ML050480651

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Er 05000440-04-301(DRS); 11/29/2004-12/09/2004; Perry Nuclear Power Plant; Initial License Examination Report
ML050480651
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 02/17/2005
From: Lanksbury R
Division of Reactor Safety III
To: Richard Anderson
FirstEnergy Nuclear Operating Co
References
50-440/04-301, IR-04-301 50-440/04-301
Download: ML050480651 (38)


See also: IR 05000440/2004301

Text

February 11, 2005

EA 03-214

Mr. Mark B. Bezilla

Vice President-Nuclear, Davis-Besse

FirstEnergy Nuclear Operating Company

Davis-Besse Nuclear Power Station

5501 North State Route 2

Oak Harbor, OH 43449-9760

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION

NRC INTEGRATED INSPECTION REPORT 05000346/2004016

Dear Mr. Bezilla:

On December 31, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Davis-Besse Nuclear Power Station. The enclosed inspection report

documents the inspection findings which were discussed on January 6, 2005, with members

of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

For the entire inspection period, the Davis-Besse Nuclear Power Station was under the

Inspection Manual Chapter (IMC) 0350 Process. The Davis-Besse Oversight Panel assessed

inspection findings and other performance data to determine the required level and focus of

followup inspection activities and any other appropriate regulatory actions. Even though the

Reactor Oversight Process had been suspended at the Davis-Besse Nuclear Power Station, it

was used as guidance for inspection activities and to assess findings.

Based on the results of this inspection, the NRC has determined that a violation of NRC

requirements occurred. The report documents one NRC identified finding of very low safety

significance which involved a violation of NRC requirements. However, because the violation

was of very low safety significance and because it was entered into your corrective action

program, the NRC is treating this issue as a Non-Cited Violation consistent with Section VI.A

of the NRC Enforcement Policy.

If you contest the severity of a Non-Cited Violation, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

M. Bezilla

-2-

copies to the Regional Administrator Region III, 2443 Warrenville Road, Suite 210, Lisle, IL

60532-4352; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington DC 20555-001; and the NRC Resident Inspector at Davis-Besse.

The inspectors performed enhanced inspection activities in the 2nd, 3rd, and 4th quarters of

CY2004 associated with the Initiating Events, Mitigating Systems, and Barrier Integrity

Cornerstone Performance Indicators. Based on the results of these inspections and evaluation

of the data you submitted for each of these Performance Indicators, the Oversight Panel has

determined that the Performance Indicators will be returned to normal monitoring under the

baseline inspection program.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Steven A. Reynolds, Chairman

Davis-Besse Oversight Panel

Docket No. 50-346

License No. NPF-3

Enclosure:

Inspection Report 05000346/2004016

w/Attachment: Supplemental Information

cc w/encl:

The Honorable Dennis Kucinich

G. Leidich, President - FENOC

J. Hagan, Senior Vice President

Engineering and Services, FENOC

L. Myers, Chief Operating Officer, FENOC

Plant Manager

Manager - Regulatory Compliance

M. OReilly, Attorney, FirstEnergy

Ohio State Liaison Officer

R. Owen, Administrator, Ohio Department of Health

Public Utilities Commission of Ohio

President, Board of County Commissioners

of Lucas County

J. Papcun, President, Ottawa County Board of Commissioners

D. Lochbaum, Union Of Concerned Scientists

J. Riccio, Greenpeace

P. Gunter, N.I.R.S.

DOCUMENT NAME: C:\\Karen's Documents\\ML050450453.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with DB0350

attachment/enclosure "N" = No copy

OFFICE

RIII

RIII

NAME

CLipa:dtp

SReynolds

DATE

02/11/05

02/11/05

OFFICIAL RECORD COPY

M. Bezilla

-3-

ADAMS Distribution:

GYS

SPS1

RidsNrrDipmIipb

GEG

HBC

KGO

CST1

CAA1

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

JRK1

WDL (IRs only)

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-346

License No:

NPF-3

Report No:

05000346/2004016

Licensee:

FirstEnergy Nuclear Operating Company (FENOC)

Facility:

Davis-Besse Nuclear Power Station

Location:

5501 North State Route 2

Oak Harbor, OH 43449-9760

Dates:

November 14 through December 31, 2004

Inspectors:

S. Thomas, Senior Resident Inspector

J. Rutkowski, Resident Inspector

M. Salter-Williams, Resident Inspector

J. Jacobson, Senior Engineer

J. House, Senior Radiation Specialist

H. Peterson, Senior Operations Engineer

R. Walton, Operations Engineer

Approved by:

Christine A. Lipa, Chief

Branch 4

Division of Reactor Projects

Enclosure

1

SUMMARY OF FINDINGS

IR 05000346/2004016; 11/14/2004-12/31/2004; Davis-Besse Nuclear Power Station; Other

Activities.

This report covers a 7 week period of resident inspection. The inspection was conducted by

regional inspectors and resident inspectors. One Green finding associated with one Non-Cited

violation was identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a finding of very low safety significance for the

licensees failure to take timely corrective action to remove visible corrosion on several

terminal connections on the stations safety-related 2P and 2N batteries. The primary

cause of this finding was related to the cross-cutting area of problem identification and

resolution.

The inspectors determined that the finding was more than minor because it impacted

the Mitigating Systems cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. This issue was determined to be of very low safety significance

because there were no documented cases of any of the affected battery cells terminal

resistance measurements in excess of 150 micro-ohms. This was considered to be a

Non-Cited Violation of 10CFR 50, Appendix B, Criterion XVI. (Section 4OA5)

B.

Licensee Identified Findings

None

Enclosure

2

REPORT DETAILS

Summary of Plant Status

At the beginning of the inspection period, the plant was operating at approximately 100 percent

power. During this inspection period, brief planned power reductions of less than 10 percent

occurred on two occasions (November 21, 2004, and December 19, 2004) to support planned

testing. On each occasion, the testing was completed and power was restored to

approximately 100 percent. The plant operated at approximately 100 percent power for the

remainder of the inspection period.

For the entire inspection period, the Davis-Besse Nuclear Power Station was under the

IMC 0350 Process.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R05

Fire Protection (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection inspections focused on the availability,

accessibility, and condition of fire fighting equipment; the control of transient

combustibles; and the condition and status of installed fire barriers. The inspectors

selected fire areas for inspection based on their overall contribution to internal fire risk,

as documented in the Individual Plant Examination of External Events, and their

potential to impact equipment which could initiate a plant transient. Inspectors

determined whether fire hoses and extinguishers were in their designated locations and

available for immediate use; fire detectors and sprinklers were unobstructed; transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals were in satisfactory condition.

The following area was inspected and constitutes one sample:

Decay Heat Cooler Room and Hatch Area

b.

Findings

No findings of significance were identified.

Enclosure

3

1R11

Licensed Operator Requalification (71111.11)

.1

Facility Operating History

a.

Inspection Scope

The inspectors reviewed the plants operating history from October 2002 through

October 2004, to assess whether the Licensed Operator Requalification Training

(LORT) program had addressed operator performance deficiencies noted at the plant.

b.

Findings

No findings of significance were identified.

.2

Licensee Requalification Examinations

a.

Inspection Scope

The inspectors performed a biennial inspection of the licensees LORT program. The

inspectors reviewed the current year requalification biennial written examinations and

annual operating test material to evaluate general quality, construction, and difficulty

level. The biennial written examination material consisted of forty questions in a

multiple-choice format. The questions addressed plant and control systems,

administrative controls, and procedural limits. The operating test material consisted of

dynamic simulator scenarios and job performance measures (JPMs). The inspectors

reviewed the methodology for developing the examinations, including the LORT

program 2-year sample plan, probabilistic risk assessment insights, previously identified

operator performance deficiencies, and plant modifications. The inspectors assessed

the level of examination material duplication during the current year annual

examinations. The inspectors also interviewed members of the licensees management

and training staff, and discussed various aspects of the examination development.

b.

