cycle number 17

(EOC17) for Unit 3. In the ISI schedule, this will be the first outage

in the second 40-month period of the third 10-year inspection interval.

The ISI American Society of Mechanical Engineers (ASME) Code of record

for the second interval is ASME Section XI, 1989 Edition with No

Addenda.

The inspectors reviewed the ISI program, including the incorporation of

relief requests and ASME Code Cases that had been approved by the NRC.

The inspectors found that the inspection plans for the Unit 3 EOC17

outage appeared to be complete.

The inspectors also examined the nozzle mock-up used to qualify

procedures and personnel for the ultrasonic examination (UT) of the HPI

nozzle inner radius area. The mockup was a full-scale representation of

the actual in-plant installation, with an inside-surface defect in the

nozzle inner radius. The inspectors agreed that the use of the mock-up

would provide meaningful training for UT examiners.

The inspectors reviewed the estimated work scope.for steam generator

inspections planned for the Unit 3 EOC17. The planned examinations

appeared. to be comprehensive, examining all of the critical locations of

the Once Through Steam Generators (OTSGs).

c. Conclusions

The licensee's plans for inservice inspection and steam generator

examinations during the Fall 1998, Unit 3 refueling outage were

comprehensive.

M8

Miscellaneous Maintenance Issues (92902.92700)

M8.1 (Closed) LER 50-269/97-11-00: Steam Generator Leak Results in TS Unit

Shutdown Due to Inadequate Process Control

The subject of this LER was discussed in Section M1.4 of IR

50-269,270.287/97-18. The completion of the licensee's root cause

investigation and issuance of the LER did not provide additi.onal

information over what was discussed earlier. This LERis closed.

.15

M8.2 (Closed) LER 50-270/98-01-00:

Operation With Steam Generator Tube

Indications In Excess of Limits Due to Manufacturing Error

The subject of this LER was discussed in Section M1.3 of IR

50-269,270,287/98-05. The completion of the licensee's root cause

investigation and issuance of the LER did not provide additional

information over what was discussed earlier. This LER is closed.

M8.3 (Closed) LER 50-287/97-02-00: Reactor Building Cooling Units Technically

Inoperable

(Closed) LER 50-287/97-02-01: Reactor Building Cooling Units Technically

Inoperable Due to a Manufacturing Deficiency

This event was discussed in IRs 50-269.270,287/97-02 and 50-269,270.

287/97-12. No new issues were revealed by the LER. This LER is closed.

III. Engineering

El

Conduct of Engineering

E1.1 Oconee Safety-Related Designation Clarification (OSRDC) Program

a. Inspection Scope (37550,40500)

The inspectors reviewed the licensee's OSRDC program and compared the

current status with the program schedule and content commitments that

had been described to the NRC in meetings and letters.

b. Observations and Findings

The licensee had described the schedule and content for the OSRDC

program to the NRC in meetings on February 6 and May 1. 1995; in a

letter dated April 12, 1995, titled "Oconee QA-1 Licensing Basis and

Generic Letter 83-28, Section 2.2.1, Subpart 1 Supplemental Response;"

and during bimonthly meetings on the Oconee Recovery Plan in 1997 and.

1998.

The OSRDC program schedule, as described in the meeting of May 1, 1995,

included completion by January 1997. However, the OSRDC program had not

been completed in 1997 and it was then included in the Oconee Recovery

Plan. The September 15, 1997, Oconee Recovery Plan schedule for OSRDC

program completion was November 1. 1998. The most recent (June 30,

1998) Oconee Recovery Plan schedule for OSRDC program completion was

January 1999.

The inspectors verified the licensee was currently on track for OSRDC

program completion by January 1999. The licensee had 12 engineers

working on the program (one onsite and 11 in Charlotte) and expressed a

determination to meet the January 1999 completion schedule. In

comparison, the licensee had about four engineers working on the OSRDC

program during 1995-1997. Also, higher priority programs and projects

16

had impacted the OSRDC program schedule during that time. During 1995

1997, the 20-month OSRDC program had fallen over 22 months behind its

original schedule. The inspectors concluded that, during 1995-1997, the

licensee had been ineffective in keeping the OSRDC program on schedule.

However, during the increased oversight in 1997-1998, the licensee had

essentially kept the OSRDC program on its revised schedule.

As described in the May 1, 1995, meeting summary, the OSRDC program was

designed to provide additional maintenance and testing to non-safety

equipment that was relied upon to mitigate design basis accidents. At

Oconee, quality assurance requirements for systems, structures, and

components (SSCs) have been addressed separately from design

requirements. The terms safety-related and quality assurance (QA)

category QA-1 were used interchangeably. QA-1 SSCs, as listed in UFSAR

Chapter 3.3.1, must-meet 10 CFR 50, Appendix B, quality assurance

requirements. The OSRDC program included identifying all SSCs relied

upon to mitigate approximately 25 design basis accidents and determining

which of those SSCs were not already designated as QA-1.

Those non-QA-1

SSCs that did not operate during normal plant operation in the same mode

that they would .function during an accident would be designated as QA-5.

QA-5 SSCs would then be given maintenance and testing of similar quality

as that given to QA-1 SSCs.

The inspectors verified that the licensee had completed the listing of

SSCs relied upon for almost all of the design basis accidents, and had

not yet determined which of those SSCs were not designated as QA-1. The

information was assembled in a computerized database with 11 columns

including:

Event, Component Identification, Drawing. Operation

(required action). Actuation Method, Notes (further describing the

required action). System Function, Related Indication, and Associated

Components. The database was capable of sorting and printing the

information in various ways. The inspectors noted that some of the

level of detail in the data was good in that-related indication and

associated components were included. However, some equipment was

notably missing such as electrical power supplies (e.g.. breakers and

relays).

Licensee engineers stated that they planned to add electrical

components to the database.

c. Conclusions

The inspectors concluded that, while the OSRDC program was two years

behind its original completion schedule of January 1997, the licensee

had essentially kept the OSRDC program on its revised schedule during

the last 11 months. Some of the level of detail in the partially

completed database of components relied upon to mitigate accidents was

good, in that related indication and associated components were

included, and some equipment was notably missing such as electrical.

power supplies. Overall progress on the OSRDC program during the last

year was adequate.

0II

17

E1.2 Unit 1 RCP Problem Resolution

a. Inspection Scope (37551)

During the period, Unit 1 developed problems with two of the RCPs which

culminated in a Unit 1 shutdown on August 8. 1998. The inspectors

followed the engineering evaluation, resolution of these problems, and

independently inspected the other RCPs.

b. Observations and Findings

IBI RCP

PIP 1-98-3836 indicated that the 1B1 RCP had an oil leak (8

drops/minute) at a slight (1/32 inch height) mis-alignment of its two

piece cover on the lower motor oil reservoir. The cover was distorted

from the mis-alignment and had 1/16 inch gouges in the gasket seating

area. A review of historical work orders (WO) revealed that a slight

oil leak had been present for some time (WOs 96099135 and 97085335), and

had not been resolved (inspectors reviewed the WOs).

Both the WOs had

been worked but the repair shop had reused the existing cover. The

existing cover contributed to the leakage in that the distorted cover

coupled with gasket seating area gouges reduced the effectiveness of the

oil sealing joint.

During the current repair, a spare aluminum cover

was used to replace the existing cover thereby eliminating this

cOntribution.

The licensee was also proceeding with the replacement of existing

aluminum covers with steel covers in an effort to reduce distortion and

leakage possible with the exi-sting aluminum covers. This effort had

been started before, but was abandoned. Visual inspections by the

licensee and the inspectors revealed no other oil leakage on the other

three .RCPs.

The inspectors concluded that the lack of effective corrective action on

the previously identified oil leak was a weakness. The pump reservoir

is non-safety .related equipment and not subject to enforcement.

1A2 RCP

The 1A2 RCP had.an increasing leakage trend on its number one seal. On

disassembly, the licensee discovered that the Teflon double seal delta

channel seal (DSCS) had begun to deteriorate. The licensee had

documented their review and evaluation under failure investigation

process (FIP) in PIP 1-98-3832. The final process report was signed off

August 26, 1998. The inspectors examined the DSCS, observed portions of

the shaft seal disassembly and inspection, reviewed the report, and.

reviewed the pump vendor information on the probable cause.

During the Unit 1 startup, the inspectors observed that all seals

behaved as expected and seal leak off values were within expected

ranges. The evaluation for the problem was good and the inspection

effort was methodical. The inspectors agree that the seal manufacturer

information and facts tend to support the licensee's theory that the

seals exhibited higher leakage rates as a result of two thermal

18

transients coupled with elevated RCS suspended solids, which occurred in

late December 1997 and May 1998.

c. Conclusions

The repair practice on the non-safety related 1B1 RCP lower oil

reservoir that had perpetuated a repetitive minor oil leak was poor.

The leak from the reservoir was the reason for the Unit 1 shutdown this

period. Engineering analysis of the current self-disclosing IBI RCP

reservoir leak was good.

Engineering analysis of the self-disclosing 1A2 RCP pump seal problem

was good.

E1.3 Emergency Power System Open Items and Commitments (Recovery Plan)

a. Inspection Scooe (37551)

The inspectors reviewed the licensee's initiative involving the

emergency power system open items and commitments with the NRC. This

licensee initiative was part of the recovery plan. The scope of the

initiative was to resolve several NRC open items and-7to close several

commitments concerning the emergency power system.

b. Observations and Findings

The initiative contained ten line items consisting of the following:

five items involving responses to violations: two items, commitments,

provided a response-to the interim Keowee report and the installation of

electrical protection for Keowee: one item, a VIO and a related LER.

documented corrective actions involving a Keowee event:.one item, an IFI

and an associated commitment, to install new ground detection equipment;

and one item, an IFI. to complete the root cause evaluation for relay

failures.

The licensee issued PIPs on the issues and performed failure

identification process of selected PIPs concerning these items.

As a result of the review of the initiative, the inspectors determined

the following: the five violations were being addressed in conjunction

with applicable PIP forms and three of the items were associated with a

FIP team report; the commitment involving the interim report was

completed on June 18, 1998, and the protection commitment is to be

implemented by Nuclear Station Modification (NSM) ON-53014; the

violation and the related LER for the Keowee event were being addressed

in conjunction with a PIP and were reviewed by the licensee using a FIP

team report: the ground detection commitment is to be implemented by NSM

ON-53004; and the IFI for the relay failures was being addressed by a

PIP and was reviewed using a FIP team report.

The PIPs and the FIP team reports were in general well written: the

problem identifications were easily understood, covered the individual

19

problem items, and listed related PIPs: the screening, operability, and

reportability reviews referenced TS. quality classifications, and

regulatory issues: the problem evaluations discussed the problem items

extensively and throughly; the FIP team results were technically sound.

and .showed good engineering judgement; and the corrective actions were

comprehensive and addressed the individual problem items. The PIP

corrective actions also contained, where applicable, the responses to

the NRC open items.

The inspectors observed that .the five violations were being prepared for

NRC closure and the PIP corrective actions associated with the

violations have been completed. The two modifications are scheduled for

INN67..a non-refueling outage'time frame, starting in November 1998.

c. Conclusions

The inspectors concluded that the use of the problem investigation

process to track to closure corrective actions for NRC open items and

commitments involving the emergency power system and the quality thereof

were good.

