ML14191B028

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Insp Rept 50-261/88-28 on 880911-1010.Violations Noted.Major Areas Inspected:Followup on Previous Insp Items,Operational Safety Verification,Physical Protection,Maint Observation & Solid Radwaste & Transportation
ML14191B028
Person / Time
Site: Robinson 
Issue date: 11/09/1988
From: Garner L, Latta R, Starkey R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191B024 List:
References
50-261-88-28, NUDOCS 8811280096
Download: ML14191B028 (17)


See also: IR 05000261/1988028

Text

. '

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION il

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/88-28

Licensee:

Carolina- Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: September 11 -

October 10, 1988

Inspectors:

L. W. Garner, Senior

dent Inspector

DaTe Signed

R. M. Lata, Res1 en

spector

Date Signed

R. D. Starkey, R actor Inspector

Uste Signed

C. .

ass~e

,Radiation

Spefialis t

att bigned

Approved by:

P. E Fredrickson, Chief, Section 1A

Date'SigneT

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of

followup on previous inspection items, operational safety verifica

tion, physical protection, surveillance observation, maintenance

observation, onsite followup of events at operating power reactors,

onsite review committee, solid radioactive waste, and transportation.

Results:

Three violations were identified:

Failure to Have a Program To Use

Calibrated Stop Watches For Required TS and ASME Section XI Testing,

Paragraph 6; Failure to Correct Sump Pump Controls Which Resulted in

Radioactive Releases to the Storm Drain System, Paragraph 10; and

Failure to Indicate Proper Physical Form of Material on Shipping

Papers, Paragraph 11.

8811280096 881110

0

ADOCK 05000261

PNU

REPORT DETAILS

1. Licensee Employees Contacted

R. Barnett, Maintenance Supervisor, Electrical

  1. D. Baur, Supervisor, Quality Assurance
  • J. Benjamin, Unit Head, Systems Engineering

C. Bethea, Manager Training

H. Bryon, Instructor

R. Chambers, Engineering Supervisor, Performance

  • S. Clark, Project Engineer, Design Engineering

D. Crocker, Supervisor, Radiation Control

  1. J. Curley, Director, Regulatory Compliance
  • C. Dietz, Manager, Robinson Nuclear Project Department

J. Eaddy, Supervisor, Environmental and Chemistry

R. Femal, Shift Foreman, Operations

W. Flanagan, Manager, Design Engineering

W. Gainey, Support Supervisor, Operations

  1. S. Griggs, Aide, Regulatory Compliance

P. Harding, Project Specialist, Radiation Control

  1. E. Harris, Director, Onsite Nuclear Safety
  • M. Heath, Project Engineer, Technical Support

R. Johnson, Manager, Control and Administration

D. Knight, Shift Foreman, Operations

E. Lee, Shift Foreman, Operations

D. McCaskill, Shift Foreman, Operations

R. Miller, Maintenance Supervisor, Mechanical

R. Moore, Shift Foreman, Operations

  • R. Morgan, Plant General Manager

D. Myers, Shift Foreman, Operations

D. Nelson, Operating Supervisor, Operations

  • M. Page, Engineering Supervisor,.Plant Systems
  • D. Quick, Manager, Maintenance
  • D. Sayre, Acting Director, Regulatory Compliance

D. Seagle, Shift Foreman, Operations

J. Sheppard, Manager, Operations

R. Steele, Shift Foreman, Operations

  • H. Young, Director, Quality Assurance/Quality Control

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

NRC Resident Inspectors

    • L. Garner
  • R. Latta
  • Attended exit interview on October 19, 1988.
  1. Attended exit interview on October 26, 1988.

2

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Licensee Action on Previous .Enforcement Matters (92702)

This area was not inspected.

3. Licensee Action on Previously Identified Inspection Items (92701)

(Closed) IFI 261/08-01, Implementation of the LER Writer's Guide.

During

a previous inspection, the licensee committed that a LER Writer's Guide,

with particular attention paid to corrective actions to prevent recur

rence, would be completed and implemented.

That Writer's Guide entitled

LER Handbook, was completed and implemented on June 15, 1988.

This item

is considered closed.

(Closed)

IFI 261/88-08-03, Track Commitments Made to the NRC in LERs

Through the RAIL Commitment Tracking System.

Examples were identified of

corrective action commitments made in LERs to the NRC, but which were not

tracked in the licensee's RAIL commitment tracking system. A review of

all LERs issued since that time indicated that all corrective action

commitments to the NRC as described in LERs have been entered into the

RAIL commitment tracking system. This item is considered closed.