Findings

No findings of significance were identified.

.3

Licensee Administration of Requalification Examinations

a.

Inspection Scope

The inspectors observed administration of the requalification operating test to assess

the licensees effectiveness in conducting the test and to assess the facility evaluators

ability to determine adequate performance using objective, measurable performance

standards. The inspectors evaluated, in parallel with the facility evaluators, the

performance of seven licensed operators for one operating shift crew during two

dynamic simulator scenarios. The shift crew was divided into two 5-person simulator

crews for evaluation purposes, with the two remaining individuals rotating into their

respective licensed positions during the second scenario. Each crew consisted of three

Enclosure

4

senior reactor operators and two reactor operators. In addition, the inspectors observed

licensee evaluators administer five JPMs to a select number of operators. The

inspectors observed the training staff personnel administer the operating test, including

pre-examination briefings, observations of operator performance, and individual and

crew evaluations after the dynamic simulator scenarios.

b.

Findings

No findings of significance were identified.

.4

Examination Security

a.

Inspection Scope

The inspectors observed and reviewed the licensees overall licensed operator

requalification examination security program related to examination physical security

(e.g., access restrictions and simulator considerations) and integrity (e.g., predictability

and bias). The inspectors also reviewed the facility licensees examination security

procedure, any corrective actions related to past or present examination security

problems at the facility, and the implementation of security and integrity measures

(e.g., security agreements, sampling criteria, bank use, and test item repetition)

throughout the examination process.

b.

Findings

No findings of significance were identified.

.5

Licensee Training Feedback System

a.

Inspection Scope

The inspectors assessed the methods and effectiveness of the licensees processes for

revising and maintaining its LORT program up to date, including the use of feedback

from plant events and industry experience information. The inspectors interviewed

licensee personnel (operators, instructors, and management) and reviewed applicable

procedures. In addition, the inspectors reviewed the licensees quality assurance

oversight activities, including licensee training department self-assessment reports. The

inspectors evaluated the licensees ability to assess the effectiveness of its LORT

program and their ability to implement appropriate corrective actions.

b.

Findings

No findings of significance were identified.

Enclosure

5

.6

Licensee Remedial Training Program

a.

Inspection Scope

The inspectors assessed the adequacy and effectiveness of remedial training conducted

since the previous annual requalification examinations. The inspectors reviewed the

remedial training documentation for one individual who demonstrated unsatisfactory

performance during the current biennial written examination and the subsequent

post-remedial re-examination administered the previous week. The inspectors also

reviewed the remedial training package for one individual who demonstrated

unsatisfactory performance during the current annual operating test. The inspectors

reviewed the training package to determine whether performance and knowledge

weaknesses identified during the annual examination were adequately addressed. The

inspectors also reviewed remedial training procedures and records to determine whether

the subsequent re-evaluation was properly completed prior to returning the individuals to

licensed duties.

b.

Findings

No findings of significance were identified.

.7

Conformance with Operator License Condition

a.

Inspection Scope

The inspectors evaluated facility and individual operator license conformance with the

requirements of 10 CFR Part 55. The inspectors reviewed the licensees program for

maintaining active operator licenses to assess compliance with 10 CFR 55.53(e) and (f).

The inspectors reviewed the licensees procedural compliance and the process for

tracking on-shift hours for licensed operators. The inspectors also conducted reviews to

determine whether proficiency watch-standing hours were credited to the correct control

room positions in accordance with Technical Specifications. The inspectors reviewed

six licensed operator medical records to ensure compliance with 10 CFR 55.21 and

55.25, and medical standards delineated in ANSI/ANS-3.4. In addition, the inspectors

reviewed the licensees LORT program to assess compliance with the requalification

program requirements prescribed by 10 CFR 55.59(c).

b.

Findings

No findings of significance were identified.

.8

Conformance with Simulator Requirements

a.

Inspection Scope

The inspectors assessed the adequacy of the licensees simulation facility (simulator) for

use in operator licensing examinations and for satisfying experience requirements as

prescribed in 10 CFR 55.46, Simulation Facilities. The inspectors reviewed a sample

Enclosure

6

of simulator performance test records (i.e., transient tests, malfunction tests, and reactor

core performance tests), simulator work order records, and the process for ensuring

continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The

inspectors reviewed and evaluated the discrepancy process to ensure that simulator

fidelity was maintained. This was accomplished by a review of discrepancies noted

during the inspection to determine whether they were entered into the licensees

corrective action system and by an evaluation to verify that the licensee adequately

captured simulator problems and that corrective actions were performed and completed

in a timely fashion commensurate with the safety significance of the item (prioritization

scheme). Open simulator discrepancies were reviewed for importance relative to impact

on 10 CFR 55.45 and 55.59 operator actions as well as nuclear and thermal hydraulic

operating characteristics. Closed simulator discrepancies were reviewed for the last

12 months for timeliness of resolution. The inspectors reviewed the licensees recent

simulator core modeling performance testing to assess the adequacy of the simulator to

replicate the actual reactor plant cores performance characteristics. The inspectors

also conducted interviews with the licensees simulator configuration control personnel

and completed the checklist described in Appendix C of NRC Inspection Procedure (IP) 71111.11 to evaluate whether or not the licensees plant-referenced simulator was

operating adequately as required by 10 CFR 55.46 (c) and (d).

b.

Findings

No findings of significance were identified.

.9

Biennial Written Examination and Annual Operating Test Results

a.

Inspection Scope

The inspectors reviewed the overall pass/fail results of the comprehensive biennial

written tests, the annual job performance measure operating tests, and the annual

simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered

by the licensee during calendar year 2004. The overall results were compared with the

significance determination process in accordance with NRC Manual Chapter 0609,

Appendix IProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix I" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Operator Requalification Human Performance Significance Determination

Process (SDP). Year 2004 was the second year of the licensees 24-month training

program. This represents one sample.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness (71111.12)

a.

Inspection Scope

The inspectors evaluated the licensees handling of performance issues related to the

auxiliary feedwater system. This inspection consisted of evaluating the following

licensee activities:

Enclosure

7

work scheduling practices, including consideration of risk of transient initiation

while performing work on operating components;

use of the condition report process and WO notification system in identifying

deficiencies and issues with the equipment;

problem solving and issue resolution associated with the failures and

degradations of components associated with the system;

that maintenance activities on the components had been assigned appropriate

risk classification;

that corrective actions for the long-term reliability were appropriate;

that pump performance trends were appropriate for normal pump testing

frequency;

that alert and action levels, per the inservice testing program, were appropriately

considered in reviewing auxiliary feedwater pump performance;

that short-term corrective actions were appropriate for deficiencies with potential

to become operator workarounds or the potential to become transient initiators;

and

that maintenance rule system status determination was appropriate for the

equipments recent history and current open work items.

The inspectors also observed that the licensee was aware of the small performance

margins available in the system and was developing plans for system improvements

designed to increase the available margins.

This constitutes one sample.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

Condition Report 04-07274 discussed instrument inaccuracies which were not

accounted for during bench testing of snubbers. These inaccuracies could have

potentially resulted in nine snubbers exceeding their Technical Specification

requirements for bleed rates and lockup velocities. The licensee reviewed their as-

found data and determined that eight of the snubbers were within the technical

specification operability range even when taking instrument inaccuracies into account.