The inspectors concluded that, at management direction, the use of the

failure investigation process reports by engineering, when necessary, to

address significant issues involving the emergency power system and the

quality of the reports were excellent.

The inspectors concluded that the onsite engineering group was

addressing the open items and commitments involving the emergency power

system in a sound technical manner, with appropriate resources, using

approved methods, and with management and supervisory oversight.

This Recovery Plan item is closed.

E1.4 Emergency Core Cooling System (ECCS) Pumps' Net Positive Suction Head

(NPSH) and Containment Over Pressure Licensing Basis Assumption

a. Inspection Scooe (92903.37550)

The inspectors reviewed the licensee's actions associated with a 50.72

reported condition of being outside the station licensing basis that. was

identified by the NRC while reviewing the licensee's response to GL 97

04, NPSH for Emergency Core Cooling and Containment Heat Removal Pumps.

dated October 7. 1997. The licensee issued LER 50-269/98-011. Available

NPSH for RBS Pumps. Outside Design Bases Due to Incorrect Interpretation,

on September 17. 1998. to document this issue.

b. Observations and Findings

The NRC's request for additional information letter to Duke Power

Oconee, dated August 11. 1998. identified that the licensee's response

to GL 97-04. dated January 5, 1998. indicated a condition outside the

NRC reviewed and approved licensing basis. This condition was that the

20

ECCS pumps NPSH analysis reviewed and approved in the licensing basis,

as documented in .the Safety Evaluation Report dated July 6. 1973. did

not credit containment over pressure as an input in the determination of

available NPSH for ECCS pumps during a design basis accident: whereas

the revised licensee analysis in 1991 did credit containment over

pressure to assure the available NPSH was adequate for the RBS pumps

which are ECCS pumps. Containment over pressure is defined as that

pressure which is the difference between actual containment building

pressure and the vapor pressure due to containment sump water

temperature.

In 1991, the licensee identified that RB-over pressure was required to

assure RBS pumps' operability. This was documented in calculation OSC

4361, RBS Pump NPSH Analysis, dated May 31, 1991. This calculation was

performed when the licensee identified that the previous NPSH analysis

used non-conservative design inputs in that the most restrictive flow

path was not evaluated and an incorrect RBS pump NPSH requirement was

used. The calculation concluded that a minimum of 2 psig RB over

pressure was required to assure adequate NPSH for RBS pump operability.

The calculation verified that adequate RB pressure was available as

documented in calculation OSC-4240, UFSAR 15.14.5, LBLOCA Long Term

Containment Responsedated March 19. 1991. It was not identified that

this condition of crediting RB over pressure to assure RBS operability

was inconsistent with the licensing basis. UFSAR Table 6-1. NPSH

Available to ES Pumps During Recirculation, specified that adequate NPSH

was available without crediting RB over pressure.

The UFSAR was not

updated to reflect the late.st information.

In 1992. the licensee identified additional non-conservative design

inputs and again evaluated the RBS NPSH requirements with respect to RB

pressure. Calculation OCS-4467. RB Pressure Needed for RBS Pump

Operation, dated March 9. 1992. determined a slightly higher RB pressure

of 2.8 psig was required to assure RBS pump operability.

The

availability of -this RB pressure was documented in OSC-4240 as stated

above. The licensee again did not identify that credit for RB over

pressure was inconsistent with the licensing basis. The UFSAR was not

updated to reflect the latest information regarding NPSH and RB pressure

requirements. The failure to update the UFSAR was a non-compliance with

10 CFR 50.71e which requires the UFSAR to be updated to assure the UFSAR

contains the latest material developed.. This 1991 and 1992 failure to

update the UFSAR with this information does not reflect present licensee

performance. Additionally, a comprehensive program was initiated in

1997 to review the accuracy and revise the UFSAR. In accordance with

the Enforcement Policy,Section VII.B.3. a violation will not be

identified for this non-compliance with 10 CFR 50.71e.

In a 1996 UFSAR revision, the licensee revised the ECCS NPSH accident

analysis description to delete Table 6-1. All detailed reference to the

available and required LPI and RBS NPSH values were deleted.

This

included the Table 6-1 information that specified that .adequate NPSH was

available for the RBS pumps without crediting RB over pressure.

The

related 10 CFR 50.59 evaluation, dated May 22. 1996. addressed the

21

change as an editorial change dhly and did not recognize the revised

analysis was inconsistent with the licensing basis as described in the

SER, dated July 6, 1973. Subsequently, the 50.59 evaluation response to

the questions defining an unreviewed safety question (USQ) were

incorrect. Specifically, the response. should have been yes to item four

regarding the increased probability of malfunction of equipment

important to safety. The condition of crediting containment over

pressure to assure RBS pump operability was not included in the NRC

approved licensing basis, and was therefore an unreviewed safety

question. This is identified as VIO 50-269.270.287/98-08-02: Inadequate

50.59 Safety Evaluation for 1996 UFSAR Revision Related to ECCS Pumps'

NPSH Analysis.

A related issue identified by the licensee during this review was that

the containment pressure assumed in the NPSH analysis at event

initiation was not. consistent with a containment pressure value in TS,

It appeared that the negative .1

psig assumed in the analysis was less

limiting than the negative 2.45 psig referenced in TS 3.6.4.

This was

addressed in PIP 0-098-3976. . Revision 5 of Calculation OSC 4467. RB

Pressure Needed for RBS Operation revision 5. was completed on August

31. 1998. The revised analysis used negative 2.45 psig and 80 degrees F

as input to the model and determined that the initial conditions of

negative 1 psig and 160 degrees as used in the previous analysis

(revision 4) was more limiting for NPSH considerations.

This condition

was identified in the PIP as operable but degraded for the RBS pumps.

Compensatory actions were implemented to assure the assumptions in the

calculation were assured during plant operations. These actions

included establishment of periodic surveillance for reactor building

pressure and more restrictive values for boron water storage tank

temperature and lake temperature.. These were incorporated in procedure

PT/1.2.3/A/0600/01. Periodic Instrument Surveillance, dated August 21.

1998. A 50.59 safety evaluation was documented for the compensatory

actions in PIP 0-98-3976. dated August 21, 1998.

The licensee's actions to evaluate and initiate corrective actions

following NRC identification of this USQ and the related TS RB pressure

inconsistency issue were appropriate, timely, and consistent with the

requirements of GL 91-18. Revision 1, Information to Licensees Regarding

NRC Inspection Manual Section on Resolution of Degraded and

Nonconforming conditions. A 50.72 report was submitted on August 19,

1998. The operability was promptly evaluated and it was determined that

adequate containment pressure was available during a LOCA to assure pump

operability. This was documented in PIP 0-098-3889 dated August 11.

1998. and supported by Calculations OSC-6521.

Containment Response with

30 Minute Delay in LPSW Flow, revision 3 and OSC-4467.

RB Pressure

Needed for RBS Operation, revision 5. These calculations demonstrated

that containment pressure during a design base accident exceeded that

pressure required for RBS operation. A license submittal was being

developed to change the licensing basis to reflect the 1991 analyzed

condition crediting RB over pressure for RBS NPSH determination.

The

LER report 50-269/98-011 was issued on September 17, 1998. and included

22

corrective actions taken and- planned to correct the violation and

prevent recurrence.

The primary contributor to this issue regarding the licensee being

outside the licensing basis was that the licensee did not correctly

identify the licensing basis condition in their interpretation of the

SER. dated July 6. 1973. It was apparent in their January 5, 1998,

response to GL 97-04 that they interpreted the licensing condition to

include crediting containment over pressure. The ambiguity in the SER

regarding the use of "over pressure" when addressing vapor pressure and

the UFSAR Table 6-1 listing NPSH values which included containment over

pressure could lead the evaluating engineers to incorrectly conclude

that containment over pressure was an approved license condition.

The

documentation of the 1996 UFSAR revision 50.59 safety evaluation was

limited and did not reference these documents. Additionally, as

previously stated, the evaluation stated the UFSAR revision was

primarily editorial; therefore, it is indeterminate to what extent the

evaluator investigated the licensing basis.

c. Conclusions

A violation of 10 CFR 50.59 was identified for an inadequate safety

evaluation that did not identify the USQ associated with being outside

the licensing basis for LOCA accident analysis associated with RBS NPSH.

The NRC concluded that information regarding the reason for the

violation and corrective actions planned to correct and prevent

recurrence were adequately addressed on the docket in LER 98-011, dated

September 17. 1998. Although the licensee performance was poor in

identifying the licensing basis related to this design base assumption,

their performance was adequate in evaluating the operability of the RBS

pumps in the revised design base condition. The licensee's evaluation

demonstrated there was no safety concern related to this issue and no

modifications were required to assure RBS pump operability.

E2

Engineering Support of Facilities and Equipment

E2.1 Corrective Action Program

a. Inspection Scope (40500)

The inspectors reviewed the licensee's corrective action program which

was implemented by Nuclear System Directive (NSD) 208. Problem

Investigation Process. Revision 18. Aspects of the process reviewed

included significance screening. operability evaluations, cause

determination, adequacy of corrective actions, and timeliness of

corrective actions. A sample of approximately 100 PIPs were reviewed.

The majority of the sample were Level 3, less significant event (LSE)

PIPs, and a smaller number of Level 1 and Level 2. more significant

event (MSE) PIPs, initiated'in 1997 and 1998. The sample included both

completed and in-process PIPs.

23

b. Observations and Findings

(1)

Significance Screening

The criteria for determining the significance of PIPs were provided by

directive NSD 208. A multi-organizational screen team evaluated each

PIP for significance in accordance with these criteria during work week

daily meetings. Many PIPs were conservatively categorized as Level 2

MSE PIPs initially to ensure that an operability evaluation was

performed on those problems with potential operability' impact.

These

PIPs were downgraded to LSE PIPs if no operability or reportability

concerns were identified. Downgrading of PIPs was adequately controlled

by the SRG. The inspectors' sample indicated that the licensee was

effectively categorizing PIPs with respect to significance.

One

exception was noted related to a Level 3 LSE PIP (1-098-2616) which

addressed repeated RCS sample valve failures. The criteria indicated

that this PIP should have been categorized as a level two MSE PIP

because it appeared to be an adverse trend. Overall, screening

performance was generally good.

(2)

Operability Evaluations

Operability evaluations were adequate to determine the impact on

equipment and system operation. The inspectors noted that the

operability justification was routinely documented in the problem

evaluation section of the PIP rather than in the designated operability

section.

(3) Cause Determinations - Corrective Actions

Level 3 LSE PIPs received a less rigorous cause determination than MSE

PIPs and the documentation was generally less detailed. The inspectors

assessed cause determinations by the adequacy of the assigned corrective

actions for these PIPs. In the sample reviewed, the corrective actions

were appropriate to address the identified problem. Cause

determinations for the MSE PIPs reviewed were adequate and assigned

corrective actions were appropriate. The timeliness of corrective

actions was addressed in the review of the PIP backlog.