No violations or deviations were identified within the areas inspected.

4. Operational Safety Verification (71707)

The inspectors observed licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements,

and that the licensee management control system was effectively dis

charging its responsibilities for continued safe operation.

These

activities were confirmed by direct observations, tours of the facility,

interviews and discussions with licensee management

and personnel,

independent verifications of safety system status and limiting conditions

for operation, and reviews of facility records.

Periodically, the inspectors reviewed shift logs, operations records, data

sheets, instrument traces, and records of equipment malfunctions to verify

operability of safety related equipment and compliance with TS.

Specific

items reviewed include control room logs, maintenance work requests,

auxiliary logs, operating orders, standing orders, and equipment tagout

records. Through periodic observations of work in progress and discus

sions with operations staff members,

the inspectors verified that the

staff was knowledgeable of plant conditions; responding properly to alarm

conditions; adhering to procedures and applicable administrative controls;

and aware of equipment out of service, surveillance testing, and mainte

nance activities in progress.

The inspectors routinely observed shift

3

changes to verify that continuity of system status was maintained and that

proper control room-staffing existed.

The inspectors also observed that

access to the control room was controlled and operations personnel were

carrying out their assigned duties in an attentive and professional

manner. The control room was observed to be free of unnecessary distrac

tions. The inspectors performed channel checks, reviewed component status

and safety related parameters,

including SPDS information, to verify

conformance with the TS.

During .this reporting interval, the inspectors verified compliance with

selected LCOs.

This verification was accomplished by direct observation

of monitoring instrumentation, valve positions, switch positions, and

review of completed logs and records.

The inspectors verified the axial

flux difference was within the values required by the TS.

Plant tours were routinely conducted to verify the operability of standby

equipment; assess the general condition of plant equipment; and verify

that radiological controls, fire protection controls and equipment tag out

procedures were being properly implemented.

These tours verified the

absence of unusual fluid leaks; the lack of visual degradation of pipe,

conduit and seismic supports; the proper positions and indications of

important valves and circuit breakers; the lack of conditions which could

invalidate EQ; the operability of safety related instrumentation; the.

calibration of safety related and control instrumentation including area

radiation monitors, friskers and portal monitors; the operability of fire

suppression and fire fighting equipment; and the operability of emergency

lighting equipment. The inspectors also verified that housekeeping was

adequate and areas were free of unnecessary fire hazards and combustible

materials.

a. CV Temperature Distribution (TI 2515/98)

The inspectors reviewed the results of SP-797, Special Procedure For

Monitoring CV Temperature.

This procedure measured temperatures

at different elevations adjacent to EQ equipment installed inside

containment. Temperatures were taken on all three major operating.

levels (e.g., first level, second level, and operating deck, as well

as in the seal table room,

PZR cubicle and CV sump entrance).

The

temperatures taken were compared to the average CV temperature as

indicated on the RTGB.

Data was taken weekly from March 10 to

August 31,

1988,

while the reactor was operating.

Preliminary

engineering review has revealed that the PZR cubicle routinely

operates above the 120 degrees F maximum operating temperature

assumed in the EQ program.

EQ components in the PZR cubicle are

ASCO solenoid valves, NAMCO limit switches, conduit seals and valve

position indication accelerometers.

These components are all

associated with the PZR PORV equipment.

An analysis was performed

which demonstrated that these components had not exceeded their

4

lifetime rating at the higher temperatures. The licensee is in the

process of factoring this higher PZR cubicle temperature into their

EQ program. Analysis of approximately four months'of data, March 3

through June 29, 1988, showed the following:

AREA

>120F

.<110F

FIRST LEVEL

1 WK

10 WKS

SECOND LEVEL

4 WKS

11 WKS

OPS DECK

4 WKS

10 WKS

SEAL TABLE

1 WK

11 WKS

SUMP ENTRANCE

3 WKS

10 WKS

CV AVERAGE

5 WKS

6 WKS

It is indeterminate at this time if the above data is representative

of the percent of time temperatures may be in excess of 120 degrees

F.

For example, reactor power was limited to 60% of full power from

February to June 20,

1988.

