ML12031A265

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IR 05000331-11-005, on 10/01/2011 - 12/31/2011; Duane Arnold Energy Center; Operability Determinations and Functionality Assessments and Identification and Resolution of Problems
ML12031A265
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 01/31/2012
From: Ring M
NRC/RGN-III/DRP/B1
To: Wells P
NextEra Energy Duane Arnold
References
IR-11-005
Download: ML12031A265 (45)


See also: IR 05000331/2011005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

January 31, 2012

Mr. Peter Wells

Vice President

NextEra Energy Duane Arnold, LLC

3277 DAEC Road

Palo, IA 52324-9785

SUBJECT:

DUANE ARNOLD ENERGY CENTER - NRC INTEGRATED INSPECTION

REPORT 05000331/2011005

Dear Mr. Wells:

On December 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Duane Arnold Energy Center. The enclosed inspection report documents the

inspection results which were discussed on January 12, 2012, with you and other members of

your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

One NRC-identified traditional enforcement Severity Level IV violation and two

self-revealed findings of very low safety significance (Green) were identified during this

inspection. The two findings were determined to also involve violations of NRC requirements.

Further, a licensee-identified violation, which was determined to be of very low safety

significance, is listed in this report. The NRC is treating these violations as non-cited violations

(NCVs) consistent with Section 2.3.2 of the NRC Enforcement Policy.

If you contest these non-cited violations, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the

Regional Administrator, Region III, the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Duane Arnold Energy Center.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region III; and the NRC Resident Inspector at the

Duane Arnold Energy Center.

P. Wells

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Mark Ring, Branch Chief

Branch 1

Division of Reactor Projects

Docket No. 50-331

License No. DPR-49

Enclosure:

Inspection Report 05000331/2011005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-331

License No:

DPR-49

Report No:

05000331/2011005

Licensee:

NextEra Energy Duane Arnold, LLC

Facility:

Duane Arnold Energy Center

Location:

Palo, IA

Dates:

October 1 through December 31, 2011

Inspectors:

L. Haeg, Senior Resident Inspector

R. Murray, Resident Inspector

R. Orlikowski, Project Engineer

R. Edwards, Reactor Inspector

J. Beavers, Emergency Preparedness Inspector

M. Mitchell, Health Physicist

Approved by:

Mark Ring, Branch Chief

Branch 1

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 1

REPORT DETAILS ....................................................................................................................... 4

Summary of Plant Status ........................................................................................................... 4

1.

REACTOR SAFETY ....................................................................................................... 4

1R01

Adverse Weather Protection (71111.01) ............................................................. 4

1R04

Equipment Alignment (71111.04) ........................................................................ 5

1R05

Fire Protection (71111.05) .................................................................................. 5

1R11

Licensed Operator Requalification Program (71111.11) ..................................... 6

1R12

Maintenance Effectiveness (71111.12) ............................................................... 7

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13) ......... 8

1R15

Operability Determinations and Functionality Assessments (71111.15) ............. 9

1R19

Post-Maintenance Testing (71111.19) .............................................................. 10

1R22

Surveillance Testing (71111.22) ....................................................................... 11

1EP4

Emergency Action Level and Emergency Plan Changes (71114.04) ............... 12

1EP6

Drill Evaluation (71114.06) ................................................................................ 13

2.

RADIATION SAFETY ................................................................................................... 13

2RS1

Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 13

2RS2

Occupational As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and

Controls (71124.02) .......................................................................................... 19

4.

OTHER ACTIVITIES ..................................................................................................... 20

4OA1

Performance Indicator Verification (71151) ....................................................... 20

4OA2

Identification and Resolution of Problems (71152) ........................................... 22

4OA3

Follow-Up of Events and Notices of Enforcement Discretion (71153) .............. 27

4OA5

Other Activities .................................................................................................. 28

4OA6

Management Meetings ...................................................................................... 29

4OA7

Licensee-Identified Violations ........................................................................... 29

SUPPLEMENTAL INFORMATION ............................................................................................... 1

Key Points of Contact ................................................................................................................ 1

List of Items Opened, Closed and Discussed ............................................................................ 2

List of Documents Reviewed ..................................................................................................... 3

List of Acronyms Used .............................................................................................................. 9

1

Enclosure

SUMMARY OF FINDINGS

IR 05000331/2011005, 10/01/2011 - 12/31/2011; Duane Arnold Energy Center; Operability

Determinations and Functionality Assessments and Identification and Resolution of Problems.

This report covers a three-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. One Severity Level IV violation was identified by

the inspectors and two Green findings were self-revealed. The violation and findings were

considered NCVs of NRC regulations. The significance of most findings is indicated by their

color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A.

NRC-Identified and Self-Revealed Findings and Violations

Cornerstone: Initiating Events

Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed on

August 11, 2011, when both river water supply subsystems were rendered inoperable

following a sediment intrusion event. Specifically, the cause of the event was attributed

to the cancellation of a river bed survey that would have identified the increased

sediment buildup requiring increased monitoring and corrective actions (dredging, sand

pumping, and/or structural repairs). The cancellation of the river bed survey work order

was contrary to the requirements of Administrative Control Procedure 1208.3,

Preventive Maintenance Program, that required management approval prior to

cancelling the work order that was tied to the corrective action program. This issue of

concern was documented in the licensees corrective action program as condition report

01676836. Corrective actions included revision to affected river survey work orders to

ensure that they could not be cancelled without adequate review and approval, and

completion of river dredging and repairs to the upstream spur dikes.

The inspectors determined that the issue of concern represented a performance

deficiency because it was the result of the licensees failure to meet a procedural

requirement, and the cause was reasonably within the licensees ability to foresee and

correct and should have been prevented. The performance deficiency was determined

to be more than minor and a finding because it was associated with the Initiating Events

Cornerstone attribute of equipment performance, and it affected the cornerstone

objective to limit the likelihood of those events that upset plant stability and challenge

critical safety functions during power operations. The inspectors applied IMC 0609,

Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, to this

finding. Because the finding did not contribute to both the likelihood of a reactor trip and

the likelihood that mitigation equipment or functions would not be available under the

Initiating Events Cornerstone column of Table 4a, the finding was determined to be of

very low safety significance (Green). The inspectors determined that the contributing

cause that provided the most insight into the performance deficiency was associated

with the cross-cutting aspect of Human Performance, having Decision Making

components, and involving the licensee making safety or risk-significant decisions using

a systematic process, including formally defining the authority and roles for decisions

2

Enclosure

affecting nuclear safety. Specifically, several decisions were made with respect to spur

dike repairs and river monitoring; however, the requisite organizational reviews and

approvals associated with the river were not performed to ensure appropriate actions

were taken. H.1(a) (Section 4OA2.4)

Cornerstone: Barrier Integrity

Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed on

October 31, 2011, when operators failed to follow Operating Instruction 999,

Reactor Building Crane. Specifically, this error resulted in the reactor building (RB)

crane striking the Independent Spent Fuel Storage Installation (ISFSI) inspection stand.

Immediate corrective actions included performing inspections of the dry storage

container transfer cask, ISFSI inspection stand, and reactor building crane.

The inspectors determined that attempting to move the crane over the ISFSI work

platform while the hand rails were installed was contrary to the RB crane operating

instruction and was an issue of concern. Failing to follow the RB crane operating

instruction was a performance deficiency because it was the result of the licensees

failure to meet a procedural requirement, and the cause was reasonably within the

licensees ability to foresee and correct and should have been prevented.

The performance deficiency was determined to be more than minor and a finding

because, if left uncorrected, the performance deficiency would have the potential to lead

to a more significant safety concern. Specifically, not following the RB crane operating

instructions could lead to a more significant event or cause damage to safety-related

equipment. The inspectors determined the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, Attachment 0609.04,

Phase 1 - Initial Screening and Characterization of Findings, Table 4a for the Barrier

Integrity Cornerstone. Because the finding only affected the fuel barrier, the finding was

determined to be of very low safety significance (Green). The inspectors determined

that the contributing cause that provided the most insight into the performance deficiency

was associated with the cross-cutting aspect of Human Performance, having Work

Control components, and involving appropriately coordinating work activities by

incorporating actions to address the need to keep personnel apprised of work status, the

operational impact of work activities, and plant conditions that may affect work activities.

Specifically, the licensee did not implement appropriate work controls to ensure the hand

rails of the ISFSI inspection stand were removed prior to moving the crane for an activity

that was not associated with the ISFSI project. H.3(b) (Section 4OA2.5)

Cornerstone: Other

Severity Level IV. A Severity Level (SL) IV NCV of 10 CFR 50.72(b)(3)(v)(B) was

identified by the inspectors for the licensees failure to report within eight hours a

condition that, at the time of discovery, could have prevented the fulfillment of the

Residual Heat Removal (RHR) system Low Pressure Coolant Injection (LPCI) safety

function. Specifically, on December 2, 2011, a sizable void was identified in the B LPCI

discharge injection line resulting in the LPCI mode of RHR being declared inoperable.

The licensee documented the issue into their corrective action program (CAP), reported

the condition to the NRC on December 8, 2011, and, was in the process of reviewing the

cause of the issue to determine additional corrective actions.

