ML040160461

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IR 05000325-03-006 and 05000324-03-006, on 09/21/03 - 12/20/03, Brunswick Steam Electric Plant
ML040160461
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 01/16/2004
From: Fredrickson P
NRC/RGN-II/DRP/RPB4
To: Gannon C
Carolina Power & Light Co
References
IR-03-006
Download: ML040160461 (38)


See also: IR 05000324/2003006

Text

January, 16, 2004

Carolina Power and Light Company

ATTN: Mr. C. J. Gannon

Vice President

Brunswick Steam Electric Plant

P. O. Box 10429

Southport, NC 28461-0429

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION

REPORT NOS. 05000325/2003006 AND 05000324/2003006

Dear Mr. Gannon:

On December 20, 2003, the Nuclear Regulatory Commission (NRC) completed an inspection at

your Brunswick Units 1 and 2 facilities. The enclosed integrated inspection report documents

the inspection findings, which were discussed on December 18, 2003, with you and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one finding concerning an inadequate design review of a Unit 2 reactor

feed pump speed control system modification. This finding has potential safety significance

greater than very low significance. This finding did present an immediate safety concern.

However, compensatory measures are in place while long-term corrective measures are being

implemented. In addition, the report documents one self-revealing finding of very low safety

significance (Green). This finding was determined to involve a violation of NRC requirements.

However, because of the very low safety significance and because it is entered into your

corrective action program, the NRC is treating this finding as a non-cited violation (NCV)

consistent with Section VI.A of the NRC Enforcement Policy. Additionally, a licensee-identified

violation which was determined to be of very low safety significance is listed in this report. If

you contest any non-cited violation in this report, you should provide a response within 30 days

of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the

Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Brunswick Steam Electric Plant.

CP&L

2

In accordance with 10CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Paul E. Fredrickson, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos.: 50-325, 50-324

License Nos: DPR-71, DPR-62

Enclosure:

Inspection Report 05000325, 324/2003006

w/Attachment: Supplemental Information

cc w/encl:

(See page 3)

CP&L

3

cc w/encl:

W. C. Noll, Director

Site Operations

Brunswick Steam Electric Plant

Carolina Power & Light

Electronic Mail Distribution

David H. Hinds

Plant Manager

Brunswick Steam Electric Plant

Carolina Power & Light Company

Electronic Mail Distribution

James W. Holt, Manager

Performance Evaluation and

Regulatory Affairs PEB 7

Carolina Power & Light Company

Electronic Mail Distribution

Edward T. ONeil, Manager

Support Services

Carolina Power & Light Company

Brunswick Steam Electric Plant

Electronic Mail Distribution

Lenny Beller, Supervisor

Licensing/Regulatory Programs

Carolina Power and Light Company

Electronic Mail Distribution

William D. Johnson

Vice President & Corporate Secretary

Carolina Power and Light Company

Electronic Mail Distribution

John H. ONeill, Jr.

Shaw, Pittman, Potts & Trowbridge

2300 N. Street, NW

Washington, DC 20037-1128

Beverly Hall, Acting Director

Division of Radiation Protection

N. C. Department of Environment

and Natural Resources

Electronic Mail Distribution

Peggy Force

Assistant Attorney General

State of North Carolina

Electronic Mail Distribution

Chairman of the North Carolina

Utilities Commission

c/o Sam Watson, Staff Attorney

Electronic Mail Distribution

Robert P. Gruber

Executive Director

Public Staff NCUC

4326 Mail Service Center

Raleigh, NC 27699-4326

Public Service Commission

State of South Carolina

P. O. Box 11649

Columbia, SC 29211

Donald E. Warren

Brunswick County Board of

Commissioners

P. O. Box 249

Bolivia, NC 28422

Warren Lee

Emergency Management Director

New Hanover County Department of

Emergency Management

P. O. Box 1525

Wilmington, NC 28402-1525

Distribution w/encl: (See page 4)