Based upon their review of the as-found data for snubber DB-SNT20, the licensee

determined that the lockup velocity for the snubber could potentially be outside of its

Technical Specification acceptance criteria and as a result required an operability

evaluation. The inspectors reviewed Operability Evaluation 2004-0027 Revision 00

which discussed potential operability issues for snubber DB-SNT20, which is a 2 1/2 inch

Grinnel snubber installed on the Emergency Diesel Generator 1-2 exhaust line. This

operability evaluation was reviewed to determine whether the operability of the

component was justified. The inspectors compared the operability and design criteria in

the appropriate sections of the Technical Specifications and USAR to the licensees

Enclosure

8

evaluations presented on the issue to verify that the component was operable. Where

compensatory measures were necessary to maintain operability, the inspectors

reviewed the documents listed at the end of the report to determine whether the

measures were in place, would work as intended, and were properly controlled.

This constitutes one sample.

b.

Findings

No findings of significance were identified.

1R16

Operator Work-Arounds (71111.16)

a.

Inspection Scope

The inspectors reviewed all of the existing operator workarounds and control room

deficiencies to determine whether the cumulative conditions had a significant impact on

plant risk or on the operators ability to respond to a transient or an accident. This

involved reviewing the entire list of operator workarounds, control room deficiencies, and

turnover sheets. In addition, the inspectors interviewed operators and staff to determine

whether that the licensee had appropriately classified the workarounds and deficiencies

for significance, that the workarounds were achievable, and that the licensee had made

or planned timely and appropriate corrective actions to resolve the deficiency

responsible for the workaround. In addition to evaluating the individual impact of each

operator workaround, the inspector evaluated the cumulative affect of all workarounds

on plant safety.

This constitutes one sample.

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

On November 16, 2004, the inspectors observed performance of DB-SS-03091, Motor

Driven Feed Pump Quarterly Test, Revision 06. The inspectors reviewed the test

procedure and Technical Specifications to determine whether the test met the Technical

Specification frequency requirements; operability and availability were properly treated

and recorded in the unit log; the test was conducted in accordance with the procedures,

including establishing the proper plant conditions and prerequisites; and the test

acceptance criteria were met.

This constitutes one sample.

Enclosure

9

b

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1

Plant Walkdowns and Radiation Work Permit Reviews

a.

Inspection Scope

The inspectors identified radiologically significant work areas within a Technical

Specification locked high radiation area (LHRA) and also identified potential airborne

radioactivity areas in the containment building. The inspectors reviewed the radiation

work permit (RWP) and work package, which included radiological controls and surveys

of these areas, to determine if radiological controls including surveys, air sampling data,

postings, and barricades were adequate. These reviews and observations, along with

those contained in Section 2OS1(.1) of Inspection Report 50-346/04-015 represented

one sample.

The inspectors observed work activities in the LHRA and potential airborne radioactivity

areas and reviewed the surveys for these areas in order to determine whether the

prescribed RWP, procedures, and engineering controls were in place; licensee surveys

and postings were complete and accurate; and air samplers were properly located.

These reviews and observations, along with those contained in Section 2OS1(.1) of

Inspection Report 50-346/04-015 represented one sample.

The inspectors reviewed the RWP and associated radiological controls used to access

the containment building, and evaluated the work control instructions and control

barriers that were specified in order to determine whether the controls and requirements

were met. Site technical specification requirements for high radiation areas and LHRAs

were used as standards for the necessary barriers. Electronic dosimeter alarm set

points for both integrated dose and dose rate were evaluated for conformity with survey

indications and plant policy. The inspectors determined whether the pre-job briefing

emphasized to workers the actions required when their electronic dosimeters noticeably

malfunctioned or alarmed. These reviews and observations, along with those contained

in Section 2OS1(.1) of Inspection Report 50-346/04-015 represented one sample.

b.

Findings

No findings of significance were identified.

Enclosure

10

.2

Job-In-Progress Reviews

a.

Inspection Scope

The inspectors accompanied licensee personnel during an at power containment entry

and observed work activities in LHRAs, potential airborne radioactivity areas, and high

radiation areas that presented the greatest radiological risk to workers. Radiological

conditions involved neutron and gamma streaming that produced radiological gradients

which could result in a high collective dose to workers.

The inspectors reviewed radiological job requirements including RWP and work

procedure requirements, and attended as low as is reasonably achievable (ALARA) job

briefings. Job performance was observed with respect to these requirements to verify

that radiological conditions in the work area were adequately communicated to workers

through pre-job briefings and postings. These reviews and observations, along with

those contained in Section 2OS1(.3) of Inspection Report 50-346/04-015 represented

one sample.

The inspectors also verified the adequacy of radiological controls including required

radiation, contamination, and airborne surveys for entry into a LHRA; radiation

protection job coverage which included surveillance for both gamma and neutron

radiation and streaming paths; and contamination controls. These reviews and

observations, along with those contained in Section 2OS1(.3) of Inspection

Report 50-346/04-015 represented one sample.

Work in high radiation areas having significant dose rate gradients, both neutron and

gamma, was observed to evaluate the application of dosimetry to effectively monitor

exposure to personnel, and to verify that licensee controls were adequate. The

inspectors observed radiation protection (RP) technicians coverage of the containment

entry. This involved controlling worker and observer locations relative to radiation

survey data and real time monitoring for both gamma and neutron radiation in order to

maintain personnel radiological exposure ALARA. These reviews and observations

represented one sample.

b.

Findings

No findings of significance were identified.

.3

Radiation Worker Performance

a.

Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation protection work requirements. The

inspectors also evaluated whether workers were aware of the significant radiological

conditions in their workplace, the RWP controls and limits in place, and that their

performance had accounted for the level of radiological hazards present. These

Enclosure

11

reviews and observations, along with those contained in Section 2OS1(.5) of Inspection

Report 50-346/04-015 represented one sample.

Radiological problem reports, which found that the cause of an event resulted from

radiation worker errors, were reviewed to determine if there was an observable pattern

traceable to a similar cause, and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. These reviews

and observations, along with those contained in Section 2OS1(.5) of Inspection Report

50-346/04-015 represented one sample.

b.

Findings

No findings of significance were identified.

.4

Radiation Protection Technician Proficiency

a.

Inspection Scope

The inspectors observed and evaluated RP technician performance with respect to

RP work requirements. This was done to evaluate whether the technicians were aware

of the radiological conditions in their workplace, the RWP controls and limits in place,

and if their performance was consistent with their training and qualifications with respect

to the radiological hazards and work activities. These reviews and observations, along

with those contained in Section 2OS1(.6) of Inspection Report 50-346/04-015

represented one sample.

Radiological problem reports, which found that the cause of an event was RP technician

error, were reviewed to determine if there was an observable pattern traceable to a

similar cause, and to determine if this perspective matched the corrective action

approach taken by the licensee to resolve the reported problems. These reviews

and observations, along with those contained in Section 2OS1(.6) of Inspection

Report 50-346/04-015 represented one sample.

b.

Findings

No findings of significance were identified.

2OS2 As Low As Is Reasonably Achievable (ALARA) Planning And Controls (71121.02)

.1

Job Site Inspections and ALARA Control

a.

Inspection Scope

The inspectors observed work activities in areas having the potential for significant

radiation exposure levels as well as potential airborne radiological hazards during an at

power containment entry. The licensees use of ALARA controls for these work

activities was evaluated using the following:

Enclosure

12

The licensees use of engineering controls to achieve dose reductions was

evaluated to verify that procedures and controls were consistent with the

licensees ALARA reviews. The use of containment structures to provide

radiation shielding and avoidance of areas of potential radiation (gamma and

neutron) streaming was observed;

During the evolution, personnel were observed to determine if they were utilizing

low dose waiting areas and were effective in maintaining their doses ALARA by

using lower dose areas while traversing areas within the containment building;

and

The inspectors attended the work briefing and observed ongoing work activities

to determine if workers received appropriate on-the-job supervision to ensure the

ALARA requirements were met. This included verification that the first-line job

supervisor ensured that the work activity was conducted in a dose efficient

manner by minimizing work crew size, ensuring that workers were properly

trained, and that proper tools and equipment were available when the job

started.

b.

Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

2PS2

Radioactive Material Processing and Transportation (71122.02)

.1

Radioactive Waste System

a.

Inspection Scope

The inspectors reviewed descriptions of the liquid and solid radioactive waste systems

in the Updated Final Safety Analysis Report (UFSAR). The inspectors reviewed the

2003 effluent release report for information on the types and amounts of radioactive

waste (radwaste) generated and disposed. The inspectors reviewed the scope of the

licensees audit program for the radioactive material processing and transportation

programs to verify that the audit program met the requirements of 10 CFR 20.1101©).

These reviews represented one sample.

b.

Findings

No findings of significance were identified.

Enclosure

13

.2

Radioactive Waste System Walkdowns

a.

Inspection Scope

The inspectors performed walkdowns of the liquid and solid radwaste processing

systems to verify that the systems agreed with the descriptions in the UFSAR and the

Process Control Program, and to assess the material condition and operability of the

systems. The inspectors reviewed the status of radioactive waste process equipment

that was not operational or was abandoned in place, along with the licensees

administrative and physical controls, in order to ensure that the equipment would not

contribute to an unmonitored release path, affect operating systems, or be a source of

unnecessary personnel exposure.

No significant changes had been made to the radwaste processing system since the last

inspection. The inspectors reviewed the current processes for transferring waste resin

and sludge discharges into shipping or disposal containers to determine if appropriate

waste stream mixing and/or sampling procedures were utilized. This included the

methodologies for waste concentration averaging to determine if representative samples

of the waste product were provided for the purposes of waste classification specified in

10 CFR 61.55 for waste disposal. These reviews represented one sample.

b.

Findings

No findings of significance were identified.

.3

Waste Characterization and Classification

a.

Inspection Scope

The inspectors reviewed the licensees radio-chemical sample analysis results for each

of the waste streams, including dry active waste, ion exchange resins, filters, sludge,

and activation products. The inspectors also reviewed the licensees use of scaling

factors to quantify difficult-to-measure radionuclides such as pure alpha or

beta emitters, and isotopes that decay by electron capture. The reviews were

conducted to verify that the licensees program assured compliance with 10 CFR 61.55

and 10 CFR 61.56, as required by Appendix G of 10 CFR Part 20. The inspectors also

reviewed the licensees waste characterization and classification program to ensure that

the waste stream composition data accounted for changing operational parameters and

thus remained valid between the annual sample analysis updates. These reviews

represented one sample.

b.

Findings

No findings of significance were identified.

Enclosure

14

.4

Shipment Preparation

a.

Inspection Scope

The inspectors were unable to perform detailed observations of shipment preparation

during this inspection. From shipping records, the inspectors were able to verify that

receiving licensees were authorized to receive the shipments and that the requirements

of the transport cask Certificate of Compliance were met.

From limited observations of shipment preparation in the radwaste building and a

review of training materials and records, the inspectors verified that the workers had

adequate skills to accomplish each task and that the shippers were knowledgeable of

the shipping regulations; and that shipping personnel demonstrated adequate skills to

accomplish the package preparation requirements for public transport with respect to

NRC Bulletin 79-19 and 49 CFR Part 172 Subpart H. The inspectors reviewed the

training records of shipping personnel, which included shipment packaging, surveying,

labeling, marking, placarding, vehicle checks, emergency instructions, disposal

manifest, shipping papers provided to the driver, and licensee verification of shipment

readiness. The review was conducted to verify that the licensees training program

provided training consistent with NRC and Department of Transportation requirements.

These reviews represented one sample.

b.

Findings

No findings of significance were identified.

.5

Shipping Records

a.

Inspection Scope

The inspectors reviewed five non-excepted package shipment manifests/documents

completed in 2003 and 2004 to verify compliance with NRC and Department of

Transportation requirements (i.e., 10 CFR Parts 20 and 71, and 49 CFR Parts 172 and

173). This included required emergency response information and the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> contact

telephone number. This review represented one sample.

b.

Findings

No findings of significance were identified.

.6

Identification and Resolution of Problems For Radioactive Material Processing and

Transportation

a.

Inspection Scope

The inspectors reviewed condition reports, an audit, and field observations that covered

the period from the last inspection of this area and that addressed deficiencies in the

radioactive waste and radioactive materials shipping program. This was done in order

Enclosure

15

to verify that the licensee had effectively implemented the corrective action program and

that problems were identified, characterized, prioritized and corrected. The inspectors

also verified that the licensee's self-assessment program was capable of identifying and

addressing repetitive deficiencies or significant individual deficiencies that had been

identified in problem identification and resolution.

The inspectors also reviewed corrective action reports from the radioactive material and

shipping programs since the previous inspection, interviewed staff, and reviewed

documents to determine if the following activities were being conducted in an effective

and timely manner commensurate with their importance to safety and risk:

Initial problem identification, characterization, and tracking;

Disposition of operability/reportability issues;

Evaluation of safety significance/risk and priority for resolution;

Identification of repetitive problems;

Identification of contributing causes;

Identification and implementation of effective corrective actions;

Resolution of Non-Cited Violations (NCVs) tracked in corrective action system(s);

and

Implementation/consideration of risk significant operational experience feedback.

These reviews represented one sample.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

Cornerstones: Mitigating Systems, Initiating Events

Reactor Safety Strategic Area

.1

Mitigating System Cornerstone Performance Indicator Review

a.

Inspection Scope

The inspectors reviewed the reported data [3rd quarter 2003 to 3rd quarter 2004] for the

following Mitigating System Cornerstone performance indicator:

Safety System Unavailability, Auxiliary Emergency AC Power.

The inspectors used the definitions and guidance contained in Nuclear Energy

Institute 99-02, Regulatory Assessment Indicator Guideline, Revision 2, during the

conduct of this review. The inspectors reviewed station logs and condition reports to

determine the accuracy of the licensees data submission.

Enclosure

16

This constitutes one sample.

b.

Findings

No findings of significance were identified.

.2

Initiating Events Cornerstone Performance Indicator Review

a.

Inspection Scope

The inspectors reviewed the reported data [1st quarter 2004 to 4th quarter 2004] for the

following Initiating Event Cornerstone performance indicators:

Unplanned Scrams per 7000 Critical Hours;

Unplanned Scrams with Loss of Normal Heat Sink; and

Unplanned Power Changes per 7000 Critical Hours

The inspectors used the definitions and guidance contained in Nuclear Energy

Institute 99-02, Regulatory Assessment Indicator Guideline, Revision 2, during the

conduct of this review. The inspectors reviewed station logs and condition reports to

verify the accuracy of the licensees data submission.

This constitutes three samples.

b.

Findings

No findings of significance were identified.

.3

Review of Returning Performance Indicator Monitoring to the Baseline Inspection

Program

The inspectors performed enhanced inspection activities in the 2nd, 3rd, and 4th quarters

of CY2004 associated with the Initiating Events, Mitigating Systems, and Barrier

Integrity Cornerstone Performance Indicators. Based on the results of these inspections

and evaluation of the licensees submitted data, the Oversight Panel has determined

that the PIs will be returned to normal monitoring under the baseline inspection program.

4OA2 Identification and Resolution of Problems (71152)

.1

Daily Review

a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment deficiencies or specific human

performance issues for follow-up, the inspectors performed a daily screening of items

entered into the licensees corrective action program. This screening was accomplished

by reviewing documents entered into the licensee corrective action program and review

Enclosure

17

of document packages prepared for the licensees daily Management Alignment and

Ownership Meetings.

b.

Findings

No findings of significance were identified.

.2

Semi-Annual Trend Review

a.