(4)

PIP Corrective Action Backlog

The inspectors reviewed the timeliness of PIP corrective actions

relative to the impact on the PIP corrective action backlog. The PIP

corrective action backlog was one of the initiatives discussed in the

Oconee Recovery Plan under the Management Focus Area of Self-Assessment.

During review of the PIP corrective action backlog, the inspectors noted

that the licensee's stated goal in the Oconee Recovery Plan was to

reduce the number of PIP corrective actions greater than six months old

from over 500 in August 1997 to less than 200 by December 31, 1998. The

licensee's performance indicators in the Oconee Recovery Plan showed

that at the end of July 1998, there were 232 PIP corrective actions

greater than six months old.

The 232 PIP corrective actions were in

24

line with the licensee's target of 240 by the end of July 1998.

During

further review of this initiative, the inspectors noted that there were

other licensee performance indicators of open PIP corrective actions

which were not discussed in the Oconee Recovery Plan.

There was also a

category of PIP corrective actions designated as management exception.

The performance indicators showed that there were 428 PIP corrective

actions in the management exception category that were greater than six

months old. The inspectors questioned why the PIP corrective actions in

the management exception category greater than six months old were not

included in the PIP corrective action backlog discussed in the Oconee

Recovery Plan. Licensee management stated that the PIP corrective

action backlog did not include management exception items because the

management exception items did not meet the licensee's definition of

what was considered to be a backlog item. The inspectors concluded that

there was a weakness in the PIP corrective action backlog discussed in

the Oconee Recovery Plan in that it was not an accurate reflection of

the overall backlog of PIP corrective actions at Oconee.

c. Conclusion

Screening of PIPs was good in that the significance was appropriately

identified. Downgrading of PIPs was adequately controlled.

Operability evaluations of the identified problems were adequate.

Cause

determinations and assigned corrective actions were adequate.

The PIP

corrective action backlog, as stated in the Oconee Recovery Plan.

provided an unclear and inaccurate assessment of the overall PIP

corrective action backlog.

Specifically, the recovery plan stated that

there were 232 open PIP corrective actions greater than six months old.

while other performance indicators .showed the actual number was

approximately 660 (which included 428 management exception items) open

PIP corrective actions.

E7

Quality Assurance in Engineering Activities

E7.1 Self-Assessment Activities

a. Inspection Scope (40500)

The inspectors reviewed selected licensee initiatives in the Oconee

Recovery Plan under the management focus area of self-assessment.

These

initiatives included Corrective Action PIP Backlog (discussed in Section

E2.1 of this inspection report). PIP Quality, Manager Observation/Group

Ass-essment Effectiveness and Benchmarking, and Enhance SRG Self

Assessment Processes.

b. Observations and Findings

(1)

PIP Quality

The purpose of this initiative was to raise the level of PIP quality by

having the SRG review closed PIP activities for compliance with

Directive NSD 208 and reopen those PIP reports where improvements were

25

needed. The inspectors reviewed several SRG assessment reports and

noted that the SRG has been identifying areas for improvement in the PIP

process.

The SRG has been providing the results of their reviews and

feedback to the responsible organizations and to plant management. The

SRG also updated the Oconee PIP data base to provide additional guidance

to PIP report preparers for those areas identified in the assessments as

needing improvements. These efforts by the SRG have contributed to the

reduction in the percentage of PIPs being rejected from approximately 24

percent in August 1997, to approximately 9 percent in July 1998.

The inspectors concluded that the PIP quality reviews performed by the

Safety Review Group were effective in identifying areas for improvement

in the PIP process.

(2)

Enhance SRG Self-Assessment Processes

The purpose of this initiative was to improve the structure of the

Independent Nuclear Oversight Team (INOT) based on the Safety Assurance

strategic study. The INOT included SRG members for each of the NRC

systematic assessment of licensee performance (SALP) functional areas.

The INOT was performing in-plant reviews of activities based on the NRC

SALP functional areas. The inspectors revi.ewed some--of the milestones

established in the Oconee Recovery Plan for this initiative.

All INOT

members were transferred to the SRG by the established date of June 1,

1998.

However, the operations SALP area SRG member returned to

operations. Actions to replace the operations area SRG member were in

progress at the conclusion of this inspection. The inspectors reviewed

the Oconee 1998 assessment schedule (which included SRG in-plant

reviews) and noted that SRG in-plant reviews were being performed in

accordance with established schedules. The inspectors also noted that

the programs and directives under which the INOT will function

(including INOT roles and responsibilities) were being revised and/or

developed to reflect the current SRG organization.

The inspectors concluded that in-plant reviews were being performed in

accordance with established schedules. However, programs and directives

under which the INOT will function were still in the process of being

revised to reflect the SRG organization (including the INOT roles and

responsibilities).

E7.2 Licensee Safety System Engineering Audit (SSEA) of Emergency Feedwater

(EFW)

a. Inspection Scope (37550,40500)

The inspectors reviewed the licensee's SSEA of EFW to assess the

inspection scope and findings.

b. Observations and 'Findings

The inspectors found that the licensee's.SSEA of EFW had an appropriate

scope, which was similar to the scope of an NRC Safety System

26

Engineering Inspection. The SSEA. final report included some good

findings (e.g. , numerous calculation deficiencies and drawing errors

which the licensee evaluated as having no impact on the calculation

conclusions or on system operability). Also. the inspectors verified

that the.SSEA findings and recommendations were appropriately entered

into the licensee's corrective action system for resolution.

All of the

SSEA findings were appropriately assessed by the licensee as less

significant issues, for which no operability evaluation was needed.

However, the inspectors noted that the SSEA may have missed some

significant issues.

(See Section E8.1 of this report for potential EFW

design issues raised by the -inspectors.)

The SSEA also failed to

identify an incorrect statement in the UFSAR that stated that once

started, the EFW pumps would continue to run until stopped by an

operator. The UFSAR statement overlooked an automatic trip of the

turbine-driven EFW Pump at a low OTSG pressure of 500 psig.

The

inspector noted that the licensee's -UFSAR review project had also missed

the EFW design issues and UFSAR error. Therefore, the overall inspector

assessment of the licensee's SSEA of'EFW will not be completed until the

significance of these inspector-identified potential design issues is

.resolved.

c. Conclusions

The licensee's EFW SSEA had an appropriate scope and included some good

findings (e.g., calculation deficiencies), but both the SSEA and the

UFSAR review project missed some significant issues.

The overall

inspector assessment of the EFW SSEA will not be completed until the

significance of inspector-identified potential design issues is

resolved.

E8

Miscellaneous Engineering Issues (92903)

E8.1

(0oen) URI 50-269.270.287/98-03-09:

Licensing Basis Issues With Single

Failure and QA For Non-Safety Equipment Required To Mitigate An Accident

a. Insoection Scooe (92903.37550)

This URI was opened for further NRC review of licensing basis issues

with single failure vulnerabilities and quality assurance for non-safety

equipment that was relied upon to mitigate a design basis accident.

The

inspectors reviewed the OSRDC Program and its treatment .of quality

.assurance .and single failure.

b. Observations and Findinas

The inspectors found that the licensee's OSRDC Program was identifying

non-safety equipment that was relied upon to mitigate a design basis

accident and addressing quality assurance treatment of that equipment

(in the form of maintenance and testing).

The OSRDC Program was not

looking for or in any way addressing single failure vulnerabilities.

27

The inspectors also found that the equipment that was designated QA-1

(which meant that 10 CFR 50. Appendix B was applicable) was not

necessarily the same equipment that was included in various programs to

improve safety; such as single failure, seismic, environmental

qualification (EQ).

GL 89-10 motor-operated valve (MOV)

testing.

Regulatory Guide (RG)

1.97 instrument qualification, in-service testing

(IST).

preventive maintenance (PM),

TS. or probabilistic risk.assessment

(PRA). To better understand the application of *design standards and

programs at Oconee, the inspectors selected 31 components that were

relied upon to mitigate design basis accidents and then.reviewed whether

they had been included in these programs.

0A-1

In selecting the 31 components for review. the inspectors tried to

include some that should have been classified as QA-1 and some that

likely were not QA (10 CFR 50. Appendix B did not apply).

The

inspectors also included several components that were in the EFW system.

to gain some knowledge of that system to use in part as a basis for

evaluating the licensee's current EFW SSEA. After further review. the

inspectors found that approximately half (16) of the 31 components

selected were QA-1 and approximately half (15) were not fully QA.

This

supported the previous licensee and NRC assessments that many .components

that were relied upon to mitigate design basis accidents were not in a

QA program.

The 31 components and their QA status were as follows:

Comoonent

OA Status

1) Turbine-Driven Emergency Feedwater

Not Fully QA

(FDW PU-003)

(Lubricating Pump Oil

System Not QA)

2) Motor-Driven EFW Pump (FDW PU-004)

QA-1

3) EFW Flow Control Valve (FDW VA-315)

Not Fully QA (Air

Operator and Air Supply

Not QA)

4) FDW VA-315 Manual Loader (FDW ML-0046)

Not QA

(for manual operation from the control

room)

5) EFW Minimum Flow Bypass Valve

QA-1

(FDW VA-370)

6) Main Feedwater Pump Hydraulic Oil

QA-1

Pressure (FDW PS-0382) (used to

autostart EFW)

7) Motor-Driven EFW Pump From Upper Surge

QA-1

Tank (UST) Suction Isolation Valve

(C VA-573)

28

8) Turbine-Driven EFW Pump From Hotwell

QA-1

Suction Isolation Valve (C

VA-391)

9) EFW Cross-Tie Valve (FDW VA-0313)

QA-1

(to get EFW from other units)

10) Condenser Hotwell Emergency Makeup

QA-1

Valve (C VA-0187) (dumps UST.to hotwell)

11) Main Condenser Vacuum Breaker Valve

Not QA

(V VA-186)

12) UST Level Transmitter (C LT-0015A)

QA-1

13) UST Level Indicator (C P-0081)

QA-1

14) Condenser Hotwel.l Level Transmitter

Not QA

(C LT-0019A)

15) Control Room Ventilation System (CRVS)

Not QA

Outside Air Damper CD-10A

16) CRVS Booster Fan AH-26

Not QA

17) CRVS Radiation Monitor (RIA RT-0039)

Not QA

18) Letdown Storage Tank Level Transmitter

Not QA. but

(HPI LT-0033)

Modi fication Scheduled

to Upgrade to QA-1

19) Caustic Pump (CA PU-004)

Not QA

20) Caustic System Valve (CA VA-0039)

Not QA

21) Main'Turbine Stop Valve (MS VA-0102)

QA-1

22) Main Turbine Stop Valve Trip Solenoid

QA-1

Valve Not (EHC SV-1083)

23) Main Feedwater Flow Control Valve

Not.Fully QA (Air

(FDW VA-0032)

Operator and Air Supply

Not QA)

24) Main Feedwater Block Valve (FDW VA-0031)

Not QA

25) Main Steam Pressure Transmitter

QA-1

(MS PT-0277)

26) Steam Generator A Level Transmitter

QA-1

(FDW LT-0080)

29

27) Steam Generator Shell Temperature

Not QA

Indication (FDW IOA-0972)

28) Steam Generator Level Control System

QA-1

(SGLCS)

29) Main Steam Isolation Logic Manual Switch

QA-1

(S-1016)

30) Steam Generator Atmospheric Dump Valve

Not QA

(MS VA-0162)

31) Block Valve for Steam Generator

QA-1

Atmospheric Dump Valve (MS VA-0153)

The inspectors found that the licensee's basis for designating

components as QA-1 was not based on safety function, but instead was

based on being designated as QA-1 equipment in Chapter 3 of the UFSAR.

