ML111290768

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IR 05000482-11-002, on 01/01/11 - 03/31/11, Wolf Creek
ML111290768
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 05/09/2011
From: Geoffrey Miller
NRC/RGN-IV/DRP/RPB-B
To: Matthew Sunseri
Wolf Creek
References
IR-11-002
Download: ML111290768 (73)


See also: IR 05000482/2011002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I V

1600 EAST LAMAR BLVD

ARLINGTON, TEXAS 76011-4125

May 9, 2011

Matthew Sunseri, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Subject: WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION

REPORT 05000482/2011002

Dear Mr. Sunseri:

On March 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at your Wolf Creek Generating Station. The enclosed integrated inspection report documents

the inspection findings, which were discussed on April 7, 2011, with you and other members of

your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the NRC has identified 11 issues that were evaluated

under the risk significance determination process as having very low safety significance

(Green). The NRC has determined that violations are associated with all of these issues.

However, because of the very low safety significance and because they were entered into your

corrective action program, the NRC is treating these findings as noncited violations, consistent

with Section 2.3.2 of the NRC Enforcement Policy.

If you contest the violations or the significance of the noncited violations, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.

20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission,

Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the

NRC Resident Inspector at the facility. In addition, if you disagree with the crosscutting aspect

assigned to any finding in this report, you should provide a response within 30 days of the date

of this inspection report, with the basis for your disagreement, to the Regional Administrator,

Region IV, and the NRC Resident Inspector at the facility.

Wolf Creek Nuclear Operating Corporation -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response, if you choose to provide one for cases where a response is not

required, will be made available electronically for public inspection in the NRC Public Document

Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not

include any personal privacy or proprietary, information so that it can be made available to the

Public without redaction.

Sincerely,

/RA/

Geoffrey B. Miller

Chief, Project Branch B

Division of Reactor Projects

Docket No. 50-482

License No. NPF-42

Enclosure:

NRC Inspection Report 05000482/2011002

w/Attachment: Supplemental Information

Distribution via Listserv

Wolf Creek Nuclear Operating Corporation -3-

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Art.Howell@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

DRP Deputy Director (Troy.Pruett@nrc.gov)

DRS Director (Anton.Vegel@nrc.gov)

Senior Resident Inspector (Chris.Long@nrc.gov)

Resident Inspector (Charles.Peabody@nrc.gov)

Resident Inspector (Brian.Tindell@nrc.gov)

Resident Inspector (Dustin.Reinert@nrc.gov)

WC Administrative Assistant (Shirley.Allen@nrc.gov)

Branch Chief, DRP/B (Geoffrey.Miller@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

Project Engineer, DRP/B (Greg.Tutak@nrc.gov)

Project Engineer, DRP/B (Nestor.Makris@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Randy.Hall@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

Executive Technical Assistant (Stephanie.Bush-Goddard@nrc.gov)

OEMail Resource

ROPreports

DRS/TSB STA (Dale.Powers@nrc.gov)

RSLO (Bill.Maier@nrc.gov)

NSIR (Robert.Kahler@nrc.gov)

NSIR/DPR/EP (Eric.Schrader@nrc.gov)

R:\_REACTORS\_WC\2011\WC2011002-CML.docx

ADAMS: No Yes SUNSI Review Complete Reviewer Initials: GM

Publicly Available Non-Sensitive

Non-Publicly Available Sensitive

SRI:DRP/B RI:DRP/B SRI:DRP/B RI:DRP/B

CLong CPeabody BTindell DReinert

/E-Mail for / /E-Mail for/ /E-Mail for / /E-Mail for /

5/9/2011 5/9/2011 5/9/2011 5/9/2011

C:DRS/EB1 C:DRS/EB2 C:DRS/PSB C:DRS/OB

TFarnholtz NOKeefe MShannon MHaire

/RA/ /RA/ /EByre for/ /RA/

5/6/2011 5/6/2011 5/6/2011 5/6/2011

DRS/PSB2 C:DRP/B

GWerner GMiller

/RA/ /RA/

5/6/2011 5/9/2011

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000482

License: NPF-42

Report: 05000482/2011002

Licensee: Wolf Creek Nuclear Operating Corporation

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane NE

Burlington, Kansas

Dates: January 1 to March 31, 2011

Inspectors: C. Long, Senior Resident Inspector

B. Tindell, Acting Senior Resident Inspector

J. Drake, Senior Reactor Inspector

C. Peabody, Resident Inspector

D. Reinert, Acting Resident Inspector

C. Smith, Reactor Inspector

A. Fairbanks, Reactor Inspector

G. Guerra, CHP, Emergency Preparedness Inspector

L. Carson II, Senior Health Physicist

C. Alldredge, Health Physicist

Approved By: G. Miller, Chief, Project Branch B

Division of Reactor Projects

-1- Enclosure

SUMMARY OF FINDINGS

IR 05000482/2011002, 1/1/2011 - 3/31/2011; Wolf Creek Generating Station, Integrated

Resident and Regional Report; Equipment Alignment, Maintenance Effectiveness, Operability

Determinations and Functionality Assessments, Postmaintenance Testing, Refueling and Other

Outage Activities, Surveillance Testing, and Radiological Hazard Assessment and Exposure

Controls.

The report covered a 3-month period of inspection by resident inspectors and announced

baseline inspections by region-based inspectors. Eleven Green noncited violations of

significance were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination

Process. The crosscutting aspect is determined using Inspection Manual Chapter 0310,

Components Within the Cross Cutting Areas. Findings for which the significance

determination process does not apply may be Green or be assigned a severity level after NRC

management review. The NRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,

dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors reviewed a self-revealing noncited violation of Technical

Specification 5.4.1.a, Procedures, involving the failure to follow the requirements of

Procedure AP 21E-001, Clearance Orders. This procedure violation resulted in an

inadequate tagout for the Train A solid state protection system resulting in an unplanned

swap of the volume control tank charging pump suction to the reactor water storage tank

and an unplanned entry into Technical Specification 3.4.12 due to the de-energization of

power operated relief valve A low temperature overpressure protection relays.

Operators took manual actions to restore the pump suction, and power was restored

after approximately four hours. This finding has been entered into the licensees

corrective action program as Condition Reports 35288 and 35318.

The failure to follow procedures to complete clearance orders with adequate boundaries

is a performance deficiency. The performance deficiency was more than minor because

it impacted the Initiating Events Cornerstone objective of configuration control to limit the

likelihood of those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. The significance of the finding was

determined using Inspection Manual Chapter 0609, Significance Determination Process,

Appendix G, Checklist 2, and determined to be of very low safety significance, because

it did not cause the loss of mitigating capability of core heat removal, inventory control,

power availability, containment control, or reactivity control. Additionally, the cause of

the finding is related to the human performance crosscutting component of work control.

Specifically, the licensee did not appropriately plan for the maintenance work scope by

-2- Enclosure

ensuring work groups and an offsite organization communicate the necessary electrical

boundaries to assure plant and human performance H.3(b) (Section 1R20).

Cornerstone: Mitigating Systems

Green. The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B,

Criterion III, for the failure to assure that applicable regulatory requirements and the

design basis were met. Specifically, the licensee failed to ensure that the fuel oil storage

tank fill system minimized turbulence, as required by the Updated Safety Analysis

Report, such that the emergency diesel generators can be refueled while running

uninterrupted. The licensee entered this issue in the corrective action program and will

develop corrective actions as part of Condition Report 34730.

The failure to establish measures to assure that applicable regulatory requirements and

the design basis are met was a performance deficiency. The performance deficiency

was more than minor because it impacted the Mitigating Systems Cornerstone attribute

of design control and affects the associated cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using Inspection Manual Chapter 0609.04,

"Phase 1 - Initial Screening and Characterization of Findings," the inspectors

determined that the finding had very low safety significance because it did not result in a

loss of system safety function, an actual loss of safety function of a single train for

greater than its technical specification allowed outage time, or screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event. This finding has

a crosscutting aspect in the area of human performance associated with the decision

making component because the licensee failed to use conservative assumptions in

decision making and adopt a requirement to demonstrate the proposed action is safe in

order to proceed rather than a requirement to demonstrate that it is unsafe in order to

disapprove the action H.1(b) (Section 1R04).

Green. The inspectors reviewed a self-revealing noncited violation of Technical Specification 5.4.1.a involving the failure to properly implement the clearance order

procedure resulting in a failure to provide adequate cooling to inservice safety-related

equipment. Operators restored cooling water flow after approximately one hour. The

licensee entered the finding into their corrective action program as Condition

Report 33357.

The inspectors determined that the failure to ensure that plant conditions could support

establishing the clearance order boundaries, which resulted in a component cooling

water heatup and trip of the inservice control room air conditioner, was a performance

deficiency. The inspectors determined that this finding was more than minor because it

is associated with the configuration control attribute for the Mitigating Systems

Cornerstone and it affected the cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, the finding was determined to have very low safety

significance because it was confirmed not to result in loss of operability of control room

-3- Enclosure

air conditioning Train B for greater than its technical specification allowed outage time

and it did not result in the loss of the normal service water function for greater than 24

hours. This finding has a crosscutting aspect in the area of human performance

associated with work control because the licensee failed to plan the work activity by

incorporating the impact on the plant H.3(a) (Section 1R04).

Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(1) with three

examples involving the failure to monitor the performance of stand by nonsafety-related

systems and components that exceeded performance criteria against goals. First, the

inspectors identified that the licensee failed to monitor the turbine-driven main feedwater

pumps against their standby restart function to fill the steam generators in emergency

operating procedures. Failures of the two turbine-driven main feedwater pumps

occurred which could have prevented fulfillment of this function. Second, the inspectors

identified that the licensee failed to evaluate reactor trips caused by the main feedwater

system against the systems plant level monitoring criteria. Third, the inspectors

identified that the licensee failed to monitor the instrument air compressor system

against its emergency operating procedure function to restart and provide compressed

air. Several instrument air compressor trips have occurred in the last 18 months which

could have prevented fulfillment of this function. The licensee entered this issue in the

corrective action program and will develop corrective actions as part of Condition Report

36600.

The failure to establish performance monitoring goals commensurate with the mitigating

safety function specified in the emergency operating procedures and the plant level

criteria is a performance deficiency. The performance deficiency is more than minor, and

therefore a finding, because it impacts equipment performance attribute of the Mitigating

Systems Cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences (i.e., core

damage). Using the NRC Inspection Manual Chapter 0609, Attachment 0609.04,

Phase 1 - Initial Screening and Characterization of Findings, the finding screened to a

Phase 2 significance determination because it involved a potential loss of safety function

of the main feedwater system and failure of the instrument air system. A Region IV

senior reactor analyst performed a Phase 2 significance determination and using the

pre-solved worksheet from the Risk Informed Inspection Notebook for the Wolf Creek,

Revision 2.01a; however, the presolved worksheet did not include the simultaneous

failure of multiple components in different systems. Therefore, the senior reactor analyst

performed a bounding Phase 3 significance determination using Appendix M of

Inspection Manual Chapter 0609, Significance Determination Process Using Qualitative

Criteria, Section 4.1.2. The analyst determined that the finding was of very low safety

significance (Green). The bounding change to the core damage frequency was

approximately 8 E-7/year. The relatively low risk worth of the instrument air system at

Wolf Creek helped to mitigate the significance. To evaluate the change to the large early

release frequency (LERF), the analyst used Inspection Manual Chapter 0609,

Appendix H, Containment Integrity Significance Determination Process. The finding

screened as having very low safety significance for LERF because it did not affect the

intersystem loss of coolant accident or steam generator tube rupture categories. The

inspectors determined that the finding had a crosscutting aspect in the area of problem

-4- Enclosure

identification and resolution. Specifically, when Wolf Creek evaluated exceeding the

plant level monitoring criteria for reactor trips, their analysis did not identify that failures

within the main feedwater system were the cause of four of the six reactor trips, and did

not place the affected system function in a(1) monitoring P.1(c) (Section 1R12).

Green. The inspectors identified a noncited violation of 10 CFR 50.65 a(2), involving the

failure to demonstrate that the performance of main control board annunciator power

supplies was effectively controlled through preventive maintenance such that the

annunciators remained capable of performing their intended function. The licensee

entered this issue into the corrective action program and will develop corrective actions

as part of Condition Report 34681.

The failure to properly evaluate the failed main control board annunciator power

supplies, establish performance goals, and monitor their performance is considered a

performance deficiency. This finding is more than minor because it is associated with

the Mitigating Systems Cornerstone attribute of equipment performance and it adversely

affects the cornerstone objective ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Using

the Inspection Manual Chapter 0609, Significance Determination Process, Phase 1

Worksheets, the finding is determined to have very low safety significance since it did

not result in a loss of system safety function, an actual loss of safety function of a single

train for greater than its technical specification allowed outage time, or screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

This finding was determined to have a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action program because the

licensee failed to properly classify, prioritize, and evaluate a condition adverse to quality

P.1(c) (Section 1R12).

Green. The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B,

Criterion III, involving an inadequate calculation supporting vital switchgear room

temperatures with only one vital switchgear cooler operable. The licensee entered this

issue in the corrective action program and will develop corrective actions as part of

Condition Reports 27276, 28252, and 31452.

The inspectors considered the inadequate heat loads and assumptions used in

calculation GK-06-W to be a performance deficiency. The performance deficiency is

more than minor, and therefore a finding, because it impacted with the equipment

performance attribute of the Mitigating Systems Cornerstone and it affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events. Using Inspection Manual Chapter 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, the inspectors screened the finding

to Green because the additional temperatures would not have caused the loss of

functionality of vital switchgear or batteries, and it did not screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event. No crosscutting

aspects were identified because the supporting documentation was prepared in the late

1990s and was not representative of current licensee performance (Section 1R15).

-5- Enclosure

Green. The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B,

Criterion V, involving the failure to follow plant procedures. Specifically, the licensee

failed to follow procedure and perform an operability determination when a

nonconforming or degraded condition was identified in the Train B emergency diesel

generator fuel oil storage tank, as required by Procedure AP 26C-004, Operability

Determination and Functionality Assessment, Revision 21. The licensee subsequently

performed an operability determination and concluded the fuel oil storage tank was

operable but degraded. The licensee entered this issue in the corrective action program

as Condition Reports 33355 and 34068.

The failure to follow Procedure AP 26C-004, Operability Determination and

Functionality Assessment, Revision 21, when a nonconforming or degraded condition

was identified was a performance deficiency. This performance deficiency was more

than minor because it could become a more significant safety concern if left uncorrected.

Using Inspection Manual Chapter 0609.04, "Phase 1 - Initial Screening and

Characterization of Findings," the inspectors determined that the finding had very low

safety significance (Green) because it did not result in a loss of system safety function,

an actual loss of safety function of a single train for greater than its technical

specification allowed outage time, or screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with the corrective

action program component because the licensee failed to thoroughly evaluate problems,

including evaluating for operability, such that the resolution addressed the cause P.1(c)

(Section 1R15).

Green. The inspectors identified a noncited violation of 10 CFR Part 50 Appendix B,

Criterion III, involving a failure to perform periodic testing to verify that ultimate heat sink

sedimentation remained within design basis limits. The licensee subsequently verified

the ultimate heat sink depth remained acceptable using SONAR. The licensee entered

this issue in the corrective action program as Condition Report 27144.

Wolf Creeks failure to perform periodic testing to verify that ultimate heat sink

sedimentation remained within design basis limits is a performance deficiency. The

issue is more than minor, and therefore a finding, because if left uncorrected the issue

has the potential to become a more significant safety concern. The inspectors

concluded that the issue screened to Green under the significance determination

process using Inspection Manual Chapter 0609.04, Phase 1-Initial Screening and

Characterization of Findings, because the finding was a design deficiency that was later

confirmed not to result in the loss of operability or functionality of the ultimate heat sink.

