ML13329A191

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Insp Repts 50-206/92-23,50-361/92-23 & 50-362/92-23 on 920717-0826.Violations Noted.Major Areas Inspected: Operational Safety Verification,Radiological Protection, Security & Evaluation of Plant Trips & Events
ML13329A191
Person / Time
Site: San Onofre  
Issue date: 09/29/1992
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13329A189 List:
References
50-206-92-23, 50-361-92-23, 50-362-92-23, NUDOCS 9210230020
Download: ML13329A191 (53)


See also: IR 05000206/1992023

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos.

50-206/92-23, 50-361/92-23, 50-362/92-23

Docket Nos.

50-206, 50-361, 50-362

License Nos.

DPR-13, NPF-10, NPF-15

Licensee:

Southern California Edison Company

Irvine Operations Center

23 Parker Street

Irvine, California 92718

Facility Name:

San Onofre Nuclear Generating Station

Units 1, 2 and 3

Inspection at:

San Onofre, San Clemente, California

Inspection conducted: July 17, 1992 through August 26, 1992

Inspectors:

C. W. Caldwell, Senior Resident Inspector

D. L. Solorio, Resident Inspector

C. D. Townsend, Resident Inspector

Accompanying Inspector: M. Fields, Project Manager

Approved By:

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H. J. Wong,thief

Date Signed

Reactor Projects Section 2

Inspection Summary

Inspection on July 17 through August 26, 1992 (Report Nos.

50-206/92-23, 50-361/92-23, 50-362/92-23)

Areas Inspected: Routine resident inspection of Units 1, 2 and 3 Operations

Program including the following areas: operational safety verification,

radiological protection, security, evaluation of plant trips and events,

engineered safety feature walkdown, plant modifications, licensee self

assessment, calibration, electrical maintenance, falsification of plant

records, monthly surveillance activities, monthly maintenance activities,

independent inspection, licensee event report review, followup of previously

identified items, and a meeting held in Region V. Inspection procedures

37700, 37701, 37828, 40500, 56700, 60710, 61726, 62703, 62705, 71707, 71710,

90712, 92700, 92701, 93702, TI 2515/115 were covered.

Safety Issues Management System (SIMS) Items:

None

9210230020 920930

PDR

ADOCK 05000206

0

PDR

Results:

General Conclusions and Specific Findings:

Strengths

During simulator observations, the inspectors noted that there were

weaknesses in command and control, and communications during scenarios

involving the emergency operating instructions. The inspector noted that

licensee management had also identified these weaknesses and was actively

involved in enhancing operator performance in these areas (Paragraph

3.b).

The inspector reviewed the licensee's temporary facility modification

(TFM) to the Unit 2 containment purge system. This TFM was implemented

due to leakage across the outboard mini-purge valve. In general, the TFM

appeared to be well designed and implemented (Paragraph 7).

A number of strengths were noted in the licensee's self-assessment

program. The 10 CFR 50.59 safety evaluation program appeared to be

effective in assessing plant changes and deficiencies (Paragraph 13.a).

The licensee's Nuclear Oversight Division (NOD) performed a number of

audits that were critical of licensee performance and that provided

recommendations that were insightful.

One example, concerning operator

performance issues during a recent Unit 3 refueling outage, was

considered valuable in focusing on enhanced performance (Paragraph 13.b).

In addition, a stop work order was issued for welding operations as a

result of a NOD surveillance that identified program weaknesses in the

control of weld filler material (Paragraph 13.c).

Weaknesses

The inspector noted that Maintenance and Station Technical personnel did

not understand the significance of nitrogen leakage from the accumulators

of Unit 1 valve HV852B. The inspector also noted that there was no

formal program to check the sub-components of the accumulators. With the

absence of knowledge as to the impact of nitrogen leakage and the lack of

a surveillance program to monitor accumulator piston location, HV852B was

in a degraded condition when nitrogen leakage occurred over a three month

period. On June 23, 1992, the valve was determined to have been

inoperable based on the results of the significant piston misalignment

identified on May 19, 1992 (Paragraph 15.e).

The licensee performed an evaluation of plant record keeping and found

several examples where log entries were made for areas in which the plant

operator did not enter. The licensee initiated a program to perform

periodic surveillances to ensure that log readings are properly obtained

(Paragraph 12).

The inspector reviewed the licensee's measuring and test equipment (M&TE)

control program. The inspector found that the program was very difficult

to audit. In addition, the inspector considered that the M&TE program

2

was poorly defined and that proper implementation of the program relied

heavily on the M&TE supervisor (Paragraph 11).

The NRC considered that, in general, the licensee correctly assessed

plant problems and effected timely resolution. However, several

weaknesses in timely and thorough assessment of plant problems or in

effective communication of proposed corrective actions to the NRC were

observed. In one instance, prompt visual assessment of pressurizer

instrument line leakage in Unit 3 would have resolved questions that

arose when unidentified leakage from the pressurizer vapor space was

considered to be occurring. In another case, a detailed assessment of

vital battery cracks in Unit 3 took more than a week (the NRC considered

that the licensee's evaluation was still inconclusive).

In addition,

with regard to HV852B, the licensee was not correct in their technical

assessment of the safety significance of the nitrogen leakage. Based on

these examples, the NRC stressed the importance of timely and accurate

assessment of emerging plant problems and encouraged continued licensee

emphasis in this area and effective communications of these problems with

the NRC (Paragraph 8).

Three examples of weaknesses in the interface between Station Technical

and Operations personnel were observed in this report period. Examples

involved performance of an in-service test in Unit 1 (Paragraph 4.b) and

a thermographic test that resulted in a Unit 2 reactor trip (Paragraph

4.a).

The third example involved a discrepancy between the simulator and

the Units 2 and 3 control panel. A change made to the control panel in

1988 was not properly reflected in design documents or in the simulator

due to a poor interface between Engineering and Operations that resulted

in the design change being a backlog item for more than four years

(Paragraph 10).

A similar organizational weakness was also identified in

NRC Inspection Report 50-206/92-20.

During plant tours, the inspector noted that operators were attaching

non-qualified equipment on the Unit 1 safety injection piping without any

evaluation. Further review indicated that there was no specific guidance

for placing temporary non-qualified equipment on or near safety-related

equipment (Paragraph 3.a).

Significant Safety Matters:

Summary of Violations:

One violation was identified during this inspection period which involved

inadequate corrective actions for Unit 1 valve HV852B (Paragraph 15.e).

A non-cited violation is identified in paragraph 14 and is related to the

misalignment of a Unit 2 saltwater cooling pump emergency cooling water

supply valve (LER 50-361/92-09).

Open Items Summary:

During this report period, 4 new followup items were opened and 5 were

closed; I was examined and left open.

3

DETAILS

1. Persons Contacted

Southern California Edison Company

H. Ray, Senior Vice President, Nuclear

  • H. Morgan, Vice President and Site Manager
  • R. Krieger, Station Manager
  • J. Reilly, Manager, Nuclear Engineering & Construction

B. Katz, Manager, Nuclear Oversight

  • R. Rosenblum, Manager, Nuclear Regulatory Affairs

K. Slagle, Deputy Station Manager

  • R. Waldo, Operations Manager
  • L. Cash, Maintenance Manager
  • M. Short, Manager, Station Technical
  • M. Wharton, Manager, Nuclear Design Engineering

P. Knapp, Manager, Health Physics

W. Zint], Manager, Emergency Preparedness

  • D. Herbst, Manager, Quality Assurance

Chiu, Manager, Quality Engineering

J. Schramm, Plant Superintendent, Unit 1

V. Fisher, Plant Superintendent, Units 2/3

  • G. Hammond, Supervisor, Onsite Nuclear Licensing
  • J. Reeder, Manager, Nuclear Training

H. Newton, Manager, Site Support Services

  • R. Plappert, Manager, Technical Support and Compliance
  • R. Borden, Supervisor, Quality Assurance
  • J. Jamerson, Lead Engineer, Onsite Nuclear Licensing
  • J. Travis, Maintenance Manager, Unit 1
  • J. Fee, Assistant Manager, Health Physics
  • M. Herschthal, Assistant Manager, Station Technical
  • A. Thiel, Supervisor, Station Technical
  • C. LaPorte, Supervisor, Maintenance
  • M. Motamed, Nuclear Safety Group

San Diego Gas and Electric Company

  • R. Erickson, Site Representative

City of Riverside

  • C. Harris, Site Representative
  • Denotes those attending the exit meeting on August 26, 1992.

The inspectors also contacted other licensee employees during the course

of the inspection, including operations shift superintendents, control

room supervisors, control room operators, QA and QC engineers, compliance

engineers, maintenance craftsmen, and health physics engineers and

technicians.

2. Plant Status

Unit 1

Unit 1 operated at power for the entire inspection period.

Unit 2

Unit 2 operated at power until an automatic trip occurred on July 31,

1992. The trip was due to a sensed undervoltage condition created when a

potential transformer drawer was opened (Paragraph 4.a).

The Unit

restarted on August 2, 1992, and operated at power for the remainder of

the inspection period.

Unit 3

Unit 3 operated at power for the entire inspection period.

3. Operational Safety Verification (71707)

The inspectors performed several plant tours and verified the operability

of selected emergency systems, reviewed the tag out log and verified

proper return to service of affected components. Particular attention

was given to housekeeping, examination for potential fire hazards, fluid

leaks, excessive vibration, and verification that maintenance requests

had been initiated for equipment in need of maintenance. The inspectors

also observed selected activities by licensee radiological protection and

security personnel to confirm proper implementation of and conformance

with facility policies and procedures in these areas.

a. Non-Qualified Components Tied To Safety-Related Equipment

During a plant tour on August 13, 1992, the inspector noted that

operators were installing an airhorn (used for cooling) on safety

related equipment in Unit 1. In particular, the operators were

tying the airhorn between a vertical run of safety injection piping

and an associated snubber.

The inspector discussed this with an on

shift senior reactor operator (SRO) who agreed that the action did

not appear to be appropriate.