3

Enclosure

The inspectors determined that the issue of concern represented a performance

deficiency because it was the result of the licensees failure to meet a regulatory

requirement, and the cause was reasonably within the licensees ability to foresee and

correct and should have been prevented. Because the performance deficiency is

considered to potentially impede or impact the ability of the NRC to perform its

regulatory oversight function, the performance deficiency was dispositioned using the

traditional enforcement process. Per NRC Enforcement Policy, Section 6.9.d.9, failing to

make a report required by 10 CFR 50.72 is categorized as an example of a Severity

Level IV violation. Additionally, because the violation was entered into the licensees

CAP, compliance was restored in a reasonable period of time, and was not repetitive or

willful; this violation is being treated as a non-cited SL IV violation, consistent with

Section 2.3.2 of the NRC Enforcement Policy. Because the performance deficiency was

not considered a finding using IMC 0612, Appendix B, Issue Screening, and did not

impact the Reactor Oversight Process Cornerstones of Safety, a cross-cutting aspect

was not assigned. (Section 1R15)

B.

Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee was

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees CAP. The violation and condition report is listed in

Section 4OA7 of this report.

4

Enclosure

REPORT DETAILS

Summary of Plant Status

Duane Arnold Energy Center (DAEC) operated at full power for the entire inspection period

except for brief down-power maneuvers to accomplish rod pattern adjustments and to conduct

planned surveillance testing activities.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1

Winter Seasonal Readiness Preparations

a.

Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect risk-significant systems from the effects of adverse weather. Documents for

the selected systems were reviewed to ensure that the systems would remain functional

when challenged by inclement weather. During the inspection, the inspectors focused

on plant-specific design features and the licensees procedures used to mitigate or

respond to adverse weather conditions. Additionally, the inspectors reviewed the

Updated Final Safety Analysis Report (UFSAR) and performance requirements for

systems selected for inspection, and verified that operator actions were appropriate as

specified by plant specific procedures. Cold weather protective components, such as

heat tracing and area heaters, were verified to be in operation where applicable.

The inspectors also reviewed CAP items to verify that the licensee was identifying

adverse weather issues at an appropriate threshold and entering them into the CAP in

accordance with station corrective action procedures. Specific documents reviewed

during this inspection are listed in the Attachment to this report. The inspectors reviews

focused specifically on the following plant systems due to their risk significance or

susceptibility to cold weather issues:

Control Building and Pump House Heating and Ventilation systems.

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b.

Findings

No findings were identified.

5

Enclosure

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a.

Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

High Pressure Coolant Injection (HPCI) system; and

B Standby Diesel Generator (SBDG) and B Emergency Service Water (ESW)

subsystems during A SBDG surveillance testing.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders (WOs), condition reports (CRs), and the impact of ongoing work activities on

redundant trains of equipment in order to identify conditions that could have rendered

the systems incapable of performing their intended functions. The inspectors also

walked down accessible portions of the systems to verify system components and

support equipment were aligned correctly and operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the CAP with the appropriate significance characterization.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two quarterly partial system walkdown samples as defined in

IP 71111.04-05.

b.

Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

Area Fire Plan (AFP) 03 and 07; Reactor Building - HPCI, Reactor Core Isolation

Cooling (RCIC); and Elevation 786 Corridor and Laydown Area;

AFP 74 and 79; Switchyard; and ISFSI;

6

Enclosure

AFP 4, 5 and 6; Reactor Building North Control Rod Drive (CRD) Module Area,

CRD repair and CRD Cable Rooms; Reactor Building South CRD Module Area

and Offgas Recombiner Rooms and Railroad Airlock; and Reactor Building RHR

Valve Room Elevation 7576;

AFP 10, 11 and 12; Main Exhaust Fan Room, Heating Hot Water Pump Room

and the Plant Air Supply Fan Room; Reactor Building Laydown Area Elevation

833-6; and Reactor Building Decay Tank and Condensate Phase Separator

Rooms; and

AFP 20; Aux Boiler Room, Emergency Diesel Generator Rooms and Generator

Day Tank Rooms Elevation 7576.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or non-functional fire protection

equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b.

Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1

Resident Inspector Quarterly Review (71111.11Q)

a.

Inspection Scope

On October 27, 2011, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems; and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

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Enclosure

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b.

Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

.1

Routine Quarterly Evaluations (71111.12Q)

a.

Inspection Scope

The inspectors evaluated the following:

DAEC Cycle 22 Periodic Evaluation; March 2, 2009, through December 9, 2010;

and

Feedwater Heater and Moisture Separator Drain Tank level control systems.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

verifying appropriate performance criteria for structures, systems, and

components/functions classified as (a)(2), or appropriate and adequate goals and

corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

8

Enclosure

This inspection constituted two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b.

Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

Work Week 1140 risk management during RHR system maintenance,

Electro-Hydraulic Control pump replacement, and ISFSI operations;

Work Week 1141 risk management during switchyard maintenance;

161 kV Tiffin Hills line out of service for transmission system operator

modifications;

Feedwater Heater and Moisture Separator Drain Tank operational decision

making issue;

RHR system LPCI function declared inoperable due to air voiding found in LPCI

injection piping; and

Inability to retract B Traversing In-core Probe (TIP) from reactor vessel.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted six maintenance risk assessments and emergent work

control samples as defined in IP 71111.13-05.

b.

Findings

No findings were identified.

9

Enclosure

1R15 Operability Determinations and Functionality Assessments (71111.15)

.1

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following issues:

Operability evaluation for A SBDG system exhaust manifold leak;

Prompt Operability Determination (POD) for corroded Standby Gas Treatment

subsystem drain piping;

Intake structure ventilation system issues and impact on River Water Supply

(RWS) system;

River level instrumentation and intake structure sand gate position impact on

ultimate heat sink and RWS system operability; and

Void found in B RHR system LPCI discharge piping.

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR with the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors reviewed a sampling of CRs to verify that the

licensee was identifying and correcting any deficiencies associated with operability

evaluations. Documents reviewed are listed in the Attachment to this report.

This inspection constituted five operability determinations and functionality assessment

samples as defined in IP 71111.15-05.

b.

Findings

(1) Failure to Make Required Eight Hour Event Report per 10 CFR 50.72(b)(3)(v)(B)

Introduction: A Severity Level IV NCV of 10 CFR 50.72(b)(3)(v)(B) was identified by the

inspectors for the licensees failure to report within eight hours a condition that, at the

time of discovery, could have prevented the fulfillment of the RHR system LPCI safety

function.

Description: On November 18, 2011, the licensee performed a monthly surveillance test

to verify that the RHR system was full of water. The test consisted of, in part, static

venting of various portions of the system. During the venting, an abnormal amount of air

was vented from the B RHR LPCI injection piping. The licensee documented the

condition in the CAP and initiated a technical assessment for reportability (TAR) to

review past operability and reportability of the condition. At approximately 1300 hrs on

December 2, 2011, the licensee performed an ultrasonic examination of the B RHR

LPCI injection piping as part of the TAR evaluation and identified a 2-3 ft3 void within the

10

Enclosure

piping. After quantifying the void, the operations shift manager declared the LPCI

function of RHR inoperable and entered Technical Specification LCO 3.5.1, Condition B

for one low pressure emergency core cooling system subsystem inoperable (7 day

completion time to restore to an operable status). On December 4, 2011, while the

licensee continued to evaluate the significance of the void and determine corrective

actions, the inspectors were concerned that the void condition resulting in LPCI being

declared inoperable represented a condition that, at the time of discovery, could have

prevented the fulfillment of the RHR system LPCI safety function. Further, if it was a

condition that, at the time of discovery, could have prevented the fulfillment of the RHR

system LPCI safety function, the inspectors questioned why it wasnt reported to the

NRC within the eight-hour timeliness requirement of 10 CFR 50.72(b)(3)(v). The

licensee documented the inspectors questions and concerns in the CAP as CR

01714014, subsequently agreed that the condition was subject to an NRC report, and

made the report on December 8, 2011.

Analysis: The inspectors determined that the issue of concern represented a

performance deficiency because it was the result of the licensees failure to meet a

regulatory requirement, and the cause was reasonably within the licensees ability to

foresee and correct and should have been prevented. Because the performance

deficiency could potentially impede or impact the ability of the NRC to perform its

regulatory oversight function, the performance deficiency was dispositioned using the

traditional enforcement process. Per NRC Enforcement Policy, Section 6.9.d.9, failing to

make a report required by 10 CFR 50.72 is categorized as an example of a Severity

Level IV violation. Because the performance deficiency was not considered a finding

using IMC 0612, Appendix B, Issue Screening, and did not impact the Reactor

Oversight Process Cornerstones of Safety, a cross-cutting aspect was not assigned.