In addition, some data was taken during

or immediately following CV purges. A review of average CV tempera

ture during the hottest months, after June 30 to September 30, 1987,

indicated that the average temperature had exceeded 120 degrees F for

every week except one week which was associated with a shutdown. The

need to provide a more representative data base than presented by

SP-797 in order to establish EQ equipment lifetimes inside contain

ment was discussed with plant management.

This is an IFI:

Estab

lishment of EQ Lifetimes Inside CV Based Upon Actual Temperature

Conditions (261/88-28-01).

No violations or deviations were identified within the areas inspected.

5. Physical Protection (71707)

In the course of the monthly activities, the inspectors included a review

of the licensee's physical security program. The inspectors verified by

general observation, perimeter walkdowns and interviews that measures

taken to assure the physical protection of the facility met current

requirements.

The performance of various shifts of the security force was observed

to verify that daily activities were conducted in accordance with the

requirements of the security plan.

Activities inspected included

protected and vital areas,

access controls, searching of personnel,

packages and vehicles, badge issuance and retrieval, patrols, escorting

of visitors, and compensatory measures.

In addition, the inspectors

routinely observed protected and vital area lighting and barrier

integrity.

5

No violations or deviations were identified within the areas inspected.

6. Monthly Surveillance Observation (61726)

The inspectors observed certain surveillance related activities of safety

related systems and components to ascertain that these activities were

conducted in accordance with license requirements.

For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were met, the tests were completed at the required frequency, the

tests conformed to TS requirements, the required administrative approvals

and tagouts were obtained prior to initiating the tests, the testing was

accomplished by qualified personnel in accordance with an approved test

procedure, and the required test instrumentation was properly calibrated.

Upon completion of the testing, the inspectors observed that the recorded

test data was accurate, complete, met TS requirements, and test discrep

ancies were properly rectified.

The inspectors independently verified

that the systems were properly returned to service.

Specifically, the

inspectors witnessed/reviewed portions of the following test activities:

a.

OST-202 (revision

13),

Steam Driven Auxiliary Feedwater System

Component Test.

During the performance of this surveillance, the

acceptance criteria for pump horizontal vibration was exceeded,

causing the pump to be declared inoperable and a 7 day LCO to be

entered. A work request was written and an engineering evaluation

was initiated to determine the cause of the vibration.

The inspector observed that during the stroke timing of SDAFW Pump

Temperature Control Valve SW-TCV-1902A that the operators conducting

the surveillance used an uhcalibrated watch to stroke time the valve.

Upon further inquiry the inspector discovered that the licensee does

not use, nor have available for use, calibrated stop watches for the

purpose of timing equipment which has safety significance.

Failure

to assure that measuring and testing devices affecting quality,

specifically stop watches, are properly controlled and calibrated

is identified as a violation:

Failure To Have A Program To Use

Calibrated Stop Watches For Required TS and ASME Section Testing

(261/88-28-02).

b.

PLP-006 (revision 6), Containment Vessel Inspection/Closeout. The

inspectors observed completion of PLP-006 attachment 6.3, Auxiliary

Operator Weekly Checks, on September 21, 1988. This procedure had

been modified to incorporate performance measurements of HVH 4 as

described in paragraph 8.b.

One violation was identified within the areas inspected.

7. Monthly Maintenance Observation (62703)

The inspectors observed several maintenance related activities of safety

related systems and components to ascertain that these activities were

6

conducted in accordance with approved procedures,

TS and appropriate

industry codes and standards.

The- inspectors determined that these

activities were -not violating LCOs and that redundant components were

operable.

The inspectors also determined that activities were accom

plished by qualified personnel using approved procedures, QC hold points

were established where required, required administrative approvals and

tagouts were obtained prior to work initiation, proper radiological

controls were adhered to, appropriate ignition and fire prevention

controls were implemented,

replacement parts and materials used were

properly certified and the effected equipment was properly tested before

being returned to service.

In particular, the inspectors observed/

reviewed the following maintenance activities:

WR/JO 88-AEUJI Inspection and Cleaning of HVH 1-4 Units

'0

WR/JO 88-AIQW1 Repair CV Purge Exhaust Valve V12-9

o

WR/JO 88-AJYG1 Repair CV Purge Exhaust Valve V12-8

WR/JO 88-BEF535 Inspection of HVH 1-4 and Motor Coolers per CM-201

No violations or deviations were identified within the areas inspected.