Discussions with the Unit 1 Operations Superintendent indicated

that, historically, they have allowed operators to hook up cooling

equipment (such as this) to safety-related components on a temporary

basis. In addition, operators were free to make the judgment as to

where to put the equipment. However, this has not been done per the

work authorization process and as a result, installation of the

equipment has not been evaluated in such cases.

The inspector considered that this condition did not appear to be

safety significant since the weight of the airhorn was small in

relation to the size of the piping and supports involved. However,

the inspector was concerned since this could be construed as a

2

modification to the system. As such, it should undergo the

  • 0

appropriate reviews. Further review revealed that there was no

direct guidance in any procedure to control this activity.

Procedure S01-7-2, "Main Feedwater System," alluded to the potential

dangers to equipment during a seismic event, but it did not give any

specific guidance for temporary equipment being installed on or near

safety-related equipment.

The inspector discussed this concern with the Unit 1 Operations

Manager who indicated that he would revise documents to provide

better guidance. The inspector will review the licensee's actions

as part of the routine inspections.

b. Simulator Observations

The resident inspectors conducted a number of observations of Units

2 and 3 simulator activities for the period of May to July 1992.

During those observations, the inspectors noted several weaknesses

in crew performance. In particular, weaknesses in command and

control, and communications were observed during simulator scenarios

involving the emergency operating instructions (E0Is).

The

continuation of these types of difficulties was not expected by the

inspector since some crews had been operating together for a long

time; however, the inspector noted that none of the weaknesses

resulted in improper implementation of the EQls.

During the observations, the inspector noted that the licensee was

effectively dealing with these communication and command/control

weaknesses. The shift superintendent (SS) debriefed the crew after

each scenario and the simulator instructors critiqued the SS's

debriefing as well as the crew's performance. The inspector

considered that these critiques were detailed and self-critical.

In

addition, they emphasized the need for better communications and

team work. The licensee's critiques appeared to be valuable in

working through the difficulties observed. The inspector also noted

a considerable amount of management presence at the simulator.

The inspector concluded that, although there were weaknesses in the

performance of several crews, the licensee appeared to be

effectively dealing with them. The inspector encouraged the

licensee's efforts and will continue to monitor the licensee's

performance in this area as part of the routine inspection effort.

No violations or deviations were identified.

4. Evaluation of Plant Trips and Events (93702)

Automatic Trip Due To Opening Potential Transformer Drawer - Unit 2

On July 31, 1992, Unit 2 automatically tripped from 100% power after a

loss of two of the four reactor coolant pumps (RCP's).

The RCP's tripped

on a sensed undervoltage condition when a potential transformer (PT)

3

drawer was opened for thermographic inspections. The reactor trip was

generated from the core protection calculators on a low departure from

nucleate boiling ratio (DNBR) due to the low flow condition on the loss

of two RCP's. In addition, the auxiliary feedwater system automatically

started due to the decrease in steam generator level following the trip.

Both of these automatic functions were expected and performed as designed

for the conditions present.

The thermographic inspections were being performed by Station Technical

(STEC) personnel as part of a routine surveillance in accordance with

STEC procedure S0123-V-2.4, "Thermal Inspection Of Plant Components."

The fact that the RCP's would trip and therefore cause a reactor trip was

not commonly understood, and was not identified either in the procedure

or by the personnel involved in the testing.

The licensee reported in Licensee Event Report (LER)92-012 that the root

cause was attributed to inadequate positive controls in the work package

and an inadequate warning sign on the PT drawer. The licensee is taking

corrective actions to develop positive controls in the work package and

install improved signs. The inspector considered the licensee's

corrective actions to be appropriate. However, this event appears to be

another example in which a STEC program was not adequate to maintain

proper configuration control in the plant. NRC Inspection Report 50

206/92-20 discussed two instances of a weak interface between STEC and

Operations which led to configuration control problems. The licensee

will address the concerns raised in Inspection Report 92-20 in their

response to Notice of Violation from that report.

The inspector noted that Operations personnel had an opportunity for more

effective communications with Station Engineering during a Unit I main

feedwater pump inservice test (IST) in July 1992. In this case, the

engineer was utilizing procedure SO1-V-2.14.10, "Feedwater Inservice Pump

Test," to perform the IST of the west feedwater pump, G3B. Earlier in

the year (on January 2, 1992), an instrument drift problem occurred in

conjunction with the same feedwater pump test (see NRC Inspection Report

92-06).

In the January occurrence, the east feedwater pump discharge

pressure gauge had drifted low. This resulted in the pump being

inoperable (according to the IST program) until the gauge was

recalibrated. In the July case, while it was not Operations

responsibility to assure an accurate gauge was used for the test,

Operations had the opportunity to alert Engineering of the past problem

which resulted in unnecessarily declaring a piece of plant equipment

inoperable.

No violations or deviations were identified.

5.

Monthly Maintenance Activities (62703)

During this report period, the inspectors observed or conducted

inspection of the following maintenance activities:

4

a. Observation of Routine Maintenance Activities (Unit 1)

92071359000

"'Y' Channel SIS Block LED Is

Extinguished on Card 11

LED#3 'X'

Channel Corresponding LED Is Illuminated."

90060431000

"Adjust/Rework N2 Regulators For Train 'B' SIS Valves

As Required."

b. Observation of Maintenance Activities (Unit 3)

CWO 92090192

"Install a Temporary Battery Rack Adjacent to Battery

Rack 3EB007 per Temporary Facility Modification

(TFM)."

No violations or deviations were identified.

6. Engineered Safety Feature Walkdown (71710)

Unit 2

An evaluation of the safety alignments was performed on the Unit 2

Component Cooling Water (CCW) system with no significant findings. The

following drawings and procedures were utilized: Piping and Instrument

Drawings 40126, 40127, 50127, and Procedures 5023-2-17 and SD-S023-400-1

3.

An evaluation was also performed of the Unit 2 Auxiliary Feedwater (AFW)

System safety alignments with piping and instrument drawing 40160. No

significant findings were identified.

No violations or deviations were identified.

7. Plant Modification and Refueling Activities (37700 and 37828)

Temporary Facility Modification On Unit 2 Mini-Purge Line

The inspector reviewed a temporary facility modification (TFM) to the

Unit 2 containment purge system. The TFM was implemented because the

outboard containment mini-purge valve leaked after the completion of

containment venting on four occasions in June and July 1992. The leakage

was determined to be due to buildup of small pieces of debris under the

seat of mini-purge valve 2HV9825.

The scope of the design change was to install one-inch diameter tubing to

the containment air sampling line outside of containment. The tubing was

routed from radiation monitor 2RT7804 to the inlet ducting for normal

containment mini-purge fan flow. The containment purge isolation (CPIS)

contacts in the control circuits for mini-purge isolation valves 2HV9824

and HV9825 were moved to the containment atmosphere sample line isolation

valves HV7800 and HV7801. Due to the reduced purge flow diameter (from

eight inches to one inch), the time to complete a containment purge was

substantially increased.

The inspector noted that a probabilistic risk assessment (PRA) is not

required when performing a 10 CFR 50.59 review. However, the inspector

questioned if the licensee had evaluated the potential impact of having

this line open much longer than when using the eight inch mini-purge line

(almost continuously versus four hours every 20 days).

The licensee

indicated that they had assessed the impact of having the purge line open

continuously. However, as a result of the inspector's question, a

limited PRA assessment was performed in which it was calculated that

there was an insignificant increase in core damage or off-site release

probability as a result of this TFM.

In general, the TFM appeared to be well designed, implemented and within

program requirements. However, the inspector was concerned that there

were no corrective actions other than to blow the debris away from the

seat of HV9825 when the valve was found leaking. This had been done four

times between June 9 and July 2, 1992. Thus, during that period, when

the valve was opened, it could not perform its leak tight function.

However, the inspector considered that this was of minor safety

significance; the licensee assured that the valve was leak tight before

they left it, leakage through the penetration was less than TS allowable,

and the inboard valve appeared to be relatively leak tight.

No violations or deviations were identified.

8. Independent Inspection (40500)

Weaknesses in Timely and Thorough Assessment of Plant Problems or In

Effective Communication of Actions to the NRC

The inspector monitored the licensee's performance in assessing events

and plant problems that had recently occurred. In general, licensee

performance has been adequate in implementing timely and effective

corrective action for plant problems. However, there were several

examples where the NRC considered that performance could have improved or

that more effective communications of assessments and corrective actions

could have been provided to the NRC. In addition to past issues (e.g.,

Unit 1 refueling water storage tank leakage discussed in Inspection

Report 206/92-12), recent examples concerned pressurizer instrument line

leakage in Unit 3, 125 VDC vital battery cracking in Unit 3, and valve

HV852B accumulator nitrogen leakage in Unit 1. The concerns were as

follows:

a) Pressurizer Instrument Line Leakage in Unit 3

On July 20, 1992, the licensee determined that there was a

problem with one of the pressurizer level instruments. The

licensee sampled the containment normal sump and found high

levels of tritium which indicated pressurizer steam space

leakage. The licensee concluded that the steam space leakage

was linked to the problems noted with the pressurizer level

instrument.

6

The small amount of leakage (.076 gpm) was evident by a 5.5%

high deviation in level in Channel Y, transmitter 3LT01102, in

comparison to the redundant channel. It was believed that such

a deviation could be caused by a leak in the reference leg of

the transmitter. As a result, the licensee initiated non

conformance report (NCR) 92070079 to assess the implications of

the leak on the operation of the Unit.

During discussions with the licensee, they were not able to

exclude the possibility that the leak was from the reactor

coolant system pressure boundary. However, they believed that

the leak was most likely from the reference leg isolation valve

(e.g., body to bonnet canopy weld), the flexible hose

connecting the transmitter tubing to the isolation valve, or

the connections between the tubing and the flexible hose. The

licensee also believed that the leakage source was downstream

of a loss-of-coolant-accident (LOCA) limiting orifice. Thus, a

break would be limited to within analyzed values.