The inspectors further reviewed components that were not QA and that

were either: 1) relied on in a system that was described in the UFSAR as

safety-related and QA-1 or 2) vulnerable to single failure.

The

inspectors assessed components as vulnerable to singTe failure if the

single active failure of a component would challenge the system design

basis or the accident mitigation strategy. Those non-QA components that

were further reviewed are discussed under Single Failure below:

Sinale Failure

The inspectors assessed that 11 of the 31 components were vulnerable to

single failure. Two of the 11 were also in a system that was described

in the UFSAR as safety-related and QA-1.

Those 11 components included:

  • 1)

An air-operated 12-inch valve in a 20-inch line that dumped UST

water to the main .condenser hotwell. C-187.

Since the UST was the

suction source for all EFW pumps, the inspectors noted that a

failure open of C-187 could result in a rapid loss of all UST

water and a consequent loss of EFW. Each Oconee unit had a

hotwell level transmitter that, on a low hotwell level, would

automatically open valve C-187 to dump water from the UST to the

hotwell.

However, at a UST level of seven feet. the hotwell level

signal would be overridden by a UST level signal and C-187-would

go closed to protect sufficient UST water to supply the EFW pumps.

C-187 would also fail closed on a loss of instrument air. Valve

C-187 was QA-1 and seismic, was not in a harsh environment (EQ was

not applicable), was in the IST program, was in a PM program, was

not in TS or selected licensee commitments'(SLC).

and was in the

PRA. The potential untimely dumping of the UST to the hotwell,

due to the failure open of C-187 during a main feedwater line

break, was identified in the PRA as a significant contributor to

the probability of a loss of all EFW.

30

The UFSAR stated that the EFW system could.withstand a single

failure coincident with a secondary pipe break and a loss of

offsite power. However, the PRA apparently contradicted the UFSAR

when it stated that a single failure of C-187 coincident with a

main feedwater line break would cause a loss of all EFW. . Also.

the inspectors found that a 1973 licensee report to the NRC on

high energy line breaks outside containment stated that a main

feedwater line break in the turbine building would cause a loss of

all main feedwater, a loss of all EFW.

and also may cause a loss

of 4160-volt switchgear 1TC. 1TD., and 1TE.

These 4160-volt

switchgear were the three trains of safety-related power to the

motor-driven EFW pumps and also to engineered safeguards equipment

including high pressure injection pumps, low pressure injection

pumps, building spray pumps. and low pressure service water pumps.

The inspectors noted that, in addition to apparently contradicting

the UFSAR. this information did not seem to be reflected in the

PRA. The 1973 report was still the analysis of record for main

feedwater line break and was currently referenced in the FSAR.

(Note: Main feedwater line break was not a licensed design basis

event and was not discussed in the.accident analysis chapter of

the UFSAR.)

In response to concerns about the potential inability of the EFW

system to withstand a main feedwater line break or a single

failure coincident with a secondary pipe break, the licensee

initiated a PIP to review.the issue.

The inspectors plan to

follow up on this issue.

2&3) An. air-operated EFW flow control valve, FDW-315. and the manual

loader for control room operation of that valve. Each Oconee unit

had two EFW flow control valves, one in the discharge piping from

each motor-driven EFW pump. During certain events, including a .

main steam line break, operators were to immediately throttle EFW

flow to prevent damage to the EFW pumps.

As. a result of low pump

discharge pressure that could result from a main steam or feed

line break, two of the three EFW pumps could have insufficient

NPSH:

the safety-related motor-driven pump that supplied water to

the affected OTSG and the non-safety related turbine-driven pump.

which supplied water to both OTSGs.

The EFW system design basis

included.the ability to respond to a design basis event (e.g.,

main steam line break) coincident with a single failure and a loss

of offsite power. If two EFW pumps could be damaged due to the

event, the EFW system would not be able to then withstand a single

failure of the remaining EFW pump.

inside containment, operators were also relied-upon to manually

stop EFW flow to affected OTSG within 10 minutes to prevent

overpressurizing the containment.

There was a motor-operated

valve in the discharge piping from each motor-operated EFW pump

that the operators could close from the control room to stop EFW

flow.

However, the inspectors considered the operator action to

throttle EFW a type of single failure vulnerability because one

31

operator could be relied upon to correctly perform all of the

required manual actions.

The EFW system was described in the UFSAR as safety-related and

QA-1. The EFW flow control valve bodies were QA-1 and seismic.

The air operators were not QA-1 but were seismic.

The manual

loaders and instrument air supply to the valve operators were not

QA-1 or seismic. A two-hour supply of nitrogen, to assure the

ability to operate the valves from the control room, was not QA-1

and was not seismic. However, the licensee had committed to the

NRC in 1987 to walk down the nitrogen supply lines and verify that

they would withstand a seismic event. The valves were EQ. were in

the IST program, were in a PM program, were in the TS. and were in

the PRA. The manual loaders were not QA or seismic, but were

included in the licensee's Seismic Qualification Users' Group

(SQUG) program. (See Seismic below for a description of the SQUG

program.) An inspectors' walkdown reviewing the seismic

ruggedness of the nitrogen supply lines to the EFW flow control

valves is documented in Section E8.7 of this report.

The loaders

were not in a harsh environment, were in a PM program, were in the

TS. and were in the PRA.

The PRA described the operator action to

immediately throttle EFW flow (using the EFW flow control valves

and manual loaders) as a significant contributor to the

probability for the loss of all EFW.

During a walkdown of portions of the EFW system, the inspectors

observed that operator access to the handwheel of Unit 3 EFW flow

control valve FDW-316 during an event would involve the operator

climbing off a platform, over a handrail. and walking about 6 feet

on a horizontal pipe that was about 15 feet above the floor.

(The

platform did not go to the valve and there was no room to use a

ladder.)

The air operator for FDW-316 was non-safety related, and

the licensee had documented to the NRC that operators could

readily operate the valve by handwheel during an event.

An

operator and the Operations Superintendent stated that, during an

event, plant safety would take priority over personal safety and

the operator would walk on the pipe to access the handwheel.

The

inspectors noted that this design condition, that placed operators

in the position of jeopardizing personal safety to support plant

safety during a design basis event, had existed.in the plant for

many years without the licensee identifying it.

In response to

this inspectors concern, the licensee initiated a PIP on this

issue. The inspectors plan to follow up on the licensee's

resolution of operator access to FDW-316.

The inspectors found that a licensee analysis concluded that the

EFW pumps, that were feeding an OTSG affected by a steam line

break, could experience insufficient NPSH or pump runout in less

that one minute as a result of rapid depressurization of the OTSG

to less than about 500 psig. Licensee personnel stated that,

based on training simulator drills, they had concluded that

operators could be relied on to throttle EFW within three minutes

32.

during a main steam line break event. Licensee personnel also

stated that they had no valid test or other data to support their

contention that the EFW pumps could operate for several minutes

with insufficient NPSH without suffering -damage.

The inspectors

noted that the-NRC typically has not approved reliance on simple

operator actions (e.g. , turning a switch in response to an alarm)

in less than 10 minutes or reliance on complex operator actions

(e.g., throttling flow to a specified value a.s read on a meter) in

less than 20 minutes, to mitigate design basis events. The NRC

also has not typically .approved reliance on operating multiple

stage pumps (like the EFW pumps) with insufficient NPSH, to

mitigate design basis events.

The inspectors found that the reliance on operating the EFW pumps

with insufficient NPSH had been identified as the most important

finding of a 1987 NRC Safety System Functional Inspection (SSFI)

of EFW. The issue had been cited as a Severity Level III design

control violation with a civil penalty. However, the violation

had subsequently.been with*drawn by the NRC because the licensee's

original design requirements did not include pump runout concerns.

The violation withdrawal stated that further enforcement action

was not warranted because the licensee planned:to eliminate the

NPSH problem by installing flow limiting ventiris.

However, the

licensee had subsequently decided not to install the flow limiting

venturis and had withdrawn the related commitment.

In response to the current inspectors' concerns with the reliance

on operators performing complex actions within three minutes and

the reliance'on EFW pumps operating with inadequate NPSH for about

two minutes. the licensee initiated a PIP. performed an

operability evaluation, and discussed this issue with the NRC.

The licensee stated that, as part of their operability evaluation,

they discussed the issue with the EFW pump vendor and received a

document from the vendor stating that the EFW pumps could operate

for at least five minutes with insufficient NPSH without being

damaged. The inspectors noted that the licensee had installed a

main steam line break protection circuitry in about 1996 that

.automatically stopped main feedwater and also automatically

stopped the turbine-driven EFW pump on a low OTSG pressure of 500

psig.

This circuitry could potentially protect the turbine-driven

pump from running with insufficient NPSH.

However, the licensee

did not want to rely on this circuitry, as part of their licensed

EFW design basis, to protect the turbine-driven EFW pump from

operating with insufficient NPSH. Instead, the licensee's

operability evaluation concluded that the EFW system was operable

based on a 1981 NRC SER that had approved the EFW system design

with reliance on operator action, and the fact that the SER did

not place time constraints on the operator action.

The NRC will continue to review the following potential design

vulnerabilities: 1) the reliance on.operator action to

immediately throttle EFW flow while using non-safety related

33

equipment and while the EFW pumps operate with insufficient NPSH:

2) poor operator access to the handwheel of Unit 3 EFW flow

control valve FDW-316; and 3) the licensee's plans for modifying

the EFW system to eliminate the reliance on immediate operator

action, using -non-QA equipment, and pump operation in runout.

4&5)

A caustic pump and a caustic valve. Each Oconee unit had one

caustic pump and several handwheel-operated caustic valves,

located in the auxiliary building, that must be manually operated

during a loss of coolant accident.

Operators would use this

equipment to add sodium hydroxide to the containment sump for pH

and iodine control.

(At newer plants, this function was typically

included in the automatic safety-related ECCS systems.)

The

caustic pump and valve were not QA (10 CFR 50. Appendix B did not

apply). were not seismic, were not in a harsh environment (EQ was

not applicable), were not in the IST program, and were not .in

the

TS or another administrative control program. The pump was in a

periodic testing program but the valve was not.

(See Preventive

Maintenance below.)

The pump and valve were not in the PRA. since

the lack of caustic addition would not have any impact on core

damage probability and would have little effect on releases to

atmosphere within the first 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of an acc.tdent.

(Note: The

PRA only considers the first 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of an accident.)

The inspectors found that the licensee had recognized the single

failure vulnerability of the caustic addition system and engineers

were informally investigating an alternate backup method for

caustic addition. In response to inspectors' questions, the

licensee opened a PIP to develop and write a procedure for an

alternate method of caustic addition.

6) A main feedwater flow control valve.

Each Oconee unit had two

main feedwater flow control valves, one for each steam generator.

These were air operated valves that received an automatic signal

to close following a main steam line rupture.

Each was designed

to close fast enough to prevent overpressurizing the containment

building.