The inspectors concluded that this findings cause has a crosscutting aspect in the area

of human performance associated with the work control component because Wolf Creek

did not appropriately coordinate work activities by incorporating actions to address the

impact of changes to the work scope or activity on the plant and human performance.

Specifically, when Wolf Creek performed and planned dredging preventive maintenance

on the ultimate heat sink, they did not consider the need to confirm as-found and as-left

sediment depth to verify that their design basis was met H.3(b) (Section 1R19).

-6- Enclosure

Green. The inspectors reviewed a self-revealing noncited violation of Technical Specification 5.4.1.a, Procedures, involving the failure to perform an adequate fill and

vent of the component cooling water system which resulted in voiding of the system.

The licensee entered the finding into their corrective action program and will develop

corrective actions as part of Condition Report 33925.

The inspectors determined that the failure to perform an adequate fill and vent of

component cooling water that resulted in system voiding was a performance deficiency.

The inspectors determined that this finding was more than minor because it is

associated with the human performance attribute of the Mitigating Systems Cornerstone

and it affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, the finding was determined to have very low safety

significance (Green) because it did not result in a loss of system safety function, an

actual loss of safety function of a single train for greater than its technical specification

allowed outage time, or screen as potentially risk significant due to a seismic, flooding,

or severe weather initiating event. This finding has a crosscutting aspect in the area of

problem identification and resolution associated with the corrective action program

because the licensee failed to take appropriate corrective actions from previous voiding

events P.1(d) (Section 1R19).

Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a,

Procedures, involving the failure to follow Procedure AP 21-001, Conduct of

Operations. Specifically, the licensee failed to enter into technical specification limiting

condition of operation 3.7.5.B.1 for one auxiliary feedwater pump inoperable during

performance of 92-day check valve surveillance tests. Wolf Creek took prompt

corrective action to amend the procedures to include instructions for maintaining the

pumps operable with manual actions. This occurred prior to the next check valve test.

This issue is captured in Condition Report 34469.

The failure to enter technical specification action statements in accordance with

Procedure AP 21-001 was a performance deficiency. The performance deficiency was

more than minor, and therefore a finding, because it impacted with the human

performance attribute of the Mitigating Systems Cornerstone and its objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using Inspection Manual Chapter 0609.04,

Phase 1 - Initial Screening and Characterization of Findings, the finding was

determined to be of very low safety significance (Green) because the issue did not result

in a loss of operability for a time period greater than the action statement, and did it not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The inspectors determined that the finding has a crosscutting aspect in

the area of human performance associated with decision making. Specifically, informally

maintained pre-job briefing sheets were being relied upon to determine technical

specification applicability instead of the licensees decision making process of operator

review on a case by case basis H.1.a. (Section 1R22).

-7- Enclosure

Cornerstone: Occupational Radiation Safety

Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a,

Procedures, involving the failure to follow procedure requirements related to adding

work to existing radiation work permits. Specifically, welding was performed in a locked

high radiation area on radiation work permit 110039, which did not cover that type of

activity. The licensee placed the finding into the corrective action program as Condition

Report 35522 and acknowledged that the radiation work permit used was inappropriate

for the work completed.

The failure to follow a procedure was a performance deficiency. The finding was more

than minor because it negatively impacted the Occupational Radiation Safety

Cornerstones attribute of program and process, in that the inappropriate use of a

radiation work permit led to workers unplanned and unintended dose. Using Inspection

Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance

Determination Process, the finding was determined to be of very low safety significance

because: (1) it was not associated with ALARA planning or work controls, (2) there was

no overexposure, (3) there was no substantial potential for an overexposure, and (4) the

ability to assess dose was not compromised. This deficiency had a crosscutting aspect

in the area of human performance related to work controls. Specifically, there was

inappropriate coordination and communication of work activities between work groups

H.3.b] (2RS01).

B. Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee, have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

condition report numbers are listed in Section 4OA7.

-8- Enclosure

REPORT DETAILS

Summary of Plant Status

Wolf Creek began the inspection period at 100 percent power. On January 6, 2011, Wolf Creek

decreased reactor power to 97 percent to perform testing on the auxiliary feedwater pump Train

A. Wolf Creek resumed operation at 100 percent power the same day. Wolf Creek commenced

an orderly shutdown for a scheduled refueling outage on March 18, 2011. The reactor

shutdown was completed March 19, 2011, and Wolf Creek ended the inspection period in a

refueling outage.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R04 Equipment Alignments (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk significant

systems:

  • January 5, 2011, Chemical and volume control system during tagout for vent

valve leakage

generator B was inoperable

Train B was inadvertently isolated

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Safety Analysis Report (USAR), technical specification

requirements, administrative technical specifications, outstanding work orders, condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also inspected accessible portions

of the systems to verify system components and support equipment were aligned

-9- Enclosure

correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

a. Findings

.1 Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, for the failure to assure that applicable regulatory requirements

and the design basis were met. Specifically, the licensee failed to ensure that the fuel oil

storage tank fill system minimized turbulence, as required by the Updated Safety

Analysis Report, such that the emergency diesel generators can be refueled while

running uninterrupted.

Description. The Wolf Creek USAR requires, in part, that the addition of fuel oil to the

fuel oil storage tanks be done in a way that minimizes the creation of turbulence such

that the emergency diesel generators can be refueled while running uninterrupted,

consistent with Regulatory Guide 1.137. Turbulence has the potential to stir up

sediment which could cause the overall quality of fuel oil in the storage tank to become

unacceptable and clog engine fuel oil filters.

The NRC examined this issue during plant licensing. NRC question 430.14, as stated in

the USAR, proposed two alternatives for minimizing turbulence:

1. Design a fuel oil storage tank fill system that will minimize turbulence in the tank.

2. Cross connect the fuel oil storage tank of each diesel in a manner that will permit

supply of fuel oil to either engine from either tank. In this manner, one tank could

be filled while the other tank supplies fuel to the operating diesel generator. After

filling the tank, fuel would not be drawn from the tank for a period of time to

permit settling of sediment.

From the period of initial operation to 2001, Wolf Creek utilized the cross-connect lines

to allow for the settling of sediment when filling the diesel storage tanks (alternative 2)

which would not interrupt operation of either engine. Originally, the cross-connect lines

were tested by technical specification surveillance requirement 4.8.1.1.2g.10. Wolf

Creek converted from Westinghouse standard technical specifications to improved

technical specifications in 1999, at which point this surveillance requirement was moved

to the licensee controlled USAR.

After the conversion to improved technical specifications, USAR Section 9.5.4.4 stated,

A verification that the fuel oil transfer pump is capable of transferring fuel oil from each

- 10 - Enclosure

fuel oil storage tank to the day tank of the opposite train via the installed cross-connect

line is performed every 18 months during a refueling outage. However, a series of

performance improvement requests (PIR), were written to address the fact that there

were no operating procedures for cross tying the fuel oil storage tanks. PIR 2001-1104

provided the justification for the deletion of surveillance Procedure STN JE-002,

Emergency Fuel Oil System Crosstie Flow Test, and the applicable portion of USAR

Section 9.5.4.4. PIR 2001-1104 stated the fuel oil storage tank was, in fact, designed to

minimize turbulence during filling operations (alternative 1 of NRC question 430.14).

The inspectors questioned how the licensee was in compliance with Regulatory

Guide 1.137, as endorsed by the USAR, with the deletion of requirements for cross tying

the fuel oil storage tanks when no other physical changes or analyses were performed.

PIR 2001-1104 identified that another plant modified its fuel oil fill lines to minimize

turbulence consistent with Regulatory Guide 1.137; however, Wolf Creek did not adopt

similar changes.

On March 7, 2011, the licensee generated engineering disposition Condition

Report 30468 which stated that Wolf Creek, Does not have a calculation to evaluate the

hydraulic effects of the fuel oil filling the tank. However, the churning and buouyancy

[sic] effects on the sediment of 2 gallons per second falling less than 15 feet into 6,694

gallons (initially) of fuel oil is judged to be minimal. The inspectors determined that the

qualitative statements provided inadequate justification for asserting the design of the fill

system minimizes turbulence. The inspectors further identified USAR Section 9.5.4.2.1

states, System operation provides flow to motivate water toward sump, tank

replenishment provides similar motive force. The inspectors concluded that the fill

system was not designed to minimize turbulence, and the licensees justification that the

design prevented turbulence lacked an adequate technical basis. The licensee initiated

Condition Report 34730 which will restore compliance with the USAR and Regulatory

Guide 1.137.

Analysis. The failure to establish measures to assure that applicable regulatory

requirements and the design basis are met was a performance deficiency. The

performance deficiency was more than minor because it impacted the Mitigating

Systems Cornerstone attribute of design control and affects the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Using Inspection Manual

Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the

inspectors determined that the finding had very low safety significance because it did not

result in a loss of system safety function, an actual loss of safety function of a single train

for greater than its technical specification allowed outage time, or screen as potentially

risk significant due to a seismic, flooding, or severe weather initiating event. This finding

has a crosscutting aspect in the area of human performance associated with the

decision making component because the licensee failed to use conservative

assumptions in decision making and adopt a requirement to demonstrate the proposed

action is safe in order to proceed rather than a requirement to demonstrate that it is

unsafe in order to disapprove the action H.1(b).

- 11 - Enclosure

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,

in part, that measures shall be established to assure that applicable regulatory

requirements and the design basis are correctly translated into specifications, drawings,

procedures, and instructions. Contrary to the above, from 2001 until 2011, the

measures established by the licensee failed to assure that applicable regulatory

requirements and the design basis were correctly translated into specifications,

drawings, procedures, and instructions. Specifically, the licensee failed to ensure the fill

system for the fuel oil storage tanks minimized the creation of turbulence to ensure that

emergency diesels run without interruption, as required by the USAR, consistent with

Regulatory Guide 1.137. Because this violation was of very low safety significance and

was entered into the licensee's corrective action program (Condition Report 34730), this

violation is being treated as a noncited violation, consistent with Section 2.3.2 of the

NRC Enforcement Policy: NCV 05000485/2011002-01, Inadequate Design Control of

the Fuel Oil Storage Tank Fill System.

.2 Introduction. The inspectors reviewed a Green self-revealing noncited violation of

Technical Specification 5.4.1.a involving the failure to properly implement the clearance

order procedure resulting in a failure to provide adequate cooling to inservice safety-

related equipment.

Description. On February 10, 2011, operations personnel isolated Train B essential

service water return to the ultimate heat sink in preparations for motor-operated valve

testing in accordance with clearance order D-EF-B-021. Approximately 10 minutes after

the return line was isolated, operations personnel in the control room noted that the

temperature of some components was unexpectedly increasing. Operations personnel

then determined that all service water cooling to Train B had been lost due to the

isolation of the ultimate heat sink return line and restored cooling water flow. The

licensee initiated Condition Report 33357 to document the error.

Licensee personnel who had planned the work and prepared and authorized the ultimate

heat sink return line isolation failed to consider that the normal service water system

uses the ultimate heat sink return line to return water to the lake during the winter. As a

result, when the return line was isolated, flow through various Train B heat exchangers

was isolated for approximately one hour. Equipment that lost cooling included inservice

Train B mitigation equipment, such as component cooling water, all Train B pump room

coolers, containment air coolers, the vital switchgear air conditioner, and the control

room air conditioner.

Analysis. The inspectors determined that the failure to ensure that plant conditions

could support establishing the clearance order boundaries, which resulted in a

component cooling water heatup and trip of the inservice control room air conditioner,

was a performance deficiency. The inspectors determined that this finding was more

than minor because it is associated with the configuration control attribute for the

Mitigating Systems Cornerstone and it affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using Inspection Manual Chapter 0609.04, Phase

1 - Initial Screening and Characterization of Findings, the finding was determined to

have very low safety significance because it was confirmed not to result in loss of

- 12 - Enclosure

operability of control room air conditioning Train B for greater than its technical

specification allowed outage time and it did not result in the loss of the normal service

water function for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. This finding has a crosscutting aspect in the

area of human performance associated with work control because the licensee failed to

plan the work activity by incorporating the impact on the plant H.3(a).

Enforcement. Technical Specification 5.4.1.a, Procedures, requires that written

procedures be established and implemented covering activities specified in Appendix A,

Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality

Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,

Appendix A, Section 1, requires, in part, that the licensee control equipment (e.g. locking

and tagging) in accordance with written instructions. Wolf Creek

Procedure AP 21E-001, Clearance Orders, Revision 26, is used for equipment control.

Step 5.11.2 of Procedure AP 21E-001, requires, in part, ensuring that plant conditions

support establishing the clearance order boundaries. Contrary to the above, on

February 10, 2011, the licensee implemented clearance order D-EF-B-021 without

ensuring that plant conditions supported establishing the clearance order boundaries.

Specifically, the clearance order boundary inadvertently isolated cooling water to

inservice safety-related equipment. Because of the very low safety significance of this

finding and because the licensee entered this issue into the corrective action program as

Condition Report 33357, this violation is being treated as a noncited violation in

accordance with Section 2.3.2 of the NRC Enforcement Policy:

NCV 05000482/2011002-02, Inadequate Clearance Order Isolated Cooling to Inservice

Train B Safety-Related Equipment.

.2 Complete Walkdown

a. Inspection Scope

On March 28, 2011, the inspectors performed a complete system alignment inspection of

the spent fuel pool cooling system to verify the functional capability of the system. The

inspectors selected this system because it was considered both safety significant and

risk significant in the licensees probabilistic risk assessment. The inspectors inspected

the system to review mechanical and electrical equipment line ups, electrical power

availability, system pressure and temperature indications, as appropriate, component

labeling, component lubrication, component and equipment cooling, hangers and

supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. The inspectors reviewed a sample of

past and outstanding work orders to determine whether any deficiencies significantly

affected the system function. In addition, the inspectors reviewed the corrective action

program database to ensure that system equipment alignment problems were being

identified and appropriately resolved. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as

defined in Inspection Procedure 71111.04-05.

- 13 - Enclosure

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk significant

plant areas:

  • January 27, 2011, Fire Area A2
  • January 27, 2011, Fire Area A4
  • February 7, 2011, Fire Area F15
  • February 7, 2011, Fire Area F17

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants individual plant examination of external events with later

additional insights, their potential to affect equipment that could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples

as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

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1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

On February 18, 2011, the inspectors observed essential service water Train B cable

vaults to verify the cables were not submerged. In addition, the inspectors observed the

material condition of the cable supports. The inspectors reviewed the licensees efforts

to maintain the cables in a qualified environment. The inspectors reviewed the

corrective action program to determine if licensee personnel identified and corrected

flooding problems.

These activities constitute completion of one bunker/manhole sample as defined in

Inspection Procedure 71111.06-05.

b. Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed licensee programs, verified performance against industry

standards, and reviewed critical operating parameters and maintenance records for the

component cooling water heat exchangers. The inspectors verified that performance

tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for

problems or errors; the licensee utilized the periodic maintenance method outlined in

EPRI Report NP 7552, Heat Exchanger Performance Monitoring Guidelines; the

licensee properly utilized biofouling controls; the licensees heat exchanger inspections

adequately assessed the state of cleanliness of their tubes; and the heat exchanger was

correctly categorized under 10 CFR 50.65, Requirements for Monitoring the

Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed

during this inspection are listed in the attachment.