Enforcement: Title 10 CFR Part 50.72(b)(3)(v)(B), requires, in part, that operating

reactor licensees shall notify the NRC within eight hours of the occurrence of any event

or condition that at the time of discovery could have prevented the fulfillment of the

safety function of systems that are needed to remove residual heat. Contrary to this

requirement, on December 2, 2011, the licensee failed to report the void condition that at

the time of discovery could have prevented the fulfillment of the RHR system LPCI

safety function to the NRC within eight hours. Because the violation was entered into

the licensees CAP, compliance was restored in a reasonable period of time, and was

not repetitive or willful; this violation is being treated as a non-cited Severity Level IV

violation, consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000331/2011005-01, Failure to Make Required Eight Hour Event Report per

10 CFR 50.72(b)(3)(v)(B)).

1R19 Post-Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

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Enclosure

TIP primary containment isolation valve testing;

Standby and T1 transformers, and M breaker testing;

Main feedwater Leading Edge Flow Meter (LEFM) system testing; and

Intake structure ventilation system testing.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted four post-maintenance testing samples as defined in

IP 71111.19-05.

b.

Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

Surveillance Test Procedure (STP) 3.8.1-04B; B Standby Diesel Generator

Operability Test (Slow Start from Normal Starting Air) (Routine);

STP 3.6.1.6-01; Pressure Suppression Chamber to Reactor Building Vacuum

Breaker Operability Test (In-service test);

STP 3.7.4-01B; B Standby Filter Unit - Logic System Functional Test and

Simulated Automatic Actuation (Routine);

STP NS300002; Tracer Gas Test of Control Building Envelope (Routine); and

STP 3.5.3-04; RCIC Simulated Auto Actuation Test (Routine).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

12

Enclosure

did preconditioning occur;

were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the UFSAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers Code, and reference values were consistent with the

system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted four routine surveillance testing samples, and one in-service

test sample as defined in IP 71111.22, Sections -02 and -05.

b.

Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

Since the last NRC inspection of this program area, revisions of the Emergency Plan

and of the Emergency Action Levels were implemented based on the licensees

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Enclosure

determination, in accordance with 10 CFR 50.54(q), that the changes resulted in no

decrease in effectiveness of the Plan and that the revised Plan as changed continued to

meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The

inspectors conducted a sampling review of the Emergency Plan changes and a review of

the Emergency Action Level changes made between December 2010 and September

2011 to evaluate for potential decreases in effectiveness of the Plan. However, this

review does not constitute formal NRC approval of the changes. Therefore, these

changes remain subject to future NRC inspection in their entirety.

This inspection constituted one emergency action level and emergency plan changes

inspection sample as defined in IP 71114.04-05.

b.

Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06)

.1

Emergency Preparedness Drill Observation

a.

Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on

November 9, 2011, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities.

The inspectors observed emergency response operations in the Control Room

Simulator and the Technical Support Center to determine whether the event

classification, notifications, and protective action recommendations were performed in

accordance with procedures. The inspectors also attended the licensee drill critique to

compare any inspector-observed weakness with those identified by the licensee staff

in order to evaluate the critique and to verify whether the licensee staff was properly

identifying weaknesses and entering them into the corrective action program. As part

of the inspection, the inspectors reviewed the drill package and other documents listed

in the Attachment to this report.

This inspection constituted one emergency preparedness drill inspection sample as

defined in IP 71114.06-05.

b.

Findings

No findings were identified.

2.

RADIATION SAFETY

Cornerstones: Occupational and Public Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

This inspection constituted one complete radiological hazard assessment and exposure

controls sample as defined in IP 71124.01-05.

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Enclosure

.1

Inspection Planning (02.01)

a.

Inspection Scope

The inspectors reviewed all licensee performance indicators for the occupational

exposure cornerstone for follow-up. The inspectors reviewed the results of radiation

protection program audits (e.g., licensees quality assurance audits or other independent

audits). The inspectors reviewed any reports of operational occurrences related to

occupational radiation safety since the last inspection. The inspectors reviewed the

results of the audit and operational report reviews to gain insights into overall licensee

performance.

b.

Findings

No findings were identified.

.2

Radiological Hazard Assessment (02.02)

a.

Inspection Scope

The inspectors determined if there had been any changes to plant operations since the

last inspection that could have resulted in a significant new radiological hazard for onsite

workers or members of the public. The inspectors evaluated whether the licensee

assessed the potential impact of any changes and had implemented periodic monitoring,

as appropriate, to detect and quantify the radiological hazard(s).

The inspectors reviewed the last two radiological surveys from selected plant areas and

evaluated whether the thoroughness and frequency of the surveys where appropriate for

the given radiological hazard(s).

The inspectors conducted walkdowns of the facility, including radioactive waste

processing, storage, and handling areas to evaluate material conditions and performed

independent radiation measurements to verify conditions.

The inspectors selected the following radiologically risk-significant work activities that

involved exposure to radiation:

Entry into Heater/Condenser Bay.

For these work activities, the inspectors assessed whether the pre-work surveys

performed were appropriate to identify and quantify the radiological hazard(s) and to

establish adequate protective measures. The inspectors evaluated the radiological

survey program to determine if hazards were properly identified, including the following:

identification of hot particles;

the presence of alpha emitters;

the potential for airborne radioactive materials, including the potential presence

of transuranics and/or other hard-to-detect radioactive materials;

the hazards associated with work activities that could suddenly and severely

increase radiological conditions and that the licensee had established a means to

inform workers of changes that could have significantly impacted their

occupational dose; and

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Enclosure

severe radiation field dose gradients that could have resulted in non-uniform

exposures of the body.

The inspectors observed work in potential airborne areas and evaluated whether the air

samples were representative of the breathing air zone. The inspectors evaluated

whether continuous air monitors were located in areas with low background to minimize

false alarms and were representative of actual work areas. The inspectors evaluated

the licensees program for monitoring levels of loose surface contamination in areas of

the plant with the potential for the contamination to become airborne.

b.

Findings

No findings were identified.

.3

Instructions to Workers (02.03)

a.

Inspection Scope

The inspectors selected various containers holding non-exempt licensed radioactive

materials that could have caused unplanned or inadvertent exposure of workers, and

assessed whether the containers were labeled and controlled in accordance with

10 CFR 20.1904, Labeling Containers, or met the requirements of 10 CFR 20.1905(g),

Exemptions To Labeling Requirements.

The inspectors reviewed the following radiation work permits used to access high

radiation areas and evaluated the specified work control instructions or control barriers.

In-Service Project - N2 Penetration Work;

Segregation of Hot Trash and Vacuum Cleaner High Efficiency Particulate Air

Filter Change Out; and

Traversing In-core Probe Room Maintenance.

For these radiation work permits, the inspectors assessed whether allowable stay times

or permissible dose (including from the intake of radioactive material) for radiologically

significant work under each radiation work permit were clearly identified. The inspectors

evaluated whether electronic personal dosimeter alarm set-points were in conformance

with survey indications and plant policy.

The inspectors reviewed selected occurrences where a workers electronic personal

dosimeter noticeably malfunctioned or alarmed. The inspectors evaluated whether

workers had responded appropriately to the off-normal condition. The inspectors

assessed whether the issue was included in the corrective action program and dose

evaluations were conducted as appropriate.

For work activities that could suddenly and severely increase radiological conditions,

the inspectors assessed the licensees means to inform workers of changes that could

significantly impact their occupational dose.

b.

Findings

No findings were identified.

16

Enclosure

.4

Contamination and Radioactive Material Control (02.04)

a.

Inspection Scope

The inspectors observed locations where the licensee monitored potentially

contaminated material leaving the radiological control area and inspected the methods

used for control, survey, and release from these areas. The inspectors observed the

performance of personnel surveying and releasing material for unrestricted use and

evaluated whether the work was performed in accordance with plant procedures and

whether the procedures were sufficient to control the spread of contamination and

prevent unintended release of radioactive materials from the site. The inspectors

assessed whether the radiation monitoring instrumentation had appropriate sensitivity for

the types of radiation present.

The inspectors reviewed the licensees criteria for the survey and release of potentially

contaminated material. The inspectors evaluated whether there was guidance on how to

respond to alarms that would indicate the presence of licensed radioactive material.

The inspectors reviewed the licensees procedures and records to verify that the

radiation detection instrumentation was used at its typical sensitivity level based on

appropriate counting parameters. The inspectors assessed whether or not the licensee

has established a de facto release limit by altering the instruments typical sensitivity

through such methods as raising the energy discriminator level or locating the instrument

in a high-radiation background area.

The inspectors selected several sealed sources from the licensees inventory records

and assessed whether the sources were accounted for and verified to be intact.

The inspectors evaluated whether any transactions, since the last inspection, involving

nationally tracked sources were reported in accordance with 10 CFR 20.2207.

b.

Findings

No findings were identified.

.5

Radiological Hazards Control and Work Coverage (02.05)

a.

Inspection Scope

The inspectors evaluated ambient radiological conditions (e.g., radiation levels or

potential radiation levels) during tours of the facility. The inspectors assessed whether

the conditions were consistent with applicable posted surveys, radiation work permits,

and worker briefings.

The inspectors evaluated the adequacy of radiological controls, such as required

surveys, radiation protection job coverage (including audio and visual surveillance for

remote job coverage), and contamination controls. The inspectors evaluated the

licensees use of electronic personal dosimeters in high noise areas as high radiation

area monitoring devices.