The valve bodies were QA-1 but the air operators were

not QA and the air supply was not QA.

On a loss of air pressure,

the valves did not move - they failed 'as is. ' The main feedwater

flow control valve bodies were seismic but the air supply and .

operators were not: the valves were not in a harsh environment (EQ

was not applicable), were in the IST program, and were in a PM

program.

The valves were not in TS but were in the SLC program

which was an administrative control program similar to TS.

The

valves were not in the PRA because the core damage probability of

the steam line rupture event was less than the PRA truncation

level of 10 E-8.

The inspectors found that the NRC was currently reviewing the

licensee's design for mitigating a main steam line break inside

containment, including the design of the main feedwater flow

control valves, pursuant to NRC Bulletin 80-04 and a related

34

license amendment request. The inspectors provided comments on

this issue to the assigned NRC reviewers.

7&8) A main turbine stop valve and a main turbine stop valve trip

solenoid valve.

Each Oconee unit had four main turbine stop

valves (two valves in parallel from each steam generator) located

at the main turbine and two main turbine stop valve'trip solenoid

valves (in series) that tripped the four turbine stop valves.

Each hydraulically operated main turbine stop valve must

automatically close on a reactor trip to prevent RCS overcooling.

(Note: There were no separate main steam stop valves.)

The main

turbine stop valve was QA-1 and seismic, as were the main steam

lines from the steam generator to the main turbine stop valves.

However, the trip solenoid valve was not QA and was not seismic.

The stop valve and solenoid valve Were not in a harsh environment

(EQ was not applicable). were in the IST program, were in a PM

program, and were in the TS. They were not in the PRA because

their failure was bounded by a stuck open main steam relief valve.

The turbine control valves also closed when the stop valve trip

solenoid valves tripped and provided some backup for the turbine

stop valves. Also. the turbine mechanical trip valve and

immediate operator action to manually trip the-turbine from the

control room provided some backup for the stop valve trip solenoid

valves. In response to a 1993 Unit 1 transient (documented in PIP

1-093-0950) caused by a stop valve trip solenoid valve failure

(due to sticking). and also in response to 1993 requirements from

their insurance company. the licensee had instituted a PM to

periodically replace the turbine stop valve trip solenoid valves.

The inspectors found that the NRC had approved the licensee's

turbine trip design, including the fact that the main turbine stop

valve trip solenoid valves were not QA-1, in an NRC SER regarding

GL 83-23. Required Actions Based on Generic Applications of the

Salem Anticipated Transient Without Scram (ATWS)

Event, dated

August 3, 1995. The NRC.had also addressed this issue in a letter

  • dated October 6, 1995, which withdrew Deviation 50-269.270.287/95

09; Solenoid Valves Associated With Main Steam Stop Valves Are Not

Safety-Related.

9&10) A control room ventilation system (CRVS) booster fan and a CRVS

outside air damper. Each Oconee control room (one for.Units 1 and

2 and one for Unit 3) had two outside air dampers and two 50%

capacity booster fans. To provide 1/8-inch water gauge pressure

in the control room for habitability during certain accidents,

both outside air dampers and both booster fans must operate.

The

CRVS booster fan and damper were not QA. were not seismic, were

not in a harsh environment (EQ was not applicable), were not in

the IST program but were periodically tested by a performance'test

(PT).

and were in the TS.

The booster fan was in a PM program but

the damper was not.

The-fan and damper were not in the PRA

because their failure did not directly affect core damage

probability or.releases to the atmosphere. The inspectors

35

verified that. the licensee's emergency operating procedures (EOPs)

did not direct the operators to abandon the control room in the

event of high radiation levels in the CRVS or in the control room.

The licensee recognized that the CRVS was vulnerable to a single

failure of a booster fan or a damper. In response-to related NRC

concerns documented in IR 50-269.270.287/98-03. the licensee was

working to better seal the control rooms toward removing this

single failure vulnerability. The licensee's sealing efforts

included sealing leaks in ventilation ducts, repairing weak damper

actuators, and repairing leaking dampers.

The licensee contended

that the NRC had not required that the CRVS be able to withstand a

single failure when post-TMI action item III.D.3.4, Control Room

Habitability, was applied to Oconee.

The licensee's position, that the CRVS was not required to be able

to withstand a single failure, was currently under review.by the

NRC as part of URI 50-269.270,287/98-03-08.

11)

A steam generator shell temperature computer point.

Information

from this computer point was relied on by operators to control the

plant cooldown rate and ensure that it was not excessive.

This

temperature indication was not QA. was not seismic, was not in a

harsh environment (EQ was not applicable), was not in the RG 1.97

program, was not in a PM program, was not in TS. and was not in

the PRA. The inspectors found that the purpose of the operator

use of this indication was to minimize temperature stresses in the

OTSGs.

Faster cooldown was not expected to immediately damage the

OTSGs. but could increase the probability of future OTSG damage.

Also, the operators had other indications to rely on for

controlling the overall RCS cooldown rate.

The inspectors

concluded that, due to the low safety significance of a failure of

this instrument, this item did not warrant further review.

Almost all (nine of eleven) of these examples of components that were

vulnerable to single failure were not fully QA.

None were major

contributors to the PRA core damage probability. but two of the examples

were significant contributors to the PRA probability of EFW system

failure. Also, a main feedwater line break analysis that described a

consequential loss of all EFW and all three trains of safety-related

4160 volt switchgear was apparently not addressed by the PRA.

The

inspectors plan to follow up on the following potential design

vulnerabilities: 1) a single active failure in the open pbsition of

valve C-187 coincident with a main feedwater line break causing a loss

of EFW: 2) a main feedwater line break in the turbine building causing

consequential failures of the EFW system and all three trains of safety

related 4160 volt electrical switchgear 3) the reliance on operator

action to throttle EFW flow within three minutes while using non-safety

related equipment and while the EFW pumps operate with insufficient

NPSH: and 4) poor operator access to the handwheel of Unit 3 EFW flow

control valve FDW-316.

36

Seismic

Thirteen of the 30 components were not seismically designed.

Each of

the components that was not seismically designed was not QA. Six of the

thirteen were included in the SQUG Program. Under the SQUG Program,

each non-seismic component needed to safely shut down the plant during

normal (non-accident) conditions should be inspected by individuals

experienced with seismic design.

They should judge whether the

installed components look like they would withstand an earthquake or

whether modifications would be needed.

The licensee would then install

modifications as needed. The licensee's SQUG Program was included in

the Oconee Recovery Plan.

Seven of the thirteen were not included in the SQUG Program:

a hotwell

level transmitter, caustic pump. caustic valve, steam generator shell

temperature indication, control room ventilation radiation monitor, main

feedwater block valve, and main steam stop valve trip solenoid valve.

The inspectors verified that UFSAR Section 3.2.2 described the seismic

design requirements and it did not require any of these components to be

seismically designed. The main steam stop valve trip solenoid valve is

discussed further under Single Failure above. The inspectors noted that

thePRA identified a seismic event as the largest contributor to the

potential for core damage.

Environmental Qualification

Five of the 30 components were in a potentially harsh environment. All

five were QA-1 and were also EQ.

GL 89-10 MOV Proaram

Three of the 30 components were MOVs. One was QA-1 and -was also in the

GL 89-10 Program.

Two were not QA and were not in the GL 89-10 Program.

Those two, a main feedwater block valve and a main condenser vacuum

breaker, were not vulnerable to single failure.

While the main

feedwater block valve was automatically closed on a main steam line

rupture and provided some backup to the main feedwater flow control

valve in mitigating a main steam line break, the licensee did not take

credit for the valve closing ih their accident analysis. Operators

would have to open the main condenser vacuum breaker valve to use the

water in the condenser hotwell as a backup source of water for the EFW

pumps.

However, the licensee did not take credit for the motor operator

of.the main condenser vacuum breaker but instead relied on handwheel

operation of the valve. The inspectors verified that the licensee had

satisfactorily tested the ability of operators to open the vacuum.

breaker valve to break condenser vacuum by using the handwheel.

RG 1.97 Program

Nine of the 30 components were instruments that provided indication on

which operators would rely to perform emergency procedures.

Six were in

the RG 1.97 Program and also were QA-1. Three were not in the RG 1.97

37

Program and also were not QA. Those three were:

Hotwell level indication, which would indicate to operators the

availability of TS-required water in the condenser hotwell. for

use as a backup source of water for the EFW pumps, as directed by

EOPs. The licensee stated that the operators did not need to know

the hotwell level 3s the EOPs contained no operator actions based

on hotwell level.

Steam generator shell temperature, which would be relied on by

operators to control the plant cooldown rate. The licensee stated

that operators could safely cool down the plant without reliance

on steam generator shell temperature indication (see Single

Failure above).

Control room ventilation radiation monitor alarm. which had been

relied on.by operators as the signal to start the control room

booster fans. Recently, the licensee revised emergency operating

procedures to require operators to start the control room booster

fans without relying on this alarm.

In-Service Testing

Eighteen of the 30 components were the type for which IST or other

testing would be appropriate. Nine were in the IST Program, four were

in the licensee's Appendix B Program (a periodic testing program similar

to IST).

and four were periodically tested under a Performance Test (PT)

Program. One was not in any periodic testing program and also was not

QA. The component, a caustic valve, is discussed above under Single

Failure and is also discussed below under Preventive Maintenance.

The

licensee's OSRDC Program was designed to identify the lack of periodic

testing for components like these and to add periodic testing.

Preventive Maintenance

Seven of the 30 components were not in a routine PM or calibration

program. However, six of those seven components were in a periodic

testing program - the one exception was a manual caustic valve that was

not QA.

The inspectors verified that EOPs required that the manual

caustic valves be opened following a LOCA, to add sodium hydroxide to

the containment sump during recirculation.

The inspectors found that

the licensee had an annual Caustic Injection System Pump Test.

(PT/1&2/A/0203/009. Revision 13. for Units 1 and 2 and PT /3/A/0203/009.

Revision 11. for Unit 3) that tested the caustic pump and all but one of

the caustic valves for each unit. The one valve per unit that was not

tested was a manual caustic injection valve. (1CA-62,

2CA-63, and 3CA

62).

The inspectors found that the licensee's maintenance rule program had

addressed these caustic injection valves in closed PIP 0-090-3488, dated

July 9. 1998. The PIP stated that an acceptable'performance criteria

for the chemical addition system function to "provide caustic addition

38

to sump" has not been identified. The PIP response. from the system

engineer, stated that the annual performance test. PT/1&2/A/203/09 and

PT/3/A/203/09. that recirculates the caustic to a bin, was the

performance test for this function. The PIP response had overlooked the

fact that the annual performance test did not test the manual caustic

injection valves. A review of maintenance records found that valve 1CA

62 had last been stroked (the valve was replaced) in 1991: yalve 2CA-63

had last been stroked (the valve was repacked) in 1994: and valve 3-CA

62 had last been stroked (a body to bonnet leak was repaired) in 1981.

Since one of these valves had.apparently not been operated in 17 years,

the inspectors asked the licensee how they could assure that the valves

were currently capable of fulfilling their intended function (being

manually opened). In response, the licensee promptly revised the annual

Caustic Injection System Pump Test procedures to include opening and

reclosing the three manual caustic injection valves.