CP&L

4

Distribution w/encl:

B. Mozafari, NRR

L. Slack, RII EICS

RIDSRIDSNRRDIPMLIPB

PUBLIC

OFFICE

DRP/RII

DRP/RII

DRP/RII

DRS/RII

DRS/RII

DRS/RII

DRS/RII

SIGNATURE

GTM

EMD

JDA

MAS1

JLK1

KFO

EXL2

NAME

GMacdonald:as

EDiPaolo

JAustin

MScott

JKreh

KODonohue

ELea

DATE

01/15/04

01/16/04

01/16/04

01/15/04

01/15/04

01/15/04

01/15/04

E-MAIL COPY?

YES

NO YES

NO YES

NO YES

NO YES

NO YES

NO YES

NO

PUBLIC DOCUMENT

YES

NO

OFFICIAL RECORD COPY DOCUMENT NAME: C:\\ORPCheckout\\FileNET\\ML040160461.wpd

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-325, 50-324

License Nos:

DPR-71, DPR-62

Report Nos:

05000325/2003006 and 05000324/2003006

Licensee:

Carolina Power and Light (CP&L)

Facility:

Brunswick Steam Electric Plant, Units 1 & 2

Location:

8470 River Road SE

Southport, NC 28461

Dates:

September 21, 2003 - December 20, 2003

Inspectors:

E. DiPaolo, Senior Resident Inspector

J. Austin, Resident Inspector

G. MacDonald, Senior Project Engineer (Section 1R06)

M. Scott, Senior Reactor Inspector (Section 1R12)

J. Kreh, Emergency Preparedness Inspector (Section 1EP 2-5)

K. ODonohue, Senior Reactor Inspector (Section 1R11)

E. Lea, Senior Operations Engineer (Section 1R11)

Approved by:

Paul Fredrickson, Chief,

Reactor Projects Branch 4

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000325/2003-006, 05000324/2003-006; 09/21/2003-12/20/2003; Brunswick Steam

Electric Plant, Units 1 and 2; Maintenance Effectiveness, Permanent Plant Modifications.

The report covered a three-month period of inspection by resident inspectors, a senior project

engineer, a senior operations engineer, senior reactor inspectors, and a regional emergency

preparedness inspector. One Green non-cited violation (NCV) was identified. The significance

of most findings is indicated by its color (Green, White, Yellow, Red) using Inspection Manual

Chapter (IMC) 609, Significance Determination Process (SDP). Findings for which the SDP

does not apply may be Green or be assigned a severity level after NRC management review.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. A self-revealing non-cited violation was identified for the licensees

failure to position the Unit 2 high pressure coolant injection (HPCI) system

turbine exhaust stop check valve in the open position following system

maintenance, in accordance with plant procedures. This resulted in failure of

the exhaust line rupture discs during testing, a primary containment isolation

of the system, and activation of the HPCI room fire protection system.

This finding is greater than minor because it is associated with system

configuration control and affected the mitigating availability of the HPCI system.

This finding was determined to be of very low safety significance (Green)

because the HPCI system was returned to an operable status within the

Technical Specification allowed outage time. The finding was related to the

cross-cutting aspect of Human Performance because the cause was determined

to be due to plant operators using improper techniques in verifying the valves

position. Other contributing causes including operator knowledge deficiencies of

valve operation, failure to perform an independent check of valve position, and

the pre-job briefs limited scope were also related to Human Performance.

(Section 1R12)

Cornerstone: Initiating Events and Mitigating Systems

To Be Determined (TBD). A self-revealing finding was identified for an

inadequate design review of a Unit 2 reactor feed pump speed control

modification. The modification replaced the existing mechanical-hydraulic speed

control system with a digital speed control system. The system is powered by

internal power supplies that would fault, and thus cease to supply output power,

with one cycle of sensed abnormal supply voltage. As a result, the reactor feed

pumps would trip following a unit trip due to the supply voltage transient caused

by the swap of in-house loads from the unit auxiliary transformer to the startup

auxiliary transformer.