Inspection Scope

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

the inspectors performed a review of the licensees corrective action program (CAP) and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors review was focused on repetitive equipment

issues, but also considered the results of daily inspector CAP item screening discussed

in section 4OA2.1 above, licensee trending efforts, and licensee human performance

results. The inspectors review considered the 6 month period of July 2004 through

December 2004. Inspectors also reviewed collective significance condition reports and

Quality Trend Summary Reports. The review also included issues documented in the

licensees system health reports and maintenance rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees latest

quarterly trend reports.

The inspectors also evaluated the reports against the requirements of NOP-LP-2001,

Condition Report Process, Revision 8 and NG-NA-00711, Quality Trending,

Revision 06, and 10 CFR Part 50, Appendix B.

b.

Assessment and Observations

During the 3rd and 4th quarters of 2004, the Davis-Besse Nuclear Power Station

remained under the IMC 0350 Process. As part of approval process which granted

restart approval to the facility, the licensee was issued a Confirmatory Order which

required, in part, that the licensee, on an annual basis, contract for independent

assessments in the areas of operations performance, organizational safety culture, the

corrective action program implementation, and the engineering program effectiveness.

Assessments in each of these areas was completed during the 3rd and 4th quarters of

2004 and each assessment, either directly or indirectly, assessed the licensees ability

to identify and resolve issues. Senior inspectors have been assigned to review each of

the completed assessments.

Although the Agencys evaluation of these Independent Assessment Reports continue,

to date no new significant adverse performance trends have been identified as a result

of these assessments. Additionally, based on the inspectors evaluation of condition

reports, trending reports, quality assessment reports, system health reports, and daily

observations of licensee performance. There were no examples identified where the

licensee failed to identify an adverse performance trend.

Enclosure

18

.3

Biennial Licensed Operator Training Program Sample Review

a.

Inspection Scope

The inspectors reviewed licensee self-assessments and eleven corrective action

documents written to document deficiencies identified in the licensed operator training

program. The licensees self-assessments included a review of the licensed operator

training program completed approximately a month prior to this inspection activity.

The self-assessments and corrective action documents were reviewed to ensure that

the full extent of the issues were identified, an appropriate evaluation was performed,

the condition report was appropriately prioritized, and that actions were planned or

in-progress to resolve the issues.

b.

Findings

No findings of significance were identified.

4OA3 Event Followup (71153)

.1

On December 23, 2004, at 0614 , the plant declared a station isolation and implemented

their emergency plan off-normal procedure RA-EP-02870, Station Isolation, due to a

winter storm quickly depositing large amounts of snow in Ottawa and surrounding

counties. The weather conditions caused Ottawa County, the plants county of

residence, to declare a category 3 snow emergency. At 1345, the licensee made an

8-hour notification to the NRC (Event 41286) under 10 CFR 50.72(b)(3)(xiii) for a loss of

emergency response capability due to the potential inability of local population to

perform an evacuation. At 1805 hours0.0209 days <br />0.501 hours <br />0.00298 weeks <br />6.868025e-4 months <br /> on December 23, 2004, after weather conditions

improved, Ottawa County downgraded the weather emergency and the plant exited the

off-normal procedure. The inspectors observed the licensees implementation of

RA-EP-02780 and sampled the licensees manning relative to commitments for

emergency planning and for normal station operations. No items of significance were

identified.

.2

(Closed) LER 05000346/1998-002-01: Plant Trip Due to High Pressurizer Level as a

Result of Loss of Letdown Capability

Licensee Event Report 05000346/1998-002-00, Plant Trip Due to High Pressurizer

Level As a Result of Loss of Letdown Capability was previously evaluated and closed

by inspectors in Inspection Report 05000346/99009(DRP). The details of the event, the

licensees actions, and corrective actions were documented in Inspection Report

05000346/98005(DRP). No violations of regulatory requirements or findings of

significance were observed.

On November 7, 2003, the licensee submitted Revision 01 to this LER. The purpose of

this revision was to update their commitments which addressed this issue. These

commitments included: determining the failure mechanism for Makeup and Purification

Demineralizer #3; flushing of the letdown flow path, as necessary; evaluating and testing

Enclosure

19

Valve MU4; and evaluating the Integrated Control System for a trip at low power to

determine if operating practices could be enhanced.

The inspectors reviewed the licensee's corrective actions and determined them to be

acceptable. This item is closed.

4OA5 Other Activities (93812)

Following restart authorization, Inspection Procedure 93812 remained in effect to

facilitate the evaluation and documentation of issues not specifically covered by existing

procedures, but important to the evaluation of the licensees performance post-restart.

This inspection procedure remains in effect as part of the integrated resident inspection

report until a time to be determined by the Davis-Besse Oversight Panel.

.1

Evaluation of the Independent Engineering Assessment Report

a.

Inspection Scope

As part of the inspection activities performed to verify the licensees compliance with the

requirements for independent assessments, as described in the March 8, 2004,

Confirmatory Order Modifying License No. NPF-3, the inspectors reviewed the

Confirmatory Order Independent Assessment Report of the Engineering Program

Effectiveness at the Davis-Besse Nuclear Power Station, dated December 6, 2004. The

inspectors reviewed the report to determine whether the report provided an overall

assessment of Engineering performance, the Teams assessment activities supported

the reports conclusions, and the licensee documented specific action plans to address

deficiencies that were documented in the report.

b.

Observations and Findings

The first annual Davis-Besse Independent Engineering Assessment required by the

Order was performed during the time period of October 11, 2004 to October 22, 2004.

The inspectors reviewed and documented their evaluation of the Independent

Assessment Plan and implementation in Inspection Report 05000346/2004015. During

the time period that the assessment team was on site, the inspectors observed many of

the assessment activities while they were in progress. On December 6, 2004, the

licensee submitted the Engineering Independent Assessment Final Report to the NRC.

This report documented the findings of that assessment.

The final report was broken down into six areas of assessment:

Modifications Process;

Calculations;

System Engineering;

Use of the Corrective Action Program by Engineering;

Management Topics; and

Self Assessment

Enclosure

20

The independent assessment team reviewed engineering products in a number of areas

and did not identify any discrepancies that were considered significant in terms of the

validity of the work product, or indicative of a systematic deficiency in engineering work

performance or management. The team identified a number of areas where changes

could be made to enhance Engineering performance. These Noteworthy Items were

captured by the licensee in the corrective action program. As a direct result of the

assessment activities, the team developed conclusions in each of the assessment areas

and identified the following three Areas for Improvement:

Slow closure of some modifications - The team identified that approximately

550 Engineering Change Requests have not yet been dispositioned and

approximately 57 modifications, some installed as early as 1998, were not

closed out;

Declining focus on and rate of progress of the Calculation Improvement Program

- Relatively few items have been addressed since restart and most items initially

due in the March - June 2004 time frame were extended through the end of the

year. Many of these items were reported as 0 percent complete; and

Slippage of the Self Assessment schedule and mixed quality of assessment

findings and corrective actions - The team found that of the 34 engineering self

assessments scheduled for 2004, 7 were completed, 10 were pending

completion, and 17 were canceled. Of the 16 self assessments that the team

reviewed, half were found to be thorough and to identify appropriate corrective

actions while the remaining half were found to be average or below average,

particularly with respect to corrective actions.

In response to these issues, the licensee developed and committed to several Action

Plans in the December 6, 2004 submittal. These commitments are scheduled for

completion during 2005 with the exception of the classification of the 550 proposed

engineering changes, which is scheduled for completion by the end of Cycle 14

(February 2006 time frame).

The assessment team also identified the following strengths during the assessment

activities:

Rapid Response Team effectiveness in supporting resolution of emergent

issues;

Internalization of Engineering Principles and Expectations; and

Engineering Assessment Board influence on the quality of engineering work

products.

c.