Also, the licensee

promptly opened and closed each valve and verified that they were

capable of performing their intended function.

10 CFR 50.65 requires that the licensee monitor the performance of

components, that are used in plant EOPs, in a manner sufficient to

provide reasonable assurance that the components are capable of

fulfilling their intended functions. Contrary to that requirement, the

licensee had not monitored the performance of caustic injection valves

1CA-62. 2CA-63. and 3CA-62.

Also, while 10 CFR 50. Appendix B. did not

apply to these non-safety related valves, the licensee's corrective

action for PIP 0-098-3488, dated July 9. 1998. had been poor in that it

overlooked these caustic injection valves. After this issue was

identified by the inspectors, the licensee took prompt corrective

action. Also, the licensee's OSRDC Program had already included the

caustic valves in a list of components relied on to mitigate accidents.

and would have identified and corrected the lack of caustic valve

testing within the next year. Further, the licensee stated that the

OSRDC Program will coordinate any lack of testing and maintenance that

it identifies with the Maintenance Rule Program.. This non-repetitive,

licensee-corrected violation that the licensee's established OSROC

Program would have soon identified is being treated as a Non-Cited.

Violation, consistent.with Section VII.B.1 of the NRC Enforcement

Policy. This is identified as NCV 50-269.270.287/98-08-03:

Failure to

Monitor the Performance of Manual Caustic Injection Valves.

TS and SLC

Fourteen of the 30 components were in TS and five were in SLC.

Eleven

of the 30 components were not included in either the TS or SLC

administrative control programs.

Those eleven included:

atmospheric

dump valve, block valve for atmospheric dump valve, condenser vacuum

breaker valve, motor-driven EFW pump UST suction isolation valve,

turbine-driven EFW pump hotwell suction valve, caustic pump, caustic

valve, UST level indication, condenser hotwell level transmitter, steam

generator shell.temperature indication, and control room ventilation

radiation monitor.

The inspectors found that six of these components

were included in a licensee maintenance rule administrative control

39

program. The five components that were not in any administrative

control program were:

steam generator shell temperature indication,

caustic pump, caustic valve, condenser vacuum breaker, and control room

ventilation radiation monitor. Based on the low safety importance of

these five components not being in an administrative control program,

the inspectors did not pursue this issue any further.

Probabilistic Risk Assessment

Thirteen of the 30 components were not in the PRA. Eight are discussed

above under Single Failure..'The other five included:

Letdown storage tank level indication. The licensee.planned to

include this in the next revision to the PRA as a result of the

recent High Pressure Injection Study.

Main steam pressure indication and main feedwater block valve.

These components are involved in main steam line rupture event and

are not in the PRA for the same reason as for the main feedwater

flow control valve (see Single Failure above):

Control room ventilation radiation monitor.

This component was

not in the PRA for the same reason as for the CRVS booster fan and

damper (see Single Failure above).

Manual valve for isolating the motor-driven- EFW pump suction from

the UST. Based on the inspectors questions. the licensee

initiated a PIP to review why this valve was not included in the

PRA.

c. Conclusions

The inspectors found that many components that were relied upon to

mitigate design basis accidents were not in a QA program.

Almost half

(15 of 31) of the components reviewed were not fully QA. In addition,

many of those same components (11 of 31) were vulnerable to single

failure. URI 50-269,270,287/98-03-09 remains open pending further NRC

review of the licensee's OSRDC program.

A non-cited violation of the maintenance rule was identified by the

inspectors for a failure to monitor the performance of manual caustic

injection valves. The licensee promptly responded to this issue,

including cycling the caustic injection valves to assure that they were

capable of fulfilling their intended function and revising a procedure

to include cycling the valves annually.

The inspectors also identified a poor design condition for both timely

access to equipment and personnel safety. in that operator access to the

handwheel of Unit 3 EFW flow control valve FDW-316 involved walking on a

horizontal pipe about 15 feet above the floor. This condition had

existed for many years without licensee identification and corrective

action.

40

Inspector Followup Item (IFI) 50-269,270.287/98-08-05. EFW Potential

Design Basis Issues, will be identified for further NRC review of the

following potential design vulnerabilities: 1) a single active failure

in the open position of valve C-187 coincident with a main feedwater

line break causing a loss of EFW; 2Y a main feedwater line break in the

turbine building causing consequential failures of the EFW system and

all three trains of safety-related 4160 volt electrical switchgear; 3)

the reliance on operator action to throttle EFW flow within three

minutes while using non-safety related equipment and while the EFW pumps

operate with insufficient NPSH: and 4) poor operator access to the

handwheel of Unit 3 EFW flow control valve FDW-316.

E8.2 (Ooen) VIO 50-269.270.287/98-03-07: Incorrect and Nonconservative

Assumptions in Control Room Operator Dose Calculations

a. Insoection Scooe (92903.37550)

In response to this violation, the licensee committed to perform CRVS

tracer gas testing to determine the amount of unfiltered inleakage into

the control room while the booster fans were operating.

The inspectors

observed portions of this testing.

b. Observations and Findings

The inspectors observed the pre-evolution briefing and the tracer gas

testing of the Unit 3 CRVS. conducted during evening off-hours.

The

inspectors observed that the sealing of leaks in the Unit 3 CRVS

ventilation ducting. that was located outside the control room in the

auxiliary building. looked very thorough and professional.

Also. the

sealing resulted in a substantial improvement in the attainable pressure

in the Unit 3 control room. with two outside air-booster fans running,

from less that 0.125 inches water gauge (w.g.) early in 1998 to 0.4

inches w:g. during this inspection. The test prerequisites were

appropriately met, tracer gas was injected, and some samples were taken:

however, the observed test was voided because of problems with the

laboratory equipment that was located in a nearby office building.

The

office building air conditioning had automatically turned off at night,

causing the temperature*-sensitive laboratory equipment to begin to

overheat and potentially become less accurate.

The test was rerun

another night after reprogramming the air conditioner controls. The

inspectors noted that preliminary test results, for tracer gas tests of

both control rooms, were well within the licensee's test acceptance

criteria.

The inspectors plan to review the official test report after

it is completed.

c. Conclusions

The inspectors observed that the sealing of leaks in the Unit 3 CRVS

ventilation ducting, that was located outside the control room in the

auxiliary building, looked very thorough and professional.

Also, the

sealing resulted in a substantial improvement in the.attainable pressure

in the Unit 3 control room, with two outside air booster fans running:

from less that 0-125 inches w.g. early in 1998 to 0.4 inches w.g. during

this inspection.

.

41

E8.3

(ODen) VIO 50-269.270.287/98-03-02: Failure to Perform Penetration Room

Ventilation System (PRVS)

Surveillance in Accordance with TS

a. Insoection Scooe (92903.37550)

In response to.this violation, the licensee committed to perform PRVS

Surveillance testing for air flow by using a pitot tube, as required by

TS 4.5.4.1.b.1. The inspectors observed portions of this testing.

b. Observations and Findings

The inspectors observed the testing of the Unit 2 Train B PRVS system,

per procedure TT/2/A/0110/202. Penetration Room Ventilation System 2B

Pitot Tube Flow Test, Rev. 0, Change A, dated August 4. 1998.

The

inspectors verified that the procedure implemented the requirements of

the TS and that licensee personnel followed the procedure using

appropriate test instruments. The straight run of pipe in the flowpath

upstream of the pitot tube testing location was 15 pipe diameters (15

feet of 12-inch pipe), which exceeded the seven pipe diameters usually

needed for good flow measurement accuracy.

The pitot tube was held by

hand during the flow measurements by a licensee contractor who was

experienced in performing such flow measurements.

At the inspector's

request, the licensee verified and the inspectors observed that angular

movement of the pitot tube by as much as about 20 degrees did not affect

the flow measurement.

The initial test result indicated a flowrate of 1156 cfm. which exceeded

the TS allowable flowrate of 1000 cfm +/- 10 percent.

The licensee

appropriately adjusted the flowrate and ran the test again, with an

acceptable result of 989 cfm. and then properly. re-blocked the position

of the 2B.PRVS flow control valve.

The licensee then tested the Unit 2

penetration room pressure: with the 2B PRVS fan running. and verified

that the penetration room pressure was still negative with respect to

all adjacent rooms (as required for PRVS operability).

That

satisfactorily completed the 2B PRVS testing.

The licensee

appropriately kept the Unit 2 PRVS in the required TS action statement

throughout the testing. Licensee test procedures. oversight, and

performance were good.

c. Conclusions

The inspectors concluded that the licensee's procedures, oversight. and

performance of the surveillance testing of the Unit 2B PRVS air flow.

using a pitot tube, were good.

E8.4 (Closed) IFI 50-269.270/97-01-01: Reactor Trip Confirm Circuit Fuse

Inspection

On or about March 3. 1997, the licensee identified that fuses'installed

in the redundant trip confirm circuity were of the wrong size.

For

example, the vendor's drawing for Unit 3 showed several fuses as 0.5 amp

and others as 5.0 amps. In addition some fuses were shown as 0.25 amp

42

and 10 amp. Units 1 and 2 exhibited similar discrepancies.

The correct fuses were determined and installed in all three units.

The

instrument and electrical (I&E)

procedure for breaker testing.

(IP/01A/0305/014-1: RPS Control Rod Drive Breaker Trip and Events

Recorded Timing Test) that led to the discovery of improper size fuses,

was revised to include a visual inspection for blown fuses prior to

beginning breaker testing. This was apparently the cause of the Unit 3

reactor trip on March 3, 1997. It was determined that a reactor trip

may occur if a blown fuse existed in the circuit when performing

IP/01A/0305/014-1.

The licensee issued PIP 0-097-1014 on March 3. 1997. to resolve the fuse

size discrepancies found while troubleshooting the root causes of the

Unit 3 reactor trip.

The licensee's review of the history and causal factors with an issue

involving fuses in the reactor trip confirm circuit was thorough and

timely. The vendor drawings have been revised and the correct fuses

have been installed. This IFI is closed.

E8.5 (Closed). URI 50-269/98-02-09: Failure of Valve 1HP-27 to Close

(Closed) LER 50-269/98-05-01: Valve Fails to Close Requiring Unit

Shutdown Due to Inadequate Procedure

(Closed) LER 50-269/98-05-00:

Valve Fails to Close Requiring Unit

Shutdown

This URI and LER involved the failure of Valve 1HP-27 to close during

engineered safeguards (ES) testing on February 14. 1998.

At that time

the licensee determined that the design basis should have assumed the

worst case static pressure acting under the seat instead of worst case

differential pressure across the valve. This item has remained

unresolved pending NRC review of the past operability evaluation.

The licensee determined that even though Valve 1HP-27 would not throttle

. closed under some conditions, the HPI system would have performed its

safety functions. In addition, the licensee reworked and tested valve

1HP-27 and revised the design basis calculations for all HPI injection

and crossover valves to include the higher static pressure.

The

licensee also planned to replace the motor operators for all HPI

injection and crossover valves with larger ones.

This has already been

completed on Unit 2 and has been scheduled for Units 1 and 3 during

upcoming outages.

The inspectors reviewed the past operability evaluation and determined

it was acceptable.