The NRC staff was concerned that a crack in small bore tubing

or piping such as this could lead to small break LOCA event.

Data suggested that a leak before break scenario with slow

propagation was not as credible in small bore tubing as it was

in large diameter piping. Subsequent discussions with the

licensee revealed that they were not aware of this concern, but

would consider it in future situations.

Subsequent observations indicated that the licensee's technical

judgement of the situation was correct. However, the NRC was

concerned that they did not perform a visual inspection of the

plant equipment until questioned by the NRC, even though

discussions failed to disprove the presence of pressure

boundary leakage. The NRC considered that, given that the

leakage was unidentified leakage, and that it was possible that

it may not have been isolable, it would have been prudent for

the licensee to conduct a visual inspection without NRC

involvement.

b) Vital Battery Cracks in Unit 3

On July 14, 1992, the licensee identified that cell # 14 of

vital battery 3D1 (125 VDC) had a terminal voltage less than

required by Technical Specifications (TS).

As a result, the

licensee initiated NCR 92070043 to assess the implications of

jumpering out that cell and jumpering in cell 53.

Cell 53 had been jumpered out of the battery with its adjacent

cell, number 54, in May 1992, as a result of several cracks

that radiated out from one of the posts on the top of cell 54

(cells 53 and 54 are located in the same jar).

Since the

licensee was in a short duration action statement (two hours)

with cell 14 inoperable, they performed a quick evaluation of

7

continued operation with cell 53 jumpered in and determined

that it would not adversely impact battery operability. This

was then supported by the licensee's evaluation of the

applicability of a Wyle Laboratory test report for similar

cells with cracks from batteries at Palo Verde Nuclear

Generating Station. Portions of the test report were received

by the Nuclear Engineering Design Organization (NEDO) on July

14 and evaluated. However, the entire test package was not

received until July 17 and the NEDO review was not completed

until July 23, 1992.

The inspector was concerned with the licensee's evaluation of

the condition as detailed in NCR 92070043 as follows:

0

The NCR gave the impression that the licensee had looked

at the issue in more detail than they really had, given

that it was a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> TS action statement. In fact, the

licensee did not have the opportunity to review the

partial Wyle test results until a day later, and the full

Wyle test package several days later. For example, the

licensee indicated in the NCR that no additional cracking

resulted during the Wyle test of the Palo Verde battery

cells. However, if they had reviewed the preliminary test

package in more detail, they would have found that some

additional cracking took place during the seismic shake

test. It appears that the licensee reached some

conclusions based on a limited review of the information.

The licensee indicated that the mechanism causing the

existing seal nut and jar lid cracking was corrosion

induced. The licensee indicated that a qualitative

assessment by the site materials specialist concluded that

it was not expected that the existing jar lid cracks in

cell 54 would propagate into the jar wall or the other

cell.

However, there was no justification documented to

support this assessment.

The NCR indicated that a seismic test of several cells

with existing jar lid cracks was conducted by Wyle Labs.

The tests (of similarly designed cells used at Palo Verde)

showed that the cells remained operable after a seismic

event. The licensee's NEDO organization completed their

evaluation of the Wyle report and considered that it was

applicable to SONGS. However, the NRC reviewed the Wyle

test report and had a number of questions regarding the

acceptability of the test. For example, the NRC staff

questioned whether or not capacity tests for the cracked

jars were required to demonstrate that the cells could

perform their safety function after a seismic event (in

accordance with American Nation Standards

Institute/Institute of Electronic and Electrical Engineers

(ANSI/IEEE)

Standard 535).

8

The NRC also questioned the lack of acceptance criteria

and requirements for monitoring electrical functions such

as current and voltage during and after the seismic tests.

As a result of the above observations, the NRC was concerned

that the licensee made their judgements without having a

detailed assessment that was applicable to SONGS until nine

days after the problem was identified. In addition, several

questions remained unresolved as of the end of this inspection

period. The inspector noted that additional corrective actions

were implemented after the close of this inspection period. In

particular, the licensee added a temporary battery rack and

jumpered in four new cells (in place of cells with existing

cracks).

Discussions with the Vice President and Site Manager indicated

that the licensee agreed that they did not do a complete

analytical evaluation, but they believed that their engineering

judgement at the time was satisfactory. The NRC is still

reviewing this matter.

c) Nitrogen Leakage from Unit 1 Valve HV852B

As discussed in Paragraph 15.e, the inspector was concerned

that the knowledge of the personnel evaluating the condition of

HV852B was insufficient to identify that the excessive nitrogen

leakage could.affect piston positions and valve stroke timing.

In this case, the technical judgement of the condition was not

adequate and a more timely and thorough assessment of the

problem could have prevented further degradation of the valve.

In addition, ultrasonic testing of similar valves would have

been appropriate to ensure operability when the problem with

HV852B was first identified.

The NRC considered that, in general, the licensee correctly assesses

plant problems and effects timely resolution. A recent example was

noted when the licensee entered Unit 2 containment to verify

adequate reactor coolant pump (RCP) 2P003 oil sump level when

anomalies were noted with the sump level transmitter. Although the

licensee was correct in their assessment, as discussed in the first

example, a visual assessment of the instrument leakage would have

left no doubt as to the condition of the pressurizer instrument

line. In the second example, a detailed assessment of the battery

cracks took a week and the NRC considered that it was still

inconclusive. In the third example, the licensee was not correct in

their technical judgement of the significance of nitrogen leakage in

HV852B. As a result, the NRC stressed the importance of timely and

accurate assessment of emerging plant problems and encouraged

continued licensee emphasis in this area, accompanied by more

effective communications of these problems to the NRC.

No violations or deviations were identified.

9

9. Electrical Maintenance (62705)

The inspector continued with a review of electrical maintenance issues.

In particular, the licensee's performance of battery surveillance testing

was reviewed during this inspection period. In general, surveillances

were performed adequately. However, one concern was identified as

discussed below.

On the morning of July 14, 1992, the licensee identified that cell 14 of

125 VDC vital battery 3D1 had an individual cell voltage (ICV) reading

less than required by TS. As a result, the licensee initiated NCR

92070043 to assess the implications of jumpering out that cell and

jumpering in cell 53 as discussed in paragraph 8b.

The inspector noted that as soon as the problem with cell 14 was

identified, maintenance personnel stopped, as required by procedure, and

contacted appropriate personnel for resolution of the inoperable cell.

As a result, the inspector was concerned that the licensee did not check

the specific gravities of the cells after the ICV measurements revealed

that cell 14 was inoperable. Apparently, the assumption in the procedure

was that there was no reason to believe that there might be multiple cell

failures.

The inspector noted that approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> passed before

the surveillance testing of the battery was continued. Engineering

evaluations had been performed assuming only one inoperable cell.

The inspector noted that cell 29 in battery 3D1 had been a poor performer

for several years. During performance of the July 14 surveillance test,

the specific gravity of cell 29 was greater than 20 points below the

average of the rest of the cells. However, the specific gravity of the

cell was greater than 1.195 (a TS limit).

Thus, the cell was operable

although degraded. The inspector was concerned that if the cell had been

inoperable on low specific gravity, it would not have been noticed until

the evening of July 14, long after the two hour TS action had expired.

The inspector discussed with the Maintenance Manager the concern that

current battery surveillance test methods could prevent detection of

multiple inoperable cells for periods of time exceeding TS allowable.

The Maintenance Manager indicated that he would evaluate the inspector's

concern. This evaluation will be reviewed as part of the routine

inspection effort.

No violations or deviations were identified.

10. Discrepancy Between Simulator And Control Room Panel (71707, 37700,

37701)

On June 3, 1992, the inspector was observing simulator training

activities when a difference between the simulator and the Units 2 and 3

control panels was noted. The inspector discussed this condition with

the control operators and the simulator instructors and noted the

following discrepancy.

10

In 1988, an NRC safety system functional inspection of several safety

systems identified a concern with operation of the component cooling

water (CCW) system. The concern was that the CCW surge tank outlet

valves would shut on a low-low level in the tank to prevent air binding

of the CCW pumps. However, it was postulated that this isolation feature

could result in a loss of net positive suction head for the pumps during

a seismic event concurrent with a break in the non-critical CCW loop. As

a result, the licensee removed the surge tank outlet valve thermal

overloads.

The change to the physical configuration of the plant was such that

removal of the thermal overloads would prevent operation of the valve

from the control room or on a low surge tank level.

The valves had to be

shut locally by manual operation. However, this design change was not

reflected in the simulator as observed during the scenario when the valve

closed automatically.

The inspector discussed this concern with the licensee who had performed

an assessment of the situation. Surveillance report SOS-235-92

documented the licensee's review. The licensee found that the change to

the valve control circuitry was assessed through the disposition of an

NCR, and it was to be implemented by a maintenance order (MO) and a

proposed facility change (PFC).

The licensee determined that

implementing the change in this manner was allowed by procedure. The

evaluation revealed that the MO was implemented, but, the PFC was not.

Instead, a retrofit problem report (RPR) was written in 1989. The

Construction Organization (also referred to as "Projects") was unable to

implement the PFC due to disagreements between Operations and the Nuclear

Engineering and Design Organization (NEDO)

as to what the full scope of

the change would be. The RPR remained unanswered since 1989 and went

into the backlog of items awaiting attention by the licensee.

The licensee determined that Units 2 and 3 operated in a plant

configuration that was not reflected in the appropriate design documents

or in the simulator for over 4 years. The licensee considered that there

was no programmatic or procedural non-compliance with this concern.

However, the root cause was that existing programs did not make

supervision and upper management aware when due dates were not met,

allowing a backlog of documents to accumulate.

In addition to the concern with the backlog of items, the inspector noted

that in this instance, a poor interface between and within organizations

existed. In particular, Operations did not like the PFCs, the Station

Technical engineers were not aware of the status of their assigned system

configurations, and it appeared that STEC was expecting NEDO to do all of

the design corrections and changes without NEDO being aware of that

expectation.