8. Onsite Followup of Events at Operating Power Reactors (93702)

a. Rx Head Vent Valves Not in EQ Program

On September 14, 1988, with Unit 2 in cold shutdown, the inspectors

were advised of a reportable event involving the licensee's determi

nation that the reactor head vent valves were not environmentally

qualified. Subsequent to this determination the subject valves and

their associated containment penetration splices were repaired, EQ

packages were developed, and the system was returned to service on

September 16, 1988.

The determination that the reactor head vent system, which utilized

Target Rock solenoid operated valves, were not qualified was made

following a notification to the site on September 9, 1988, that

similar valves utilized at the Shearon Harris site were found to

have degraded reed switch wires and unidentified terminal blocks

installed. An evaluation of the reactor head vent valves at Robinson

indicated that although the RCS and reactor vessel head vent system

had been installed in 1984 as a seismically qualified and EQ system,

they had been omitted from the licensee's EQ file inventory.

The

failure to have vent valves in the EQ Program is an UNR:

Failure to

Have Rx Head Vents Environmentally Qualified (261/88-28-03).

The inspectors witnessed portions of the valve disassembly and repair

efforts conducted in accordance with WR/JO 88-AJRY1 and determined

that the manufacturer had provided reed switches and terminal blocks

.7

of a different configuration than had been originally qualified and

certified by Target Rock. These components along with the internal

jumper wiring were replaced with qualified materials. Additionally,

Patel conduit seals not specified in the original installation were

installed and the penetration splices originally configured as butt

splices with Ray-Chem sleeves were replaced with qualified penetra

tion splices.

b. Containment Fan Cooler Biological Fouling

As described in Inspection Report 261/88-23, the licensee took the

unit to cold shutdown because of reduced heat removal capability of

containment fan coolers HVH 3 and 4.

The licensee's inspection of

HVH Units 1, 2, 3 and 4 and subsequent determination of fouling and

pitting due to biological growth are the subject of Inspection Report

261/88-27. This writeup provides an update on inspection activities

associated with restart on September 19, 1988.

The licensee performed cleaning of HVH 1, 2, 3 and 4 to remove

the fouling.

In addition, an inspection was conducted of other

potentially susceptible safety related heat exchanges.

No other

degraded conditions were found.

The inspectors examined the tube

bundles of selected heat exchangers, including at least one of each

pair of ESF pump room coolers (e.g. , SI pump room,

RHR pump room and

MDAFW pump room coolers), as well as the containment fan coolers. No

adverse conditions which would render the subject coolers inoperable

were observed.

As described in Inspection Report 261/88-27, a hydrostatic test was

performed on the containment coolers and associated service water

piping. This hydrostatic test provides confidence that the pitting

observed in the HVH units had not progressed to through-wall leaks.

The licensee is in the process of contracting with Westinghouse to

perform eddy current testing of 12% of the tubes in HVH 4. during the

refueling outage which is scheduled to begin November 12, 1988.

In

addition, the licensee, is planning to visually inspect the contain

ment fan coolers for indication of resumption of biological growth

during the refueling outage.

These items are considered an IFI:

Review Visual and Eddy Current Testing of HVH 1-4 During November

1988 Refueling Outage (261/88-28-04).

Between resumption of power operation on September 19,

and the

refueling outage, the licensee has initiated temporary monitoring

of the performance of HVH 4 by trending differential service water

pressure across the unit, service water discharge pressure from the

unit and inlet and outlet air temperatures.

The inspectors observed

the taking of baseline data and has reviewed subsequent data.

To

date, adverse trends have been observed. However, the inspectors are

.8

concerned that these methods will not provide early detection of

biological fouling prior to significant fouling occurring. This has

been expressed to the licensee. The licensee had already been in the

process of evaluating options to provide some means of detecting

the onset of biological fouling in the coolers.

This is an IFI:

Licensee to Develop Methodology to Detect Biological Growth in HVH

1-4 (261/88-28-05).

c. Shutdown and Unusual Event Due To Loss of Containment Integrity

On September 22,

1988, the licensee determined that a leakage path

existed from containment via the 42" diameter series purge exhaust

valves V12-8 and V12-9.

Because- the leak path could not be isolated

within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the initial discovery, an unusual event was

declared in accordance with the licensee's emergency plan.

In

accordance with TS 3.0 the reactor was placed in hot shutdown for.

repairs of the subject valves. The sequence of events and subsequent

repair activities are described below.

On September 19,

1988, at 4:50 a.m.,

the Unit was taken critical

after the HVH 1-4 outage described in paragraph 8.b above.