However, the use of differential pressure instead of

static pressure acting under the seat in the design basis constituted a

violation of 10 CFR 50 Appendix B, Criterion III. This non-repetitive.

licensee-identified and corrected violation is being treated as a NCV,

consistent with Section VII.B.1 of the NRC Enforcement Policy. This is

43

identified as NCV 50-287/98-08-04: Improper Design Basis Assumptions for

HPI Valves. These items are closed.

A non-cited violation was identified for improper design basis

assumptions regarding the high pressure injection system injection and

crossover valves.

The identification, analysis, and resolution of the design basis

concerns related to the failure of Valve 1HP-27 to close were adequate.

E8.6 Seismic Qualification Utilitv Grouo (SOUG)

Program Imblementation

a. InsDection Scooe (92903)

The inspectors reviewed the SQUG program implementation. outlier

resolutions, and modifications to determine the adequacy of the SQUG

program.

b. Observations and Findings

The inspectors discussed the SQUG program and.its implementation with

engineering personnel. The licensee had completed the selection and

walkdowns of the safe shutdown equipment.

The forms used for the

walkdown screening or evaluation were called "Screening Evaluation Work

Sheets (SEWS)"

which were provided by the General Implementation

Procedure (GIP) for more than 20 types of equipment or devices.

If

equipment or devices were outside those lists, they would be identified

as outliers.

The licensee completed 1692 walkdowns and generated 466

outliers for equipment. The licensee also evaluated 6135 devices for

chatter contact and generated 730 outliers.

The licensee resolved about 630 outliers.

The remaining outliers will

be repaired, replaced, modified, or require further analyses.

The

licensee recently completed modifications in the Keowee hydro station.

The inspectors randomly selected a portion of the Emergency Feed Water

(EFW)

line for walkdowns to verify that the equipment or devices for.the

safe shutdown alongthis line had been walked down and documented by the

licensee. The portion of the line selected was from Upper Surge Tank 3A

at the turbine building deck to valve 3CVA0391 in the turbine building

basement, approximately 120 feet.

The equipment included one upper

surge tank, three air operated valves, one motor-driven emergency feed

water pump, .one isolation valve, one motor-operated valve, two pressure

switches, four oil pressure switches, two level transmitters, two water

level indicators, and associated relays, cabinets, and other control

switches.

The inspectors reviewed the SEWS and other information

provide by the engineers for equipment and the devices identified along

the line and found that they were adequately documented and evaluated.

The upper surge tank required outliers for the evaluation of the.saddle

spacing, anchorage type, and the support legs. Modifications were

required to resolve the outliers.

44

The inspectors randomly selected five repairs or modifications completed

in the Keowee hydro station to determine if the resolution of the

outliers was adequate.

The following five repairs or modifications

stated in PIP 0-096-2783 were walked down by the inspectors and are

listed below:

ComDonent

DescriDtion of Work

SYDC-1 and 2

Increased weld size for anchorage

SYTC cabinets

Added padding between cabinets and columns for

interaction

Battery Racks

Replaced multiple compressible styrofoam with

rigid plexiglass at each end of the racks

HVAC AHU003

Added a horizontal restraint to prevent it from

hitting the cabinets

Cabinet ILCI

Added padding between cableway and 1LCI to

reduce the seismic impact on essential relays

The inspectors measured the weld size. length, anchor bolt diameters,

end attachments. steel wire, and examined the padding and plexiglass.

All the repairs or modifications met the drawing requirements.

The inspectors reviewed.the SEWS and associated outliers related to the

equipment and devices in the EFW line walkdown.

The outliers were

stated in the comments of the SEWS and the reasons for the further

evaluations or reviews were stated.

The inspectors also reviewed five

resolved outliers for the High Pressure Injection (HPI)

and Emergency

Feed Water (EFW)

Systems.

They involved remote starter enclosures 3RSC

3HP-409 and -410 for HPI: nitrogen supply bottles for feedwater valves

315 and 316: main steam valves 87. 126. and 129; and

EFW pump turbine

oil tanks ITDTKOOD2 and 3TOTKO02.

The licensee adequately resolved the.

outliers reviewed.

c. Conclusions

Based on-the sample-.reviewed. the licensee exhibited good progress in

the evaluation and resolution of the outliers for the SQUG program.

Most outliers resolved to date have been through

analyses or

documentation review. More complex outliers remain to be resolved by

repairs, -modifications, or refined analyses.

This Recovery Plan Item is closed.

45

E8.7

Walkdown of Nitrogen Supoly System for EFW Line

a. Insoection .Scooe (92903)

The inspectors walkeddown the nitrogen supply system to determine if

the system met seismic qualified requirements.

b. Observations and Findings

This nitrogen supply system was required to be seismically qualified per

the NRC letter from John F. Stolz, Director. PWR Project Directorate

Number 6. to Hal B. Tucker, Vice President - Nuclear Operations, dated

January 14. 1987. subject. "Seismic Qualification of the Emergency

Feedwater System."

This letter stated that the licensee has committed

to assure that the automatic bottled nitrogen system, including power to

the solenoid valves, will withstand an MHE.

The MHE is defined as

Maximum Hypothetical Earthquake or Safe Shutdown Earthquake (SSE).

The inspectors walked down non-safety-related nitrogen lines from the.

nitrogen supply bottles to valves FDW 315 and 316 for all three units

with the licensee's engineers and instrument operators.

These lines are

required for safe shutdown. The inspectors identified minor

discrepancies which were provided to the licensee for resolution.

The licensee issued PIP 0-098-4187. Revisions 0 and 1 to record the

deficiencies found by the inspectors and to evaluate the root cause and

their resolution. The PIP stated that the deficiencies found in the

nitrogen supply systems degraded the systems and did not meet the

standards for seismic mounting.

The nitrogen supply lines were not

safety-related and remained operable. The inspectors agreed with the

licensee's operability evaluation for the systems.

In.1996 the SQUG program personnel did perform the walkdowns for valves

FDW 315 and 316 and nitrogen bottles and no equipment deficiencies were

identified.

These walkdowns did not include the nitrogen supply lines

where the inspectors identified the deficiencies.

c. Conclusions

The deficiencies found in the seismic mounting of the nitrogen supply

lines for all three units degraded the EFW systems and indicated a

weakness in maintaining the nitrogen supply line supports.

IV.

Plant Support Areas

R1

Radiological Protection and Chemistry Controls

R1.1 Tour of Radiological Protected Areas

a. Inspection Scooe (86750)

The inspectors reviewed implementation of selected elements of the

46

licensee's radiation protection program as required by 10 CFR Parts

20.1902, and 1904. The review included observation of radiological

protection activities for control of radioactive material, including

postings and labeling, and radioactive waste processing.

b. Observations and Findings

The inspectors reviewed survey data of radioactive material storage

areas. Observations and independent radiation and contamination survey

results determined the licensee was effectively controlling and storing

radioactive material and all material observed was appropriately labeled

as required by 10 CFR Part 20.1904. All areas observed were

appropriately posted to specify the radiological conditions.

The inspectors determined the licensee was processing radioactive waste

to maintain exposures As Low As Reasonably Achievable (ALARA)

and to

minimize quantities of radioactive waste stored on site.

During the

inspection, the inspectors observed a liquid radioactive waste discharge

of 28.000 gallons and determined licensee personnel were following the

discharge procedure CP/O/B/5200/48. "Resin Recovery System Operation",

Revision 58. The inspectors also determined licensee personnel involved

with the discharge were knowledgeable about release criteria, alarm

limits, and discharge pathways. The licensee was trending liquid

radioactive waste to meet licensee established goals.

As of August 26,

1998. the licensee had released approximately 0.236 curies which was

below the year to date goal of 0.380 curies.

Work.practices observed

during radioactive waste processing were good.

c. Conclusions

The inspectors determined the licensee was effectively maintaining

controls for radioactive material storage and radioactive waste

processing. Work practices observed during radioactive waste processing

were good.

R1.2 Water Chemistry Controls

a. Inspection Scooe (84750)

The inspectors reviewed implementation of selected elements of the

licensee's water chemistry control program for monitoring primary and

secondary water quality as described in the TS limits, the Station

Chemistry Manual,

and the UFSAR.

The review included examination of

program guidance and implementing procedures and analytical results for

selected chemistry parameters, and observation of chemistry technicians

collecting water samples.

b. Observations and Findings

The inspectors toured the primary and secondary chemistry laboratories

and observed work in progress.

The inspectors observed a survey of the

primary laboratory and observed personnel frisking with laboratory coats

47

worn.

Personnel observed were using good radiological work practices.

The inspectors reviewed selected analytical results recorded for Unit 1

reactor coolant taken-between the period April 15. 1998, and August 26.

1998. and secondary samples taken between the periods May 25. 1998. and

August 3. 1998.

The selected parameters reviewed for primary chemistry

included dissolved oxygen, chloride, pH. and fluoride.

The selected

parameters reviewed for secondary chemistry included hydrazine, iron,

copper, sodium. dissolved oxygen, and chloride.

Those primary

parameters reviewed were maintained within the relevant TS limits for

power operations.

Those secondary parameters reviewed were maintained

within the limits of the Station Chemistry Manual.

The inspectors observed a boron sample collection from Unit 1 primary

system during startup. The inspectors verified that the sample

collection was performed as required by licensee chemistry sampling

procedure CP/1/A/2002/001. "Unit 1 Primary Sampling System". Revision

34.

The sample was analyzed as required by licensee procedure LM-0

P003A. "Determination of Boron Using the Mettler DL40GP". Revision 4.

Chemistry personnel performing the sampling and analysis followed the

procedures and appeared well trained to perform the task.

The inspectors observed a test of the Unit 2 post-accident liquid

sampling system (PALS).

The individuals observed followed the

established procedure CP/2/A/2002/004D.

- Test Procedure for the Post

Accident Liquid Sampling System". Revision 23.

However, the PALS test

was secured due to system leakage.

The system was removed from service

for maintenance.

c. Conclusions

The inspectors concluded that the licensee's water chemistry control

program for monitoring primary and secondary water quality had been

effectively implemented in accordance with the TS requirements and the

Station Chemistry Manual for water chemistry.

The inspectors also

concluded that the collection of the samples was performed in eccordance

with the licensee's chemistry sampling procedure.

R2

Status of RP&C Facilities and Equipment

R2.1 Process and Effluent Radiation Monitors

a. Insoection Scooe (84750)

The inspectors reviewed selected licensee procedures and records.for

required surveillance on process and effluent radiation monitors and for

radiation monitor. availability as required by TS, and Chapter 16 of the

UFSAR.

48

Observations and Findings

During tours of the auxiliary building, turbine building, and radwaste

building, the inspectors-observed the physical operation of process

radiation effluent monitors in service.

The inspectors also toured the

control rooms and observed the status of radiation.monitoring equipment.

The inspectors reviewed radiation and process monitor surveillance

procedures and records for performance of channel checks. source checks,

channel calibratiohs. and channel operational tests. for four monitors.

The inspectors also observed control room personnel perform.alarm set

points for four monitors as required by licensee procedure

PT/O/A/0230/001, "Radiation Monitor Check". Revision 112.