The inspectors assessed whether radiation monitoring devices were placed on the

individuals body consistent with licensee procedures. The inspectors assessed whether

17

Enclosure

the dosimeters were placed in the location of highest expected dose or that the licensee

properly employed an NRC-approved method of determining effective dose equivalent.

The inspectors reviewed the application of dosimetry to effectively monitor exposure to

personnel in high-radiation work areas with significant dose rate gradients.

The inspectors reviewed the following radiation work permits for work within airborne

radioactivity areas with the potential for individual worker internal exposures.

Segregation of Hot Trash and Vacuum Cleaner High Efficiency Particulate Air

Filter Change Out;

Dry Fuel Storage Project; and

Cask Pit Clean-up and Transport of Tri-Nuc 260 Hoses and Filters.

For these radiation work permits, the inspectors evaluated airborne radioactive

controls and monitoring, including potential for significant airborne levels

(e.g., grinding, grit blasting, system breaches, entry into tanks, cubicles, and

reactor cavities). The inspectors assessed barrier (e.g., tent or glove box) integrity and

temporary high-efficiency particulate air ventilation system operation. The inspectors

examined the licensees physical and programmatic controls for highly activated or

contaminated materials (nonfuel) stored within spent fuel and other storage pools.

The inspectors assessed whether appropriate controls (i.e., administrative and physical

controls) were in place to preclude inadvertent removal of these materials from the pool.

The inspectors examined the posting and physical controls for selected high radiation

areas and very high radiation areas to verify conformance with the occupational

performance indicator.

b.

Findings

No findings were identified.

.6

Risk-Significant High Radiation Area and Very High Radiation Area Controls (02.06)

a.

Inspection Scope

The inspectors discussed with the radiation protection manager the controls and

procedures for high-risk high radiation areas and very high radiation areas.

The inspectors discussed methods employed by the licensee to provide stricter control

of very high radiation area access as specified in 10 CFR 20.1602, Control of Access to

Very High Radiation Areas, and Regulatory Guide 8.38, Control of Access to High and

Very High Radiation Areas of Nuclear Plants. The inspectors assessed whether any

changes to licensee procedures substantially reduced the effectiveness and/or level of

worker protection.

The inspectors discussed the controls in place for special areas that have the potential

to become very high radiation areas during certain plant operations with first-line health

physics supervisors (or equivalent positions having backshift health physics oversight

authority). The inspectors assessed whether these plant operations required

communication beforehand with the health physics group, so as to allow corresponding

timely actions to properly post, control, and monitor the radiation hazards including

re-access authorization.

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Enclosure

The inspectors evaluated licensee controls for very high radiation areas and areas with

the potential to become very high radiation areas to ensure that individuals were not able

to gain unauthorized access to the very high radiation area.

b.

Findings

No findings were identified.

.7

Radiation Worker Performance (02.07)

a.

Inspection Scope

The inspectors observed radiation worker performance with respect to stated radiation

protection work requirements. The inspectors assessed whether workers were aware of

the radiological conditions in their workplace and the radiation work permit controls/limits

in place, and whether their performance reflected the level of radiological hazards

present.

The inspectors reviewed radiological problem reports since the last inspection that found

the cause of the event to be human performance errors. The inspectors evaluated

whether there was an observable pattern traceable to a similar cause. The inspectors

assessed whether this perspective matched the corrective action approach taken by the

licensee to resolve the reported problems. The inspectors discussed with the radiation

protection manager any problems with the corrective actions planned or taken.

b.

Findings

No findings were identified.

.8

Radiation Protection Technician Proficiency (02.08)

a.

Inspection Scope

The inspectors observed the performance of the radiation protection technicians with

respect to all radiation protection work requirements. The inspectors evaluated whether

technicians were aware of the radiological conditions in their workplace and the radiation

work permit controls/limits, and whether their performance was consistent with their

training and qualifications with respect to the radiological hazards and work activities.

The inspectors reviewed radiological problem reports since the last inspection that found

the cause of the event to be radiation protection technician error. The inspectors

evaluated whether there was an observable pattern traceable to a similar cause.

The inspectors assessed whether this perspective matched the corrective action

approach taken by the licensee to resolve the reported problems.

b.

Findings

No findings were identified.

19

Enclosure

.9

Problem Identification and Resolution (02.09)

a.

Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensees corrective action program.

The inspectors assessed the appropriateness of the corrective actions for a selected

sample of problems documented by the licensee that involve radiation monitoring and

exposure controls. The inspectors assessed the licensees process for applying

operating experience to their plant.

b.

Findings

No findings were identified.

2RS2 Occupational As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and Controls

(71124.02)

These inspection activities supplement those documented in Inspection Report 05000331/2010004, and constitute one complete occupational ALARA planning and

controls sample as defined in IP 71124.01-05.

.1

Inspection Planning (02.01)

a.

Inspection Scope

The inspectors reviewed pertinent information regarding plant collective exposure

history, current exposure trends, and ongoing or planned activities in order to assess

current performance and exposure challenges. The inspectors reviewed the plants

three year rolling average collective exposure.

The inspectors reviewed the site-specific trends in collective exposures

(using NUREG-0713, Occupational Radiation Exposure at Commercial Nuclear Power

Reactors and Other Facilities, and plant historical data) and source term (average

contact dose rate with reactor coolant piping) measurements (using Electric Power

Research Institute) TR-108737, BWR Iron Control Monitoring Interim Report, issued

December 1998, and/or plant historical data, when available).

The inspectors reviewed site-specific procedures associated with maintaining

occupational exposures ALARA, which included a review of processes used to estimate

and track exposures from specific work activities.

b.

Findings

No findings were identified.

20

Enclosure

.2

Radiological Work Planning (02.02)

a.

Inspection Scope

The inspectors compared the results achieved (dose rate reductions, person-rem used)

with the intended dose established in the licensees ALARA planning for these work

activities. The inspectors compared the person-hour estimates provided by maintenance

planning and other groups to the radiation protection group with the actual work activity

time requirements, and evaluated the accuracy of these time estimates. The inspectors

assessed the reasons (e.g., failure to adequately plan the activity, failure to provide

sufficient work controls) for any inconsistencies between intended and actual work

activity doses.

The inspectors determined whether post-job reviews were conducted and if identified

problems were entered into the licensees corrective action program.

b.

Findings

No findings were identified.

4.

OTHER ACTIVITIES

Cornerstones: Mitigating Systems and Barrier Integrity

4OA1 Performance Indicator Verification (71151)

.1

Mitigating Systems Performance Index - Residual Heat Removal System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Residual Heat Removal System Performance Indicator (PI) for the period

from the fourth quarter 2010 through the third quarter 2011. To determine the accuracy

of the PI data reported during those periods, PI definitions and guidance contained in

Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6, was used. The inspectors reviewed the licensees

operator narrative logs, condition reports, MSPI derivation reports, event reports and

NRC Integrated Inspection Reports for the period of October 2010 through September

2011 to validate the accuracy of the submittals. The inspectors reviewed the MSPI

component risk coefficient to determine if it had changed by more than 25 percent in

value since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees CAP to determine

if any problems had been identified with the PI data collected or transmitted for this

indicator and none were identified. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted one MSPI residual heat removal system sample as defined in

IP 71151-05.

b.

Findings

No findings were identified.

21

Enclosure

.2

Mitigating Systems Performance Index - Cooling Water Systems

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Cooling Water Systems PI for the period from the fourth quarter 2010 through the

third quarter 2011. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, was used. The inspectors

reviewed the licensees operator narrative logs, condition reports, MSPI derivation

reports, event reports and NRC Integrated Inspection Reports for the period of October

2010 through September 2011 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees CAP to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one MSPI cooling water system sample as defined in

IP 71151-05.

b.

Findings

No findings were identified.

.3

Safety System Functional Failures

a.

Inspection Scope

The inspectors sampled licensee submittals for the Safety System Functional Failures PI

for the period from the fourth quarter 2010 through the third quarter 2011. To determine

the accuracy of the PI data reported during those periods, PI definitions and guidance

contained in NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72

and 50.73" definitions and guidance, were used. The inspectors reviewed the licensees

operator narrative logs, operability assessments, maintenance rule records,

maintenance work orders, condition reports, event reports and NRC Integrated

Inspection Reports for the period of October 2010 through September 2011 to validate

the accuracy of the submittals. The inspectors also reviewed the licensees CAP to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted one safety system functional failures PI sample as defined in

IP 71151-05.

b.

Findings

No findings were identified.

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Enclosure

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1

Routine Review of Items Entered into the Corrective Action Program

a.

Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

Findings

No findings were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b.

Findings

No findings were identified.

23

Enclosure

.3

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue.

The inspectors review was focused on repetitive equipment issues, but also considered

the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the six month period of June 2011 through November 2011,

although some examples expanded beyond those dates where the scope of the trend

warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self-assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy.

This inspection constituted one semi-annual trend review sample as defined in

IP 71152-05.

b.

Findings

No findings were identified.

.4

Selected Issue Follow-Up Inspection: Root Cause Evaluation 01676836, Both River

Water Supply (RWS) Subsystems Inoperable

a.