These activities constitute completion of one heat sink inspection sample as defined in

Inspection Procedure 71111.07-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On February 10, 2011, the inspectors observed a crew of licensed operators perform a

shutdown to Mode 5 in the plants simulator to verify that operator performance was

adequate, evaluators were identifying and documenting crew performance problems and

- 15 - Enclosure

training was being conducted in accordance with licensee procedures. The inspectors

evaluated the following areas:

  • Licensed operator performance
  • Crews clarity and formality of communications
  • Crews ability to take timely actions in the conservative direction
  • Crews prioritization, interpretation, and verification of annunciator alarms
  • Crews correct use and implementation of abnormal and emergency procedures
  • Control board manipulations
  • Oversight and direction from supervisors
  • Crews ability to identify and implement appropriate technical specification

actions and emergency plan actions and notifications

The inspectors compared the crews performance in these areas to pre-established

operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed operator requalification

program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

  • February16, 2011, NF-01, Load shedding and emergency load sequencer
  • March 8, 2011, AD-04, Condensate pump discharge to main feed suction
  • March 9, 2011, KA-01, Instrument air compressors
  • March 21, 2011, RK-01, Main control board annunciators and power supplies

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

- 16 - Enclosure

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of five quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b. Findings

.1 Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65(a)(1)

with three examples involving the failure to monitor the performance of standby

nonsafety-related systems and components that exceeded performance criteria against

goals. First, the inspectors identified that the licensee failed to monitor the turbine-driven

main feedwater pumps against their standby restart function to fill the steam generators

in emergency operating procedures. Failures of the two turbine-driven main feedwater

pumps occurred which could have prevented fulfillment of this function. Second, the

inspectors identified that the licensee failed to evaluate reactor trips caused by the main

feedwater system against the systems plant level monitoring criteria. Third, the

inspectors identified that the licensee failed to monitor the instrument air compressor

system against its emergency operating procedure function to restart and provide

- 17 - Enclosure

compressed air. Several instrument air compressor trips have occurred in the last 18

months which could have prevented fulfillment of this function.

Description. Regulatory Guide 1.160, Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants, provides industry guidance for compliance with 10 CFR 50.65,

The Maintenance Rule. This regulatory guide endorses NUMARC 93-01, Industry

Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants,

Revision 2, with some exceptions as specified in the regulatory guide. The scope of

10 CFR 50.65 includes nonsafety-related components that are utilized in emergency

operating procedures.

The inspectors reviewed the main feedwater system maintenance rule functions and

scoping. Function AE-01 requires feedwater to the steam generators using only

turbine-driven main feedwater pumps. This function monitors nonsafety equipment

which could cause a plant trip or actuation of safety-related systems, as well as for a

nonsafety-related function which is used in the emergency operating procedures to

provide accident mitigation. Function AE-01 monitored the steam-driven pumps at the

plant level and was in a(2) status. The inspectors identified that the steam-driven main

feed pumps were not monitored for their emergency operating procedure function, per

the AE-01 scoping. The licensee had concluded that the emergency operating

procedure function for the steam-driven main feedwater pumps was not subject to

monitoring under the maintenance rule because it did not perform a significant fraction of

the mitigating function (i.e., it was not risk significant) in accordance with Section 1.1.2 of

Regulatory Guide 1.160. The inspectors reviewed the regulatory guide and determined

that Wolf Creek had improperly applied the guidance. Section 1.1.2 of Regulatory Guide 1.160 requires that all equipment that is explicitly addressed in the emergency operating

procedures be monitored for maintenance effectiveness. Regulatory Guide 1.160

specifies that only equipment that is not explicitly addressed, but the use of which is

implied, may be excluded on the basis of risk. The inspectors concluded that the

exclusion of the turbine-driven main feedwater pumps based on risk consideration was

not appropriate since the pumps are explicitly identified to mitigate an accident in

emergency operating Procedure FR-H1, step 14.

The inspectors performed additional inspection samples of Wolf Creek maintenance rule

functions and identified that additional standby mitigating components explicitly

referenced in the emergency operating procedures were not being monitored for the

following systems:

  • Condensate pumps - function AD-04
  • Instrument air compressors - function KA-01
  • Non-IE electrical - functions PA-01, PB-01, PG-01, PK-01, and SL-01

The inspectors reviewed the equipment history over the past 3 years for these systems

and found that the instrument air compressors had a history of component failures due

to maintenance practices, most notably repetitive lube oil pressures and levels being out

of specification, leading to subsequent failures. The inspectors identified seven

compressor demand failures between November 18, 2008, and March 1, 2011, but no

- 18 - Enclosure

maintenance rule functional failure evaluations were performed. The inspectors

concluded the licensee had failed to appropriately monitor the performance of the

instrument air compressors standby emergency restart function

Regulatory Guide 1.160, Section 1.7.1, Plant Level Cause Determinations, states, in

part, for all structures, systems or components that are being monitored using plant level

performance criteria, a cause determination is required whenever any of these

performance criteria are exceeded in order to determine which structure, system or

component caused the criterion to be exceeded or whether the failure was a repetitive

maintenance preventable functional failure. As part of the cause determination, it would

also be necessary to determine whether the structure, system or component was within

the scope of the maintenance rule and, if so, whether corrective action and monitoring

(tracking, trending, and goal setting) under 10 CFR 50.65(a)(1) should be performed.

Wolf Creek plant level criteria has been in a(1) status for reactor trips since May 13,

2010. Over the past 3-year monitoring period, Wolf Creek has experienced the following

reactor trips:

  • March 17, 2008, XPB03 13.8kV transformer failure
  • April 28, 2009, Main feed regulating valve closure due to fuse failure
  • August 19, 2009, Loss of offsite power
  • March 2, 2010, Main feed pump A trip due to PN09 bus failure
  • March 8, 2010, Main feed pump A trip due to servo malfunction

oscillations caused by feed regulating bypass valve control

The inspectors identified that four plant trips were related to the main feedwater system.

Furthermore, all of the main feedwater events were maintenance related. The PN09 bus

and servo failures were direct results of maintenance activities and the fuse failure was

caused by a lack of preventive maintenance. However, the licensee evaluation did not

attribute any of the failures to the feedwater system. Since the main feedwater system

and function is a dominant contributor to the plant level monitoring function for reactor

trips it should have also been placed in a(1) and appropriate corrective actions to restore

to a(2) status established. This issue is captured in Condition Report 27144.

Analysis: The failure to establish performance monitoring goals commensurate with the

mitigating safety function specified in the emergency operating procedures and the plant

level criteria is a performance deficiency. The performance deficiency is more than

minor, and therefore a finding, because it impacts equipment performance attribute of

the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage). Using the NRC Inspection Manual Chapter 0609,

Attachment 0609.04, Phase 1 - Initial Screening and Characterization of Findings, the

finding screened to a Phase 2 significance determination because it involved a potential

loss of safety function of the main feedwater system and failure of the instrument air

system. A Region IV senior reactor analyst performed a Phase 2 significance

determination and using the pre-solved worksheet from the Risk Informed Inspection

Notebook for the Wolf Creek, Revision 2.01a; however, the pre-solved worksheet did

- 19 - Enclosure

not include the simultaneous failure of multiple components in different systems.

Therefore, the senior reactor analyst performed a bounding Phase 3 significance

determination using Appendix M of Inspection Manual Chapter 0609, Significance

Determination Process Using Qualitative Criteria, Section 4.1.2. The analyst

determined that the finding was of very low safety significance (Green). The bounding

change to the core damage frequency was approximately 8 E-7/year. The dominant

core damage sequences involved a loss of component cooling water, failure of operators

to recover component cooling water, the failure of operators to start a charging pump

and a reactor coolant pump seal loss of coolant accident. The relatively low risk worth of

the instrument air system at Wolf Creek helped to mitigate the significance. To evaluate

the change to the large early release frequency (LERF), the analyst used Inspection

Manual Chapter 0609, Appendix H, Containment Integrity Significance Determination

Process. Wolf Creek has a large dry containment. The finding screened as having very

low safety significance for LERF because it did not affect the intersystem loss of coolant

accident or steam generator tube rupture categories. The inspectors determined that

the finding had a crosscutting aspect in the area of problem identification and resolution.

Specifically, when Wolf Creek evaluated exceeding the plant level monitoring criteria for

reactor trips, their analysis did not identify that failures within the main feedwater system

were the cause of four of the six reactor trips, and did not place the affected system

function in a(1) monitoring P.1(c).

Enforcement: Title 10 CFR 50.65(a)(1) requires, in part, that each holder of an operating

license for a nuclear power plant shall monitor the performance or condition of

structures, systems, or components, against licensee-established goals, in a manner

sufficient to provide reasonable assurance that these structures, systems, and

components, as defined in paragraph (b) of this section, are capable of fulfilling their

intended functions. These goals shall be established commensurate with safety and,

where practical, take into account industry-wide operating experience. The scope of

paragraph (b) includes, in part, nonsafety-related structures, systems, and components

that are used in emergency operating procedures. Title 10 CFR 50.65(a)(2) states in

part, that monitoring as specified in paragraph (a)(1) is not required where it has been

demonstrated that the performance or condition of a structure, system or component is

being effectively controlled through the performance of preventive maintenance such

that the structure, system or component remains capable of performing its intended

function.

Contrary to the above, from January 1, 2008, to March 3, 2011, the licensee did not

establish goals sufficient to provide reasonable assurance that structures, systems, and

components, as defined in paragraph (b) of 10 CFR 50.65, were capable of fulfilling their

intended functions. Specifically, (1) Wolf Creek did not establish appropriate goals to

monitor the performance of the turbine-driven main feedwater system functions under

operating conditions. This function was not fulfilled when failures in the main feedwater

system caused reactor trips on April 28, 2009, March 2 and 8, and October 17, 2010.

(2) Wolf Creek did not establish appropriate goals to monitor the performance of the

turbine-driven main feedwater system standby restart function, as specified in

emergency operating procedures. This function was not fulfilled when the pumps failed

to restart during the recovery from the reactor trips of April 28 and August 19, 2009, and

- 20 - Enclosure

the failures were not evaluated against any goals or criteria. (3) Wolf Creek did not

establish appropriate goals to monitor the performance of the instrument air

compressors standby emergency restart function. Specifically, seven compressor

demand failures occurred on November 18 and December 18, 2008; January 7,

February 6, and May 14, 2009; March 10, 2010; and March 1, 2011. No monitoring

goals were set and no evaluation of these failures was performed, leaving insufficient

basis for the function to remain in 10 CFR 50.65(a)(2) status.

Because this violation is of very low safety significance (Green) and has been entered

into the licensees corrective action program as Condition Report 36600, this violation is

being treated as a noncited violation consistent with Section 2.3.2 of the NRC

Enforcement Policy: NCV 05000482/2011002-03, Failure to Monitor the Performance

of Nonsafety-Related Systems and Components Used in the Plant Emergency

Operating Procedures under 10 CFR 50.65 Programs.

.2 Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65 a(2),

involving the failure to demonstrate that the performance of main control board

annunciator power supplies was effectively controlled through preventive maintenance

such that the annunciators remained capable of performing their intended function.

Description. The maintenance rule a(2) reliability criteria for function RK-01, to provide

the control room operator a visual and audible plant status condition, is less than two

functional failures per 18 months. A functional failure is defined as an unplanned loss of

more than six percent of the total annunciators. Performance of this function is

monitored by tracking power supply failures since any power supply failure will result in a

loss of more than six percent of the total annunciators. On October 13, 2009, 23 percent

of main control board annunciators were lost due to independent failures of two power

supplies, RK045E1PS2 and RK045E3PS1. Power supply E3PS1 fed 10.7 percent of

the annunciators and power supply E1PS2 fed 12.1 percent of the annunciators. The

two power supplies that failed are physically located in two separate plant annunciator

system cabinets that are about six feet apart and are electrically separated with different

125Vdc power supply sources. Additionally, there are no common loads shared

between the two power supplies.

The licensee classified the loss of the power supplies on October 13, 2009, as a single

functional failure because greater than six percent of main control board annunciators

had been lost and the power supplies had failed at nearly the same time. However, the

licensee found no causal link between their failures. The inspectors concluded the

licensees evaluation lacked a technical basis to consider the failures as a single

functional failure of the RK-01 function, and the failure of power supplies RK045E1PS2

and RK045E3PS1 represented two functional failures of the RK-01 function. As a result

of the inadequate maintenance rule evaluation, the licensee did not recognize that the

plant annunciator system exceeded its maintenance rule a(2) performance criteria.

Because the power supply failures had not been correctly counted, goal setting, and

monitoring were not performed as required by paragraph a(1) of the maintenance rule.

Analysis. The failure to properly evaluate the failed main control board annunciator

power supplies, establish performance goals, and monitor their performance is

- 21 - Enclosure

considered a performance deficiency. This finding is more than minor because it is

associated with the Mitigating Systems Cornerstone attribute of equipment performance

and it adversely affects the cornerstone objective ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using the Inspection Manual Chapter 0609, Significance Determination

Process, Phase 1 Worksheets, the finding is determined to have very low safety

significance since it did not result in a loss of system safety function, an actual loss of

safety function of a single train for greater than its technical specification allowed outage

time, or screen as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. This finding was determined to have a crosscutting aspect in

the area of problem identification and resolution associated with the corrective action

program because the licensee failed to properly classify, prioritize, and evaluate a

condition adverse to quality P.1(c).

Enforcement. Title 10 CFR 50.65(a)(1) requires, in part, that the licensee monitor the

performance or condition of structures, systems, or components, against licensee-

established goals, in a manner sufficient to provide reasonable assurance that such

structures, systems, or components are capable of fulfilling their intended functions.

Title 10 CFR 50.65 paragraph (a)(2) states, Monitoring as specified in paragraph a(1) of

this section is not required where it has been demonstrated that the performance or

condition of a structure, system, or component is being effectively controlled through the

performance of appropriate preventive maintenance, such that the structure, system, or

component remains capable of performing its intended function. Contrary to the above,

on December 10, 2009, Wolf Creek failed to demonstrate that performance of the main

control board annunciator power supplies was being effectively controlled through the

performance of appropriate preventive maintenance such that the system remained

capable of performing its intended function and did not establish goals in a manner

sufficient to provide reasonable assurance that the system was capable of fulfilling its

intended functions. Specifically, the licensee did not identify that the main control board

annunciator power supplies had exceeded their functional failure reliability criteria and

did not establish performance monitoring goals for the system. Because the finding is of

very low safety significance and has been entered into the licensees corrective action

program as Condition Report 34681, this violation is being treated as a noncited

violation, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000482/2011002-04, Failure to Follow 10 CFR 50.65 a(2) for Main Control Board

Annunciator Power Supply Failures.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk significant and

safety-related equipment listed below to verify that the appropriate risk assessments

were performed prior to removing equipment for work:

  • January 8 to 13, 2011, Main generator exciter overvoltage

- 22 - Enclosure

emergency core cooling systems swap over response time

  • March 1, 2011, Refueling Outage 18 scheduled March 19 to May 7, 2011
  • March 22, 2011, Low temperature overpressure protection control power

emergent work

assessment

The inspectors selected these activities based on potential risk significance relative to

the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five maintenance risk assessments and

emergent work control inspection samples as defined in Inspection

Procedure 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues

  • March 3, 2010, Vital switchgear rooms temperature

- 23 - Enclosure

compression coupling failure

  • February 25, 2011, Component cooling water B voiding
  • March 7, 2011 , Refueling water storage tank boron concentration

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and USAR to

the licensee personnels evaluations to determine whether the components or systems

were operable. Where compensatory measures were required to maintain operability,

the inspectors determined whether the measures in place would function as intended

and were properly controlled. The inspectors determined, where appropriate,

compliance with bounding limitations associated with the evaluations. Additionally, the

inspectors also reviewed a sampling of corrective action documents to verify that the

licensee was identifying and correcting any deficiencies associated with operability

evaluations. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of seven operability evaluations inspection

samples as defined in Inspection Procedure 71111.15-04

b. Findings

.1 Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, involving an inadequate calculation supporting vital switchgear

room temperatures with only one vital switchgear cooler operable.

Description. Wolf Creek is designed with two vital switchgear air conditioning units.