Corrective actions included revising the appropriate design documents to

correctly reflect that the thermal overloads (for the respective CCW

surge tank outlet valves) had been removed. The simulator was brought up

to date on June 12, 1992. In addition, the licensee was in the process

11

of modifying procedures to require higher levels of management review to

ensure that each backlog item received an adequate evaluation.

The inspector considered that the effort by the Nuclear Oversight

Division to determine the scope and the root cause of this problem to be

critical and thorough. The inspector also noted that the licensee has

been aggressively pursuing the reduction of backlog items so that items

such as this should be identified and resolved in a more timely manner.

No violations or deviations were identified.

11.

Review Of Licensee's Measuring And Test Equipment Program (56700)

The inspector performed a review of the licensee's measuring and test

equipment (M&TE) program to determine if the portable equipment was

properly controlled and capable of ensuring the operability of installed

plant equipment. The inspector found that the control of M&TE equipment

was very difficult to audit. In addition, the inspector considered that

the M&TE program was poorly defined and that the proper implementation of

the program relied heavily on the M&TE supervisor.

The inspector noted that the program was difficult to audit since

portions of the documentation were located at the site and the remainder

were at the licensee's Shop Services and Instrumentation Division (SSID)

facility in Westminster, California. In addition, much of the

documentation had to be indexed and cross-referenced manually. Equipment

"travelers" (used to monitor the use of M&TE as discussed below) was one

type of document that was particularly difficult to retrieve.

The inspector considered that the poor program definition could lead to

installed plant instrumentation being out of tolerance for long periods

of time based on the following observations:

o

M&TE used in performing a maintenance activity was recorded in the

Maintenance Order (MO). It takes many months for the MO and M&TE

information to get recorded in the computer database. As a result,

the licensee had implemented a document called a "traveler" which

was provided to the technician with each piece of M&TE issued from

the tool room. The user recorded on the traveler (not a controlled

document) which maintenance/surveillance activities the piece of

M&TE was used in. When the M&TE was returned, the traveler

information was loaded into a database for tracking its use. Thus,

if a calibration failure notice (CFN) was issued on that M&TE, the

plant equipment that it was used on could be easily tracked.

This system places heavy reliance upon individuals to properly fill

out this paperwork and return all pages to the tool room upon

completion of use. This was complicated somewhat by the fact that

procedures allowed different individuals to use the same piece of

test equipment (M&TE). Therefore, the person responsible for the

accuracy of the traveler would change. If a page was lost or

information was improperly recorded, then usage of the M&TE on plant

12

equipment could not be established until the MO was loaded into the

database some months later. If no usage was shown in the computer

(e.g., a lost traveler), then the CFN would not get evaluated for

potential impact on installed plant equipment. The only exception

was M&TE used by the Quality Control (QC) organization, which has

its own program for dealing with CFNs.

o

Approximately one-third of the time, CFNs went unanswered or

unassessed for more than 30 days.

o

The requirements for what to do when a piece of M&TE had sequential

calibration failures were not well defined in the SSID or site

procedures.

o

Procedural guidance was weak in defining the situations when

technicians needed to verify the accuracy of test equipment before

or after using it on installed plant equipment. Thus, if a piece of

M&TE had gone out of calibration during the interval, this fact may

not be identified until it was sent to SSID for a calibration check.

This could result in a long interval in which the calibration status

of plant equipment could be in question.

o

There was no easy way to find a detailed history of calibration

failures in the measuring and test equipment data base. Thus, a

technician would not know if there had been a history of problems

with the equipment being used.

o

When a CFN was received from SSID, the first line supervisor was

responsible for evaluating the condition and the M&TE supervisor

verified the first line supervisor's assessment. The inspector

noted that the resolution of the M&TE supervisor's comments

contributed to the excessive time used to respond to CFNs.

o

It took greater than 30 days (40% of the time) for the M&TE to be

calibrated and returned to the site after being sent to SSID. This

could lead to excessive periods during which plant equipment could

be out of calibration.

The inspector discussed these concerns with licensee management. To the

licensee's credit, a quality action team (QAT) was assembled to address

other M&TE issues (such a temperature sensitivities of M&TE) as a result

of a Nuclear Oversight Division audit. The inspector noted that the QAT

was aware of the extensive time to return M&TE after it was sent off-site

and the excessive time to respond to CFNs. The licensee indicated that

the QAT would factor the inspector's concerns into their evaluation of

the M&TE program. The inspector also noted that the licensee was in the

process of implementing a program to track the history of calibration

failures of equipment.

As of the end of this inspection period, no operability issues were

identified. However, the inspector was in the process of performing

documentation reviews to determine if personnel practices were adequate

13

to compensate for the weaknesses in program definition. The inspector

will continue a review of M&TE activities as a Followup Item (50-361/92

23-01).

12.

Verification Of Plant Records

(TI 2515/115)

Temporary Instruction (TI) 2515/115 to the NRC Inspection Manual was

issued to provide guidance for evaluating each licensee's ability to

obtain accurate and complete log readings from either licensed or non

licensed personnel.

The inspector reviewed the licensee's program to

determine if SCE had implemented a self-monitoring program which could

detect plant mechanics, technicians, or operators whose practices might

have included falsifying logs.

The inspector discussed this issue with the licensee in June 1992. At

the time, the licensee did not have a program to verify plant records.

However, after review of the issue, as discussed in NRC Information

Notice 92-30, "Falsification Of Plant Records," the licensee elected to

implement such a program. In August 1992, the licensee issued quality

assurance guideline (QAG)-005 to provide a periodic surveillance program

for comparative analysis between documented division surveillance

requirements and security access records data.

The inspector reviewed the QAG and considered that it would be effective

in detecting personnel practices which might lead to falsified log

readings. The inspector also noted that the Vice President and Site

Manager issued a memorandum to all nuclear organization personnel on May

21, 1992, dealing with the issue.

The licensee also performed an assessment of log keeping practices of

plant equipment operators for the period of April 4 to April 7, 1992.

Several inconsistencies with operator round sheets were noted and

documented in surveillance report SOS-195-92, "NRC Information Notice 92

30:

Falsification Of Plant Records." In particular, the following

concerns were identified:

O

A non-licensed nuclear plant equipment operator (NPEO) did not make

the required vital area entries to perform shiftly surveillances on

three occasions, but signed the surveillance indicating that he had.

According to the licensee's surveillance, on March 8 and April 4,

1992, the night shift Radwaste NPEO (commonly referred to as the 43

position) was required to enter the Units 2 and 3 control element

drive mechanism control system (CEDMCS) vital area by procedure

S023-0-9, TCN 0-29, "Routine Rounds and Inspections." The NPEO was

required to make a general area inspection of equipment (e.g.,

panels, motor-generators, relays, etc.) in the Unit 2 CEDMCS room as

required by the rounds sheet and document any abnormalities.

However, contrary to the requirement of the operator rounds sheet,

the assigned responsible NPEO did not enter the area as reflected by

plant security data. In addition, on March 18 the same operator did

not enter the Unit 2 main steam isolation valve area on March 18,

1992, as required by the (23 position) operator round sheet. In

14

this case, the NPEO was required to make a general area inspection

and take specific readings of instrumentation associated with the

atmospheric dump valves, main steam isolation valves, and other

safety-related equipment.

In the cases discussed above, there did not appear to be any safety

significance to the failure to make the appropriate area entries

since subsequent operator rounds indicated that the equipment was

functioning properly. The licensee took disciplinary actions

against the equipment operator. Failure to take and record

information that is complete and accurate in all material respects

is an Unresolved Item pending the NRC's determination of the policy

for handling these types of record discrepancies (Unresolved Item

50-361/92-23-02).

Three examples were identified in which two NPEOs allowed their

trainees to enter an area without the assigned responsible NPEO in

attendance to perform rounds required by S023-0-5, TCN 0-1, "Plant

Equipment Operator's Responsibilities and Duties."

In particular,

on April 6, 1992, the responsible NPEO (turbine building 24

position) did not enter the Unit 2 non-1E uninterruptible power

supply (UPS) vital area or the Unit 2 salt water cooling (SWC) pump

room. On April 7, 1992, the (24 position) NPEO did not enter the

Unit 2 non-1E UPS vital area. In addition, on April 8, 1992, the

(24 position) NPEO did not enter the Unit 2 non-1E UPS area or the

Unit 2 SWC pump room. Instead, on these occasions, non-qualified

trainees entered these areas to take readings.

This practice is contrary to the licensee's procedural requirements.

In particular, procedure S0123-0-20, "Use Of Procedures," Revision

0, TCN-6, specified that, "Only qualified operators are permitted to

obtain readings required by Operating Instructions unless

specifically allowed otherwise by the procedure." In addition, the

procedure specified that the assigned responsible NPEOs sign for

performance of the surveillance. In the cases discussed, the NPEO

was required to make a general area inspection of pumps, motors,

piping etc. There did not appear to be any safety significance

since subsequent operator rounds indicated that the equipment was

functioning properly. The licensee counseled the individuals

involved on the inappropriate use of trainees in these instances.

This is an Unresolved Item pending the NRC's determination of the

policy on handling these types of record discrepancies (Unresolved

Item 50-361/92-23-03).

Two unresolved items were identified.

13.

Licensee Self Assessment (40500)

a. 50.59 Program Assessment

A resident inspector and the Nuclear Reactor Regulation (NRR)

project manager reviewed the licensee's 10 CFR 50.59 evaluation

15

program to determine its adequacy for performing effective safety

evaluations.

Attachment 3 to Nuclear Engineering, Safety, And Licensing (NES&L)

procedure 24-10-15, "Preparation, Review, And Approval Of Facility

Change Evaluations (FCEs) for SONGS 1,2 & 3," was reviewed to

determine the adequacy of the program in implementing 10 CFR 50.59

requirements and its conformance with Nuclear Safety Analysis Center

(NSAC)-125 recommendations. The inspector also reviewed the

licensee's training program and several completed 50.59 evaluations.