Inspection Scope

As a follow-up to the unplanned shutdown of the plant on August 11, 2011, due to the

RWS system being declared inoperable, the inspectors reviewed the root cause

evaluation (RCE) performed by the licensee. This review was to determine whether the

causal factors, contributing factors, and corrective actions were appropriate for the

circumstances surrounding the event. Based on the inspectors review of the RCE

several issues of concern were noted, one of which represented a self-revealed

performance deficiency discussed below. Overall, the inspectors concluded that the root

cause evaluation was performed in a thorough, probing manner; and several corrective

actions were identified that should be appropriate to prevent recurrence of the event.

This inspection constituted one selected issue follow-up sample as defined in

IP 71152-05.

24

Enclosure

b.

Findings

(1) Cancellation of River Survey Work Order Causes Inoperability of River Water Supply

System

Introduction: A finding of very low safety significance and associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

was self-revealed on August 11, 2011, when both river water supply subsystems were

rendered inoperable following a sediment intrusion event.

Description: On August 11, 2011, the licensee entered a forced outage after declaring

the RWS system inoperable due to a sand intrusion event that rendered both intake

structure travelling screens non-functional (see NRC Inspection Report 05000331/2011004 for additional information). The licensee performed a RCE for the

event and determined several causal factors were involved. The inspectors reviewed

the RCE, specifically focusing on the two root causes that were determined by the

licensee. Root Cause #1 involved the decision to cancel a July 2011 river survey that

would have detected the degrading conditions of the ultimate heat sink. Root Cause #2

involved the failure to establish preventive maintenance in the form of a river survey

following high river flow or level conditions.

The inspectors focused their review of the licensees evaluation of Root Cause #1 and

its contributing causes since it represented a self-revealed issue of concern and should

have been prevented. The evaluation determined that the July 2011 river survey would

have identified the increased sediment buildup upstream of the intake due to

degradation of upstream spur dikes. This survey would have triggered increased

monitoring and corrective actions in the form of dredging, sand pumping, and/or

structural repairs to the spur dikes themselves. The RCE also determined that the

July 2011 river survey WO 40056778 was cancelled without receiving review and

approval per the requirements of Administrative Control Procedure (ACP) 1208.3,

Preventive Maintenance Program. This procedure specifically required that

management approval was required prior to cancelling any work order that was tied to

the corrective action program. In the case of WO 40056778, it was a corrective action to

prevent recurrence from a RCE performed in 2003.

Analysis: The inspectors determined that the issue of concern represented a

performance deficiency because it was the result of the licensees failure to meet a

procedural requirement, and the cause was reasonably within the licensees ability to

foresee and correct and should have been prevented. The performance deficiency was

determined to be more than minor and a finding because it was associated with the

Initiating Events Cornerstone attribute of equipment performance, and it affected the

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during power operations. The inspectors applied

IMC 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,

to this finding. Because the finding did not contribute to both the likelihood of a reactor

trip and the likelihood that mitigation equipment or functions would not be available

under the Initiating Events Cornerstone column of Table 4a, the finding was determined

to be of very low safety significance (Green).

The inspectors determined that the contributing cause that provided the most insight

into the performance deficiency was associated with the cross-cutting aspect of

25

Enclosure

Human Performance, having Decision Making components, and involving the licensee

making safety or risk-significant decisions using a systematic process, including formally

defining the authority and roles for decisions affecting nuclear safety. Specifically,

risk-significant decisions were made with respect to cancelling a river survey and

deferring repairs to the spur dikes; however, the requisite organizational reviews and

approvals associated with the ultimate heat sink were not performed to ensure

appropriate actions were taken. H.1(a)

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented procedures of a type appropriate to the circumstances and shall be

accomplished in accordance with these procedures. Procedure ACP 1208.3,

Preventive Maintenance Program, establishes, in part, the licensees implementing

procedure for approving and cancelling work at the facility.

Contrary to the above, on July 19, 2011, the licensee failed to accomplish ACP 1208.3,

Section 3.11, which required, in part, Management Review Committee review of

WO 40056778 prior to voiding the WO for any reason. Corrective actions included

revision to affected river survey work orders to ensure that they could not be cancelled

without adequate review and approval, and completion of river dredging and repairs to

the upstream spur dikes. Because this violation was of very low safety significance and

was entered into the licensees corrective action program as CR 01676836, the violation

is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement

Policy (NCV 05000331/2011005-02, Cancellation of River Survey Work Order

Causes Inoperability of River Water Supply System).

.5

Selected Issue Follow-Up Inspection: Reactor Building Crane Strikes ISFSI Inspection

Stand

a.

Inspection Scope

During a review of items entered in the licensees CAP, the inspectors recognized a

condition report documenting displacement and potential damage to the ISFSI

inspection stand and reactor building (RB) crane control cab. The inspectors followed

the licensees immediate corrective actions, including their follow up inspections, since a

loaded ISFSI transfer cask was in the process of vacuum drying. The inspectors also

followed the licensees assessment of damage to the RB crane structural integrity prior

to the licensee releasing the RB crane for use. The inspectors also reviewed a RCE

conducted by the licensee for the event.

This inspection constituted one selected issue follow-up sample as defined in

IP 71152-05.

b.

Findings

(1) Procedural Non-Compliance Results in RB Crane Striking the ISFSI Inspection Stand

Introduction: A finding of very low safety significance and associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was

self-revealed on October 31, 2011, when operators failed to follow Operating Instruction

(OI) 999, Reactor Building Crane. Specifically, this error resulted in the RB crane

striking the ISFSI inspection stand.

26

Enclosure

Description: On October 31, 2011, the licensee was in the midst of a several month long

ISFSI loading campaign. Following completion of the main work activities for the day, a

decision was made to move a storage cabinet from the first floor of the reactor building

to the refuel floor, where most of the ISFSI project activities were taking place. Prior to

moving the cabinet, operators and a contract supervisor held an informal pre-job brief to

discuss the lift. The work activity being performed was not governed by a work order to

perform the task. Later investigation revealed that due to the equipment used for the

evolution and the area the work was taking place, the work activity could be considered

minor maintenance and require a minor maintenance work request and order, at a

minimum. Following the informal brief, a crane operator went to the refuel floor to get

ready to lift the storage cabinet. In order to make the lift, the operator needed to move

the crane from the north end of the refuel floor to the south end. While traversing the

crane from north to south, the operator noticed that the hand rails for the ISFSI

inspection stand were installed. Unfortunately, the crane cab was only a couple feet

from the platform when the operator noticed this, and the operator was not able to stop

the crane before it struck the ISFSI inspection stand hand rails. The ISFSI inspection

stand was displaced several inches and was stopped by the dry storage canister (DSC)

transfer cask, which was recently loaded with spent fuel undergoing a vacuum drying

process. Subsequently, the licensee verified the drying process was uninterrupted and

the DSC transfer cask was not damaged. They also performed inspections of the

inspection stand and made repairs necessary to ensure personnel safety. Inspections of

structural integrity were also performed for the RB crane prior to additional crane

operations.

The licensee performed a RCE for the event and noted that the inspection stand hand

rail interference was first identified in 2003. Corrective actions for the interference

included adding a caution statement to OI 999, Reactor Building Crane, and

performance of a periodic inspection of the RB crane. In addition, the licensee placed

an information tag on the control panel of the crane to warn operators of the potential

inspection stand hand rail interference. This information tag was removed at one point

and not in place at the RB crane control panel prior to the event.

The inspectors questioned why the RCE did not specifically identify the apparently

ineffective corrective actions from 2003 as either a root or contributing cause.

Although the RCE discussed the ineffective corrective actions from 2003, the inspectors

concluded that the inadequate controls in place to maintain the information tag was a

contributing cause to the event. Also, the inspectors noted that the placement of the

information tag in the crane cab was not identified as a long-term corrective action and

following the ISFSI campaign in 2003, the tag was removed. There was no requirement

added to have the tag reinstalled when the ISFSI inspection stand was erected for the

2011 ISFSI campaign.

Analysis: The inspectors determined that attempting to move the crane over the ISFSI

work platform while the hand rails were installed was contrary to OI 999 and was an

issue of concern. Failing to follow OI 999 was a performance deficiency because it was

the result of the licensees failure to meet a procedural requirement, and the cause was

reasonably within the licensees ability to foresee and correct and should have been

prevented. The performance deficiency was determined to be more than minor and a

finding because, if left uncorrected, the performance deficiency would have the potential

to lead to a more significant safety concern. Specifically, not following OI 999 could lead

27

Enclosure

to more significant event or cause damage to safety-related equipment The inspectors

concluded this finding was associated with the Barrier Integrity Cornerstone.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 4a for the Barrier Integrity

Cornerstone. Because the finding only affected the fuel barrier, the finding was

determined to be of very low safety significance (Green).