Each air conditioning unit cools one vital 4160V switchgear room, two sets of vital dc

battery rooms, and two sets of vital dc switchgear. On August 3, 2010, Wolf Creek

experienced a trip of the Train A vital switchgear air conditioning unit. Wolf Creek

entered technical requirements manual (formerly USAR, Chapter 16) limiting condition of

operation 3.7.23. Technical requirements manual 3.7.23 allows one vital air conditioning

unit to be out of service for 7 days provided compensatory measures are taken. After

7 days, the technical specifications must be entered. Compensatory measures are

stated in Procedure GK-200 and the inspectors found they were implemented in

accordance with the procedure. The procedure opens all doors between the vital ac and

dc switchgear rooms, places box fans between rooms, and posts continuous fire

watches. The use of one air conditioning unit to cool all switchgear is based on

configuration change package 07905. The inspectors reviewed the heat transfer

calculations supporting change package 07905. The principle calculation is GK-06-W,

- 24 - Enclosure

SGK05A/B Class IE Electrical Equipment Rooms A/C Units, Single Unit Operation

Capability.

Calculation GK-06-W determined that the final rooms temperature with one air

conditioning unit would be 94°F and 100°F for normal operations and 94°F for all rooms

during loss of coolant accident operation. However, USAR 3.11(B).2.3.2 states that the

vital switchgear rooms will not exceed 90°F, and the Wolf Creek technical requirements

manual specifies a maximum temperature limit of 87°F. Calculation GK-06-W

assumption 14 acknowledges that the calculation results contradict the USAR and

provides justification stating that 104°F is acceptable due to design of the equipment

without providing specifics other than stating that battery capacity increases with

temperature. The justification further states that 104°F may only be reached once or

twice over plant life, and is therefore acceptable. No environmental qualification

references are provided.

The inspectors reviewed Calculation GK-06-W and identified several discrepancies.

Several heat loads were missing from the calculation, including normal operating loads

such as pressurizer heater breakers that are always closed, diesel generator output

breaker that is closed for testing, and one running centrifugal charging pump breaker

that is closed for chemical and volume control duties. Loads missing during accident

operations included nearly all 4160V breakers closed by the load sequencer.

Additionally, Calculation GK-06-W assumed an 85°F room temperature for the health

physics area under the 4160V switchgear room. This area is cooled by nonvital air

conditioning units SGK02 and SGK03. These nonvital coolers are not protected under

Procedure AP GK-200 or the maintenance rule risk assessment program. Using such a

temperature effectively made the floor of rooms a plate-type heat exchanger which

removed a significant amount of heat. The inspectors concluded the 85°F room

temperature assumption was nonconservative since the nonvital coolers are not ensured

to be running and are not protected equipment.

Also, the surface area of the ceiling of the 2016 foot elevation rooms used in the

calculation was much less than the architectural drawings showed. The added surface

area increased the heat transmitted to the dc switchgear rooms. The inspectors

repeated the calculation with additional heat loads and found that room temperatures

could be as high as 100°F for the lower ac switchgear rooms and 110°F for the upper dc

switchgear rooms using the heat removal capacity stated in Calculation GK-06-W. The

inspectors identified additional margin in performance tests of an SGK05 unit, and, in

discussion with Wolf Creek engineering, estimated that the cooling coil was capable of

removing an additional 22,000 Btu/hr based on instrumented performance testing of the

cooling coil. The inspectors repeated the calculation with the cooling coils additional

capacity and found to be capable of cooling the rooms to about 97°F and 106°F,

respectively. Given the acceptance criteria at 90°F per the USAR, the inspectors

concluded that the calculations inputs and justification of its results were inadequate.

Wolf Creek initiated three Condition Reports 27276, 28252, and 31452 on this issue and

will address the rooms heat balance prior to the summer 2011.

- 25 - Enclosure

Analysis. The inspectors considered the inadequate heat loads and assumptions used

in calculation GK-06-W to be a performance deficiency. The performance deficiency is

more than minor, and therefore a finding, because it impacted with the equipment

performance attribute of the Mitigating Systems Cornerstone and it affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events. Using Inspection Manual Chapter 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, the inspectors screened the finding

to Green because the additional temperatures would not have caused the loss of

functionality of vital switchgear or batteries, and it did not screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event. No crosscutting

aspects were identified because the supporting documentation was prepared in the late

1990s and was not representative of current licensee performance.

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, required

that Wolf Creek establish measures to assure that applicable regulatory requirements

and design bases be correctly translated into specifications, and that design control

measures be provided for verifying or checking the adequacy of design such as by the

performance of design reviews, the use of alternate or simplified calculation methods, or

the performance of a suitable testing program. Contrary to the above, on April 22, 1999,

the measures established by the licensee failed to properly verify or check the adequacy

of design through the use of calculation methods. Specifically, Wolf Creek approved

Calculation GK-06-W which failed to adequately verify or check vital switch gear air

conditioning unit design in that the heat balance calculation did not ensure that the

cooling coil could remove sufficient heat from both trains of switchgear to maintain

temperature in accordance with the USAR. Because this issue was determined to be of

very low safety significance (Green) and was entered into the licensees corrective

action program as Condition Reports 27276, 28252, and 31452, this violation is being

treated as a noncited violation in accordance with Section 2.3.2 of the NRC Enforcement

Policy: NCV 05000482/2011002-05, Inadequate Calculation for Vital Switchgear

Cooling.

.2 Introduction. The inspectors identified a Green, noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, involving the failure to follow plant procedures. Specifically, the

licensee failed to follow procedure and perform an operability determination when a

nonconforming or degraded condition was identified in the Train B emergency diesel

generator fuel oil storage tank, as required by Procedure AP 26C-004, Operability

Determination and Functionality Assessment, Revision 21.

Description. On April 10 to 14, 2002, Wolf Creek personnel performed surveillance

requirement STN MT-002, Standby Diesel Fuel Oil Storage Tanks Drain and Clean,

Revision 1, on diesel fuel oil storage tank TJE01B. During the cleaning of the storage

tank, the licensee discovered approximately 40 percent of the protective interior coating

was damaged or missing from the inside tank wall. Regulatory Guide 1.137, as

endorsed by the licensees USAR, requires this coating to protect against corrosion of

the tank.

On April 13, 2002, shortly after discovery of the degraded coating, Wolf Creek personnel

prepared and issued engineering disposition CCP 10153, Missing Coating on TJE01B,

- 26 - Enclosure

Revision 1. The conclusion of CCP 10153, Revision 0, was to replace the coating during

the next outage. This engineering disposition was subsequently revised to allow use of

the tank with the coating missing.

During the week of January 19, 2011, a Wolf Creek engineering standards team

performed a self-assessment and review of engineering disposition CCP 10153. The

licensee determined that the conclusions of CCP 10153, use the fuel oil storage tank

with a missing interior coating was inadequate and generated Condition Report 32348

documenting the degraded condition in the Train B fuel oil storage tank.

Procedure AP 26C-004, Operability Determination and Functionality Assessment,

Revision 21, requires that plant personnel perform an immediate operability

determination when a nonconforming or degraded condition is identified. Specifically,

Section 4.6 states, An immediate determination of technical specification structures,

systems, or components operability is completed after confirming that a degraded or

nonconforming condition exists that could impact the capability of structures, systems, or

components to perform their specified safety function(s). The immediate operability

determination is made without delay and in a controlled manner using the best available

information.

On February 9, 2011, the inspectors questioned the current operability of the Train B fuel

oil storage tank given the determination by the engineering review team that the missing

coating was a degraded or nonconforming condition. However, the licensee had not

performed an operability determination immediately after identifying this degraded or

nonconforming condition, as required by procedure. The licensee subsequently

performed an operability determination and determined the fuel oil storage tank to be

operable, but degraded.

Analysis. The failure to follow Procedure AP 26C-004, Operability Determination and

Functionality Assessment, Revision 21, when a nonconforming or degraded condition

was identified was a performance deficiency. This performance deficiency was more

than minor because it could become a more significant safety concern if left uncorrected.

Using Inspection Manual Chapter 0609.04, "Phase 1 - Initial Screening and

Characterization of Findings," the inspectors determined that the finding had very low

safety significance (Green) because it did not result in a loss of system safety function,

an actual loss of safety function of a single train for greater than its technical

specification allowed outage time, or screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with the corrective

action program component because the licensee failed to thoroughly evaluate problems,

including evaluating for operability, such that the resolution addressed the cause

P.1(c).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Contrary to this requirement, on January 14, 2011, the

- 27 - Enclosure

licensee failed to accomplish an activity affecting quality in accordance with prescribed

procedures. Specifically, the licensee failed to follow procedure and perform an

immediate operability determination after identifying a degraded or nonconforming

condition, as required by Procedure AP 26C-004, Operability Determination and

Functionality Assessment, Revision 21. The licensee subsequently performed an

operability determination on February 9, 2011, and determined the fuel oil storage tank

to be operable, but degraded. Because this violation was of very low safety significance

and was entered into the licensee's corrective action program as Condition

Reports 33355 and 34068, this violation is being treated as a noncited violation,

consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000485/2011002-

06, Failure to Perform an Operability Determination for Degradation of the Fuel Oil

Storage Tank.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

valve replacement.

  • January 24, 2011, Diesel generator A jacket water temperature low after start
  • February 23, 2011, Ultrasonic testing of component cooling water Train B after fill

and vent

after packing and electrical maintenance

  • March 10, 2011, Diesel fire pump run after jacket water hose replacement

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

  • The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

  • Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

- 28 - Enclosure

The inspectors evaluated the activities against the technical specifications, the USAR,

10 CFR Part 50 requirements, licensee procedures, and various NRC generic

communications to ensure that the test results adequately ensured that the equipment

met the licensing basis and design requirements. In addition, the inspectors reviewed

corrective action documents associated with postmaintenance tests to determine

whether the licensee was identifying problems and entering them in the corrective action

program and that the problems were being corrected commensurate with their

importance to safety. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of six postmaintenance testing inspection samples

as defined in Inspection Procedure 71111.19-05.

b. Findings

.1 Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50

Appendix B, Criterion III, involving a failure to perform periodic testing to verify that

ultimate heat sink sedimentation remained within design basis limits.

Description. In April 1982, the NRC issued NUREG-0881, Safety Evaluation Report

Related to the Operation of Wolf Creek Generating Station, Unit 1. In Section 2.4.4.4,

Sedimentation in the Ultimate Heat Sink, the NRC approved annual visual inspections

as a means of ensuring that design basis sedimentation limits, and by extension the

safety-related function of the ultimate heat sink, were maintained and verified throughout

the period of licensed plant operation. The NRC staff considered the annual visual

inspection surveillance to be part of Wolf Creeks licensing bases for meeting the

requirements of 10 CFR Part 50, Appendix A, General Design Criterion 44, Cooling

Water. The ultimate heat sink safety design basis is described in USAR

Sections 9.2.5.1.1 and includes:

cooling water to dissipate the heat of an accident safely and to achieve and

maintain safe shutdown of one nominal 1,214 MWe unit following a design bases

accident.

water to the fuel storage pool and component cooling water systems, and is the

backup water supply for the auxiliary feedwater system.

postulated site-related events, such as loss of the main cooling lake.

The system functions are met using acceptance criteria for temperature, water level, and

sedimentation level. USAR Section 9.2.5.3.1 states: Dredging of the ultimate heat sink

will be performed whenever necessary to maintain a minimum capacity and adequate

flow to the essential service water pumps, and Section 9.2.5.4 states: The ultimate

heat sink is inspected periodically to determine degree of siltation. NUREG-0881 stated

- 29 - Enclosure

NRC approval was based, in part, on annual measurements to ensure that

sedimentation levels remained within predefined limits to keep the ultimate heat sink

capable of performing its safety-related functions. This ensured the required volume of

water in the ultimate heat sink to meet the input assumption design requirement.

The licensee took annual sediment measurements as required between January 1985,

and September 2002. On August 8, 2003, Wolf Creek developed USAR change 04-027,

which was implemented as Revision 18 to the USAR on March 11, 2005. This revision

removed the annual sediment depth surveillance of the ultimate heat and replaced it with

a periodic dredging preventive maintenance activity to be performed every five years.

The inspectors reviewed the justification for replacing the annual visual surveillance with

the five-year dredging activity. The inspectors concluded the basis for periodicity of

dredging was nonconservative since it relied upon an average sedimentation rate over a

17-year period rather than a maximum sedimentation rate. The inspectors also

reviewed the dredging work orders and data and determined that the dredging activity

did not verify as-found or as-left ultimate heat sink depth to assure conformance to the

ultimate heat sink design. The 5-year frequency was also not carried out between 2004

and 2010, but was extended under an administrative 25 percent grace period. The

inspectors concluded that the 5-year preventive maintenance activity was not adequate

to ensure that a sufficient volume of water would be maintained in the ultimate heat sink

to meet the design basis requirements .The licensee subsequently measured the

ultimate heat sink depth with SONAR on August 13 and 14, 2010, and determined that

the actual sediment depth supported ultimate heat sink operability and conformance with

the USAR design basis requirements.

Analysis. The failure to perform periodic testing to verify that ultimate heat sink

sedimentation remained within design basis limits is a performance deficiency. The

issue is more than minor, and therefore a finding, because if left uncorrected the issue

has the potential to become a more significant safety concern. Using Inspection Manual

Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the

inspectors determined that the finding had very low safety significance (Green) because

it did not result in a loss of system safety function, an actual loss of safety function of a

single train for greater than its technical specification allowed outage time, or screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

The inspectors concluded that this findings cause has a crosscutting aspect in the area

of human performance associated with the work control component because Wolf Creek

did not appropriately coordinate work activities by incorporating actions to address the

impact of changes to the work scope or activity on the plant and human performance.

Specifically, when Wolf Creek performed and planned dredging preventive maintenance

on the ultimate heat sink, they did not consider the need to confirm as-found and as-left

sedimentation data, to verify that their design basis was met H.3(b).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, states in

part that, measures shall be established to assure that applicable regulatory

requirements and the design basis are correctly translated into specifications, drawings,

procedures, and instructions. The design control measures shall provide for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

- 30 - Enclosure

use of alternate or simplified calculation methods, or by the performance of a suitable

testing program. Contrary to the above, from March 11, 2005, until August 27, 2010, the

measures established by the licensee failed to assure that applicable regulatory

requirements and the design basis of the ultimate heat sink were correctly translated into

specifications, drawings, procedures, and instructions through the performance of design

reviews, by the use of alternate or simplified calculation methods, or by the performance

of a suitable testing program. Specifically, Wolf Creek discontinued periodic verification

of sedimentation levels in the ultimate heat sink without verification that the heat sink

design would continue to be met for the effects of sediment accumulation. Because this

finding is of very low safety significance and was entered into the corrective action

program as Condition Report 27144, this violation is being treated as a noncited violation

in accordance with Section 2.3.2 of the NRC Enforcement Policy:

NCV 05000482/2011002-07, Failure to Verify Ultimate Heat Sink Sedimentation Levels

within Design Bases.

.2 Introduction. The inspectors reviewed a Green self-revealing noncited violation of

Technical Specification 5.4.1.a, Procedures, involving the failure to perform an

adequate fill and vent of the component cooling water system which resulted in voiding

of the system.

Description. On February 16, 2011, the licensee isolated and drained pump D of

component cooling water Train B for planned maintenance. The licensee intended to

maintain Train B operable with pump B available. After maintenance, the licensee filled

and vented the isolated portion of Train B. On February 23, 2011, the licensee started

pump D for postmaintenance testing. When pump D started, pump B automatically

started due to sensed low discharge pressure of pump D. In addition, the Train B

component cooling water surge tank inventory reduced approximately 23 cubic feet.

The licensee recognized these indications as symptoms of voiding in the system and

declared Train B inoperable. After extensive flushing and ultrasonic inspections for

voiding, Train B was declared operable on February 25, 2011.