2

Enclosure

The finding is unresolved pending completion of a significance determination.

This issue is greater than minor because, if left uncorrected, it would increase

the likelihood of initiating events caused by a loss of reactor feed pumps

following transients and affect the reliability and functional capability of the

reactor feed pumps to mitigate events (unit trips). The finding was determined to

have potential safety significance greater than very low because of the increased

likelihood of initiating events, resultant reduced functional capability of the

reactor feed pumps to mitigate events as a result, and the length of time the

condition existed. (Section 1R17)

B.

Licensee Identified Violations

A violation of very low safety significance, was identified by the licensee and has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

action are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 began the report period operating at full power. On September 27, 2003, power was

reduced to approximately 50 percent to perform planned maintenance on the reactor feed

pumps and testing on the control rods and main steam isolation valves. The unit returned to

maximum power on September 29. On November 14, power was reduced to approximately 50

percent for planned maintenance, control rod scram solenoid pilot valve maintenance, and

surveillance testing. The unit returned to maximum power on November 16. Power was

reduced to approximately 50 percent on November 21 to troubleshoot speed control problems

on the A reactor feed pump. Full power was achieved on November 23 where it remained for

the duration of the inspection period.

Unit 2 began the report period operating at full power. On September 23, 2003, power was

reduced to approximately 50 percent to facilitate repairs to a main condenser tube leak. The

unit returned to full power on September 25. On November 4, Unit 2 tripped due to a loss of

main generator field. The loss of field was caused by the failure of the main generator

alternator brush/collector ring (see Section 4OA3 for additional details). Following repairs to the

main generator exciter, a unit startup was commenced on November 7, and maximum power

was achieved on November 9. On December 5, the unit reduced power to approximately 50

percent to facilitate a modification to the reactor feed pumps to supply the governors with an

uninterruptible power source (see Section 1R17 for details). The unit returned to maximum

power on December 8 where it remained for the duration of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01

Adverse Weather Protection

a. Inspection Scope

The inspectors assessed the effectiveness of the licensees cold weather protection

program as it related to ensuring that the facilitys diesel-driven fire pump, emergency

diesel generators, and condensate storage tank low level switches would remain

functional and available in cold weather conditions. In addition to reviewing the

licensees program-related documents and procedures, walkdowns were conducted of

the freeze protection equipment (e.g., heat tracing, area space heaters, etc.) associated

with the above systems/components. Licensee problem identification and resolution

was also assessed. This included review of Action Request (AR) 110949 which

documented that freeze protection preventive maintenance was not completed as

scheduled for Unit 2. Documents reviewed during the course of this inspection are

listed in the Attachment.

b. Findings

No findings of significance were identified.

2

Enclosure

1R04

Equipment Alignment

a. Inspection Scope

Partial System Walkdowns

The inspectors performed three partial walkdowns of the below listed systems to verify

that the systems were correctly aligned while the redundant train or system was

inoperable or out-of-service (OOS) or, for single train risk significant systems, while the

system was available in a standby condition. The inspectors assessed conditions such

as equipment alignment (i.e., valve positions, damper positions, and breaker alignment)

and system operational readiness (i.e., control power and permissive status) that could

affect operability. The inspectors reviewed the resolution of licensee identified

equipment alignment problems that could cause initiating events or impact mitigating

system availability. The inspectors reviewed available structures, systems or

components (SSCs) to verify that they met the requirements of the licensees

configuration control program. The inspectors reviewed documents listed in the

Attachment.

Unit 1 conventional and B train nuclear service water pumps when A train

nuclear service water pump was OOS for planned maintenance on October 1,

2003.

Unit 2 HPCI system when reactor core isolation cooling (RCIC) system was OOS

for planned maintenance on October 23, 2003.