The inspectors determined that the contributing cause that provided the most insight into

the performance deficiency was associated with the cross-cutting aspect of Human

Performance, having Work Control components, and involving appropriately coordinating

work activities by incorporating actions to address the need to keep personnel apprised

of work status, the operational impact of work activities, and plant conditions that may

affect work activities. Specifically, the licensee did not implement appropriate work

controls to ensure the hand rails of the ISFSI inspection stand were removed prior to

moving the crane for an activity that was not associated with the ISFSI project. H.3(b)

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented procedures of a type appropriate to the circumstances and shall be

accomplished in accordance with these procedures. Contrary to this, on

October 31, 2011, an operator failed to accomplish an activity affecting quality in

accordance with procedures. Specifically, the operator failed to comply with procedure

OI 999, Revision 39, Reactor Building Crane, which contained a caution statement

indicating that the crane cab would not clear the handrails of the ISFSI work platform

when the cask work platform is installed. Immediate corrective actions included

performing inspections of the DSC transfer cask, vacuum drying operations,

ISFSI inspection stand, and RB crane. Because this violation was of very low safety

significance and it was entered into the licensees corrective action program as

CR 1701934, this violation is being treated as an NCV, consistent with Section 2.3.2 of

the NRC Enforcement Policy (NCV 05000331/2011005-03, Procedural

Non-Compliance Results in RB Crane Colliding with ISFSI Inspection Stand).

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1

Reactor Feedwater Pump Area Deluge Inadvertent Actuation

a.

Inspection Scope

The inspectors reviewed the plants response to an inadvertent initiation of a deluge

system in the reactor feed pump area of the turbine building on October 22, 2011.

The inspectors walked down affected equipment that was wetted in the area and verified

the plants actions to address potential impacts to indicated reactor power levels were

appropriate. Documents reviewed in this inspection are listed in the Attachment to this

report.

This event follow-up review constituted one sample as defined in IP 71153-05.

b.

Findings

No findings were identified.

28

Enclosure

.2

(Closed) Licensee Event Report (LER) 05000331/2011-002-0: Loss of Ultimate Heat

Sink and Completion of Technical Specification Required Shutdown

a.

Inspection Scope

On August 11, 2011, with the plant operating at full power, the RWS system was

declared inoperable after both intake structure traveling screens became non-functional.

With both RWS subsystems inoperable, the licensee entered TS 3.7.2, Condition B,

which required the reactor to be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Following reactor shutdown, the licensee identified a significant amount of

sand/sediment intrusion in the intake (this event is further discussed in Inspection Report 05000331/2011004). This LER documented four events or conditions subject to an

LER per 10 CFR 50.73. The inspectors verified that the events and conditions reported

in the LER were appropriate, that the safety significance was properly evaluated, and

that corrective actions planned or in place were appropriate to address the causes of the

event. The inspectors did not identify any new or additional issues of concern during

their review of the LER. Documents reviewed are listed in the Attachment to this report.

This LER is closed.

This inspection constituted one event report review sample as defined in IP 71153-05.

b.

Findings

No findings were identified.

4OA5 Other Activities

.1

Operation of an Independent Spent Fuel Storage Installation at Operating Plants

(60855.1)

a.

Inspection Scope

The inspectors observed and evaluated select licensee loading, processing, and transfer

operations of the fifth and sixth canisters during the licensees 2011 dry fuel storage

campaign to verify compliance with the applicable certificate of compliance conditions,

the associated TS, and ISFSI procedures. Specifically, the inspectors observed: heavy

loads practices associated with handling of the Transfer Cask; non-destructive

evaluations of welds on the DSC lid; transfer of the DSC to the ISFSI pad; insertion of

the DSC into a Horizontal Storage Module (HSM); and surveys being performed at the

ISFSI pad.

The inspectors performed tours of the ISFSI pad to assess the material condition of the

pad and HSMs. The inspectors reviewed the licensees evaluations of flammable

materials near the ISFSI and the radiation monitoring program. Additionally, the

inspectors performed independent radiation surveys around the ISFSI pad and HSMs

and verified that the contamination and radiation levels from the Transfer Cask were well

below the regulatory limits.

The inspectors reviewed select documents, in part, after the licensee completed certain

loading activities and a review of the fuel selection documentation was performed to

verify the fuel placed in the DSC met the TS requirements. The inspectors observed the

licensee perform crane operations and reviewed the applicable procedures for

29

Enclosure

compliance with the control of heavy loads program. In addition, the inspectors

reviewed condition reports and the associated corrective actions to verify the licensee

took adequate corrective actions in a timely manner to correct the issues.

The inspectors also reviewed 72.48 screenings and changes to the licensees

10 CFR 72.212 evaluations since the last ISFSI inspection.

b.

Findings

No findings were identified.

4OA6 Management Meetings

.1

Exit Meeting Summary

On January 12, 2012, the inspectors presented the inspection results to Mr. P. Wells,

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed

was considered proprietary.

.2

Interim Exit Meetings

Interim exits were conducted for:

The results of the Emergency Preparedness program inspection were discussed

with Mr. M. Davis via telephone on October 13, 2011.

The ISFSI operational inspection concluded with an interim exit meeting on

November 17, 2011. The inspector presented the inspection results to

Mr. C. Conklin and other members of the licensee management and staff.

Licensee personnel acknowledged the information presented.

Radiological Hazard Assessment and Exposure Controls and Occupational

ALARA Planning and Controls with Mr. P. Wells on December 2, 2011.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

Any proprietary material received during the inspection was returned to the licensee.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meets the criteria of Section 2.3.2 of the

NRC Enforcement Policy, for being dispositioned as an NCV.

The licensee identified a finding of very low safety significance (Green) and an

associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, for the failure to adequately implement post-maintenance testing of the A

intake structure ventilation subsystem temperature controller. Specifically, on

November 7, 2011, maintenance technicians incorrectly performed WO 40039255 for a

replacement temperature controller. The testing was intended to demonstrate

functionality of the A intake structure ventilation subsystem; however, human

performance errors resulted in the test not revealing improper installation issues with the

controller. On November 16, 2011, the licensee identified the performance deficiency

30

Enclosure

and declared the A intake structure ventilation subsystem non-functional and the A

RWS subsystem inoperable, entered the issue into the CAP as CR 1707561, and

restored the A intake structure ventilation subsystem to a functional status.

Because the A RWS subsystem remained available throughout the period of time the

temperature controller was incorrectly installed, reasonable assurance existed to support

the conclusion that the RWS safety function was not impacted.

This failure to meet the requirements of WO 40039255 was a performance deficiency.

The performance deficiency was more than minor because it was associated with the

Mitigating Systems Cornerstone attribute of configuration control and human

performance, and its objective of ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Specifically, had the licensee not identified the condition, environmental or operating

conditions could have occurred which could have challenged availability of the A RWS

system or impacted operability. The inspectors determined the finding could be

evaluated using the SDP in accordance with IMC 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, Table 4a. Because the inspectors answered No to

all five questions under Mitigating Systems Cornerstone column, the inspectors

screened the finding as very low safety significance (Green).

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

P. Wells, Site Vice President

D. Curtland, Plant General Manager

K. Kleinheinz, Site Engineering Director

S. Catron, Licensing Manager

G. Young, Nuclear Oversight Manager

G. Pry, Operations Director

R. Wheaton, Maintenance Site Director

R. Porter, Chemistry & Radiation Protection Manager

B. Kindred, Security Manager

B. Simmons, Training Manager

M. Davis, Emergency Preparedness Manager

B. Murrell, Licensing Engineer Analyst

D. Barta, Licensing Engineer/Analyst

C. Conklin, Project Manager

C. Harberts, Refuel Floor Project Manager

K. Peveler, Nuclear Oversight Supervisor

Nuclear Regulatory Commission

K. Feintuch, Project Manager, NRR

M. Ring, Chief, Reactor Projects Branch 1

2

Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened 05000331/2011005-01

SLIV

Failure to Make Required Eight Hour Event Report per

10 CFR 50.72(b)(3)(v)(B) (Section 1R15)05000331/2011005-02

NCV

Cancellation of River Survey Work Order Causes

Inoperability of River Water Supply System (Section 4OA2.4)05000331/2011005-03

NCV

Procedural Non-Compliance Results in Reactor Building

Crane Colliding with ISFSI Inspection Stand

(Section 4OA2.5)

Closed 05000331/2011005-01

SLIV

Failure to Make Required Eight Hour Event Report per

10 CFR 50.72(b)(3)(v)(B) (Section 1R15)05000331/2011005-02

NCV

Cancellation of River Survey Work Order Causes

Inoperability of River Water Supply System (Section 4OA2.4)05000331/2011005-03

NCV

Procedural Non-Compliance Results in Reactor Building

Crane Colliding with ISFSI Inspection Stand

(Section 4OA2.5)

05000331/2011-002-0

LER

Loss of Ultimate Heat Sink and Completion of Technical

Specification Required Shutdown

Discussed

None.