During

this forced outage, the CV purge exhaust inboard and outboard valves,

V12-8 and V12-9 respectively, had been opened for CV cooling and

routing of power cables to support CV work.

Prior to startup the

valves had been closed to establish containment integrity.

However,

on the afternoon of September 19,

these valves were reopened, as

allowed by TS 3.6.4.1, to support a routine CV entry on September 21.

Due to the relatively long period of time required to pressurize this

large penetration, PPS, which is used to maintain a pressure greater

than accident pressure on select penetrations during operation, was

not placed in service for this penetration during this time. It was

only after the CV entry on September 21 was completed that the CV

purge exhaust penetration was pressurized.

After approximately

eight hours, the time allowed by procedure to fully pressurize the

penetration,

the RTGB instrumentation indicated a high PPS header

flow rate. With the reactor at 89% power, at 3:20 a.m., the licensee,

observed that V12-8 was leaking. A CV entry subsequently determined

that V12-9 was also leaking.

Attempts to stop the leakage were

unsuccessful.

Consequently, at 7:21 a.m.,

an unusual event was

declared in accordance with PEP-101, item 6, which requires declara

tion of an unusual event if

one or more automatic CV isolation

valve(s)

is (are)

inoperable for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and not isolated or

repaired.

Because repair of the valves required the valves to be

fully opened,

the licensee elected to work one valve at a time,

thereby minimizing the leak path out of containment as much as

possible while the reactor was above 200 degrees F. At 9:08 a.m., a

post repair test on V12-9 proved unsuccessful.

Consequently, at

9:52 a.m., the licensee began reducing load to remove the unit from

9

service in accordance with TS 3.0.

At 11:54 a.m., the Unit was in

hot shutdown.

The V12-8 butterfly type valve was subsequently

repaired by replacing the seal and was successfully tested at 9:45

p.m. The conditions to exit the unusual event were met at that time

and the unusual event was terminated. By 1:50 p.m., on September 23,

the V12-9 valve was repaired, tested and returned to service.

The

reactor was taken critical at 4:10 a.m., on September 24.

Preliminary investigation by the licensee indicated that hard foreign

material had been embedded in the soft sealing surfaces of each

valve. In addition, the leakage by V12-9 may have been compounded by

a partial separation of the sealing material from its backing ring.

The licensee plans to document their final determinations, root

causes, and corrective actions in LER 88-022. The NRC review of this

LER and the circumstances surrounding the failure to ensure that

these valves would tightly close after being used as a service route

for cables is considered an UNR:

Review LER 88-022 and CV Oper

ability Requirements After Opening of CV Purge Exhaust Valves

(261/88-28-06).

d. Motor Driven Feedpump A Trip

On September 27,

1988, .while at -88% power, the A motor driven.

feedwater pump tripped on low oil pressure.

Reactor power was

stabilized at 47% power in accordance with abnormal operating

procedures by manually reducing turbine load and placing control rods

in automatic control.

Fourteen minutes prior to the trip, the

auxiliary oil pump had begun to cycle on and off every 2-3 seconds.

Subsequent investigation indicated that the oil system relief valve

was partially open due to trash under its seat and an oil pressure

switch was malfunctioning.

The repairs were completed and power

ascension commenced at 4:45 a.m., on September 29, 1988.

e. Dedicated Shutdown RCS Th and Tc Instruments Routed Through Fire Area

Review of plant modification M-896 revealed that RCS Th and Tc

circuits, TE-410 and TE-413 loops respectively, had been routed

through Appendix R Fire Area A. These instruments are used per

DSP-002,

Hot Shutdown Using The Dedicated/Alternate Shutdown System,

to stabilize the plant in hot shutdown via natural circulation if a

fire occurs in Fire Area A. Per modification M-445, these circuits

had been routed outside of the fire area.

However, modification

M-896, which isolated these instrument loops from class IE equipment

per R.G. 1.97, resulted in the circuits being rerouted back into Fire

Area A.

On October 5, 1988,

the licensee issued engineering evaluation 88-128, JCO 88-008, to address this issue.

In summary, the licensee

concluded that the likelihood of cable damage sufficient to disable

10

these ,instrument loops is extremely low because of the low combus

tible loading and the automatic capability to rapidly detect and

suppress fires which may occur in the area.

Furthermore, if these

loops are disabled by a fire, an indirect means of obtaining RCS

temperature is available from a S/G Pressure - RCS Temperature graph.