In general, it was considered that the program was adequate and

conformed to NSAC-125 recommendations. The project manager reviewed

a number of safety evaluations and considered that they were

adequate. However, the project manager considered that the process

by which SCE identifies licensing criteria and their impact on the

safety evaluation could be enhanced. In particular, there were

examples noted in which the safety evaluations did not list all the

licensing criteria considered in the 50.59 evaluation. The project

manager attributed the weakness of some safety evaluations to the

following observations:

o

There was not a formal process for verifying that the proper

licensing design bases were chosen by the engineer performing

the 50.59 evaluation.

0

10 CFR 50.59 evaluations sometimes did not list the licensing

design bases of the components under consideration (e.g.,

backup nitrogen supply for the CCW surge tank simply stated

that CCW performs heat removal from accidents in Chapter 15 of

the FSAR).

It was not discussed in the safety evaluation which

accidents were actually being considered.

The inspector concluded that the licensee's program was adequate and

should result in sound, justified safety evaluations. However, the

inspector discussed the observations noted above with the

appropriate licensee management for evaluation. The licensee's

evaluation will be reviewed as part of the routine inspection

effort.

b. Operator Performance Issues During The Unit 3 Refueling Outage

As a result of the inspector's concern over the number of operator

errors during the Unit 3 Cycle VI refueling outage, the licensee

reviewed selected events to determine if there was a common cause.

The results of the review were addressed in a memo from C. Chiu to

R. W. Waldo and J. L. Reeder, dated August 24, 1992. In that

evaluation, the licensee considered that these events were primarily

the result of individuals performing tasks that were only done

infrequently or individuals performing routine tasks under

infrequently occurring plant conditions or system lineups.

In

addition, the licensee considered that there were weaknesses in the

.16

operation and method of controlling operations for the spent fuel

pool cooling system.

As corrective actions, the Nuclear Oversight Division recommended

that the licensee form a QAT to address improvements in the

operation of the spent fuel systems. In addition, prior to future

refueling outages, training should develop a lessons learned

training course to heighten awareness of things to look for during

off normal conditions.

c. Stop Work Order For Welding Operations

On August 25, 1992, the Maintenance Manager issued a stop work order

for all welding as a result of a Quality Assurance surveillance that

found uncontrolled weld filler material.

The order was applicable

to all work except that specifically approved by the Maintenance

Manager. The majority of the filler material (rods) was found at

the Mesa facility and at the Administrative Warehouse & Supply/Shop

Building (AWS) machine shop. However, some was found in the plant.

For corrective action, the licensee planned on retaining tight

restrictions on the use of filler material and performing a

maintenance incident investigation report. As of the end of this

inspection period, there were no indications that there was impact

on plant safety. The inspector will monitor the licensee's actions

to resolve this issue as followup item (50-206/92-23-04).

No violation or deviations were identified.

14.

Review of Licensee Event Reports (90712, 92700)

Through direct observations, discussion with licensee personnel, or

review of the records, the following LERs were closed:

Unit 1

91-14, Revision 0

"Entry Into 3.0.3 Technical Specifications Due To

Inoperable Volume Control Tank Level Transmitter."

92-01, Revision 0 "HV852B Inoperable Due To Hydraulic Accumulator

Piston Level."

92-02, Revision 0

"Shift Supervisor And Control Room Supervisor Both

Left Control Room."

Unit 2

88-15, Revision 1 "Operator Error Causing Fuel Handling Isolation

System Response."

91-08, Revision 0

"Erratic Ammonia Analyzer Caused Toxic Gas Isolation

System To Actuate."

17

92-02, Revision 0

"Inadvertent Control Room Isolation System

Actuation."

92-04, Revision 0

"EFAS Manual Actuation After Loss Of One Main

Feedwater Pump."

92-09, Revision 0 "Saltwater Cooling Valve MU019 Out Of Position

(Closed) Greater Than 72 Hours."

This LER describes the licensee's failure to maintain a pump

cooling water valve open and is considered a violation of

Technical Specifications 3.7.4. This violation will not be

subject to enforcement action because the licensee's efforts in

identifying and correcting the violation meet the criteria

specified in Section VII.B of the Enforcement Policy.

Unit 3

92-03, Revision 0 "Reactor Coolant Pump Trip Due To Faulted Surge

Capacitor."

One non-cited violation was identified.

15.

Follow-Up of Previously Identified Items (92701)

a.

(Closed) Open Item (50-361, 50-362/91-01-05) "Temperature

Sensitivity of Excore Nuclear Detectors"

The NRC instrument and control (I&C) setpoint team noted that the

excore nuclear instrument detectors could be subject to elevated

temperatures during certain accident conditions. The licensee did

not have information on the affect of elevated temperatures on

excore detector uncertainty calculations.

As a result of the concern, the licensee obtained vendor

certification that the excore nuclear instrument detectors would not

be effected by elevated containment temperatures.

The inspector reviewed the vendor information and concluded that it

supported the conclusion that excore nuclear instrument detectors

would not be effected by elevated containment temperatures. Based

on the inspector's review, this item is closed.

b. (Closed) Unresolved Item (50-361, 50-362/91-01-06) "Inaccurate

Calculation of Instrument Uncertainties for Emergency Operating

Instructions"

The licensee prepared and submitted to the NRC, for approval, a TS

amendment requesting that certain transmitter surveillance intervals

be changed from 18 months to 24 months. One of the supporting

documents for the amendment was Functional Analysis M-89068,

18

"Accident Monitoring System and Remote Shutdown Panel." An NRC I&C

setpoint inspection team reviewed Function Analysis M-89068 and

found errors in the document. Based on the number and types of

errors identified, the team questioned the validity of the document

as a supporting document for the TS amendment.

Based on the findings, the licensee:

o

withdrew the TS amendment request,

o

committed to review the implications of the inaccuracies in

M-89068 on their emergency operating instructions, and

o

committed to perform a review of the technical validity of

M-89068.

The licensee review concluded:

o

Calculation M-89068 did not receive the proper engineering and

quality assurance review required for engineering documents.

o

The results of M-89068 did not support the extension of

surveillance intervals.

Based on the NRC findings and the licensee review, the licensee

performed new calculations for instrument uncertainties. These new

calculations showed that instrument uncertainties were larger than

had been previously utilized in certain emergency and abnormal

procedures. Based on the results of the new calculations, the

licensee concluded that no safety limits would have been exceeded in

emergency or abnormal operating procedures. However, the licensee

found that conditions such as the lifting of safety relief valves

might occur, even when the operators were in compliance with

abnormal operating limitations. The licensee concluded that

emergency and abnormal operating procedures required revision to

incorporate the revised calculated instrument uncertainties. The

licensee committed to make these changes.

The inspector reviewed the licensee's administrative actions and

found them adequate; therefore, this item is closed.

Review of the new calculations and changes to emergency and abnormal

operation procedures will be accomplished as part of Unresolved Item

(50-361, 50-362/91-01-09).

c.

(Closed) Unresolved Item (50-361, 50-362/91-01-08) "Validation of

Study M-89047"

The NRC I&C setpoint team noted that Study M-89047, "Instrument

Drift Study," was performed during the same time frame as Functional

Analysis M-89068. The team was concerned that the type of errors

found in M-89068 were contained in M-89047.

19

The team noted that in a TS Amendment request, the licensee had

stated that M-89047 was based on worst case instrument drift. The

team noted that only 1/2 the data was analyzed to determine worst

case. Data was available for both increasing data points and

decreasing data points. The licensee had only considered the

increasing data, which did not always include the worst case drift.

The team concluded that the licensee had not used the worst case

drift values as stated in the TS amendment request. Based on the

problems with M-89068 and the team's finding that the worst case

drift data had not been used as stated, the licensee agreed to

determine if M-89047 was a valid study.

The licensee acknowledged that the wording of the TS amendment may

have been misleading. The licensee hired an independent contractor

to validate study M-89047. The contractor, Tetra Engineering Group,

concluded that study M-89047 contained valid data. In addition, the

licensee refined the study to use all the increasing data points.

The inspector questioned the omission of the decreasing data points,

and pointed out that many instrument safety functions occur on

decreasing data points.

The licensee stated that use of only increasing data points was

acceptable because the uncertainty associated with the decreasing

data points was covered by a separate uncertainty, hysteresis. The

licensee stated that customizing the drift analyses to match the

safety function (increasing or decreasing) for each transmitter was

an unnecessary complication. The licensee noted that study M-89047

was only for long term drift and not for evaluation of the

performance of an individual transmitter.

The inspector reviewed the study validation done by Tetra

Engineering Group and the licensee's evaluation of the use of only

increasing data for drift studies. The inspector concluded that the

study provided acceptable technical information to track long term

instrument setpoint drift at SONGS. This item is closed.

d.

(Open) Unresolved Item (50-361, 50-362/91-01-09) "Instrument

Uncertainties for Emergency Operating Instructions"

The NRC I&C setpoint team determined that the uncertainties for a

number of instruments associated with Emergency Operating

Instructions were incorrectly calculated in Functional Analysis

M-89068. The licensee agreed to recalculate the instrument

uncertainties and change the EOIs as required.

As noted in Section 15.b above, the licensee performed new

calculations associated with M-89068 and determined that some

procedural changes would be required.

NRC review of the new calculations and modified procedures will be

accomplished under this Unresolved Item.

20

e. (Closed) Unresolved Item (50-206/92-20-01) Temporary Waiver of

Compliance From Technical Specification 3.3.1 For Safety Injection

Valve HV852B

On May 19,

1992, while Unit 1 was at 92% power, main feedwater (MFW)

pump discharge/safety injection (SI) isolation valve HV852B was

removed from service for corrective maintenance (reference NRC

Inspection Report 92-20, paragraph 4.a for further discussion).

Maintenance was performed on the valve accumulators to replace the

nitrogen addition valves (schrader valves) since the valves were

leaking nitrogen. The nitrogen leakage had increased until

recharging of the accumulators was performed approximately once

every three days.