The

inspectors determined the licensee was performing checks described in

the TSs and Chapter 16 of the UFSAR.and in accordance with license

procedures.

The inspectors reviewed the licensee's 1997 Annual Environmental Report

issued in May 1998. No equipment or sampling deviations for liquid

samplers, environmental air samplers, or environmental thermoluminescent

dosimetry (TLD) were identified during 1997.

The licensee had moved one

control location air sampler due to the construction of a school.

The inspectors also performed independent environmental surface

contamination surveys of selected areas near the licensee's visitors

center and confirmed survey results to be background as consistent with

licensee survey results reviewed.

c. Conclusions

The inspectors concluded radiation and process effluent and

environmental monitors were being maintained in an operational condition

to comply with TS requirements and UFSAR commitments.

R2.2 Meteorological Monitoring Eauipment

a..

Inspection Scope (84750)

The inspectors reviewed licensee procedures to verify licensee

compliance with the UFSAR which described the operational and

surveillance requirements for the meteorological monitoring

instrumentation.

b. Observations and Findings

The inspectors toured the control room and determi-ned the meteorological

instrumentation was operable and that data for wind speed, wind

direction, air temperature, and precipitation were being collected as

described in the UFSAR.

Based on review of records, the licensee was

tracking operability for meteorology equipment during 1998.

Based on

licensee operation records reviewed for wind speed, wind direction, and

precipitation, the inspectors determined the licensee was adequately

maintaining meteorological monitoring equipment and that the

49

meteorological monitoring program had been adequately implemented.

c. Conclusions

Based on the above reviews and observations, it was concluded that the

meteorological instrumentation had been adequately maintained and that

the meteorological monitoring program had been adequately implemented.

P2

Status of EP Facilities, Equipment and Resources

P2.1 Resident Insoector Tour of the Public Document Room (PDR) (71750)

The inspectors toured the PDR located at the Oconee County Public

Library. 501 W. South Broad Street, Walhalla. S.C., 29691. Required

equipment and files were in good working order.

The inspectors verified

the condition of the equipment and files (on microfiche) by viewing and

printing pages from inspection reports and correspondence.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management on August 20 and September 4, 1998, and at the conclusion of

the inspection on September 10. 1998.

The licensee acknowledged the

findings.presented. No proprietary information was identified to the

inspectors.

Partial-List of Persons Contacted

Licensee

L. Azzerello. Mechanical Systems/Equipment Engineering Manager

E. Burchfield, Regulatory Compliance Manager

T. Coutu, Nuclear Support Section Manager

T. Curtis. Superintendent of Operations

G. Davenport, Operations Support Manager

B. Dobson, Engineering Work Control Manager

J. Forbes, Station Manager

W. Foster, Safety Assurance Manager

T. Hartis, Strategic Business Consultant

D. Hubbard, Engineering Modifications Manager

C. Little, Electrical System/Equipment Engineering Manager

W. McCollum, Site Vice.President. Oconee Nuclear Station

B. Medlin, Superintendent of Maintenance

M. Nazar, Manager of Engineering

J. Smith. Regulatory Compliance

J. Twiggs. Radiation Protection Manager

Other licensee employees contacted during the inspection included engineers,

operators, technicians, maintenance personnel, and administrative personnel.

50

NRC

D. LaBarge, Project Manager

Inspection Procedures Used

IP37550

Engineering

IP37551

Onsite Engineering

IP40500

Effectiveness of Licensee Controls In Identifying and Preventing

Problems

IP61726

Surveillance Observationis

IP62707

Maintenance Observations

IP71707

Plant Operations.

IP71750

Plant Support Activities

IP73753

Inservice Inspection

IP84750

Radioactive Waste Treatment, and Effluent and Environmental

Monitoring

IP86750

Solid radioactive Waste Management and Transportation of

Radioactive Materials

IP90712

In-Office Review of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP92700

Onsite Followup of Written Event Reports

IP92901

Followup - Plant Operations

IP92902

Followup - Maintenance

IP92903

Followup - Engineering

Items Opened, Closed, and Discussed

Oened

50-269.270,287/98-08-01

URI

Configuration Control of the Station

ASW Pump (Section M1.2)

50-269.270.287/98-08-02

VIO

Inadequate 50.59 Safety Evaluation

for 1996 UFSAR Revision Related to

ECCS Pumps" NPSH Analysis (Section

E1.4)

50-269.270.287/98-08-03

NCV

Failure to Monitor the Performance

of Manual Caustic Injection Valves

(Secti-on E8.1)

50-269,270.287/98-08-04

NCV

Improper Design Basis Assumptions

for HPI Valves (Section E8.5)

50-269.270,287/98-08-05

IFI

EFW Potential Design Basis Issues

(Section E8.1)

Closed

50-269.270,287/95-03-01

IFI

Clarification of TS 3.3.1 (Section

W

08.1)

50-269/90-15

LER

Unit Operation In an Unanalyzed

Condition Due to Design Deficiency.

Design Oversight (Section 08.1)

50-269.270,287/97-05-02

VIO

Failure to Maintain Configuration

Control (Section 08.2)

50-269.287/97-15-01

VIO

Failure to Complete Required TS

-

Surveillance on .LPI Flow Instruments

.

(Section 08.3)

50-269/97-09-00

LER

LPI Flow Instrument TS Surveillance

Interval Exceeded Due to Deficient

Work Practices (Section 08.3)

EA 96-478-01014

VIO

Failure to Properly Install MSSV

Spindle Nut Cotter Pins (Section

08.4)

50-269/97-08-00

LER

Manual Reactor Trip Due to .Equipment

Failure While Shutdown (Section

08.5)

50-270/97-02-00

LER

Grid Disturbance Results in Reactor

Trip Due to Manufacturing Deficiency

(Section 08.6)

EA 97-298-04014

VIO

Failure to Follow Operations

Procedures Relating to Low

Temperature Overpressure Protection

Requirements (Section 08.7)

EA 97-298-03014

VIO

Failure to Follow Operations

Procedure During the Unit 3 Cooldown

on May 3. 1997 (Section 08.7)

EA 97-298-05014

VIO

Failure to Follow Maintenance

Procedures for the Installation of

Tubing (Section 08.7)

50-287/97-03-00

LER

HPI System Inoperable Due to Design

Deficiency and Improper Work

Practices (Section 08.7)

50-269/97-11-00

LER

Steam Generator Leak Results in TS

Unit Shutdown Due to Inadequate

Process. Control (Section M8.1)

50-270/98-01-00

LER

Operation with Steam Generator Tube

Indications in Excess of Limits Due

to Manufacturing Error (Section

M8.2)

52

50-287/97-02-00

LER

Reactor Building Cooling Units

Technically Inoperable (Section.

M8.3)

50-287/97-02-01

LER

Reactor Building Cooling Units

Technically Inoperable Due to a

Manufacturing Deficiency (Section

M8.3)

50-269.270/97-01-01

IFI

Reactor Trip Confirm Circuit Fuse

(Section E8.4)

50-269/98-02-09

URI

Failure of Valve 1HP-27 to Close

(Section E8.5)

.50-269/98-05-01

LER

Valve Fails to Close Requiring Unit

Shutdown Due to Inadequate Procedure

(Section E8.5)

50-269/98-05-00

LER

Valve Fails to Close Requiring Unit

Shutdown (SectiorrE8.5)

Discussed

50-269.270.287/98-03-09

URI

Licensing Basis Issues With Single

Failure and QA for Non-Safety

Equipment Required to Mitigate an

Accident (Section E8.1)

50-269.270.287/98-03-07

VIO

Incorrect and Nonconservative

Assumptions in Control Room Operator

Dose Calculations (Section E8.2)

50-269.270.287/98-03-02

VIO

Failure to Perform PRVS Surveillance

in Accordance With TS (Section E8.3)

50-269/98-01

LER

Available NPSH for RBS Pumps Outside

Design Basis Due to Incorrect

Interpretation (Section E1.4)

50-269/97-02

LER

Reactor Building Cooling Units

Technically Inoperable Due to Design

Deficiency (Section 01.4)

50-269/97-02-01

LER

Reactor Building Cooling Units

Technically Inoperable Due to Design

Deficiency (Section 01.5)

50-270/98-06-00

LER

ESV (2 Trains) Inoperable (Section

01.5)

53

50-269/98-11-00

LER

Available NPSH for RBS Pumps Outside

Design Basis Due to Incorrect

Interpretation (Section E1.4)

List of Acronyms

AFC

Auxiliary Fan Coolers

ALARA

As Low As Reasonably Achievable

ASME

American Society of Mechanical Engineers

ASW

Auxiliary Service Water

ATWS

Anticipated TransientWithout Scram

BWST

Borated Water Storage Tank

CFM

Cubic Feet Per Minute

CFR

Code of Federal Regulations

CRVS

Control Room Ventilation System

DEA

Decontamination Emergency Area

DSCS

Double Seal Delta Channel Seal

ECCS

Emergency Core Cooling Systems

EFW

Emergency Feedwater.

EOC

End-of-Cycle

EOP

Emergency Operating Procedure

EQ

Environmental Qualification

ES

Engineered Safeguards

ESF

Engineered Safety Feature

ESV

Essential Siphon Vacuum

F

Fahrenheit

FIP

Failure Identification Process

GL

Generic Letter

GPM

Gallons Per Minute

HPI

High Pressure Injection

I&E

Instrument & Electrical

IFI

Inspector Followup Item

INOT

Independent Nuclear Oversight Team

IP

Inspection Procedure

IR

Inspection Report

ISI

Inservice Inspection

IST

In-Service Testing

LER

Licensee Event Report

LCO

Limiting Condition for Operation

LOCA

Loss of Coolant Accident

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

LSE

Less Significant Event

MOV

Motor Operated Valve

MSE

More Significant Event

MSSV

Main Steam Safety Valve

NCV

Non-Cited Violation

NPSH

Net Positive Suction Head

NRC

Nuclear Regulatory Commission

NSD

Nuclear System Directive

NSM

Nuclear Station Modification

OTSG

Once Through Steam Generator

54

OSRDC

Oconee Safety-Related Designation Clarification Program

PALS

Post Accident Liquid Sampling System

PDR

Public Document Room

PIP

Problem Investigation Process

PM

Preventive Maintenance

ppb

Parts per Billion

PRA

Probablistic Risk Assessment

PRVS

Penetration Room Ventilation System

psig

Pounds Per Square Inch Gauge

PT

Performance Test

QA

Quality Assurance

RB

Reactor Building

RBCU

Reactor Building Cooling Unit

RBS

Reactor Building Spray

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RG

Regulatory Guide

SALP

Systematic Assessment of Licensee Performance

SD

Shutdown

SLC

Selected Licensee Commitments

SRG

Safety Review Group

SQUG

Seismic Qualification Utility Group

SSCs

Systems. Structures. and Components

SSEA

Safety System Engineering Audit

SSF

Standby Shutdown Facility

SSFI

Safety System Functional Inspection

TAC

Technical Assignment Control

TLD

Thermoluminescent Dosimetry

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

-

URI

Unresolved Item

USQ

Unreviewed Safety Question

UST

Upper Storage Tank

UT

Ultrasonic Examination.

VIO

Violation

w.g.

Water Gauge

WO

Work Order