The inspectors verified that the applicable DSPs contain this

graph, that operating personnel are aware of how to utilize it (if

necessary), and that the appropriate S/G pressure instruments are in

service and are operable.

The licensee is planning to implement a design change to comply with

both Appendix R and R.G.

1.97 commitments.

Implementation of a

modification to correct the TE-410 and TE-413 problem created by

plant M-896 is an IFI:

Inspect PM to Establish Isolation as Required

by Appendix R for TE-410 and TE-413 (261/88-28-07).

f. CV Equipment Not EQ Because of Submergence

On October 6, 1988, the licensee discovered that the calculated CV

fluid level of 3.2 ft was non-conservative.

A new value of 6 feet 1

inch has be calculated.

On October 7, 1988, the licensee issued

engineering evaluation 88-132,

JCO 88-009, to address the equipment

which would be affected by the increased submergence level.

The

evaluation concluded that the effected equipment would either remain

operable, have had achieved its function or has backup capability.

Equipment which will not perform its functions are instruments

associated with penetration F01; one channel of the exit thermo

couples, RVLIS and the Gamma-Metrics neutron flux detectors.

RVLIS

has not yet been declared operable after installation.

The neutron

detectors are already inoperable due to a generic problem addressed

in a Part 21 notice concerning potential moisture intrusion into

soldered and threaded connections. The exit thermocouple channel has

a redundant channel and may be inoperable indefinitely per TS Table

3.5-5, note 2.

The licensee's actions to address the long term *i.ssues associated

with the additional equipment which would be submerged following a

worst case design basis CV flood level is an UNR:

Followup on

Actions to Address Equipment Effected by an Increased CV.Submergence

Level (261/88-28-08).

No violations or deviations were identified within the areas inspected.

9. Onsite Review Committee (40700)

The inspectors evaluated certain activities of the PNSC to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements. In particular, the inspectors attended

the September 14, 1988 PNSC meeting involving operability of the HVH

units.

It was ascertained that provisions of the TS dealing with member

ship,- review process,

frequency,

and qualifications were satisfied.

Previous meeting minutes were reviewed to confirm that decisions and

recommendations were accurately reflected in the minutes. The inspectors

also followed up on selected previously identified PNSC activities to

independently confirm that corrective actions were :progressing satis

factorily.

No violations or deviations were identified within the areas inspected.

10. Solid Radioactive Waste (84722)

The inspector reviewed the details of an event which involved contaminated

water being detected in the plant storm drains.

At approximately

5:00 p.m., on August 8, 1988, a contract worker informed her supervisor of

the presence of cloudy water in the storm drain on the south side of the

E&RC building.

Upon analyzing a water sample from the storm drain, the

licensee determined that the water was contaminated. An isotop.ic analysis

indicated that the radioactivity found was similar to that found in a

sample of primary coolant.

Water samples were collectedand analysed from other storm drains in-the

vicinity of the E&RC building and throughout the site, as well as from the,

west settling basin where these storm drains empty.

Contamination was

detected in the water samples from two other storm drains that are nearest

the.E&RC building.

There was none found in storm drain samples from the

remainder of the site nor. in samples from the waste settling basin.

Because the licensee suspected that the contaminated waste was coming from

the E&RC laboratory sump (the receptacle for primary coolant samples

following analysis,), the contents of the sump were pumped to the Auxiliary

Building #2 sump tank for processing as radioactive waste (radwaste).

The

licensee also collected air samples above the storm drain covers and

performed contamination surveys of the areas around the drains.

No

airborne or surface contamination was detected.

The contaminated water

from the three storm drains was also pumped to the #2 sump tank in the

Auxiliary building for future processing.

The licensee estimated that

approximately 200 gallons of contaminated liquid were pumped into the #2

sump tank.

The licensee indicated that the 200 gallons included ground

seepage water, as well as contaminated water.

The exact quantity of

ground seepage water could not be determined.

Following the immediate corrective actions to stop the release of

contaminated water, the licensee performed an investigation of the event

and a walkdown of the E&RC building waste drainage system to determine the

source of the problem. The licensee discovered that the E&RC laboratory

sump had apparently been filled beyond its capacity.

This resulted in

contaminated liquid-backing up into the floor drains in the chemistry

laboratory. The contaminated liquid then flowed through bolt holes in the

12

flange pipe of the floor drains and through voids around the drain piping

to a French Drain installed under the E&RC building.

The French Drain.

subsequently discharged into the storm drain by means of a four-inch line.