Conclusions

The inspectors concluded that the independent assessment teams activities were of

sufficient depth and scope. The results of these activities were adequately documented

Enclosure

21

and the Action Plans developed by the licensee to address the Areas For Improvement

were appropriate. This independent assessment of Engineering performance was found

to be in accordance with the requirements of the March 8, 2004, Confirmatory Order.

.2

Review of Operations Independent Assessment Report Revision Submittal

The inspectors documented their initial review of the Operations Independent

Assessment Report in inspection report 05000346/2004015.

In a meeting on December 7, 2004, the NRC requested the licensee to provide an

overall assessment of Operations Department performance beyond that already

submitted to the NRC on October 8, 2004. In addition to the overall performance

assessment, the NRC also requested that several of the reports documented Areas For

Improvement be clarified and placed in proper context. Based on the discussion, the

licensee committed to request the Operations Independent Assessment Team to revise

their report to provide a comprehensive assessment of their findings and to clarify the

Areas For Improvement associated with non-licensed operator/licensed operator training

programs (Commitment #A21355) and Shift Manager Responsibilities

(Commitment #A21341).

On December 22, 2004, the licensee submitted Revision 1 of the Independent

Assessment Report of Operations Performance for the Davis-Besse Nuclear Power

Station. The inspectors determined that the revision adequately documented the

requested information.

The inspectors concluded that the teams assessment activities were of sufficient depth

and scope; that the results of these activities were sufficiently documented; and that the

Action Plans developed by the licensee to address the Areas For Improvement were

adequate.

.3

Station Battery 2P/2N Terminal Corrosion

Introduction: The inspectors identified a Non-Cited Violation of 10CFR 50, Appendix B,

Criterion XVI, having very low safety significance, for the licensees failure to take timely

corrective action to remove visible corrosion on several terminal connections on the

stations safety-related 2P and 2N batteries. The primary cause of this finding was

related to the cross-cutting area of problem identification and resolution.

Description: On December 6, during a tour of the 2P and 2N station battery room the

inspectors noticed surface corrosion present on several terminal connections for each

battery, and a buildup of corrosion products on the terminal connection for at least two

cells.

Further inspection revealed that some corrosion had existed on several terminals of the

2P and 2N battery terminals since late 2003, and was documented in the licensees

corrective action program as Condition Report 03-10564. An apparent cause evaluation

associated with this condition report, which was approved on January 19, 2004,

documented, in part, the following:

Enclosure

22

The consequences of battery post seal leakage is slow degradation of battery

connections due to corrosion. This condition can be remedied by cleaning off

the corrosion and re-coating the affected area with no-oxide grease.

Preventative action is to replace the seals, or replace the battery. The condition

is monitored during quarterly battery surveillance. The resistance of corroded

connections is measured to determine if corrosion has progressed to the point of

affecting the electrical contact area between the battery post and inter-cell

connector. Operating history indicates that the battery can tolerate this condition

without degradation of electrical contact for several months. Two orders have

been initiated to remediate the condition.

Based on this evaluation, two corrective actions were initiated in January 2004. These

corrective actions were for the plant engineer to verify that work order for cleaning

connections of Battery 2P [2N] is scheduled and completed. These corrective actions

were subsequently deferred in July 2004. The reason for these deferrals was

documented as follows:

Battery surveillance to date indicates that the battery connection resistance

readings are not affected by the visible corrosion. Cleaning corrosion from the

battery connections involves some degree of risk associated with cleaning

energized components. The risk of battery connector cleaning must be weighed

against the risk of doing nothing until batteries 2N and 2P are replaced during

the mid-cycle outage. Based on visual inspection performed on 7/12/04 the risk

associated with cleaning battery connections outweighs the risk of extending the

maintenance.

Again in November 2004, subsequent to the performance of the DB-ME-03001, Station

Battery Quarterly Surveillance, Revision 8, for the 2P and 2N station batteries, condition

reports were written which documented corrosion present on terminal connections of

approximately 62 cells. Again, no action was taken to remove the corrosion and re-coat

the terminal connections with no-oxide grease material.

On December 7, 2004, the inspectors had several discussions regarding the issue of

battery terminal connection corrosion with senior operations department individuals.

During these discussions, the inspectors learned that the Davis-Besse electrical

maintenance procedures used to periodically inspect and test the station batteries did

not contain instructions that allowed the electricians to address minor corrosion issues

as part of those maintenance activities. Additionally, the inspectors were informed that

since none of the affected battery cells had exhibited terminal connection resistance

values in excess of 150 micro ohms, the licensee was willing to accept the terminal

corrosion until the 2P/2N batteries were replaced in January 2005.

On December 8, 2004, the inspectors discussed this issue with the Plant Manager.

Shortly after that discussion, actions were taken to clean the terminal connections on

the 2P and 2N station battery, and DB-ME-03001 was revised to include instructions to

clean corrosion on battery terminal connections when identified.

Enclosure

23

Analysis: The inspectors determined that not taking prompt action to correct a known

deficiency on the safety-related station batteries was a performance deficiency because

the issue was reasonably within the licensees ability to foresee and correct and could

have been prevented. The inspectors determined that the finding was more than minor

because it impacted the Mitigating Systems cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. This violation was determined not to constitute an

immediate safety issue and was determined to be of very low safety significance

because there were no documented cases of any of the affected battery cells terminal

resistance measurements in excess of 150 micro-ohms.

Enforcement: 10CFR 50, Appendix B, Criterion XVI, states, in part, that measures shall

be established to assure that conditions adverse to quality such as deficiencies,

deviations, and defective material and equipment are properly identified and corrected.

Contrary to this, varying degrees of corrosion existed for an extended period of time on

the terminal connections for several of the cells that comprise the 2P and 2N

safety-related station batteries. Because this finding was determined to have very low

safety significance, and because this issue was entered into the licensees corrective

action program, this violation is being treated as a Non-Cited Violation consistent with

Section VI.A of the NRC Enforcement Policy (NCV 05000346/2004016-01). The

licensee entered this issue into their corrective action program as CR 04-07545.

.4

Frazil Ice Issues

During the early morning hours of December 21, 2004, the licensee observed

decreasing service water intake forebay levels which were not consistent with level

changes in Lake Erie. The intake forebay is a reservoir that is connected to Lake Erie

by a 96 inch pipe, through which makeup water flows when there is a difference

between intake and Lake levels. Diverging levels in clear winter weather is indicative of

frazil ice blockage of the intake crib at the Lake Erie side of the makeup pipe. The

licensee entered Section 4.2, Actions During Frazil Ice Conditions, of procedure

DB-OP-06913, Seasonal Plant Preparation Checklist, and took actions to minimize

water losses from the intake forebay. Upon completion of these actions, the forebay

water level, which was at approximately the 567 feet level, was observed to be

decreasing at approximately 4 inches per hour.

At an elevation of 562 feet, the licensee has sufficient water in the forebay to meet their

design requirements for an ultimate heat sink. If the actual water level decreases to

below 562 feet, the licensees technical specifications require shutdown to hot standby

within 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. At 564 feet, the licensees procedures require them to place in service

a temporary pump that is sized to pump approximately 9000 gpm from Lake Erie, over

the dike for the intake canal, and into the forebay via the intake canal. The lowest level

reached in the intake forebay was approximately 564.8 feet before warming weather

conditions restored normal makeup flow from the lake. Although the level did not

decrease below 564 feet, the licensee conservatively decided to demonstrate the

capability to install and operate the temporary pump.

Enclosure

24

The inspectors monitored the licensees decision making process, compliance with

existing procedures, and the installation and testing of the temporary pump. The

inspectors noted that the licensee had also experienced apparent frazil ice blockage on

the mornings of December 24 and December 25 but that the levels did not decrease

below 565 feet level in the intake forebay.

No items of significance were identified.