3

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01

OP-AA-102-1002 (DAEC); Seasonal Readiness; Revision 5

OP-AA-102-1002; Seasonal Readiness; Revision 0

Abnormal Operating Procedure 903; Severe Weather; Revision 33

OP-AA-102-1002 (DAEC); Seasonal Readiness; Revision 5

CR 01688945; Track Seasonal Readiness Items to Completion Prior to 10/31

DAEC Certification Letter for 2011 Cold Weather Readiness Period

NG-270K; Plant Winterization Checklist; Revision 5

1R04

OI 152A2; HPCI System Valve Lineup and Checklist; Revision 16

OI 152A4; HPCI System Control Panel Lineup; Revision 5

OI 152A1; HPCI System Electrical Lineup; Revision 3

OI 152; High Pressure Coolant Injection System; Revision 99

CR 01706756; While Performing Routine Auxiliary Operator Rounds, a Loud Squeal Was

Discovered on 1VAC014B HPCI Room Cooling Unit

OI 324A10; SBDG Standby/ Readiness Condition Checklist; Revision 14

OI 454A4; B ESW System Valve Lineup and Checklist; Revision13

1R05

ACP 1203.53; Fire Protection; Revision 14

ACP 1412.4; Impairments to Fire Protection Systems; Revision 64

DAEC Fire Plan - Volume 1, Program; Revision 61

AFP 03; Reactor Building HPCI, RCIC & Radwaste Tank Rooms; Revision 26

AFP 07; Reactor Building Laydown Area, Corridor and Waste Tank Area and Spent Resin Tank

Room El. 786; Revision 30

AFP 74; Switchyard; Revision 5

AFP 79; Spent Fuel Storage Facility; Revision 2

AFP -04; Reactor Building North CRD Module Area, CRD repair and CRD Cable Rooms;

Revision 28

AFP-05; Reactor Building South CRD Module Area and Offgas Recombiner Rooms and

Railroad Airlock; Revision 26

AFP-06; Reactor Building RHR Valve Room EL. 757-6; Revision 24

AFP-10; Main Exhaust Fan Room, Heating Hot Water Pump Room and the Plant Air supply Fan

Room; Revision 24

AFP-11; Reactor Building Laydown Area EL. 833-6; Revision 25

AFP-12; Reactor Building Decay Tank and Condensate Phase Separator Rooms; Revision 24

Fire Protection Impairment Permit FPR-09-7320; The DAEC NFPA-805 Transition Project has

Identified Multiple Spurious Operations Vulnerabilities for the RB1 Area

Fire Protection Impairment Permit CMP-11-5115; Dry Fuel Storage Campaign

4

Attachment

AFP 20; Aux Boiler Room, Emergency Diesel Generator Rooms and Generator Day Tank

Rooms El. 7576; Revision 29

1R06

Abnormal Operating Procedure-902; Flood; Revision 39

1R11

Simulator Exercise Guide 2011E-02S; Revision 0

1R12

DAEC Maintenance Rule Program; Cycle 22 Cyclic Report; March 4, 2009 - December 9, 2010

CR 01687326; LIC-1319 Outside Normal Range During STP 3.0.0-02

WO 40112070; LIC-1319 Outside Normal Range During STP 3.0.0-02

CR 01698275; CV-1321, 1E003B Feedwater Heater Dump Valve, Could Not Maintain

Feedwater Heater Level

CR 01698276; Trend - Step Changes in Feedwater Heater 4A and 6B Pressures

CR 01698288; Received 1C06 (D-8) 1E4B Hi-Hi Level Without Receiving the Hi Level

System Level Performance Criteria Basis Document; Feedwater and Condensate; Revision 0

1R13

Work Planning Guideline -1; Work Process Guideline; Revision 47

Work Planning Guideline-2; Online Risk Management Guideline; Revision 59

OP-AA-104-1007; Online Aggregate Risk; Revision 2

WM-AA-1000; Work Activity Risk Management; Revision 11

WM-AA-1000 (DAEC); Work Activity Risk Management (DAEC); Revision 0

OP-AA-102-1003; Guarded Equipment; Revision 3

OP-AA-102-1003 (DAEC); Guarded Equipment (DAEC Specific Information); Revision 19

Work Week 1140 Work Activity Risk Management Summary and Weekly Probabilistic Risk

Analysis

1R15

EN-AA-203-1001; Operability Determinations/ Functionality Assessments; Revision 5

OP-AA-100-1000; Conduct of Operations; Revision 5

TAR 01680290-01; A EDG Exhaust Leak at Opposite Control Side from Cylinders 10, 11, and

12 Exhaust Header Plug

Condition Evaluation (CE) 01680290-02; A EDG Exhaust Leak at Opposite Control Side

Exhaust Header - Cylinders 10, 11, and 12

CR 01700990; Standby Gas Treatment Sump Piping is Corroded

Prompt Operability Determination (POD) 01700990-01; Standby Gas Treatment Sump Piping is

Corroded

OI 710; Intake Structure HVAC System; Revision 15

CR 01718078; OI 710 Provides No Guidance for Intake Unit Heaters Per ARP

Operations Shift Logs; November 7, 2011 through November 17, 2011

CR 01716448; NRC Questions TAR 1707561 Conclusion

5

Attachment

1R19

ACP 1408.1; Work Order Task(s); Revision 169

WO 40075137; Functional Check and Calibration of Transducer

WO 40076624; Oil Circuit Breaker Major Service and Inspection

WO 40079157; Transformer Condition (Diagnostic Electrical Testing)

OI 831.4; Plant Process Computer System (PPC); Revision 74

CR 01699097; LEFM Indicating Bad Inputs

CR 01699182; Degraded LEFM Affecting Indicated Reactor Power

1R22

ACP 107; Surveillance Tests; Revision 13

STP 3.6.1.6-01; Pressure Suppression Chamber to Reactor Building Vacuum Breaker

Operability Test; Revisions 7 and 8

STP 3.8.1-04B; B Standby Diesel Generator Operability Test (Slow Start from Normal Starting

Air); Revision 17

CR 01693756; 1C08B (A-2) B diesel to 1A4 breaker 1A411 Trip Alarm Cycling

CR 01692424; 3.6.1.6-01 - Pressure Suppression Chamber to Reactor Building

STP 3.7.4-01B; B Standby Filter Unit - Logic System Functional Test and Simulated Automatic

Actuation; Revision 2

STP 3.6.1.6-01; Pressure Suppression Chamber to Reactor Building Vacuum Breaker

Operability Test; Revisions 7 and 8

STP 3.8.1-04B; B Standby Diesel Generator Operability Test (Slow Start from Normal Starting

Air); Revision 17

CR 01693756; 1C08B (A-2) B diesel to 1A4 breaker 1A411 Trip Alarm Cycling

CR 01692424; 3.6.1.6-01 - Pressure Suppression Chamber to Reactor Building

1EP4

10 CFR 50.54(q) Evaluation Package; Emergency Plan Implementing Procedure (EPIP) Form

EAL-01; Emergency Action Level Matrix; Revision 8

10 CFR 50.54(q) Evaluation Package; EBD F; Fission Product Barrier Degradation;

Revision 10

10 CFR 50.54(q) Evaluation Package; EBD H; Hazards & Other Conditions Affecting Plant

Safety; Revision 7

10 CFR 50.54(q) Evaluation Package; EPIP 1.2; Notifications; Revision 40

10 CFR 50.54(q) Evaluation Package; EPIP 2.1; Activation and Operation of the Operational

Support Center (OSC); Revision 17

10 CFR 50.54(q) Evaluation Package; EPIP 2.4; Activation and Operation of the ORAA;

Revision 15

10 CFR 50.54(q) Evaluation Package; EPIP 2.8; Security Threat; Revision 8

10 CFR 50.54(q) Evaluation Package; EPIP 3.1; In-Plant Radiological Monitoring; Revision 22

10 CFR 50.54(q) Evaluation Package; EPIP 3.1; In-Plant Radiological Monitoring; Revision 23

10 CFR 50.54(q) Evaluation Package; EPIP 3.2; Field Radiological Monitoring; Revision 19

10 CFR 50.54(q) Evaluation Package; EPIP Form EOF-08; Rad & EOF Manager Checklist;

In-Plant Radiological Monitoring; Revision 13

10 CFR 50.54(q) Evaluation Package; EPIP Form EOF-09; EOF Ops Liaison Checklist;

Revision 9

10 CFR 50.54(q) Evaluation Package; EPIP Form MIDAS-01; MIDAS Operability Test;

Revision 3

6

Attachment

10 CFR 50.54(q) Evaluation Package; EPIP Form NOTE-05; EAL Notification Form;

Revision 13

10 CFR 50.54(q) Evaluation Package; EPIP Form NOTE-07; Basic Notification Flowpath;

Revision 11

10 CFR 50.54(q) Evaluation Package; EPIP Form NOTE-02; ERO Notification - Alphanumeric

Paging System Callout; Revision 8

10 CFR 50.54(q) Evaluation Package; EPIP Form OSC-011; Emergency Assignment Staffing

Board Duties; Revision 4

10 CFR 50.54(q) Evaluation Package; EPIP Form OSC-12; External Exposure Limits;

Revision 1

10 CFR 50.54(q) Evaluation Package; EPIP Form TSC-04; Technical & Engineering Supervisor

Checklist; Revision 7

10 CFR 50.54(q) Evaluation Package; EPIP Form TSC-07; TSC Administrative Supervisor

Checklist; Revision 5

10 CFR 50.54(q) Evaluation Package; EPIP Form TSC-01; TSC Emergency Coordinator

Checklist; Revision 13

10 CFR 50.54(q) Evaluation Package; EPIP Form EOF-07; Emergency Response & Recovery

Director; Revision 13

2RS1

ACP 1411.13; Control of Locked High Radiation Areas and Above; Revision 30

ACP 1411.23; Equipment and Material Controls in Radiological Controlled Areas; Revision 28