The investigation also revealed that the level probes (installed in the

E&RC building sump to automatically control the level of liquid in the

sump) and the alarm (installed to indicate when the sump was full) were

not operating properly.

Through discussions with licensee representatives and records review, the

inspector determined. that the sump pump controls, including the alarm and

the level probes, had not worked properly since being installed in 1985.

A work request was eventually submitted in September 1987, to initiate

repair of the controls. Although repairs were completed in January 1988,

and the automatic actuation of the sump pump and the alarm verified,

licensee representatives indicated that the controls still did not

function properly.

No further work requests were initiated until the

contaminated liquid was discovered in the storm drains.

The licensee is required by 10 CFR 50,

Appendix B, Criterion XVI, to

establish measures to assure that conditions adverse to quality, such as

failures, malfunctions, deficiencies, deviations, defective material and

equipment, and nonconformances are promptly identified and corrected.

Failure of the licensee to promptly correct identified problems associated

with the E&RC building sump pump controls which led to the introduction

of radioactive water into the storm drainage system is identified as

violation of 10 CFR 50, Appendix B, Criterion XVI:

Failure to Correct

Sump Pump Controls Which Resulted in Radioactive Releases to the Storm

Drain System (50-261/88-28-09).

On violation was identified within the areas inspected.

11. Transportation (86721)

The inspector reviewed selected records of radioactive waste and radio

active material shipments performed during 1988.

The inspector also

reviewed the records of the circumstances surrounding the shipment of

contaminated liquid contained inside a tank and inside a piece of

shielding to a recycling vendor.

On February 24, .1988,

the licensee made a shipment of two Sea/Land

Containers to the Quadrex Recycle Center in Oak Ridge, Tennessee.

The

containers were filled with material to be decontaminated or disposed of

as radioactive waste. The shipping papers identified the physical form of

the material as solid; no liquid was indicated on the shipping papers. In

March,

as the vendor was processing the material from the two containers,

a RCP decontamination tank was found to have about six to seven gallons

of liquid inside.

In addition, a support structure containing lead

13

shielding, which was included in the shipment, was found to have about two

gallons of liquid inside.

The vendor collected, analyzed, processed,

and disposed of the water, and decontaminated the tank and the shield.

Isotopes in the water recovered from the tank and the shield were

identified as Cobalt-57, Cobalt-60, and Manganese-54.

The tank and

shield, with fixed contamination remaining,

were sent back to the

licensee.

Following an investigation of the incident, the licensee determined that

the tank and the shield had been in storage for approximately fifteen

months prior to being shipped to the vendor. When placed in storage, the

tank had been wiped dry and -wrapped with herculite, while the shield,

which appeared to be solid, was stored without being wrapped.

The items

had been stored in a contaminated warehouse which had a leaking roof.

Apparently, the liquid discovered by the vendor was the result of rain

water leaking on and into the items.

The licensee also determined that a

second root cause of the problem was personnel error in judgement.

The

same individual who had wiped the tank and placed it in storage was the

one who checked it and prepared it for shipment.

Since it had been wiped

dry and wrapped previously, the person assumed that no water was in the

'tank and that no further inspection was necessary. The shield was assumed

to be solid and was not inspected or tapped to check for liquid.

The licensee implemented corrective actions to prevent future events of

this nature. The individual involved in the event wrote a lesson plan

describing what happened and instructed other HP personnel concerning the

circumstances of the shipment. This instruction was provided during plant

safety meetings held during April 1988.

A new procedure, HPP-201, Code

of conduct for Radioactive Material Shipment, Revision 1, dated June 24,

1988,

was developed to discuss the various aspects of shipping and

receiving radioactive material.

The new procedure was also written to

ensure that double verification of the physical aspects of the shipments,

such as the presence of liquid, was performed. The licensee also issued a

job request to repair and seal the roof of the contaminated warehouse. As

a final measure , the licensee issued a POER detailing the event, the root

causes, and the corrective actions taken.

10 CFR 71.5 requires that licensees who transport licensed material.

outside the confines of their plant or other place of use, or who deliver

licensed material to a carrier for transport, shall comply with the

applicable requirements of the regulations appropriate to the mode of

transport of the DOT in 49 CFR 170 through 189.

49 CFR 172.203(d)(1)(ii) requires that a description of the physical and

chemical form of the material being shipped and radioactive material be

included on the shipping papers which accompany the shipment.