.5

Containment Entry for Lubricating Oil Addition

On December 27, 2004, the licensee made a containment entry to add approximately 3

gallons of oil to the reservoir for RCP 1-2 motor lower bearing. The reactor power was

maintained at approximately 100 percent. Oil addition was through a remote addition

line that was located in an accessible area. Licensee personnel initially added

approximately 2 quarts of oil to verify integrity of the oil addition line. The initial fill was

sufficient to clear the low level alarm and also verified that oil was traveling to the oil

reservoir. The inspectors observed the ALARA brief and observed the licensees

activities while in containment.

No items of significance were identified.

.6

Licensee Preparations for a Potential Work Stoppage (92709)

The majority of licensees plant physical workers, including reactor operators, are

represented by Local 245 of the International Brotherhood of Electrical Workers (IBEW).

The inspectors continued to monitor the on-going contract negotiations between the

licensee and the Local 245. Although both union and licensee management

representatives have indicated a willingness to continue negotiations beyond the

expiration date, the licensee has made preparations to ensure compliance with

regulatory requirements in the event of a work stoppage. The inspectors, using

guidance in Inspection Procedure 92709, Licensee Strike Contingency Plans, have

reviewed the licensees plans for ensuring a sufficient number of qualified personnel are

available to maintain the plant in a safe condition, should a work slowdown or stoppage

occur.

No items of significance were identified.

4OA6 Meetings

.1

Exit Meeting

The inspectors presented the inspection results to Mr. B. Allen, and other members of

licensee management on January 6, 2005. The licensee acknowledged the findings

presented. No proprietary information was identified.

.2

Interim Exit Meetings

An interim exit meeting was conducted for:

Enclosure

25

Biennial Licensed Operator Requalification Program Inspection with Mr. Allen on

November 19, 2004;

Overall assessments of the annual operating test and the biennial written

examination results via telephone with Mr. Stallard on December 13, 2004; and

Access control to radiologically significant areas, ALARA planning and controls

program and radiological waste and transportation with Mr. R. Schrauder on

December 10, 2004.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

B. Allen, Director, Plant Operation

M. Bezilla, Site Vice President

B. Boles, Manager, Plant Engineering

D. Bondy, Staff Instructor

P. Faris, Senior Nuclear Assessor, Davis-Besse Oversight

J. Grabnar, Manager, Design Engineering

L. Harder, Manager, Radiation Protection

R. Hovland, Manager, Technical Services

R. Hruby, Manager, Nuclear Oversight

D. Kline, Manager, Security

D. Lange, Staff Instructor

S. Loehlein, Director, Station Engineering

L. Myers, Chief Operating Officer, FENOC

D. Noble, Radiation Protection Supervisor

K. Ostrowski, Manager, Plant Operations

C. Price, Manager, Regulatory Compliance

M. Roder, Transaction Manager, Training

J. Reuter, Radwaste Shipper

R. Schrauder, Director, Performance Improvement

A. Stallard, Supervisor, Operations Training

C. Steenbergen, Shift Manager

M. Stevens, Manager, Maintenance

M. Trump, Training Manager

D. Wahlers, Supervisor, Nuclear Oversight

D. Wuokko, Compliance Supervisor, Performance Improvement

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000346/2004016-01

NCV

Untimely Corrective Actions to Correct Safety-Related

Battery Terminal Connection Corrosion

Closed

05000346/1998-002-01

LER

Plant Trip due to High Pressurizer Level as a result of Loss

of Let Down Capability

Attachment

2

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather that

selected portions of the documents were evaluated as part of the overall inspection effort.

Inclusion of a document on this list does not imply NRC acceptance of the document or any part

of it, unless stated in the body of the inspection report.

1R05

Fire Protection

Davis-Besse Nuclear Power Station Fire Hazard Analysis Report

Drawing A-0221F; Fire Protection General Floor Plans El 545' & 555'; Revision 07

Drawing A-2132, Sheet 6; Barrier ID- Room 113; Revision 00

1R11

Licensed Operator Requalification Program

NG-NT-00601; Control of the Plant-Referenced Simulator; Revision 3; dated

November 12, 2004

NT-OT-07001; Licensed Operator Requalification Program; Revision 7

NOP-TR-1001; FENOC Conduct of Training; Revision 0

NOBP-TR-1104; FENOC Design and Development of Training Materials; Page 3;

Revision 0

DBBP-TRAN-0021; Simulator Configuration Control; Revision 0; dated

November 12, 2004

DBBP-TRAN-0502; Development and Conduct of Continuing Training Simulator

Evaluations; Revision 0

Comprehensive Biennial Written Examination; SRO #1, 2004; RO, 2004; RO #3, 2004

Simulator Scenario: ORQ-EPE-S113; Revision 7

Simulator Scenario; ORQ-EPE-S105; Revision 9

Job Performance Measure; OPS-JPM-015; Revision 0

Job Performance Measure; OPS-JPM-052; Revision 0

Job Performance Measure; OPS-JPM-053; Revision 1

Job Performance Measure; OPS-JPM-076; Revision 1

Job Performance Measure; OPS-JPM-100; Revision 1

Job Performance Measure; OPS-JPM-101; Revision 1

Shift Manager/Unit/Field Supervisor/Shift Engineer Turnover Checklist; dated

November 16, 2004

Davis-Besse Nuclear Power Station Licensed Operator Requalification Training

Program Training Plan; Revision 8; dated January 30, 2004

Pre-job Briefing Package; Cycle 04-04 Management Introduction; dated

November 15, 2004

Post-Training Assessment Report; Training Appraisal Questionnaire for Just-in-Time

Training for Startup/Criticality and Generator Synchronization; dated October 19, 2004

Sample of Crew and Individual Simulator Performance Evaluation Forms for Year 2003

Sample of Week 1 (November 1, 2004) NRC Requalification Examination Simulator

Results

Attachment

3

Sample of Remediation Packages; NOP-TR-1001-01; Remedial/Make-Up

Recommendations; Dated various

Requalification Training Attendance; Trainee Tracking - EDGs-OPS-IER-1042

Requalification Training Attendance; Trainee Tracking - RPS-OPS-SYS-1504

Requalification Training Attendance; Trainee Tracking - T.S. 2.0/3.0/4.0

Requalification Training Attendance; Trainee Tracking - OPS-GOP-1420

Requalification Training Attendance; Trainee Tracking - OPS-GOP-1430

Licensed Operator Long Term Continuing Training Schedule; Revision 3; dated

November 15, 2004

TNS-04-00322; Intra-Company Memorandum; Third Quarter 2004 Proficiency Status;

Revision 0; dated October 7, 2004

Listing of Closed Simulator Work Orders (SWO) Between January 01, 2002 through

November 16, 2004

SWO 02-0029; Open; Update NAS on Daisy for Cycle 12 Data; Issue Date

March 27, 2002

SWO 02-0116; Open; Containment RAD Reached 3600 R/hr as Read on RI 4596A/B;

Issue Date April 28, 2003

SWO 03-0071; Open; Alarms 5-1-C and 5-1-D SFAS Trip Alarms Come in When

Blocked; Issue Date October 17, 2003

SWO 04-0076; Open; Start Program on SPDS is Still Using Cycle 13 Data Need to

Update to Cycle 14; Issue Date June 22, 2004

SWO 04-0103; Open; Turbine MS Point Out of Tolerance on PPC; Issue Date

June 30, 2004

SWO 02-0012; Open; Setpoint Change or Variable P/T Trip-RPS; Issue Date

February 18, 2002

SWO 02-0084; Open; Replacement of Victoreen RAD Monitors; Issue Date

October 1, 2002

SWO 03-0002; Open; Maximum Allowed Boron on Simulator is 2500 ppm

[meter indication]; Issue Date June 3, 2003

Simulator Certification Test; TAB01; Manual Reactor Trip; dated October 6, 2004

Simulator Certification Test; TAB02; Simultaneous Trip of All Main Feedwater Pumps;

dated October 6, 2004

Simulator Certification Test; TAB05; Simultaneous Trip of All Reactor Coolant Pumps;

dated October 13, 2004

Simulator Certification Test; TAB07; Maximum Rate Power Ramp 100 percent,

75 percent, 100 percent; dated October 19, 2004

Simulator Certification Test; TAB09; Main Steam Line Failure in the Reactor Building;

dated October 19, 2004

Simulator Certification Test; N03; Zero Power Physics Testing (Core Physics Testing);

dated March 08, 2002

Simulator Certification Test; T10; Total Loss of Feedwater; dated June 21, 2000

Simulator Certification Test; T16; Generator/Turbine Trip; dated February 16, 2003