During filling and venting of pump D on February 22, 2011, licensee personnel opened

the suction isolation valve while venting from the pump casing. Since the suction

isolation valve is physically higher than the pump casing, air in the suction piping rose

into the common suction line of pumps B and D of Train B instead of being vented

through the pump casing. Clearance order D-EF-B-010A restoration instructions

required ultrasonic testing of the discharge piping, but did not direct testing on the pump

suction piping. The inspectors concluded that after introducing air into the system during

maintenance, the licensee performed an inadequate fill and vent by failing to vent from

the high point of the system. The inspectors also concluded the clearance order

restoration instructions were inadequate in that they failed to require ultrasonic testing of

the high point of the system. The inspectors determined the introduction of air to the

suction side of both component cooling water Train B pumps reduced the reliability of

the system; however, the system continued to be able to perform its safety function.

The inspectors determined the cause of the inadequate clearance restoration order was

a mistaken belief that any air on the suction side of the pumps would self-vent back to

the surge tank. This misconception was one of the root causes for previous component

- 31 - Enclosure

cooling water voiding events documented in NRC Inspection Report 05000482/2010008.

Therefore, the inspectors concluded that corrective actions from previous component

cooling water voiding events had not been fully effective.

Analysis. The inspectors determined that the failure to perform an adequate fill and

vent of component cooling water that resulted in system voiding was a performance

deficiency. The inspectors determined that this finding was more than minor because it

is associated with the human performance attribute of the Mitigating Systems

Cornerstone and it affected the cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, the finding was determined to have very low safety

significance (Green) because it did not result in a loss of system safety function, an

actual loss of safety function of a single train for greater than its technical specification

allowed outage time, or screen as potentially risk significant due to a seismic, flooding,

or severe weather initiating event. This finding has a crosscutting aspect in the area of

problem identification and resolution associated with the corrective action program

because the licensee failed to take appropriate corrective actions from previous voiding

events P.1(d).

Enforcement. Technical Specification 5.4.1.a, Procedures, requires that written

procedures be established and implemented covering activities specified in Appendix A

of Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation),

February 1978. Regulatory Guide 1.33, Appendix A, Section 9, requires, in part, that

maintenance that can affect the performance of safety-related equipment be performed

in accordance with written instructions appropriate to the circumstances. Contrary to the

above, on February 22, 2011, the license failed to perform maintenance that affected the

performance of safety-related equipment with written instructions appropriate to the

circumstances. Specifically, clearance order D-EF-B-010A restoration instructions were

not appropriate to the circumstances in that the instructions resulted in inadequate filling

and venting resulting in gas introduction to the system. Because of the very low safety

significance of this finding and because the licensee entered this issue into the

corrective action program as Condition Report 33925, this violation is being treated as a

noncited violation in accordance with Section 2.3.2.a of the NRC Enforcement Policy:

NCV 05000482/2011002-08, Inadequate Fill and Vent of Component Cooling Water.

1R20 Refueling and Other Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the refueling

outage, starting on March 19, 2011, to confirm that licensee personnel had appropriately

considered risk, industry experience, and previous site-specific problems in developing

and implementing a plan that assured maintenance of defense in depth. During the

refueling outage, the inspectors observed portions of the shutdown and cooldown

processes and monitored licensee controls over the outage activities listed below.

- 32 - Enclosure

  • Configuration management, including maintenance of defense in depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service.

  • Clearance activities, including confirmation that tags were properly hung and

equipment appropriately configured to safely support the work or testing.

  • Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met, and controls over

switchyard activities.

  • Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system.

alternative means for inventory addition, and controls to prevent inventory loss.

  • Controls over activities that could affect reactivity.
  • Licensee identification and resolution of problems related to refueling outage

activities.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage and other outage

inspection sample as defined in Inspection Procedure 71111.20-05.

b. Findings

Introduction. The inspectors reviewed a self-revealing Green noncited violation of

Technical Specification 5.4.1.a, Procedures, involving the failure to follow the

requirements of Procedure AP 21E-001, Clearance Orders. This procedure violation

resulted in an inadequate tagout for the Train A solid state protection system resulting in

an unplanned swap of the volume control tank charging pump suction to the reactor

water storage tank and an unplanned entry into Technical Specification 3.4.12 due to the

de-energization of power operated relief valve A low temperature overpressure

protection relays.

Description. On March 22, 2011, control room operators received an annunciator alarm

indicating realignment of the charging pump suction from the volume control tank to the

reactor water storage tank. The volume control tank level increased from 95 to

100 percent and tank pressure increased from 18 to 40 psi. Control room operators

re-aligned the volume control tank suction back to the charging flow path, and the

volume control tank level and pressure returned to their normal operating levels.

- 33 - Enclosure

The licensee subsequently determined that a clearance order had de-energized the

Train A solid state protection system, de-energizing both the Train A reactor water

storage tank swap over and power operated relief valve low temperature overpressure

protection relays. The Train A reactor water storage tank swap over required manual

operator action to address the increase in volume control tank level and the de-

energization of the power operated relief valve low temperature overpressure protection

relay placed the plant in Technical Specification 3.4.12, Condition F, which has a

requirement to restore the power operated relief valve to operable status within 24

hours. The low temperature overpressure protection system controls reactor coolant

system pressure at low temperatures so the integrity of the reactor coolant pressure

boundary is not compromised. Upon recognizing that the inadequate clearance order

was the cause of the reactor water storage tank swap over and de-energization of the

power operated relief valve, operators removed the clearance order and restored all

equipment to its normal operating condition approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> after receiving the

initial control room alarm.

Clearance order R-SB-A-004 was generated in preparation for a vendor to perform logic

testing of the Train A solid state protection system circuit boards consistent with industry

operating experience. The clearance order worksheet contained very limited details

describing the vendors work scope. The clearance order instructions, provided only a

few days prior to the scheduled start date, simply requested to de-energize the Train A

solid state protection system cabinet. No licensee personnel were completely cognizant

of the vendors planned scope of work. The licensee recognized that there are

numerous power sources supplying the solid state protection system cabinets, and

decided to expand the clearance order scope to include the instrument ac power,

125Vdc power, and reactor protection breakers that supply the Train A solid state

protection system cabinet. The reactor water storage tank swap over and de-

energization of the power operated relief valve was caused by a failure to recognize that

opening instrument ac power breaker NN00112 would de-energize the Train A solid

state protection system slave relay power supply.

Analysis. The failure to follow procedures to complete clearance orders with adequate

boundaries is a performance deficiency. The performance deficiency was more than

minor because it impacted the Initiating Events Cornerstone objective of configuration

control to limit the likelihood of those events that upset plant stability and challenge

critical safety functions during shutdown as well as power operations. The significance

of the finding was determined using Inspection Manual Chapter 0609, Significance

Determination Process, Appendix G, Checklist 2, and determined to be of very low

safety significance, because it did not cause the loss of mitigating capability of core heat

removal, inventory control, power availability, containment control, or reactivity control.

Additionally, the cause of the finding is related to the human performance crosscutting

component of work control. Specifically, the licensee did not appropriately plan for the

maintenance work scope by ensuring work groups and an offsite organization

communicate the necessary electrical boundaries to assure plant and human

performance H.3(b).

Enforcement. Technical Specification 5.4.1.a, Procedures, requires, in part, that

written procedures shall be established, implemented and maintained for the activities

- 34 - Enclosure

recommended in Regulatory Guide 1.33, Quality Assurance Program Requirements

(Operation), Revision 2, Appendix A, February 1978. Section 1.c of Regulatory Guide

1.33, Revision 2, Appendix A, recommends procedures for equipment control (e.g.,

locking and tagging). Wolf Creek Procedure AP 21E-001, Clearance Orders, Revision

27, step 5.7.1, requires the licensee to develop clearance order instructions, based on

the work scope, so adequate tagging boundaries can be developed. Contrary to this

requirement, on March 19, 2011, the licensee failed to provide clearance order

instructions, based on the work scope, so adequate tagging boundaries could be

developed in the tagout boundary for clearance order R-SB-A-004. Because the finding

is of very low safety significance and has been entered into the licensees corrective

action program as Condition Report 35318, this violation is being treated as a noncited

violation consistent with Section 2.3.2 of the NRC Enforcement Policy:

NCV 05000482/2011002-09, Inadequate Clearance Order Disables Power Operated

Relief Valve Low temperature Overpressure Protection Train.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the USAR, procedure requirements, and technical

specifications to ensure that the surveillance activities listed below demonstrated that the

systems, structures, and/or components tested were capable of performing their

intended safety functions. The inspectors either witnessed or reviewed test data to

verify that the significant surveillance test attributes were adequate to address the

following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements

- 35 - Enclosure

  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

  • Reference setting data

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

  • December 6, 2010, 25 year containment tendon surveillance
  • January 10, 2011, Incore-Excore axial flux difference comparison
  • January 10, 2011, Heat flux hot channel factor
  • January 24, 2011, KJ-005A Jacket water temperature control valve
  • February 15, 2011, Over-Temperature Delta-Temperature and Over-Power Delta-

Temperature trip setpoint

  • February 18, 2011, Diesel generator fuel oil storage tank cloud point
  • February 28, 2011, Safety injection pump A inservice test

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of nine surveillance testing inspection samples as

defined in Inspection Procedure 71111.22-05.

b. Findings

Introduction. The inspectors identified a Green noncited violation of Technical

Specification 5.4.1.a, Procedures, involving the failure to follow Procedure AP 21-001,

Conduct of Operations. Specifically, the licensee failed to enter into technical

specification limiting condition of operation 3.7.5.B.1 for one auxiliary feedwater pump

inoperable during performance of 92-day check valve surveillance tests.

Description. On March 7, 2011, the inspectors identified that technical

specification 3.7.5 limiting condition of operation action statement B.1 was not logged

- 36 - Enclosure

during turbine-driven auxiliary feedwater check valve testing. The check valve testing

involved opening one-inch drain lines on the upstream and downstream sides of the

suction check valves. A torque wrench is then applied to the valve disc pin, and the

valve is checked for the correct opening torque. During this time, the open drain lines

create the potential to divert suction flow from the pump. This condition affected suction

check valves from the condensate storage tank or the essential service water pumps.

The inspectors concluded this condition impacted the operability of the auxiliary

feedwater pumps since the open drain lines could result in water spray in the room,

additional flooding volume, a decrease in pump net positive suction head, lost

condensate storage tank inventory and lost ultimate heat sink inventory.

Wolf Creek initiated Condition Report 34469 to evaluate the condition. Wolf Creek

concluded that the auxiliary feedwater pumps were inoperable during each of their

respective check valve testing procedures. Wolf Creek changed all the auxiliary

feedwater check valve testing procedures to add steps to declare the pump inoperable

or take appropriate manual actions to ensure operability. The added steps provide the

option of entering the action statement or posting a nonlicensed operator with

continuous communications to the control room to shut the vent valves, if needed. The

inspectors determined that Wolf Creek had failed to recognize that Technical Specification 3.7.5.B.1 applied and did not log entry into the action statement for

Procedure STS AL-210C (turbine-driven pump) on March 12, June 10, July 29, and

December 10, 2010, and March 6, 2011; for Procedure STS AL-210A (Train A pump) on

June 1, August 31, November 27, 2010, and March 4, 2011; and Procedure STS AL-

210B (Train B pump) on June 16, August 17, September 16, and December 15, 2010.

Procedure AP 21-001, Conduct of Operations, required the licensee to review each

evolution for technical specification applicability per step 6.8.4. The inspectors

interviewed licensee personnel on procedures that do not direct entry into technical

specification action statements and determined the licensee relied on informally

maintained pre-job briefing sheets to meet this requirement. The inspectors reviewed

the pre-job briefing sheets for the suction check valve testing and concluded that the

sheets contained good guidance on error traps, expected equipment responses, internal

operating experience and acceptance criteria, but did not contain instructions on manual

actions to maintain operability or instructions to enter technical specification action

statements sufficient to address technical specification applicability.

Analysis. The failure to enter technical specification action statements in accordance

with Procedure AP 21-001 was a performance deficiency. The performance deficiency

was more than minor, and therefore a finding, because it impacted with the human

performance attribute of the Mitigating Systems Cornerstone and its objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using Inspection Manual Chapter 0609.04, Phase

1 - Initial Screening and Characterization of Findings, the finding was determined to be

of very low safety significance (Green) because the issue did not result in a loss of

operability for a time period greater than the action statement, and did it not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

The inspectors determined that the finding has a crosscutting aspect in the area of

human performance associated with decision making. Specifically, informally

- 37 - Enclosure

maintained pre-job briefing sheets were being relied upon to determine technical

specification applicability instead of the licensees decision making process of operator

review on a case by case basis H.1.a..

Enforcement. Technical Specification 5.4.1.a, Procedures, requires that written

procedures be established, implemented, and maintained covering activities related to

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978.

Regulatory Guide 1.33, Section 1(h), Administrative Procedures, requires log entries.

Procedure AP 21-001, Conduct of Operations, Revision 50, step 6.8.4, requires, in

part, plant log entries of technical specification action statements and that operations

shall review technical specification requirements for each evolution. Contrary to the

above, on March 7 and 12, June 1, 10, and 16, July 29, August 17 and 31,

September 16, November 27, and December 10 and 15, 2010, and March 4, 2011, Wolf

Creek failed to review technical specification requirements and log technical

specification action statement 3.7.5.B.1 when any of the three auxiliary feedwater pumps

were out of service for check valve testing which rendered the pumps inoperable.

Because this issue was determined to be of very low safety significance (Green) and

was entered into the licensees corrective action program as Condition Report 34469,

this violation is being treated as a noncited violation in accordance with Section 2.3.2 of

the NRC Enforcement Policy: NCV 05000482/2011002-10, Repetitive Failure to Enter

Technical Specifications for Auxiliary Feedwater Suction Valve Testing.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspector performed an in-office review of the Wolf Creek Emergency Plan;

Document APF 06-002-01, Emergency Action Levels, Revision 15. This revision

changed the bases 1-RER5 of EAL-1, Radioactive Effluent Release, for

Radiation Monitor 0-SD-RE-41 from 23,500 millirem per hour (the times 1000 value) to

10,000 millirem per hour (the upper detection limit of the monitor). Also,

Procedure OFN RP-014, Hot Standby to Cold Shutdown from Outside the Control

Room, was deleted from bases 9-LPC/SC5 of EAL-9, Loss of Plant Control/Security

Compromise, since this procedure can only be entered through other procedures

already listed.

This revision was compared to its previous revision, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in

10 CFR 50 47(b) to determine if the revision adequately implemented the requirements

of 10 CFR 50.54(q). This review was not documented in the SER and did not constitute

approval of licensee-generated changes; therefore, this revision is subject to future

inspection.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.04-05.

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b. Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on

January 11, 2011, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities. The

inspectors observed emergency response operations in the turbine failure and resulting

Alert to determine whether the event classification, notifications, and protective action

recommendations were performed in accordance with procedures. The inspectors also

attended the licensee drill critique to compare any inspector-observed weakness with

those identified by the licensee staff in order to evaluate the critique and to verify

whether the licensee staff was properly identifying weaknesses and entering them into

the corrective action program. As part of the inspection, the inspectors reviewed the drill

package and other documents listed in the attachment.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.06-05.

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstones: Occupational and Public Radiation Safety

2RS01 Radiological Hazard Assessment and Exposure Controls (71124.01)

a. Inspection Scope

This area was inspected to: (1) review and assess licensees performance in assessing

the radiological hazards in the workplace associated with licensed activities and the

implementation of appropriate radiation monitoring and exposure control measures for

both individual and collective exposures, (2) verify the licensee is properly identifying

and reporting Occupational Radiation Safety Cornerstone performance indicators, and

(3) identify those performance deficiencies that were reportable as a performance

indicator and which may have represented a substantial potential for overexposure of

the worker.