Unit 2 RCIC system when HPCI system was inoperable due to ruptured exhaust

diaphragms on November 13-14, 2003.

Complete System Walkdown

The inspectors conducted a detailed review of the alignment and condition of the

emergency diesel generators (EDGs). The inspector reviewed the Updated Final Safety

Analysis Report, associated attachments of Diesel Generator Operating Procedure

0OP-39, and the system flow diagram (drawing numbers D-02265 through D-02274).

The inspectors reviewed pending design and equipment issues to verify that the

identified deficiencies did not significantly impact the systems functions. Items included

in this review were: 1) the operator workaround list; 2) the temporary modification list; 3)

outstanding maintenance work requests/work orders (WOs); and 4) operator turnover

sheets. The following related ARs were reviewed to assure that the licensee had

properly characterized and prioritized equipment problems in the corrective action

program:

AR 49367

EDG 2 Inoperable due to high cylinder exhaust temperature

AR 55517

EDG 4 light socket short

AR 86529

Unexpected diesel generator start during SCRAM on January 1,

2003

AR 102323102323480V maintenance rule functional failure - feeder breaker to motor

control center DGC (2-E7-AY8-52) failed to trip

3

Enclosure

b. Findings

No findings of significance were identified.

1R05

Fire Protection

a. Inspection Scope

The inspectors reviewed current ARs and WOs associated with the fire suppression

system to confirm that their disposition was in accordance with OAP-033, Fire Protection

Program Manual. The inspectors reviewed the status of ongoing surveillance activities

to verify that they were current to support the operability of the fire protection system. In

addition, the inspectors observed the fire suppression and detection equipment to

determine whether any conditions or deficiencies existed which would impair the

operability of that equipment. The inspectors toured the following areas important to

reactor safety and reviewed documents listed in the Attachment to verify that the

requirements for fire protection design features, fire area boundaries, and combustible

loading were met:

Units 1 and 2 north and south emergency core cooling pipe tunnels (4 areas)

EDG fuel cells, -1 foot 6 inch elevation (1 area)

EDG basement, 2 foot elevation (1 area)

b. Findings

No findings of significance were identified.

1R06

Flood Protection Measures

a. Inspection Scope

Internal Flooding

The inspectors reviewed the licensees internal flooding analysis as described in

Updated Final Safety Analysis Report (UFSAR) Section 3.4.2, Protection From Internal

Flooding. Due to the risk significance of equipment in the diesel generator building and

the reactor buildings, the inspectors reviewed UFSAR Section 3.4.2 analysis of the

effects of postulated piping failures for these two areas to determine if the analysis

assumptions and conclusions were based on the current plant configuration. The

internal flooding design features and equipment for coping with internal flooding was

inspected. The walkdown included sources of flooding and drainage, sump pumps,

level switches, watertight doors, curbs , pedestals and equipment mounting. The

inspectors reviewed the testing of the level alarms and reviewed the procedures for

coping with internal flooding. Documents reviewed are listed in the Attachment.

4

Enclosure

External Flooding

The inspectors reviewed the licensees external flooding analysis as described in

UFSAR Section 3.4.1, Protection from External Flooding, to determine the external flood

control design features. Walkdowns were conducted to inspect the external flood

protection barriers including watertight doors, curbs, sealing of external building

penetrations below floodline, and the sump pumps and level alarm circuits. Procedures

for coping with external flooding were reviewed and the inspectors walked down the

portable flood protection equipment listed in Procedure 0AI-68, Brunswick Nuclear Plant

Response to Severe Weather Warnings. Documents reviewed are listed in the

Attachment.

b. Findings

No findings of significance were identified.