The design of hydraulic valve (HV) HV852B is to open with a

pneumatic-hydraulic pump, and to close (its safety-related function)

by two nitrogen-hydraulic fluid accumulators connected to the valve

actuator. The nitrogen in the accumulators is separated from the

hydraulic fluid by a piston with seal rings. The accumulators were

modified in 1976 to use pistons to isolate the hydraulic fluid from

the gaseous nitrogen. The nitrogen in the accumulators provides the

motive force necessary to displace the hydraulic fluid from the

accumulator, which is used to move the valve to its closed SI

position. Nitrogen was added to the accumulators by connecting a

high pressure nitrogen cylinder to accumulator schrader valves

(located on top of accumulators) through a charging manifold.

On May 19,

1992, upon removal of the schrader valves from the top of

the accumulators, the positions of the pistons were measured using

reach rods. The pistons were found to be mis-aligned, one at the

top-most position of its stroke and the other at the bottom-most

part of its stroke. Operability of the valve was indeterminate at

that time. Station Technical (STEC) initiated an evaluation, but an

NCR (which was required for conditions of this type) was not

initiated until approximately one month later, on June 17, 1992.

The inspector reviewed the NCR procedure and noted that there were

no requirements with respect to timeliness of issuing NCRs for non

conforming conditions. The mis-alignment of the pistons had

occurred due to leakage from one of the accumulator schrader valves

being greater than the other.

Immediate corrective actions consisted of replacing the schrader

valves, restoring the pistons to an even alignment, recharging the

accumulators with nitrogen, and returning HV852B to service on May

19, 1992.

On June 23, 1992, STEC, in conjunction with vendor calculations,

concluded that HV852B was inoperable in the as-found condition on

May 19, 1992. Calculations performed by the vendor indicated that

with the nitrogen and hydraulic fluid volumes as found, HV852B would

have stroked closed only 95% of its required travel.

With HV852B

inoperable, Unit 1 Technical Specifications (TS) 3.3.1, "Safety

21

Injection, Recirculation, and Containment Spray Systems" required

entrance into TS 3.0.3 because TS 3.3.1 did not provide an action

statement for the inoperability of HV852B. Technical Specification 3.0.3 required HV852B to be returned to operable status within one

hour or commence a reactor shutdown. On July 23, 1992 the licensee

submitted Unit 1 Licensee Event Report (LER) 1-92-01 describing the

events surrounding the inoperability of HV852B.

Failure of valve HV852B to fully close (there is one valve per SI

train) was not a safety significant issue because downstream main

feedwater (MFW) regulating, bypass, and motor operated isolation

valves also receive a signal to close on safety injection

initiation. These downstream valves were designed to close against

full system pressure, were incorporated into the valve inservice

testing program, were safety-related valves, and would close in a

time frame similar to HV852B. The inspector reviewed records for

previous stroke time testing of these valves and found them to be

satisfactory. Therefore, in the event of a failure of the HV852

valves to fully close, flow to the SGs would have been isolated by

the MFW regulating, bypass, and motor operated isolation valves.

The inspector noted that valves HV854A,B and HV852A,B (four valves

total) are of the dual accumulator design. Without a surveillance

program to monitor the piston position in the accumulators, there

was a potential for all four valves to be affected similarly by

continued nitrogen leakage. Valves HV854A,B and HV852A were

verified in June 1992 to have the accumulator pistons in such a

position that valve operability was not affected. In addition,

there had been no excessive nitrogen leakage noted by licensee

personnel of the accumulators for these valves.

The inspector noted that had one of the HV854 valves been found not

able to fully close (one HV854 valve per SI train), this would have

been much more significant.

The HV854 valves close on SI actuation

to preclude injecting unborated water from the condenser into the

reactor coolant system (RCS). A failure of the HV854 valves to

fully close would have prevented injection of borated water from the

refueling water storage tank to the RCS.

This was because the HV851

(SI outlet valves to RCS) valves were interlocked such that they

would not open until the HV854 valves were fully closed.

Based on the events associated with HV852B and the review of LER 50

206/92-01, the inspector had the following concerns:

o

Vendor manuals and maintenance procedures did not provide

adequate information for on-line charging of the HV

accumulators (HV851, HV852, HV853, and HV854) in that the

information provided was based on maintenance being done in the

maintenance shop rather than in the field.

"

Even with vendor assistance, when developing the initial

accumulator recharging procedures in 1986, the potential for

22

piston mis-alignment as the result of accumulator leakage was

not recognized.

The knowledge level of the personnel evaluating the condition

of HV852B was insufficient to identify that excessive leakage

could affect piston positions and stroke time, and therefore

valve operability. The inspector noted that early discussions

with personnel indicated that the repeated charging was

considered to be acceptable.

o

The potential impact of the increased accumulator charging

frequency was not discussed with the vendor until May 1992.

o

Neither vendor nor SCE instructions identified the importance

of checking accumulator piston location, especially regarding

frequent accumulator recharging. There were no programs, such

as routine surveillances, to check piston locations.

Such

activities would have clearly identified degrading conditions

(i.e., accumulator pistons changing locations).

Further, the

inspector noted that the licensee had no formal program to

check sub-components of equipment to ensure that they will

function properly.

o

On June 17, 1992, a Temporary Waiver of Compliance was

requested to regain lost margin for the HV851A accumulator

piston due to leakage from the hydraulic oil side of the

accumulator (for further discussion reference NRC Inspection

Report 92-20, paragraph 4.b).

Prompt verification of other

accumulator piston locations, after HV852B was discovered in an

inoperable condition, would have identified that HV851A was

degrading due to hydraulic oil leakage earlier.

The inspector concluded that the increased accumulator leakage and

repeated charging was not recognized by SCE as a condition which

could affect valve operability. In addition, an NCR to evaluate the

as found condition of HV852B was not written for almost one month.

Also, other MFW and SI accumulator piston locations were not

determined until over one month after discovering HV852B in its

degraded condition. While the actual safety significance of the

valve inoperability is low as described above, the inspector

considered that the inoperable condition of HV852B as found on May

19, 1992, was a violation in that the licensee actions were

inadequate to quickly identify and correct the degraded condition of

HV852B (50-206/92-23-05).

Additionally, the inspector noted that there was not a formal

program to check the sub-components of the accumulators. In the

absence of knowledge as to the impact of nitrogen leakage and in the

lack of a surveillance program to monitor accumulator piston

locations, HV852B continued to degrade over a three month period.

One violation was identified.

23

16.

Follow-Up of Items of Non-Compliance (92702)

(Closed) Violation (50-361, 50-362/91-01-07) "Inaccurate Technical

Information in a Technical Specification Amendment Request"

The NRC I&C setpoint team found that the licensee had submitted TS

Amendment requests based on incorrect engineering calculations.

These calculations were contained in Functional Analysis M-89068.

The licensee subsequently withdrew the amendment request. The

licensee determined that Functional Analysis M-89068 had not

received the normal engineering and quality review required for

engineering calculations.

The licensee issued changes to Engineering, Safety and Licensing

Department Procedures 24-7-15, Revision 7, PCN 3, "Preparation and

Verification of Design Calculations, and 24-10-9, Revision 3, PCN 2,

"Design Process Flow and Controls SONGS 1, 2 & 3."

These changes

specified that studies and analysis used as official documents shall

have formal engineering and quality reviews.

The inspector reviewed the administrative document changes and

concluded that the changes required adequate engineering and quality

review; therefore, this item is closed.

Technical issues associated with the errors in Functional Analysis

were discussed in Paragraph 15.b, Unresolved Item (50-361,

50-362/91-01-06).

Final NRC review of new calculations and

operating procedures associated with Functional Analysis M-89068

will be performed during review of Unresolved Item (50-361,

50-362/91-01-09).

17. Meeting with Southern California Edison (SCE)

Managers in Region V Office

On August 18, 1992, SCE managers, M. Short, R. Rosenblum, B. Carlisle,

and G. Hammond, came to the NRC Region V Office to discuss some recent

technical issues occurring at San Onofre. The NRC personnel present for

the discussions were K. Perkins, H. Wong, and D. Chaney. The issues

discussed included the Unit 3 pressurizer level instrument line leak, a

temporary modification to the containment purge system, and re

organization of the Station Technical engineering organization. The SCE

handouts used in this meeting are attached.

Mr. Perkins discussed the need for making conservative operating

decisions and encouraged continued open exchange of information between

all groups. Mr. Perkins also emphasized that early discussion of issues

was important in order for the NRC to be able to completely understand

the development of the issue. The SCE personnel agreed and to the extent

possible would do so. Mr. Perkins stated that the meeting was beneficial

in understanding more fully the technical issues and also the SCE thought

process in dealing with these issues.

24

18. Unresolved Item

Unresolved items are matters about which more information is required to

determine whether they are acceptable items, violations or deviations.

Unresolved items addressed during this inspection are discussed in

paragraph 12 of this report.

19.

Exit Meeting

On August 26, 1992 an exit meeting was conducted with the licensee

representatives identified in Paragraph 1. The inspectors summarized the

inspection scope and findings as described in the Results section of this

report.

The licensee acknowledged the inspection findings and noted that

appropriate corrective actions would be implemented where warranted. The

licensee did not identify as proprietary any of the information provided

to or reviewed by the inspectors during this inspection.

25

SAN ONOFRE UNIT 3 PRESSURIZER INSTRUMENT

VALVE CANOPY SEAL LEAK

INTRODUCTION:

o

on 6/14/92, Pressurizer Level Anomoly in Y Channel

o Transmitter Replaced and Channel Returned to Service

o

On 7/20/92, Pressurizer Level Control Anomoly in Y

Channel

o

Performed:

Loop Check/Calibration -

No Problems Identified

ECAD -

No Relevant Problems Identified

o Attempts to Re-Calibrate Transmitter In Containment

Identified Feedback Coil Misaligned

o Replaced Transmitter

o

5.5% Deviation Still Present

o

Suspected Deviation Due to Leak In Reference Leg

STATION TECHNICAL DIVISION

SHORT, M. P.