Simulator Certification Test; T03B; Loss of All AC Power and Loss of Both Diesels;

dated December 22, 2001

Condition Report (CR) 04-05449; Simulator Configuration Control Improvement

Opportunities; dated September 2, 2004

CR 04-00181; Missed Technical Specification Action Statement; dated January 6, 2004

Attachment

4

CR 04-01230; Missed Technical Specification Entry; dated February 12, 2004

CR 04-04406; Missed Surveillance Requirement 4.3.1.1.1 for RCS Flow Channel

Check; dated July 6, 2004

CR 02-09434; NRC Inspection 71111.11 Licensed Operator Requal Inspection

Comments; dated November 15, 2002

Operations Events Involving Technical Specifications Identified in Condition

Report 04-04425; dated August 23, 2004

Self-Assessment Report 2004-0105; Simulator Configuration Control; dated

September 2, 2004

Self-Assessment Report CR/CA 04-02029-06; Licensed Operator Requalification

Program; dated November 4, 2004

1R12

Maintenance Effectiveness

DB-PF-0003; Maintenance Rule; Revision 06

NUREG-1482; Guidelines for Inservice Testing At Nuclear Power Plants; Revision 01

Pump and Valve Basis Document; Volume II - Pump Basis; Revision 00

MRPM 15; Maintenance Rule Program Manual; Revision 15

Davis-Besse Plant Health Report; 3rd Quarter 2004

CR 04-04656; INPO 2004 Evaluation - AFI CM.1-1 (Operating and Design Margins)

1R15

Operability Evaluations

DB-MM-05001; Bench Testing Snubbers; Revision 04

DB-PF-00107; Hydraulic Snubber Program; Revision 0

CR 04-07274; Snubber Test Inaccuracies not Accounted for in Recorded Results

1R16

Operator Workarounds

DB-OP-06013; Containment Spray System; Revision 12

Shift Manager/Unit/Field Supervisor/Shift Engineer Turnover Checklist

1R22

Surveillance Testing

DB-SS-03091; Motor Driven Feed Pump Quarterly Test; Revision 06

CR 04-07062; Instrumentation Snubber Problem

Dwg OS-012A, Sheet 1; Main Feedwater System; Revision 22

2OS2 ALARA Planning And Controls

CR04-02353; ALARA Brief Not Performed per DB-HP-01154; dated March 30, 2004

RWP 2004-2001; Containment Entry; Revision 3

ALARA Plan; RWP 2004-2001 Containment Entry

2PS2

Radioactive Material Processing and Transportation

CR04-04156; Safety Concern - Resin Transfer And Changing Rad Conditions; dated

June 23, 2004

Attachment

5

CR04-05833; Contamination Found On Vendor RAM Shipment to DB; dated

September 23, 2004

CR04-06946; Provide Instructions for Transportation of Radioactive Samples Less Than

0.002 Micro-curies Per Gram; dated November 11, 2004

CR04-06943; Establish Maximum Dose Rate for Radioactive Material Area Boundary;

dated November 11, 2004

CR04-07458; Missed HIC Dewatering Verification; dated December 6, 2004

CR04-08560; Issues with 10 CFR Part 61 Sampling and Analysis Program; dated

October 7, 2003

NQA Field Observation; Process Control Program; dated October 27, 2003

NQA Field Observation; 10 CFR Part 61 Radwaste Classification; dated October 15,

2003

NQA Field Observation; Transfer of Spent Purification Filters; dated July 9, 2004

DB-HP-01502; Dewatering of Filter Media; Revision 5

DB-HP-03002; Dewatering Verification; Revision 2

NOP-OP-2; Shipment of Radioactive Material/Waste; Revision 4

DB-PCP; Process Control Program; Revision 6

DB-HP-06120; Miscellaneous Liquid Waste Demineralizer Operations; Revision 5

DB-HP-01712; 10 CFR Part 61 Sampling For Waste Classification; Revision 00

Qualification Matrix; Receiving Shipping Rad Material; dated December 7, 2004

BWXT Analysis Report; 10 CFR Part 61 Isotopic Data; dated April 30, 2004

Lesson Plan; Packaging, Transport And Disposal Of Radioactive Waste; Revision 1

Qualification Matrix DOT Training; dated December 8, 2004

Shipping Papers; 04-1001 Dewatered Resin, Type B Shipment; dated May 18, 2004

Shipping Papers; TR04-0002 Primary Resin Type B Shipment; dated April 2, 2004

Shipping Papers; Radwaste LSA TR03-0018; dated August 5, 2003

Shipping Papers; Radwaste LSA Filters TR03-022; dated September 23, 2003

Shipping Papers; Radwaste LSA TR03-0019; dated August 7, 2003

4OA1 Performance Indicator Verification

Unit Logs; October 1, 2003 through September 30, 2004

4OA2 Problem Identification and Resolution

CR 04-07142; Simulator Data Improvement Opportunity Noted During NRC Inspection;

dated November 18, 2004

CR 04-07143; Criteria Used to Evaluate Crew Performance Could Be More Objective;

dated November 18, 2004

CR-04-07144; NRC Licensed Operator Requalification Training Program Inspection

[Areas Needing Improvements/Enhancements]; dated November 16, 2004

CR 04-07545; NRC Resident Questions For Batteries 2P and 2N

4OA3 Event Followup

RA-EP-02870; Station Isolation; Revision 02

Attachment

6

4OA5 Other Activities

IP 92709; Licensee Strike Contingency Plans; August 12, 1992

DB-OP-06913; Seasonal Plant Preparation Checklist; Revision 10

4OA5 Other Activities (93812)

CR 04-07545; NRC Resident Questions For Batteries 2P and 2N

CR 03-10564; Corrosion on Battery 2P and 2N Battery Terminals

CR 04-03711; Station Battery 2P Corrosion

CR 04-03692; Station Battery 2N Corrosion

CR 04-07277; Corrosion Found on Cell Connections for 2N Station Batteries

CR 04-07270; Corrosion Found on Cell Connections for 2P Station Batteries

DB-ME-03001; Station Batteries Quarterly Surveillance; Revisions 8 and 9

Attachment

7

LIST OF ACRONYMS USED

ADAMS

Agency-wide Document Access and Management System

ALARA

As Low As Is Reasonably Achievable

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CR

Condition Report

FENOC

FirstEnergy Nuclear Operating Company

ICS

Integrated Control System

IMC

Inspection Manual Chapter

IR

Inspection Report

JPM

Job Performance Measure

JFG

Job Familiarization Guidelines

LER

Licensee Event Report

LHRA

Locked High Radiation Area

LORT

Licensed Operator Requalification Training

NCV

Non-Cited Violation

NRC

United States Nuclear Regulatory Commission

PARS

Publicly Available Records

PI

Performance Indicator

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RP

Radiation Protection

RWP

Radiation Work Permit

SDP

Significance Determination Process

SWO

Simulator Work Order

TS

Technical Specifications

USAR

Updated Safety Analysis Report

WO

Work Order