- 39 - Enclosure

The inspectors used the requirements in 10 CFR Part 20, the technical specifications,

and the licensees procedures required by technical specifications as criteria for

determining compliance. During the inspection, the inspectors interviewed the radiation

protection manager, radiation protection supervisors, and radiation workers. The

inspectors performed walkdowns of various portions of the plant, performed independent

radiation dose rate measurements and reviewed the following items:

  • Performance indicator events and associated documentation reported by the

licensee in the Occupational Radiation Safety Cornerstone

  • The hazard assessment program, including a review of the licensees evaluations

of changes in plant operations and radiological surveys to detect dose rates,

airborne radioactivity, and surface contamination levels

  • Instructions and notices to workers, including labeling or marking containers of

radioactive material, radiation work permits, actions for electronic dosimeter

alarms, and changes to radiological conditions

  • Programs and processes for control of sealed sources and release of potentially

contaminated material from the radiologically controlled area, including survey

performance, instrument sensitivity, release criteria, procedural guidance, and

sealed source accountability

  • Radiological hazards control and work coverage, including the adequacy of

surveys, radiation protection job coverage, and contamination controls; the use of

electronic dosimeters in high noise areas; dosimetry placement; airborne

radioactivity monitoring; controls for highly activated or contaminated materials

(nonfuel) stored within spent fuel and other storage pools; and posting and

physical controls for high radiation areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

  • Audits, self-assessments, and corrective action documents related to radiological

hazard assessment and exposure controls since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one required sample as defined in Inspection

Procedure 71124.01-05.

b. Findings

Introduction. Inspectors identified a Green noncited violation of Technical

Specification 5.4.1.a, Procedures, involving the failure to follow procedure

requirements for increased work scope on an existing radiation work permit.

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Specifically, welding was performed in a locked high radiation area on a radiation work

permit that did not cover that type of activity.

Description. On January 4, 2011, work was performed under maintenance work

order 11-336634-000 in a locked high radiation area on the 1988 elevation of the

auxiliary building. The radiological aspects of the work were covered using radiation

work permit 110039. The radiation work permit stated that this permit was not intended

to be used for major contamination breaches. During the work, welders cut into and

welded a contaminated pipe. This type of activity was not covered by the radiation work

permit.

Wolf Creek Procedure RPP 02-105, RWP, states that if the exposure estimate to

complete the work is greater than 100 mrem it is appropriate to consider creating a new

radiation work permit. As described in the licensee identified violation in Section 4OA7

of this report, the licensee performed an inadequate hazard assessment of the work by

performing a dose estimate for the job using the incorrect location and by

underestimating the number of workers who would be required for the work. Due to the

inadequate hazard assessment, the dose estimate did not reach the 100 mrem

threshold. This caused a missed opportunity to recognize the potential benefits of

creating a separate radiation work permit or revising radiation work permit 110039 for

this work activity.

Instead, the licensee removed a special instruction specifying that grinding and welding

activities were not allowed on radiation work permit 110039. In addition, health physics

staff changed the alarm settings on the workers electronic dosimeters to support the

new work scope. This change was contrary to Procedure RPP 02-105 which states that

health physics may assign work to an existing radiation work permit when it:

  • Appropriately covers the type of work
  • Has proper stop points
  • Meets the radiation work permit risk assessment
  • Meets the respiratory protection evaluation
  • Meets the additional dosimetry worksheet
  • Will not change the exposure goal or estimate.

The licensee did not evaluate that the above conditions were met before using radiation

work permit 110039 for the increased work scope. The change in work scope resulted in

the exposure estimate being increased from 90 mrem to 300 mrem. The licensee

placed the finding into the corrective action program as Condition Report 00035522 and

acknowledged that the radiation work permit used was inappropriate for the work

completed.

Analysis. The failure to follow a procedure was a performance deficiency. The finding

was more than minor because it negatively impacted the Occupational Radiation Safety

Cornerstones attribute of program and process, in that the use of an inadequate

radiation work permit led to workers unplanned, unintended dose. Using Inspection

Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance

Determination Process, the finding was determined to be of very low safety significance

- 41 - Enclosure

because: (1) it was not associated with as low as is reasonably achievable (ALARA)

planning or work controls, (2) there was no overexposure, (3) there was no substantial

potential for an overexposure, and (4) the ability to assess dose was not compromised.

In addition, this finding has a crosscutting aspect in the area of Human Performance

related to work controls. Specifically, there was inappropriate coordination and

communication of work activities between work groups H.3.b].

Enforcement. Technical Specification 5.4.1.a requires that procedures be established,

implemented and maintained as recommended in Regulatory Guide 1.33, Quality

Assurance Program Requirements (Operation), Revision 2, February 1978, Appendix A.

Section 7.e of Appendix A covers exposure controls, including a radiation work permit

system. Wolf Creek Procedure RPP 02-105 RWP, Section 9.2, Assigning work to an

existing radiation work permit number, states in part, that Health Physics may assign

work to an existing radiation work permit number when: the radiation work permit

appropriately covers this type of work and the work will not change the current radiation

work permit exposure goal or estimate. Contrary to the above, on January 4, 2011,

Wolf Creek inappropriately allowed maintenance work to be performed under radiation

work permit 110039 that did not appropriately cover the type of work and significantly

changed the exposure estimate. Specifically, the maintenance work order included

cutting into a contaminated system, which contradicted the radiation work permit

statement that it was not meant for major contamination breaches. Also, the added work

did change the radiation work permit exposure goal, in that it increased the exposure

estimate to 300 mrem from the original estimate of 90 mrem. Since this violation was of

very low safety significance and was documented in the licensees corrective action

program as Condition Report 35522, it is being treated as a noncited violation,

consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000482/2011002-

11, Failure to Follow Radiation Work Permit Instructions.

2RS02 Occupational ALARA Planning and Controls (71124.02)

a. Inspection Scope

This area was inspected to assess performance with respect to maintaining occupational

individual and collective radiation exposures ALARA. The inspectors used the

requirements in 10 CFR Part 20, the technical specifications, and the licensees

procedures required by technical specifications as criteria for determining compliance.

During the inspection, the inspectors interviewed licensee personnel and reviewed the

following items:

  • Site-specific ALARA procedures and collective exposure history, including the

current 3-year rolling average, site-specific trends in collective exposures, and

source-term measurements

  • ALARA work activity evaluations/postjob reviews, exposure estimates, and

exposure mitigation requirements

- 42 - Enclosure

  • The methodology for estimating work activity exposures, the intended dose

outcome, the accuracy of dose rate and man-hour estimates, and intended

versus actual work activity doses and the reasons for any inconsistencies

  • Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

  • Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

  • Audits, self-assessments, and corrective action documents related to ALARA

planning and controls since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one required sample as defined in Inspection

Procedure 71124.02-05.

b. Findings

No findings were identified.

2RS03 In-plant Airborne Radioactivity Control and Mitigation (71124.03)

a. Inspection Scope

This area was inspected to verify in-plant airborne concentrations are being controlled

consistent with ALARA principles and the use of respiratory protection devices onsite

does not pose an undue risk to the wearer. The inspectors used the requirements in

10 CFR Part 20, the technical specifications, and the licensees procedures required by

technical specifications as criteria for determining compliance. During the inspection,

the inspectors interviewed licensee personnel, performed walkdowns of various portions

of the plant, and reviewed the following items:

  • The licensees use, when applicable, of ventilation systems as part of its

engineering controls

  • The licensees respiratory protection program for use, storage, maintenance, and

quality assurance of NIOSH certified equipment, qualification and training of

personnel, and user performance

  • The licensees capability for refilling and transporting SCBA air bottles to and

from the control room and operations support center during emergency

conditions, status of SCBA staged and ready for use in the plant and associated

surveillance records, and personnel qualification and training

- 43 - Enclosure

  • Audits, self-assessments, and corrective action documents related to in-plant

airborne radioactivity control and mitigation since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection

Procedure 71124.03-05.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the performance indicator data submitted by the

licensee for the 4th Quarter 2010 performance indicators for any obvious inconsistencies

prior to its public release in accordance with Inspection Manual Chapter 0608,

Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings were identified.

.2 Unplanned Scrams per 7000 Critical Hours (IE01)

a. Inspection Scope

The inspectors sampled licensee submittals for the unplanned scrams per 7000 critical

hours performance indicator for the period from the first quarter 2010 through the

fourth quarter 2010. To determine the accuracy of the performance indicator data

reported during those periods, the inspectors used definitions and guidance contained in

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6. The inspectors reviewed the licensees operator narrative logs, issue

reports, event reports, and NRC integrated inspection reports for the period of January

1, 2010, through December 31, 2010, to validate the accuracy of the submittals. The

- 44 - Enclosure

inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one unplanned scrams per 7000 critical hours

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.3 Unplanned Scrams with Complications (IE04)

a. Inspection Scope

The inspectors sampled licensee submittals for the unplanned scrams with

complications performance indicator for the period from the first quarter 2010 through

the fourth quarter 2010. To determine the accuracy of the performance indicator data

reported during those periods, the inspectors used definitions and guidance contained in

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6. The inspectors reviewed the licensees operator narrative logs, issue

reports, event reports, and NRC integrated inspection reports for the period of January

1, 2010, through December 31, 2010, to validate the accuracy of the submittals. The

inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one unplanned scrams with complications

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.4 Unplanned Power Changes per 7000 Critical Hours (IE03)

a. Inspection Scope

The inspectors sampled licensee submittals for the unplanned power changes per 7000

critical hours performance indicator for the period from the first quarter 2010 through the

fourth quarter 2010. To determine the accuracy of the performance indicator data

reported during those periods, the inspectors used definitions and guidance contained in

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6. The inspectors reviewed the licensees operator narrative logs, issue

reports, maintenance rule records, event reports, and NRC integrated inspection reports

for the period of January 1, 2010, through December 31, 2010, to validate the accuracy

- 45 - Enclosure

of the submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Specific documents

reviewed are described in the attachment to this report.

These activities constitute completion of one unplanned transients per 7000 critical

hours sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.5 Occupational Exposure Control Effectiveness (OR01)

a. Inspection Scope

The inspectors reviewed performance indicator data for the fourth quarter 2010 through

the first quarter 2011. The objective of the inspection was to determine the accuracy and

completeness of the performance indicator data reported during these periods. The

inspectors used the definitions and clarifying notes contained in NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 6, as criteria for

determining whether the licensee was in compliance.

The inspectors reviewed corrective action program records associated with high

radiation area and very high radiation area nonconformances. The inspectors reviewed

radiological controlled area exit transactions greater than 100 mrem. The inspectors

also conducted walkdowns of high radiation areas and very high radiation area

entrances to determine the adequacy of the controls of these areas.

These activities constitute completion of the occupational exposure control effectiveness

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.6 Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (PR01)

a. Inspection Scope

The inspectors reviewed performance indicator data for the fourth quarter 2010 through

the first quarter 2011. The objective of the inspection was to determine the accuracy and

completeness of the performance indicator data reported during these periods. The

inspectors used the definitions and clarifying notes contained in NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 6, as criteria for

determining whether the licensee was in compliance.

- 46 - Enclosure

The inspectors reviewed the licensees corrective action program records and selected

individual annual or special reports to identify potential occurrences such as

unmonitored, uncontrolled, or improperly calculated effluent releases that may have

impacted offsite dose.

These activities constitute completion of the radiological effluent technical

specifications/offsite dose calculation manual radiological effluent occurrences sample

as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included the complete and accurate

identification of the problem; the timely correction, commensurate with the safety

significance; the evaluation and disposition of performance issues, generic implications,

common causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews; and the classification, prioritization, focus, and timeliness

of corrective actions. Minor issues entered into the licensees corrective action program

because of the inspectors observations are included in the attached list of documents

reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

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.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Selected Issue Follow-up Inspection

a. Inspection Scope

During a review of items entered in the licensees corrective action program, the

inspectors selected a corrective action item documenting the missed risk assessment of

the extended motor-driven main feedwater pump maintenance from November 5 to 18,

2010, for detailed followup.

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

b. Findings and Observations

No findings were identified. The licensees evaluation identified that Wolf Creek failed to

follow its procedure for turnover of maintenance that takes longer than scheduled. The

inspectors observed that the evaluation missed an opportunity to re-assess the risk

significance of the three main feedwater pumps to be consistent with the scrams and

scrams with complications root cause evaluations, which identified that Wolf Creek was

not maintaining the main feedwater system, in part, because the system was incorrectly

regarded as a low risk significance system. Elevating the risk significance would aid

Wolf Creek in assessing the risk associated with working on more than one main

feedwater pump at the same time. Wolf Creek initiated Condition Report 30245 to

evaluate this observation.

4OA3 Event Follow-up (71153)

.1 (Closed) LER 2009-007-00, Removal of Equipment from Service Required by Technical

Specifications and NRC Safety Evaluation - RETRACTED

- 48 - Enclosure

This event was reviewed by Region IV and Headquarters staff and determined not to be

reportable. Reference enforcement action EA-09-326 under ADAMS accession number

ML100630900 for further information. This licensee event report (LER) is closed.

.2 (Closed) LER 2009-008-00, Potential of Containment Coolers to Have not Automatically

Started in Slow Speed - RETRACTED.

The licensee received operating experience that indicated that thermal overloads for

containment fan coolers were set too low for fan operation in a postaccident

environment. There was insufficient evidence to show that the containment coolers

could accomplish their safety function, so the licensee reported the condition on

January 11, 2010. Subsequent to the report, the licensee evaluated the thermal

overload settings and determined that the settings were adequate. Therefore, the

licensee retracted the report on March 30, 2010. The inspectors reviewed the basis for

the retraction. No violations were identified during the inspectors review. This LER is

closed.

.3 (Closed) LER 2009-009-00; -01, Defeating Feedwater Isolation on Low Tavg Coincident

with P-4 Function Results in Missed Mode Change

On October 22, 2009, the inspectors identified a failure to report a condition prohibited

by technical specification for defeating both trains of the P-4 interlock. LER 2009-009-00

reported this condition per 50.73(a)(2)(i)(B), but the licensee did not report the event

under reporting criteria 50.73(a)(2)(v) as a safety system functional failure. The NRC

documented this failure as a Severity Level IV noncited violation,

NCV 05000482/2009005-15, Failure to Report a Condition that Could Have Prevented

Fulfillment of a Safety Function. Subsequently, Wolf Creek submitted LER 2009-009-01

which correctly reported the issue under 50.73(a)(2)(v). No additional violations were

identified during the inspectors review. These LERs are closed.

.4 (Closed) LER 2009-010-00; -01, Failure to Meet Limiting Condition for Operation 3.0.4b

During Transition from Mode 4 to Mode 3

On November 17, 2009, heat up activities were in progress to return the plant to service

following a refueling outage with the plant ready to transition from Mode 4 to Mode 3 with

the exception of completing some work activities and postmaintenance testing to restore

the turbine-driven auxiliary feedwater pump to a functional status. A risk assessment

was completed as required by limiting condition for operation 3.0.4b and required that

protected train signs be posted on the motor driven auxiliary feedwater pump rooms. On

November 18, 2009, at 12:24 a.m., the plant transitioned from Mode 4 to Mode 3 under

the provisions of limiting condition for operation 3.0.4b for the turbine-driven auxiliary

feedwater pump with no protected equipment signs posted for the motor-driven auxiliary

feedwater pump rooms. The inspectors identified the condition later that morning and

upon notification of the control room operators, the protected train signs were hung at

10:00 a.m., satisfying all actions required by limiting condition for operation 3.0.4b.

The inspectors reviewed apparent cause evaluation 22483, the hazard-barrier-target

analysis, and new and revised station procedures associated with this event. The

- 49 - Enclosure

inspectors concluded that Wolf Creeks corrective actions were adequate to ensure

compliance during future mode changes made under Technical Specification 3.0.4b. A

violation associated with this event is described in NRC Inspection

Report 05000482/2009005 as NCV 05000482/2009005-05, Mode Change under

Technical Specification 3.0.4.b Without Required Risk Management Actions. The

inspectors concluded that Wolf Creek satisfied the applicable Regulatory Commitment

associated with this LER documented in a letter from Mr. S. Hedges to the NRC dated

July 13, 2010. These LERs are closed.