14

Failure of the licensee to indicate the proper physical form of the

material listed on the shipping papers was identified as a violation of

10 CFR 71.5:

Failure to Indicate Proper Physical Form of Material on

Shipping Papers (50-261/88-28-10). As this is a violation of minor safety

or environmental concern for which, by the end of the inspection, the

licensee had already taken or was in the process of taking adequate

corrective actions to prevent recurrence, no response will be required.

One violation was identified within the area inspected.

12.

Exit Interview (30703)

The inspection scope and findings were summarized on October 19 and 26,

1988,. with those persons indicated in paragraph 1.

The inspectors

described the areas inspected and discussed in detail the inspection

findings listed below.

Dissenting comments were not received from the

licensee. Proprietary information is not contained in this report.

No

written material was given to the licensee by the Resident Inspectors

during this report period.

Item Number

Status

Description/Reference Paragraph

88-08-01

Closed

IFI -

Implementation of the LER

Writer's Guide (paragraph 3).

88-08-03

Closed

IFI

Track Commitments Made to

NRC in LERs Through the RAIL

Commitment Tracking System (para

graph 3).

88-28-01

Open

IFI -

Establishment-of EQ Lifetimes

Inside CV Based Upon Actual Tempera-.

ture Conditions (Paragraph 4).

88-28-02

Open

VIO -

Failure to Have a Program To

-

Use Calibrated Stop Watches For

Required TS and ASME Section XI

Testing (paragraph 6.a).

88-28-03

Open

UNR -

Failure To Have Rx Head Vent

Valves Environmentally Qualified

(paragraph 8.a).

88-28-04

Open

IFI - Review Visual and Eddy

Current Testing of HVH 1-4 Dring

November 1988 Refuel Outage (paragraph

8.b).

UN0

alr oHaeR edVn

15

Item Number

Status

Description/Reference Paragraph

88-28-05

Open

IFI - Licensee To Develop Methodology

to Detect Biological Growth in HVH 1-4

(paragraph 8.b).

88-28-06

Open

UNR - Review LER 88-022 and CV

Operability Requirements After Opening

of CV Purge Exhaust Valves (paragraph

8.b).

88-28-07

Open

IFI - Inspect PM to Establish

Isolation as Required by Appendix R for

TE-410 and TE-413 (paragraph

8.e).

88-28-08

Open

UNR - Followup on Actions to Address

Equipment Affected by an Increased CV

Submergence Level (paragraph 8.f).

88-28-09

Open

VIO - Failure to Correct Sump Pump

Controls Which Resulted in Radioactive

Releases to the Storm Drain System

(paragraph 10).

88-28-10

Closed,

VIO - Failure to Indicate Proper

Physical Form of Material on Shipping

Papers (paragraph 11).

13.

List of Abbreviations

ASME

American Society of Mechanical Engineers

CFR

Code of Federal Regulations

CM

Corrective Maintenance

CV

Containment Vessel

DOT

Department of Transportation

DSP

Dedicated Shutdown Procedure

E&RC

Environmental and Radiation Control

EQ

Environmental Qualification

ESF

Engineered Safety Feature

F

Fahrenheit

HP

Health Physics

HVH

Heating Ventilation Handling

IFI

Inspector Followup Item

JCO

Justification For Continued Operation

LCO

Limiting Condition for Operation

LER

Licensee Event Report

MDAFW

Motor Driven Auxiliary Feed Water

16

NRC

Nuclear Regulatory Commission

OST

Operations Surveillance Test

PEP

Plant Emergency Procedure

PLP

Plant Program

PM

Plant Modification

PNSC

Plant Nuclear Safety Committee

POER

Plant Operating Experience Report

PPS

Penetration Pressurization System

PZR

Pressurizer

RAIL

Regulatory Action Item List

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

REV

Revision

R.G.

Regulatory Guide

RHR

Residual Heat Removal

RTGB

Reactor Turbine Generator Board

RVLIS

Reactor Vessel Level Indicating System

SDAFW

System Driven.Auxiliary Feedwater

S/G

Steam Generator

SP

Special Procedure

SPODS

Safety Parameter Display System

SW

Service Water

Tc

Cold Leg Temperature

TCV

Temperature Control Valve

Th

Hot Leg Temperature

TI

Temporary Instruction

TS

Technical Specification

  • UNR

Unresolved Item

WR/JO

Work Request/Job Order

.^UNRs

are matters about which more information is required to determine

whether they are acceptable or may involve violations or deviations.