Manager,

Technical

PENSEYRES. P. H.

HERSCHTHAL. M. A.

Assistant Technical

Special Projects

Manager

PLAPPERT, R. D.

HIRSCH, J. F.

NIEBRUEGGE, D. A.

HETRICK. S. J.

Technical Support

Power Generation

NSSS Engineering

Computer & Reactor

& Compliance

Engineering

VANDENBROEK, J.

CLARK. R.

SIMPSON. J.

RAMENDICK, D.

NRC Reporting Group

Turbine Cycle

Electrical

Reactor Engineering

POWERS, D.

TUTTLE. D.

LYLE, J.

HARALSON. P.

STAs

Balance of Plant

Nuclear Systems

Information Systems

WATTSON, P. C.

BLAKESLEE, P.

QUIGLEY. N.

MITCHELL, R.

Technical Support

Heat Removal

Mechanical

Control Systems

STEPHENSON, J. 1

SCHOFIELD, P.

IRVINE, D.

KURTZ, A.

FREY. D.]_______

___

Oug

C

Dit

Performance Monitoring

Codes & Welding

Computer Tech.

Outage Coordination

9

CAROSSINO, C.

WINSLOW, J.

Special Projects

I&C

OL7/

7192

TYPICAL PRZR. INSTR. NOZZLE CONFIGURATION

PRZR SHELL

In. 690 NOZZLE

CONDENSING POT

LOCA LIMITER

MR043: ROOT VALVE

WELD

LOCATIONS

ASMEIII, CLASS2

ASMEIII, CLASS2

3/4" COUPLING

6000# SW

BRAIDED FLEXIBLE

CONNECTOR

MANIFOLD

EQUALIZING

VALVE

MRO41: ROOT VALVE

110/1

LT

ISOLATION

TRANSMITTER

@

VALVES

UNIT 2 CONTAINMENT PURGE EXHAUST INTRODUCTION

BACKGROUND

TEMPORARY FACILITY MODIFICATION

PLANS TO CORRECT CAUSE OF LLRT FAILURE

LONG TERM CORRECTIVE ACTIONS

Containment

Blank Flanges

To Plant Purge Stack

Inside

l Outside

Installed

Radmonitor and Stack

Close on

CPIS

_

_

_

_

_

_

_

_

HV-9950HV-9951

HV-9950

42911

Exhaust Fan Unit

-

19

-i

n

42"

HV-9824

-9825

Exhaust Fan Unit

Close on

Cone Diffuser with

I

CPIS CIAS, SIAS

Debris Screen

Containment Purge Exhaust System

0a

BACKGROUND - APPLICABLE TSs

(Modes 1 through 4)

Technical Specification

Limiting Conditions

Action Requirement(s)

for Operations

3.6.1.7, Containment Ventilation

a.

42" purge valves maintained

a.1

Close / blind flange in 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, else

System

closed

Mode 3 in next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 in

next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

b.

8 " mini purge valves closed to

a.2

If open for other than allowable, close or

the maximum extent practicable

blind flange in 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, else Mode 3 in

next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 in next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />

b.

If a 42" or 8" isolation valve leakage

exceeds 0.05 L. at P. during LLRT, fix or

blind flange in 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, else Mode 3 in

next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 in next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />

3.6.3, Containment Isolation

Maintain Valves Operable

Restore to operability or isolate penetration in

Valves

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, else Mode 3 in next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and

Mode 5 in next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />

3.6.1.2, Containment

Combined leakage < 0.75 L. at P.

Prior to RCS temperature exceeding 200 F (i.e.,

Leakage

LLRT Leakage < 0.6 L. at P.

if exceeded in Modes 1 - 4, enter TS 3.0.3 - Fix

in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, else Mode 3 in next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode

5 in next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />)

3.6.1.1, Containment Integrity

L, < 0.6 at P.

Fix in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, else Mode 3 in next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and

Mode 5 in next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />

Containment Wall

Inside

Outside

HV-9950

O

42"

0

HV-9951

HV-9824

HV-9825

8-Inch

8-Inch

-4---- Pressure Assisted Shutoff Side of Valve

--

Side Pressurized For Quarterly LLRT

Special LLRT with Blank Flange Installed

Performed Each Refueling Outage

Containment Purge Exhaust Penetration

42" VALVES

T - RING

COMPRESSION RING

ALVE BODY

ADJUSTION

SETSCREW

ALVE DISC

RETAINING RING

RETAINING RING SCREW

42 INCH VALVE T-RING DETAILS

8" VALVES

T - RING

SINGLE FLANGE

VALVE BODY

BUTTWELDING END

0

-RINGCONNECTION

RTINING -7

RING

COMPRESSION

.VV

DIS

RING,

.DISC

STOP WITH

ADJUSTING SET SCREW

RETAINING

RING SCREW

ADJUSTING

SETSCREW

8 INCH VALVE T-RING DETAILS

LLRT History Summary - Purge Supply and Exhaust Penetrations

o

Prior to March 30, 1992, Only Sporadic LLRT failures

o

Most Common Cause of LLRT Failures:

Valve stroke problems

T-Ring wear and adjustment problems

Particulates on valve sealing surfaces (mostly exhaust penetration)

BACKGROUND

PURGE EXHAUST PENETRATION 1992 LLRT HISTORY

3/30

Routine Quarterly LLRT Failed

Entered Penetration to Adjust Outboard 42-inch Valve T-Ring

Apr/May

Vented Containment Through Exhaust Penetration Seven Times.

6/9

Routine LLRT Failed.

Corrected by blowing particulates from mini-purge valve seats.

BACKGROUND

PURGE EXHAUST PENETRATION 1992 LLRT HISTORY - Continued

6/16-17

Performed special LLRTs on Penetration

Performed as Found LLRT, With Virtually No Leakage.

Vented Containment.

Performed As-left LLRT.

Leakage Exceeded 3 Times 0.05 La

Blew Particulates From HV-9825 and HV-9824 Seats.

Probable Cause of Valve Failure Determined To Be Particulates

BACKGROUND

PURGE EXHAUST PENETRATION 1992 LLRT HISTORY - Continued

7/2

Performed Pre-venting LLRT, With Virtually No Leakage Found.

Containment Vented.

Post-Venting LLRT Found Excessive Leakage.

Blew Off Valve Seat of HV-9825 - LLRT Satisfactory.

Postulated That Particulates Originated Within The Penetration

And Not Within Containment.

7/10

7/2 Test Repeated At Reduced Pressure And Flow.

Confirmed That Failures Caused By Particulates From Inside The

Penetration.

BACKGROUND

PURGE EXHAUST PENETRATION 1992 LLRT HISTORY - Continued

7/30-31

Implemented TFM To Bypass Purge Penetration In Order To

Vent Containment For Pressure Control.

8/2

TFM Placed Into Service

TFM

PRA RESULTS

CASE#

SYSTEM

OPERATING

SIGNIFICANT

TIME

OFF-SITE

RELEASE RISK

1

MINI-PURGE

4hrs/20days

7.6E-1 1/yr

2

MINI-PURGE

1 000hrslyr

1.OE-9/yr

3

MINI-PURGE

CONTINUOUS

9.OE-9/yr

4

TFM

4days/20days

1.OE-1 0/yr

5

TFM

CONTINUOUS

5E-10/yr

Containment

Blank Flanges

To Plant Purge Stack

Close on

Inside

Outside

Installed

Radmonitor and Stack

CPIS

HV-9950

(~HV-9951

42.

Exhaust Fan Unit

42"

2

HV-9824

9HV-9825

E

F

18"

8.

~N

Close on~

Close on Hi Plant Purge Stack Radiation

Cone Diffuser with

Close on

Debris Screen

CIAS SIAS, (CPIS)TFM

Close on

i

CIAS, *CPIS

Rad Monitor 704

SIAS

>308

S3J

Close on

HV-7801

i

HV-7800

CIAS

SIAS

s

Signals Added by TFM

RSignals

Removed by TFM

Containment Venting After TFM Implementation

NUCLEAR REGULATORY AFFAIRS DIVISION

uIoitrI

-DI~S

MIS : i. V .L

GOMfN E, ?A

BlEILLbsK.

ht

KLAf'KA, R .1

MfAWR.lE. r.

OiUBSON, G,. 7.I

AI.IMoaIfl

a. F..

KIE

J -ING. F-S.

IISFIYJ.

Suporv.sof,

14muagoe,

UR

V10,

G 0.oyur

uooor

lwIi~rlwjMrlo

a

.ms-u111.-o

Env~nngan~1

Enr~~ji~cy 'iiiim N~o~r~~n

l~gtn~tii nuconjr C;umrnwimfcvtnn

GOI-McIng lUiiili nso ijucloaf icomiuiU

l~ibi 1)

UI2d

MISSION STATEMENT

The mission of Station Technical (STEC) is to provide

expert engineering support in the day-to-day operation and

maintenance of San Onofre Nuclear Generating Station

(SONGS). This support ensures that plant systems,

components, structures (hereafter termed "systems"), and

programs achieve a level of performance meeting or

exceeding those requirements in Technical Specifications,

the FSAR, other rules and regulations, the approved design

basis, and management goals.

Deviations from these requirements are identified in the

day-to-day operation and maintenance of SONGS. STEC's

mission is to assess the impact and determine the causes

of these deviations. When necessary, STEC performs

temporary or minor modifications to the systems and

programs in support of SONGS day-to-day operations and

maintenance.

Many of the system and program requirements are not

easily understood and usable by operations and

maintenance. STEC's mission also includes interpreting

the system and program requirements and providing

usable guidance to support SONGS operations and

maintenance.

Manager

Station Technical

Connie Shelton

Secretary

Mark A. Herschthal

Allen J. Thiel IllJh

.HishDnldN*Ivn

Nuclear Systems

.