.5 (Closed) LER 2010-001-00, Automatic Start of Motor-Driven Auxiliary Feedwater Pumps

Inoperable During Startup in Mode 1

On February 4, 2010, licensee personnel reviewed industry operating experience and

identified that the anticipatory actuation of the auxiliary feedwater pumps on a trip of both

main feedwater pumps would not function under certain conditions. Specifically, the

logic would not actuate on trip of a single operating main feedwater pump if the second

main feedwater pump was secured and reset. Two channels of auxiliary feedwater

actuation logic are required to be operable in Modes 1 and 2 as specified by Technical

Specification Table 3.3.2-1, function 6.g. There is no specified required action for two

inoperable channels, so limiting condition for operation 3.0.3 would be applicable

requiring action to be initiated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to place the unit in Mode 3 in 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />. A

review by the licensee discovered occurrences where the required channels were both

inoperable and the technical specification required action was not completed. The

licensee determined that the occurrences constituted a condition prohibited by technical

specifications, a common-cause inoperability of independent channels and a

safety-system functional failure. The inspectors reviewed the licensees submittal and

determined that the report adequately documented the summary of the event, the

potential safety consequences, and the corrective actions required to address the

performance deficiency. The enforcement aspects of this violation were discussed in

NRC inspection report 05000482/2010002 in noncited violation

NCV 05000482/2010002-05, Failure to Follow Procedure for a Main Feed Pump Trip.

No additional violations were identified during the inspectors review. This LER is

closed.

.6 (Closed) LER 2010-002-00, Turbine Trip Function of Reactor Trip, P-4 Interlock

Defeated During Entry Into and in Mode 3

As part of the extent of condition review for NCV 05000482/2009005-15, Failure to

Report a Condition that Could Have Prevented Fulfillment of a Safety Function, Wolf

Creek identified that the P-4 interlock for turbine trip was being defeated in Mode 3. The

issue was reported as a condition prohibited by technical specification for defeating both

trains of the P-4 interlock. This included the reporting criteria under 50.73(a)(2)(i)(B) and

50.73(a)(2)(v). A licensee identified violation involving this issue is included in

Section 4OA7 of this report. No additional violations were identified during the

inspectors review. This LER is closed.

- 50 - Enclosure

.7 (Closed) LER 2010-014-00, Technical Specification Required Shutdown Due to

Inadequate Planning Resulting in Extended Emergency Diesel Generator Inoperability

On November 29, 2010, the licensee removed Train A emergency diesel generator from

service for a scheduled 7-day technical specification equipment outage in accordance

with Technical Specification 3.8.1, Condition B. During the outage, a number of delays

occurred and a high number of emergent work activities impacted the schedule. On

December 6, 2010, during the final surveillance run for declaring the emergency diesel

generator operable, the licensee identified that the peak firing pressure for cylinder 12

was almost 500 psig less than expected. The licensee determined that the condition

could not be fixed within the remaining time in the technical specification equipment

outage and commenced a shutdown of the reactor in compliance with technical

specifications.

The license determined that the retaining bolt for the fuel injector pump timing

adjustment lock plate on cylinder 12 had backed out due to a loose/deformed keeper

plate. This affected the timing of the injector pump and caused the reduction in the

cylinder pressure. The remaining cylinders were inspected and no other problems were

found. Work on the emergency diesel generator Train A was completed and the

emergency diesel generator was returned to operable status on December 7, 2010, and

Wolf Creek returned to Mode 1 on December 8, 2010.

The inspectors reviewed the root cause analysis and associated actions taken for this

event documented in Condition Report 30918. Wolf Creek determined that the root

cause of the unplanned shutdown was weaknesses in coordination of emergent work

into the work scheduling and work control processes. The inspectors concluded that no

violations of NRC requirements occurred during this event and that the cause evaluation

and corrective actions were appropriate. This LER is closed.

4OA6 Meetings

Exit Meeting Summary

On March 15, 2011, the inspectors discussed the results of the in-office inspection of changes to

the licensees emergency plan with Mr. T. East, superintendent emergency planning, and other

members of the licensees staff. The licensee acknowledged the issues presented. The

inspectors asked the licensee whether any materials examined during the inspection should be

considered proprietary. No proprietary information was identified.

On March 25, 2011, the inspectors presented the results of the radiation safety inspection to

Mr. M. Sunseri, President and Chief Executive Officer, and other members of the licensee staff.

The licensee acknowledged the issues presented. The inspectors asked the licensee whether

any materials examined during the inspection should be considered proprietary. No proprietary

information was identified.

On April 7, 2011, the inspectors presented the inspection results to Mr. M, Sunseri, President

and Chief Executive Officer, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspectors asked the licensee whether any materials

- 51 - Enclosure

examined during the inspection should be considered proprietary. No proprietary information

was identified.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as noncited violations.

Instrumentation, function 6.g., requires, in part, two operable channels of auxiliary

feedwater actuation upon trip of all main feedwater pumps in modes 1 and 2. There is

no specified required action for two inoperable channels, so limiting condition for

operation 3.0.3 is applicable. Limiting condition for operation 3.0.3 requires action to be

initiated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to place the plant in mode 3 in 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />. Contrary to the above, on

January 20, 2010, Wolf Creek identified that at various times, the actuation logic function

6.g. for auxiliary feedwater had been inoperable and that the licensee had failed to

initiate action within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to place the unit in mode 3 in 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />. Specifically, the

actuation logic could not be made up with one main feedwater pump operating and the

second main feedwater pump secured and reset. This condition occurred during unit

startups and shutdowns. This finding was entered in the licensees corrective action

program as Condition Report 23008. Using Inspection Manual Chapter 0609.04,

Phase 1 - Initial Screening and Characterization of Findings, the issue screened to a

Phase 2 significance determination because it involved an actual loss of safety function.

A Phase 2 significance determination using the pre-solved worksheet from the Risk

Informed Inspection Notebook for Wolf Creek Generating Station, determined the

finding was of very low safety significance (Green) because this feature was not credited

in the plants safety analysis and the auxiliary feedwater safety function was still

available.

surveys that (1) may be necessary for the licensee to comply with the regulations in this

part; and (2) are reasonable under the circumstances to evaluate (i) the magnitude and

extent of radiation levels; (ii) concentrations or quantities of radiological materials; and

(iii) the potential radiological hazards. On January 4, 2011, a dose estimate was created

for welding activities in a locked high radiation area on the 1988 elevation of the

auxiliary building. The dose estimate provided was for the incorrect valve. The incorrect

radiation survey data was used for the dose estimate. Additionally, the licensee

underestimated the number of workers that would be required for the work.

Consequently, the actual dose received was 180 mrem, which was 123 mrem over the

dose estimate of 56 mrem. Also, as stated in Section 2RS01, it caused the licensee to

fail to recognize that a revised or separate radiation work permit was required for this

work activity. Incorrectly evaluating the radiological hazard caused workers unintended

and unplanned dose. The inspectors determined this finding to be of very low safety

significance because it was not associated with ALARA planning or work controls, there

was no overexposure, there was no substantial potential for an overexposure, and the

- 52 - Enclosure

ability to assess dose was not compromised. This issue was documented in the

licensees corrective action program as Condition Report 00031818.

  • Technical Specification Table 3.3.2.1, function 8.a, requires two trains of the P-4

interlock to be operable in Modes 1, 2, and 3. Function 8.a does not provide a required

action for both trains of engineered safety features actuation system interlocks

inoperable. Wolf Creek Technical Specification 3.0.3 requires the plant to be in Mode 4

within 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> when there is no required action specified for a limiting condition of

operation that cannot be met. Contrary to the above, with both channels of the P-4 input

to the Turbine Trip function defeated in Mode 3, Wolf Creek did not take action to place

the unit in Mode 4 on November 6-8, 2006, May 10, 2008, April 30, 2009, and November

18, 2009. Using Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the issue screened to a Phase 2 significance

determination because it involved an actual loss of safety function. A Phase 2

significance determination could not be performed using the Risk Informed Inspection

Notebook for Wolf Creek Generating Station since the pre-solved worksheet did not

address the P-4 interlock. Using a Phase 3 analysis, a senior reactor analyst calculated

the core damage probability to be less than 1E-7 per year, or of very low safety

significance (Green). This issue was entered in the licensees corrective action program

as Condition Report 23108.

- 53 - Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

P. Bedgood, Manager, Radiation Protection

R. Evenson, Requalification Program Supervisor

S. Hedges, Site Vice President

S. Henry, Operations Manager

R. Hobby, Licensing Engineer

D. Hooper, Supervisor, Regulatory Affairs

T. Just, Senior Technician, Chemistry

J. Keim, Support Engineering Supervisor

M. McMullen, Technician, Engineering

C. Medency, Supervisor, Radiation Protection

W. Muilenburg, Licensing Engineer

R. Murray, Simulator Supervisor

B. Norton, Manage, Integrated Plant Scheduling

J. Pankaskie, Engineering Supervisor

G. Pendergrass, Director of Engineering

L. Rockers, Licensing Engineer

G. Sen, Regulatory Affairs Manager

R. Smith, Plant Manager

M. Sunseri, President and Chief Executive Officer

J. Truelove, Supervisor, Chemistry

J. Weeks, System Engineer

M. Westman, Training Manager

NRC Personnel

C. Long, Senior Resident Inspector

C. Peabody, Resident Inspector

D. Reinert, Acting Resident Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000482/2011002-01 NCV Inadequate Design Control of the Fuel Oil Storage Tank Fill

System (Section 1RO4)05000482/2011002-02 NCV Inadequate Clearance Order Isolated Cooling to Inservice

Safety-Related Equipment (Section 1R04)05000482/2011002-03 NCV Failure to Monitor the Performance of Nonsafety-Related

Systems and Components Used in the Plant Emergency

Operating Procedures under 10 CFR 50.65 Programs

(Section 1R12)05000482/2011002-04, NCV Failure to Follow 10 CFR 50.65 a(2) for Main Control Board

Annunciator Power Supply Failures (Section 1R12)

A-1 Attachment

Opened and Closed

05000482/2011002-05 NCV Inadequate Calculation for Vital Switchgear Cooling

(Section 1R15)05000485/2011002-06 NCV Failure to Perform an Operability Determination for Degradation

of the Fuel Oil Storage Tank (Section 1R15)05000482/2011002-07 NCV Failure to Verify Ultimate Heat Sink Sedimentation Levels within

Design Bases (Section 1R19)05000482/2011002-08 NCV Inadequate Fill and Vent of Component Cooling Water

(Section 1R19)05000482/2011002-09 NCV Inadequate Clearance Order Disables Power Operated Relief

Valve Low temperature Overpressure Function (Section 1R20)05000482/2011002-10 NCV Repetitive Failure to Enter Technical Specifications for Auxiliary

Feedwater Suction Valve Testing (Section 1R22)05000482/2011002-11 NCV Failure to Follow Radiation Work Permit Instructions

(Section 2RS01)

Closed

050002009-007-00 LER Removal of Equipment from Service Required by Technical

Specification and NRC Safety Evaluation (Section 4OA3)

050002009-008-00 LER Potential of Containment Coolers to Have Not Automatically

Started in Slow Speed (Section 4OA3)

050002009-009-00, 01 LER Defeating Feedwater Isolation on Low Tavg Coincident with P-4

Function Results in Missed Mode Change. (Section 4OA3)

050002009-010-00, 01 LER Failure to meet LCO 3.4B during transition from Mode 4 to

Mode 3. (Section 4OA3)

050002009-011-00 LER Intermediate Range Detector NI 36 Inoperable (Section 4OA3)

050002010-001-00 LER Automatic Start of Motor-Driven Feedwater Pumps Inoperable

During Startup in Mode 1 (Section 4OA3)

050002010-002-00 LER Turbine Trip Function of Reactor Trip, P-4 Interlock Defeated

During Entry Into and in Mode 3 (Section 4OA3)

A-2 Attachment

LIST OF DOCUMENTS REVIEWED

Section 1RO4: Equipment Alignment

PROCEDURES

NUMBER TITLE REVISION

CKL JE-120 Emergency Fuel Oil System Lineup 19

AP 21G-001 Control of Locked Component Status 53B

STN MT-002 Standby Diesel Fuel Oil Storage Tanks Drain and Clean 4

Surveillance TJE01B 0

STS PE-021E Train A Emergency Fuel Oil Transfer System 0

STS PE-021E Pressure Test 0

DRAWINGS

M-12EC01 Piping and Instrumentation Diagram Fuel Pool Cooling and 19

Cleanup System

M-12EC02 Piping and Instrumentation Diagram Fuel Pool Cooling and 7

Cleanup System

M-109 Emergency Fuel Oil Stg. Tk. SNUPPS 6

WCRE-03 Tank Emergency Fuel Oil Storage Tank THE 01 A&B 22

Documents

M-13JE02 Piping Isometric Emer. Fuel Oil Sys. - Train A Diesel 7

Generator Building

M-13JE01 Piping Orthographic Emergency Fuel Oil System (Below 4

Grade)

USAR Figure P&ID Emergency Fuel Oil System 19

9.5.4-1-00

MISCELLANEOUS

NUMBER TITLE REVISION

SY1406400 Lesson Plan: Fuel Oil Purpose, Power Supplies, Layout 8

Control Room IOD: B EDG FUEL OIL 0

Logs

USAR Chapter 9.5.4

A-3 Attachment

02-004 USAR Change Request

07948 CCP Engineering Disposition: correct seismic class on M- 0

12JE01

10153 CCP Engineering Disposition 3

11-337160-001 Engineering Disposition: 3/4 Diameter Tubing from Main 0

Supply to a Header (KKJ01B)

Work Orders

10-323952-00 00-223036-000

Condition Reports

00032348 0033327 2008-004248

Section 1RO5: Fire Protection

PROCEDURES

NUMBER TITLE REVISION

AP 10-106 Fire Preplans 7

Section 1RO6: Flood Protection Measures

PROCEDURES

NUMBER TITLE REVISION

AP 21B-003 Control of Non-Plant Items Inside the Plant 8

AP 10-102 Control of Combustible Materials 15

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

09-005-XX-01 Temporary Modification Order February 19,

2011

E-029-00023 Scotch Super 33+ Vinyl electrical Tape Data Sheet W01

Condition Reports

A-4 Attachment

00033842 00033847 00033959

Work Order

08-311356-020

Section 1RO7: Heat Sink Performance

PROCEDURES

NUMBER TITLE DATE

STN PE-033 CCW Heat Exchanger Performance Test March 3,

2009

STN PE-033 CCW Heat Exchanger Performance Test October 8,

2009

Section 1R11: Licensed Operator Requalification Program

PROCEDURES

NUMBER TITLE REVISION

GEN-00-005 Generator Load to Hot Standby 67

GEN-00-006 Solid Pzr Ops

LR4132601 Simulator Lab Training Materials 000

Section 1R12: Maintenance Effectiveness

Condition Reports

00020665 00034681 00034650 00034529 00033909

00033896 00010657 00025817 00016581 00019447

00019390 00016504 00016467 00033465 00033594

00033562 00030432 00033823

PROCEDURES

NUMBER TITLE REVISION

EDI 23M-050 Engineering Desktop Instruction Monitoring Performance to 3

Criteria and Goals

STS KJ-005A Manual/Auto Start, Sync & Loading of EDG NE01 54

A-5 Attachment

PROCEDURES

NUMBER TITLE REVISION

MISCELLANEOUS

NUMBER TITLE

AD-04 Final Scope Evaluation for Condensate System Function to

Provide Water to the Suction of the Main Feedwater Pumps

AE-01 Final Scope Evaluation for Feedwater System Function to

Provide Feedwater and Controls to the Steam Generators

AE-04 Final Scope Evaluation for Feedwater System Function to

Provide Feedwater and Controls to the Steam Generators

(startup feed pump)