ACP 1411.27; Rules for Conduct of Work in Radiologically Controlled Areas; Revision 34

CR 01651746; High Radiation Area Swing-gate Malfunction

CR 01654201; Issues Identified during Low Level Walkdown

CR 01666708; Waste Drum Storage Area Improvements

CR 01666722; Quality Assurance Finding-Oversight of Radioactive Waste Activities

CR 01677279; Sealed Source Leak Test Did Not Meet Schedule Adherence

CR 01685973; Energy Solutions Cask Drive Enters Radiologically Restricted Area Without an

Electronic Dosimeter

CR 01688541; Radiologically Restricted Area High Efficiency Particulate Air Filter Vacuum

Storage Room Inventory Control

HPP 3104.01; Control of Access to High Radiation Areas and Above; Revision 54

HPP3104.09; Drywell Initial Entry and Start-up/Shut-down Entries; Revision 24

HPP 3105.09; Personnel Dosimetry for External Exposure; Revision 26

HPP 3107.04; Radioactive Source Inventory, Control, Leak Check; Revision 16

HPP 3107.05; Release of Items from the Radiologically Restricted Area; Revision 17

RP-AA-100-1001; Radiation Protection Conduct of Operations Guideline; Revision 1

RFO 22; Department Report-Radiation Protection and ALARA; Revision 0

RWP 10-3014; All Cavity Work with the Vessel Filled to the Flange; Revision 00

RWP 10-3016; Pool Work RDO-22; Revision 1

RWP 10-3024; Steam Dryer Tie Bar Replacement; Revision 1

RWP 10-3025; Boron Tube Recovery from Dryer Separator Pit; Revision 00

RWP 10-4213; In-Service Project N2 Penetration Work; Revision 2

RWP 10-4252; Source Range Monitor and Intermediate Range Monitor Removals; Revision 00

RWP 11-22; Management Planning, and Routine Engineering Inquiries; Revision 00

RWP 11-182; Cask Pit Clean-up; Revision 02

RWP 11-206; High Radiation Area/Locked High Radiation Area; Revision 00

RWP 11-249; Dry Fuel Storage Project

WO 0138219; Sealed Source Leakage Test

7

Attachment

WO 40060312; Sealed Source Leakage Test

11 DFS; Dry Fuel Storage Campaign Number 2 ALARA Plan; Revision 0

11-R-004; Reactor Water Clean-up Resin Shipment ALARA Plan; Revision 0

11-1206; Survey Spent Fuel Pool Cask Pit; dated September 12, 2011

11-1065; Survey Drywell 805; dated August 17, 2011

2RS2

ALARA Review 10-N2; Post Job ALARA Review N2A Nozzle Weld Overlay; dated

March 9, 2011

DAEC 5 Year ALARA Plan; Revision 1

10-4163; Survey Drywell 757, BRAC Point Survey; dated November, 19, 2011

10-4164; Survey Drywell 742, BRAC Point Survey; dated November, 19, 2011

4OA1

MSPI Design Basis Document, Revisions 12, 13

NRC PI Data Calculation Review and Approval Packages for MSPI Cooling Water 4th Quarter

2010 through 3rd Quarter 2011

NRC PI Data Calculation Review and Approval Packages for MSPI SSFF 4th Quarter 2010

through 3rd Quarter 2011

NRC PI Data Calculation Review and Approval Packages for MSPI Residual Heat Removal 4th

Quarter 2010 through 3rd Quarter 2011

MSPI Unavailability Index Cooling Water Derivation Report; October 2010 through

September 2011

MSPI Unavailability Index Residual Heat Removal Derivation Report; October 2010 through

September 2011

MSPI Unreliability Index Cooling Water Derivation Report; October 2010 through

September 2011

MSPI Unreliability Index Residual Heat Removal Derivation Report; October 2010 through

September 2011

4OA2

ACP 1410.15; Plant Status Control Program; Revision 6

PI-AA-103-1000; Human Performance Program Error Reduction Tools; Revision 1

ACP 1410.2; LCO Tracking and Safety Function Determination Program; Revision 28

CR 01701934; Cask Service Platform Out of Position

4OA3

CR 01699090; Deluge Initiation Feed Pump Area, Fire Brigade Activated

CR 01699098; Deluge #3 Failed

CR 01699097; LEFM Indicating Bad Inputs

4OA5

ACP 103.4; 10 CFR 72.48 Screening Process; Revision 13

ACP 103.5; 10 CFR 72.48 Evaluation Process; Revision 10

DFS 104; Ancillary Equipment Receipt Inspections and Pre-Op Testing; Revision 5

EC-156669; Reactor Building Crane Trolley Restraints; Revision 3

8

Attachment

DBD-F16-001; Duane Arnold Energy Center Design Basis Document for the Dry Spent Fuel

Storage Program; Revision 11

DAEC-1FJF-11-106; Irradiated Fuel Assembly Selection for Duane Arnold Energy Center 2011

ISFSI Campaign; Revision 3

RFP 403; Performance of Fuel Handling Activities; Revision 45

DFS 203; Dry Shielded Canister Sealing Operations; Revision 27

DFS 301; Loaded Dry Shielded Canister / Transfer Cask from Refueling Floor to ISFSI

Operations; Revision 13

DFS 302; Dry Shielded Canister from Transfer Cask to Horizontal Storage Module Transfer

Operations; Revision 13

VNDR-11-017l; Spent Fuel Cask Welding: 61BT NUHOMS Canisters; Revision 0

7248SCRN-10079; DFS-203 - Dry Shielded Canister Sealing Operations, PCR 01700974;

November 11, 2011

7248SCRN-9830; DFS-203 - Dry Shielded Canister Sealing Operations, PCR 01624499

CR 00343343; HSM Dimensional Tolerances Reduced due to Base Mat Settling

CR 00566670; Additional Actions to Restore Full Qualification of ISFSI

CR 01687477; Cut 480 Cable Supplying the HPU

CR 01700575; Dust on DSC Outer Lid may Interfere with PT of Weld

CR 01700996; NRC ISFSI Inspection Regarding Reactor Building Crane

CR 01701934; Cask Service Platform Out of Position

CR 01703042; Areas for Improvement Identified by NRC ISFSI Inspector

CR 01704968; Inadequate 72.48 Review for Deletion of Helium Leak Test

4OA7

CR 01707561; Work Order Error on Input to TC7715B

WO 40039255; TC7715A Tubing Correction and Operability Testing

9

Attachment

LIST OF ACRONYMS USED

ACP

Administrative Control Procedure

ADAMS

Agencywide Document Access Management System

AFP

Area Fire Plan

ALARA

As-Low-As-Is-Reasonably-Achievable

ARP

Annunciator Response Procedure

CAP

Corrective Action Program

CFR

Code of Federal Regulations

CR

Condition Report

DAEC

Duane Arnold Energy Center

DRP

Division of Reactor Projects

DSC

Dry Storage Canister

EPIP

Emergency Plan Implementing Procedure

ESW

Emergency Service Water

HPCI

High Pressure Coolant Injection

HSM

Horizontal Storage Module

HVAC

Heating, Ventilation and Air Conditioning

IMC

Inspection Manual Chapter

IP

Inspection Procedure

IR

Inspection Report

ISFSI

Independent Spent Fuel Storage Installation

LEFM

Leading Edge Flow Meter

LER

Licensee Event Report

LPCI

Low Pressure Coolant Injection

MSPI

Mitigating Systems Performance Index

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NRC

U.S. Nuclear Regulatory Commission

OI

Operating Instruction

OSC

Operational Support Center

PARS

Publicly Available Records System

PI

Performance Indicator

RB

Reactor Building

RCE

Root Cause Evaluation

RCIC

Reactor Core Isolation Cooling

RHR

Residual Heat Removal

RWS

River Water Supply

SDP

Significance Determination Process

SL

Severity Level

STP

Surveillance Test Procedure

TAR

Technical Assessment for Reportability

TIP

Traversing Incore Probe

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

WO

Work Order

P. Wells

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Mark Ring, Branch Chief

Branch 1

Division of Reactor Projects

Docket No. 50-331

License No. DPR-49

Enclosure:

Inspection Report 05000331/2011005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

DISTRIBUTION:

See next page

DOCUMENT NAME: G:\\DRPIII\\1-Secy\\1-Work In Progress\\DUA 2011 005.docx

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Non-Publicly Available

Sensitive

Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

E RIII

RIII

RIII

NAME

MRing:cs

DATE

01/31/12

OFFICIAL RECORD COPY

Letter to P. Wells from M. Ring dated January 31, 2012

SUBJECT:

DUANE ARNOLD ENERGY CENTER - NRC INTEGRATED INSPECTION

REPORT 05000331/2011005

DISTRIBUTION:

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