Electrical Systems

Engineering

Engineering

Power Generation

Technical Services

Dave A. Niebruegge

Jim C. Winslow

Dave W. Tuttle

Paul E. Schofield

NSSS

I&C Engineering

Balance of Plant

Performance Mon.

Neal J. Quigley

Joe Simpson

Paul P. Blakeslec

Vacant

NSSS Mechanical

- Electrical Engineering J

Heat Removal

Codes & Welding

Jim M. Lyle

Steve J. Hetrick-

Ransey C. Clark]

D. Frey/J. Stephenson

NSSS Aux,.

Computer Engineering

Turbine Cycle

Outage Support

Vacant

Roger V. Mitchell

Patrick C. Wattson

Nuclear

Control Systems

Technical Support

S Danny K. Powers

Percy B. Haralson

Carlos A. Carossino

Sta. Tech. Advisors

Info. Systems

j

Prog ra ms

-David J. Ramendick

A. Kurtz/D. Meiner

Reactor Engr.

Computer Maint.

Pete H. Penseyres

Integ. Plant Ops

08/17/92

TECHNIC

IVISION

NUCLEAR SYSTEMS ENGINEERING

SOUTHERN CAUFORNIA EDISON

Mark A. Herschthal

Manager

Nuclear Systems Engineering

89301

San Onofre Nuclear Generating Station

Dave Niebruegge

Vacant

Pete H. Penseyres

NSSS Systems Supervisor

Reactor Engineering &

Integrated Plant

86103

STA Supervisor

Operations

FI

Neal J. Quigley

Jim M. Lyle

David J. Ramendick

Danny K. Powers

NSSS Mechanical

NSSS Auxillary

Reactor Engineering

Sta. Tech. Advisors

86746

89425

88704

89155

Bob Conoscenti

86807

Joe Blake

89159

Jay Iyer

RE 89156

UNIT 1

UNITS 213

Paul Leibowitz (5)

89074

David Brenner

86696

Greg Keney

RE 88734

John IV. Ryder

86859

Wayne Marsh

88701

Pete Bruno

86903

Bill Lilly (5)

RE 89096

Randall T. Benson

89802

Russ Nielsen

89214

Sal Dolcemascolo (5) 89317

Robert Margolis (5) RE 88703

Dean R. Goodwin

89129

Robin I. Baker (6)

86790

Kieth Reeser

86138

Kevin Flynn

89212

Aaron Smookler (1) RE 89096

Mark B. McKinley

89170

Michael L. Barr (6)

86839

Dwayne Roberts

89206

Dan Higgins

89211

Rogelio Soto

RE 89592

Steven E. Ross

86154

Gary L. Johnson Jr. (6) 89160

Jim Rudolph

89791

John E. Hughes

87022

Vacant (1)

Kevin C. Wood

89316

Calvin Meddings (6)

85153

Jo Tore

(1) 89493

7

Joe Toffes (1)

89493

Dale Wickman

86152

John W. Perkins (6)

89178

Beatle Tran (1)

89493

Rick Zbavitel

89135

Charlie Eischen (5)

86159

Mike Vezzuto

86759

(1) Part Time

(2) Temporary

Don Steannan 87303

(3) Cross-training

Division Office Administrator

(4) Leave Of Absence

Approve

PARL

LRS(5)

Contractor

M~ark A. flerschithal

PAYROLL CLERKS

Rosle Razo

(187) 89542

(6) Sta Trainee

Sharon AnDlaott (189) 88272

RE

M

Reactor Engineer

SDI

n

8/17/92

TECHNI MFIVISION

POWER GENERATION ENGINEERING

SOUTHERN CAUFORNIA EDISON

John Hirsch

Supervisor

Power Generation

86278

1San

Onofre Nuclear Generating Station

jean Gomez

Vacant

-.......

Secretary

Special Projects

89318

Ransey Clark

David Tuttle

Paul Blakeslee

Turbine Cycle

Balance of

Heat Removal

89169

8674989215

Juan Armas

89233

Aeri Daniels

86090

Marco Ahunada

86360

Russ Chetwynd

89703

G. Gwiazowski (3)

89985

Don Ashcraft

86210

Danny Lowenberg

86755

Henry Jones

89704

Johnson Cheng

89793

Antonio Molina

89153

Ty Kent

86205

Keith Chong

89017

Mark Mountford (1) 89479

Al Ockert

89828

Russ Cobb

86664

Dan Nougier

86742

Judy Peck (1)

85170

Bruce Friedberg (1) 86083

Bernie Phillips

89381

Tom Peterson

89706

Bill Hines (1)

89362

Guy Shelton

89783

Bill Poirier

89198

Murray Jennex

86787

Eric Schoonover (1) 85119

Jerome Marr

86041

Del Smith

86743

Steve Roberts

89139

Kevin Trout (1)

86289

Jorge Valdivia

86218

John Watkins

89829

(1) Part Time

Don Stearman 8730s

(2) Temporary

Division Office Administrator

(3) Cross-training

PAYROLL CLERKS

(4) Leave Of Absence

Rosle Razo

(187) 89542

(5) Contractor

HShift

Technical Advisor

DB 8/1792

TECHNIC

IVISION

TECHNICAL PROGRAMS SUPPORT

SOUTHERN CALIFORNIA EDISON

Donald N. Irvine

Supervisor

Technical Programs Support

89368

.San

Onofre Nuclear Generating Station

SeDaneleEaFre

Paul Schofield

Vacant

Patrick C. Wattson

Carlos A. Carossino

Daniel E. Frey

Performance Monitoring

Codes and Welding

Station Technical

867032

I

86752

89634

Jerry L. Stephenson

Chuck Elliott

86747

Jorge Blanco (1)

85114

Sean D. Baker (1)

89036

Outage Representative

Chuck

Ellot

864oreSaio

n T echn'ical

JimHedeson

8924

Letci Bambla

8960

Julius L. Bognar

86586

Seanio

TecBker(i)c903

Jim Henderson

89324

Leticia Brambila

89560

James M. Davison

89119

Jonn R. Beeson

89906

86702

Vic Herrera

89154

Dan Brown

86221

Cary L. Johnson Sr. 89037

Sarah J. Cobb (5)

85127

Sue Knowlton (1)

85179

Ken Collins (5)

89869

Marie L. Tarango

89165

Vacant (1)

Mike O'Halloran (5) 89985

Roger Holmes

89103

Mike Schwaebe

86744

Bill Lazear

89010

G. Winterscheid (1)

89985

Al Meichler

89210

Clerical Support:

Richard G. Allen

Les Ousley

89588

eCc

Support

Robert Sears

89104

RCM Support

Ramona S. Berry

89813

89604

In Service Testing

Jerry Valsvig

88953

James N. Hess

86885

Paul Croy

86386

Clerical Support:

Sherry M. Kunz

89483

David Chiang (5)

89013

Vacant

Clerical Support:

Shirley Wright

89164

(1) Part Time

Jeanine Smith

89140

Steanan

IrSs

(2) Temporary

Approved_

eanSt 84Dvuubon

Office Admnistarator

(3) Cross-training

Donald N.rvine

PAYROLL CLERKS

(4) Leave Of Absence

Rosle Razo

(187) 89542

(5) Contractor

Sharon Anstaett (189) 88272

(*) Shift Technical Advisor

SDB 8/17/92

TECHNIM DIVISION

S~tER

CUFRNA

DIONELECTRICAL

SYSTEMS ENGINEERING

SOUTHERN CAUFORNIA EDISON......

Allen J. Thiel

Manager

Electrical Systems Engineering

87048

87048_

_

San Onofre Nuclear Generating Station

Jim Winslow

Vcn

tv

erc

Instrumentation &

Vaetrcanirn

g

Soptee Hneeri

Controls Engineering

SystrmslEninerig0oter

EngMne

86584873

Usoalii Afaese

Secretary

88720

Roger V. Mitchell

Percy B. Haralson

Allen Kurtz 89833

Control Systems

Information Systems

Dan Meiner 86425

89801

F

88723

Computer Maintenance

__________

___________

_________

__________Lowell

Skinner Plan186982

Bud Bostian

88724

Paul Battish

89067

Joe Aguirre

86345

Steve Atkins

88415

Operator PAX 86410

Steve Foglio

89137

Bill Brush

89131

Mike DePano (1)

85165

Bob Boyer

89848

Tech PAX 87644

Don Frapwell

87411

Tom Graham

89179

Gale Generoso (1)

85165

G. Castellanos

88719

Shreyas Gandhi (1) 89557

Susan Hower (1)

89342

Ken Hooper

86994

Timothy Ford

88702

Lorraine Holmes

Oper

Chuck Hallett (5)

85125

Charles Kim (1)

89342

Wayne Thomas

89665

Chuck Kluz (1)

88721

Debra Knights

Oper

Gerry Lear

86703

Larry Mueller (5)

89493

Dave Knights

88728

Lani Majchrowicz

Oper

Russ Neal

89681

Ami Samanta

86705

Rory Job (1)

85165

Mark Tomlinson

Oper

Mike Root (5)

86656

Gary legich

89072

Frances Williamson

Oper

Lance Rushing (1)

85171

Paul Anderson

Tech

(1) Part Time

Mike Chandler

Tech

(2) Temporary

Ed Collins

Tech

(3) Cross-training

Charles H-ardin

Tech

(4) Leave Of Absence

Jeff Headlee

-Tech

(5) Contractor

LaryH')

Tc

Don Stearman 87303

N Shf T

l

Division Office Administrator

Approved

Tony Moreno

Tech

PAYROLL CLERKS

Oper-Computer Operator

Alle i J. Thiel

Mirk Nowak

Tech

Rosle Razo

(187) 89342

Tech-Computer Technician

Steve Schultz

Tech

SharB Anstiell (1B9) 88272

MDB

8/17/92

Bob Sorge

Tech

O ROOT VALVE MR043

'

in Carbon

Steel

Canopy

Seal Weld

Diaphragm

,_

Seal Weld

I

I

Class:

1500

Design

Pressure:

2485 psig @ 700 deg F