KA-01 Final Scope Evaluation for Compressed Air System Function

to Provide a Continuous Supply of Dry Oil-Free Air for

Pneumatic Instruments and Valves

NF-01 Final Scope Evaluation for Load Shedding and Emergency

Load Sequencing System Function to Shed and/or Sequence

Selected Loads from and/or to the Class 1E Buses

PA-01 Final Scope Evaluation for the Higher Medium Voltage

System 13,8kV Function to Distribute 13.8kV Power to

Various Loads Via Two Buses

PB-01 Final Scope Evaluation for the Lower Medium Voltage

System 4.16kV (Nonclass IE Power System) Function to

Provide Transformation of Power from 13.8kVac to 4.16kVac

and Distribute that 4.16kV Power to Supplied Loads

PG-01 Final Scope Evaluation for the Low Voltage System - 480V

(Nonclass IE Power System) Function to Provide

Transformation of Power from 13.8kVac to 480Vac and

Distribute that Power to Supplied Loads

PK-01 Final Scope Evaluation for 125Vdc System (Nonclass IE

Power System) Function to Provide 125Vdc Power to Various

Plant Loads for Control and Switching of Nonclass 1E

Electrical Systems

RK-01 Final Scope Evaluation for Plant Annunciator System

Function to Provide the Control Room Operator a Visual and

Audible Plant Status Condition

A-6 Attachment

PROCEDURES

NUMBER TITLE REVISION

SL-01 Final Scope Evaluation for Site Auxiliary Power System

Function to Provide ac Electrical Power to Service Water,

Circulating Water, and Fire Protection Systems

Work Orders

10-330047-000 10-330048-000 10-330049-000 10-331141-000 10-331148-000

10-331182-000 10-332898-000 10-332907-000 10-332894-000 09-316986-000

11-338443-000 11-338329-000 10-328341-000 10-328341-001 09-317354-000

09-317354-001 09-314014-000 08-312488-000 10-329847-001 09-320710-000

09-320710-001 09-318024-000 09-313998-000 09-313269-000 08-313088-000

08-313088-005 08-311453-000 10-336499-000 10-334406-000 10-328821-000

10-328821-001 10-326492-000 10-326377-000 08-310332-000 08-308271-003

08-304334-000 08-303649-000 08-303649-001 10-331046-000 10-325812-000

09-319777-000 09-318534-000 10-332636-000 10-332636-001 10-332636-002

10-328064-000 09-320189-000

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

MISCELLANEOUS

NUMBER TITLE REVISION

AP 22C-003 On-Line Nuclear Safety and Generation Risk Assessment 15A

ALR 00-131B Generator Field Overvoltage 8

ALR 00-131C Voltage Regulator Trip to Manual 6

ALR 00-131D Generator Voltage / Hertz Excess 10

STN AC-004 Quarterly Turbine Test 14A

SYS AC-120 Main Turbine Generator Startup 74

TSTF-IG-06-01 Implementation Guidance for TSTF-358, Missed Surveillance 6

Requirements

TSTF-358 Industry/TSTF Standard Technical Specification Change 6

Traveler

Technical Specification SR 3.3.2.10, Table B 3.3.2-2

Functional Unit 13

Technical Specification B 3.0-13, -14 34

Technical Specification 3.0-4 173

PSA-11-001 PSA Risk Evaluation of Incomplete Surveillances Tests STS 0

A-7 Attachment

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

MISCELLANEOUS

NUMBER TITLE REVISION

AL-005, STS IC-740A and STS IC-740B (CR 33352)

AP 26C-004 Operability Determination and Functionality Assessment 21

Calculation No. AN-02-006 0

M-724-00409 Instruction Manual for Gate and Check Valves W13

MGE LT-009 Limitorque Geared Limitswitch Adjustment 8A

DRAWINGS

E-13BN03A Refueling Water Storage Tank to RHR Pump MOV 8

E-13EJ06A Sump to No. 1 Residual Heat Removal Pump 7

E-13EJO6B Sump to No. 2 Residual Heat Removal Pump 9

EJHV8811A CTMT Recir Sump to RHR Pump A Suction ISO 0

EJHV8811B CTMT Recir Sump to RHR Pump B Suction ISO 0

BNHV8811A RWST to RHR PMP A Suction ISO W13

BNHV8812B RWST to RHR PMP B Suction ISO W13

44C308703 Alterrex Excitation System with S.C.R. Regulator 8

Condition Reports

00033352 00033717 00031929

Work Orders

08-310457-000 08-308676-001 08-308675-001 11-336846-001

Section 1R15: Operability Evaluations

NUMBER TITLE REVISION /

DATE

OFN-SG-003 Natural Events 20

BGV0192 to BGV0195 RWST Interface Piping 0

JE-M-003 Emergency Fuel Oil Storage Tanks Access Vaults Minimum 00

Temperature

STS CH-015 Emergency Diesel New Fuel 23

STS KJ-005A Manual/Auto Start, Sync & Loading of EDG NE01 54

A-8 Attachment

Section 1R15: Operability Evaluations

NUMBER TITLE REVISION /

DATE

STS MT-011 Snubber Visual Examination 18

SYS KJ-200 Inoperable Emergency Diesel 23A

CHS KJ-D01 Sampling Emergency Diesel A & B Fuel Oil System 1A

ASME B&PV Section XI - Subsection IWF Requirements for Class 1, 2, 3 1998

Code and MC Component Supports of Light Water Cooled Plants

MC8571 NRC Safety Evaluation, 3rd 10 Year Interval Inservice June 2, 2006

Examination Program for Snubbers Relief Request I3R-03

RER 2010-106 Broken Smith Blair Coupling Flange February 15,

2011

Work Order

10-331864-000

Condition Reports

00010832 00015385 00010833 00020515 00024818

00032420 0003718 00033730 00033953 00033486

00033653 00033758 00025988 00031020

Section 1R19: Postmaintenance Testing

CALCULATIONS

NUMBER TITLE REVISION /

DATE

Z065-C-001 Calculation Subject: Evaluation of Annual UHS 10

Sedimentation Measurements

CCP 011149 Revise Surveillance Frequency for SR Water Control 0

Structures and Reservoir (C-404)

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

C-302 Specification for Suction Dredging the Ultimate Heat Sink 2

C-302 Specification for Suction Dredging the Ultimate Heat Sink 3

A-9 Attachment

Section 1R19: Postmaintenance Testing

CALCULATIONS

NUMBER TITLE REVISION /

DATE

M-021-089-04 MDAFW A Pump Flow-Head Curve

OE AL-09-013 MDAFWP Total Discharge Flow Above 800gpm 0

PO: 750835/0 2010 Wolf Creek UHS Reservoir Hydrographic Survey August 20,

2010

PROCEDURES

NUMBER TITLE REVISION /

DATE

AP 10-103 Fire Protection Fire Impairment Control 23A

SYS FP-293 Fire Pumps Manual Operation 15

STN FP-211 Diesel Fire Pump1FP01PB Monthly Operation and Fuel 21A

Level Check

EF-M-021-000- Calculation Change Notice December 13,

CN001 2005

EFHV0039 30 Butterfly SMB-00-25

AP-16E-002 Post Maintenance Testing Development 9C

STN AE-007 Startup Main Feedwater Operational Test 0A

STS AL-101 MDAFW Pump A Inservice Pump Test (Completed) January 10,

2011

SYS AL-120 MDAFW or TDAFW Pump Operations (Completed) January 6,

2011

AP 29B-003 Surveillance Testing 11

TMP 04-016 Dredging the UHS 0

MPM KJ-004 Robertshaw Model 1285 Temperature Control Valve 2

Condition Reports

00034331 00034806 00034500 00034434 00027080

00027220 00027243 00027144 00027196 00031876

00021559 00021630 00031853 00031848 00031820

00031819 00032573 00031863 00032582 00032584

00032586

A-10 Attachment

Work Orders

11-338679-000 11-338679-001 11-338679-002 11-338509-000 11-338509-001

10-331117-003 10-331117-001 10-332847-000 10-332847-002 09-322525-001

10-335457-001 04-262017-000 02-233644-000 09-322079-000 09-322079-001

09-322079-002 11-336729-000 09-322079-006 06-248742-000 06-289298-000

09-318482-000 10-325693-000 10-332582-000

Section 1R20: Refueling and Other Outage Activities

PROCEDURES

NUMBER TITLE REVISION

GEN 00-004 Power Operation 65

GEN 00-005 Minimum Load to Hot Standby 67

GEN 00-006 Hot Standby to Cold Shutdown 76

AP 21E-001 Clearance Orders 27

SYS-SB-120 Enabling/Disabling of SSPS 9

MISCELLANEOUS

NUMBER TITLE DATE

R-SB-A-004 Clearance Order March 22,

2011

10-328830-001 Clearance Order Worksheet Audit Report March 30,

2011

Condition Reports

00035318 00035288

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER TITLE REVISION /

DATE

STS AL-103 Turbine Driven AFW Pump Inservice Test 45

STS EM-100A Safety Injection Pump A Inservice Pump Test 04A

STS RE-009 Heat Flux Hot Channel Factor Measurement (Completed) January 14,

2011

A-11 Attachment

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER TITLE REVISION /

DATE

STS RE-013A Incore-Excore Detector Axial Flux Difference Comparison January 14,

(Completed) 2011

STN EM-100A Safety Injection Pump A Reference Pump Curve 3

Determination

STS PE-061 Control Room Control Building Habitability Test 0

STS IC-202A Channel Operational Test of Tavg, dT and Pressurizer 22A

Pressure Protection Set Two

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

CCP 013427 Broken Wires in Containment Tendons V7 and V65 00

WC-N1054-002 Wolf Creek Generating Station 7th Period - 25th Year June 22,

Containment Building Tendon Surveillance 2010

WC-N1054-500 Final Report for the Wolf Creek Nuclear Plant 25th Year December 6,

Containment Building Tendon Surveillance 2010

WCGS Special Administrative Requirements for Technical Specification 1

Order 26 Required Actions for Transient Relaxed Axial Offset Control

FQW(Z) Not Within Limits

Accelerated Atmospheric Tracer Depletion (ATD) February 28,

Testing for Unfiltered Air In-Leakage Determination at the 2011

Wolf Creek Nuclear Power Plant

DRAWINGS

NUMBER TITLE REVISION /

DATE

1000872.511 Wolf Creek B-Train M-15EF01 September 10,

2010

1000872.501 Wolf Creek A-Train M-15EF01 September 1,

2011

M-744-00042 Reactor Protection System Engineered Safety Features W11

Condition Reports

00033477 00033908 2006-002097

A-12 Attachment

Section 1EP6: Drill Evaluation

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

11-SA-01 Wolf Creek Emergency Planning Drill Scenario January 11,

2011

Section 2RS01: Radiological Hazard Assessment and Exposure Controls

PROCEDURES

NUMBER TITLE REVISION

AP 19B-001 Failed Fuel Action Program 7

AP 19D-100 Radioactive Source Program 4

AP 25A-001 Radiation Protection Manual 14

AP 25A-200 Access to Locked High or Very High Radiation Areas 24

AP 25A-700 Use of Temporary Lead Shielding or Locked High Radiation 12

Areas and Very High Radiation Area Barricades

AP 25B-100 Radiation Worker Guidelines 40

RPP 01-105 Health Physics Organization, Responsibilities, and Code of 13

Conduct

RPP 02-210 Radiation Survey Methods 37

RPP 02-215 Posting of Radiological Controlled Areas 26A

RPP 02-405 RCA Access Control 17

RPP 02-515 Release of Material from the RCA 26

RPP 02-605 Control and Inventory of Radioactive Sources 14

RPP 08-105 Underwater Dive Operations 8

STS HP-001 Sealed Source Contamination Surveillance Test 22

A-13 Attachment

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

NUMBER TITLE DATE

10-09-PC Quality Assurance Audit Report Process Control November 18, 2010

Program

10-03-RP Quality Assurance Audit Report Radiological Protection March 18, 2010

Program

SEL 2010-176 Self Assessment Report SEL 2010-176 HP June 24, 2010

Operations/Instrumentation

CONDITION REPORTS

00025491 00027545 00031818 00034013 00035289

00035392 00035396 00035408 00035500 00035519

RADIATION WORK PERMITS

NUMBER TITLE

110008 NRC Access to the RCA

110060 Underwater Vacuum Filter Removal from Spent Fuel Pool

111001 Operations Rover RWP for pre-RF-18 and RF-18 Activities

111101 Under RV Cavity Seal Ring Access for RF-18

111102 Incore Tunnel Inspections & Maintenance

112600 Routine Outage Access (No High Radiation Areas Access)

112601 Routine Outage Access (No Locked High Radiation Areas Access)

112602 Routine Outage Access (No Very High Radiation Areas Access)

113022 Eddy Current Testing of Incore Flux Thimble Tubes at Seal Table

113220 Primary Side Steam Generator Secondary Side Work

116020 RV Head Preparation

116031 RV Head Lift, Transfer, & Set

SURVEYS

1101-0028 1101-0040 1101-0041 1101-0052 1101-0055

1101-0197 1101-0198

A-14 Attachment

Section 2RS02: Occupational ALARA Planning and Controls

PROCEDURES

NUMBER TITLE REVISION

AI 02-005 Primary and Radwaste Guidelines for Plant Startup and 2

Shutdown

AP 25A-001 Radiation Protection Manual 14

AP 25A-401 ALARA Program 18

AP 25A-410 ALARA Committee 15

AP 25B-300 RWP Program 21

RPP 02-105 RWP 35

CONDITION REPORTS

00025510 00025923 00026060 00030234 00031460

00033762 00034013

RADIATION WORK PERMITS

NUMBER TITLE

111000 Health Physics Rover Coverage RF-18

113220 Primary Side Steam Generator Secondary Side Work

114200 Steam Generator Secondary Side

114208 RCP Team Work Activities Reactor Vessel Head Lift Preparation and Post

Head Set Work Activities

114420 RV Head Lift, Transfer, & Set Scaffolding Erection/Removal

116020 RV Head Preparation

A-15 Attachment

MISCELLANEOUS DOCUMENTS

TITLE DATE

ALARA Report Refuel 17 August 30,2010

ALARA Committee Meeting November 16, 2010

ALARA Committee Meeting December 14, 2010

ALARA Committee Meeting February 08, 2011

ALARA Committee Meeting March 08, 2011

ALARA Long Range Source Term Reduction Plan 2010-2015 November 18, 2010

Section 2RS03: In-plant Airborne Radioactivity Control and Mitigation

PROCEDURES

NUMBER TITLE REVISION

AI 14-009 Industrial Respiratory Protection Program 5A

AP 25B-600 Respiratory Protection Program at Wolf Creek 7

AP 25A-800 Use of Vacuum Cleaners in the RCA 4A

RRP 05-205 Eberline AMS-4 Operation 8

RRP 05-920 RCA Vacuum Cleaner Maintenance 5

RRP 05-925 HEPA Portable Ventilation Unit Maintenance and Use 6

Section 4OA1: Performance Indicator Verification

PROCEDURES

NUMBER TITLE REVISION

APA 26A-2007 NRC Performance Indicators 8

OTHER DOCUMENTS

NUMBER TITLE DATE

SEL 2010-188 Self-Assessment Report November 18,

2010

CONDITION REPORTS

19369 19913 25817

Section 4OA3: Event Follow-Up

PROCEDURES

NUMBER TITLE REVISION

AP 26C-005 Technical Specification LCO 3.0.4 Mode Change Review 0

A-16 Attachment

MISCELLANEOUS

NUMBER TITLE DATE

EA-09-326 Response to Disputed Noncited Violations in NRC Inspection March 4,

Report 05000482/2009004 and Withdrawal of Noncited 2010

Violation

Condition Reports

00022483 00030918

A-17 Attachment