1R07

Heat Sink Performance

a. Inspection Scope

The inspectors reviewed activities associated with the cleaning of the EDG 4

turbocharger intercooler heat exchange per WO 453062. The inspectors reviewed the

results of the EDG 4 intercooler inspection conducted in accordance with preventive

maintenance procedures. The inspection results were analyzed to determine if

inspection frequencies were adequate to detect degradation prior to loss of heat

removal capability below design-basis values. The inspectors reviewed the documents

listed in the Attachment.

b. Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification

a. Inspection Scope

Quarterly Review

On November 4, 2003, the inspectors observed licensed operator performance and

reviewed the associated training documents during two simulator examinations. The

simulator observations and reviews included evaluations of emergency operating

procedure and abnormal operating procedure utilization. The inspectors reviewed

LORX-001 and LORX-035 which documented the associated simulator examination

scenarios. The simulator examination evaluated operator response to plant transients

initiated by plant equipment problems, reactivity manipulations, a small break loss of

coolant accident with failures of emergency core cooling systems, and an unisolable

steam leak outside containment. The inspectors reviewed operator activities to verify

5

Enclosure

consistent clarity and formality of communication, conservative decision-making by the

crew, appropriate use of procedures, and proper alarm response. Group dynamics and

supervisory oversight, including the ability to properly identify and implement appropriate

Technical Specification (TS) actions, regulatory reports, and notifications, were

observed. The inspectors assessed whether appropriate feedback was planned to be

provided to the licensed operators. The inspectors reviewed documents listed in the

Attachment.

Periodic Evaluation (Biennial)

The inspectors reviewed documentation, interviewed licensee personnel, and observed

the administration of simulator operating tests associated with the licensees operator

requalification program. Job performance measures (JPMs) associated with the

licensees operator requalification program, which the licensee administered at the

beginning of the year, were reviewed by the inspectors. Each of the activities performed

by the inspectors was done to assess the effectiveness of the licensee in implementing

requalification requirements identified in 10 CFR 55, Operators Licenses. Evaluations

were also performed to determine if the licensee effectively implemented operator

requalification guidelines established in NUREG-1021, Operator Licensing Examination

Standards for Power Reactors. The inspectors also reviewed and evaluated the

adequacy of the licensees simulation facility for use in operator licensing examinations.

The inspectors observed three crews during the performance of the operating tests.

Documentation reviewed included written examinations, JPMs, simulator scenarios,

licensee procedures, on-shift records, licensed operator qualification records,

watchstanding and medical records, simulator modification request records and

performance test records, the feedback process, and remediation plans. Documents

reviewed during the inspection are listed in the Attachment.

Following the completion of the annual operating examination testing cycle which ended

on December 9, 2003, the inspectors reviewed the overall pass/fail results of the

individual JPM operating tests, and the simulator operating tests administered by the

licensee during the operator licensing requalification cycle. These results were

compared to the thresholds established in NRC Inspection Manual Chapter 0609

Appendix IProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix I" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Operator Requalification Human Performance Significance Determination

Process.

b. Findings

No findings of significance were identified.

6

Enclosure

1R12

Maintenance Effectiveness

a. Inspection Scope

Periodic Evaluation (Biennial)

The inspectors reviewed the licensees Maintenance Rule periodic assessment, "BNP

Maintenance Rule Program Periodic Self-Assessment Plan," for June 1, 2001 to May

31, 2003, dates of assessment July 21-24, 2003, while on-site the week of September

14, 2003. The report was issued to satisfy paragraph (a)(3) of 10 CFR 50.65, and

covered the period as indicated for two units. The inspection was to determine the

effectiveness of the assessment and that it was issued in accordance with the time

requirement of the Maintenance Rule (MR) and included evaluation of: balancing

reliability and unavailability, (a)(1) activities, (a)(2) activities, and use of industry

operating experience. To verify compliance with 10 CFR 50.65, the inspectors reviewed

selected MR activities covered by the assessment period for the following MR systems:

containment isolation valves, radiation monitors, main steam isolation valves, instrument

air system, and isolated-phase bus duct. Specific procedures and documents reviewed

are listed in the Attachment.

During the inspection, the inspectors reviewed selected plant WO data, the site

guidance implementing procedure, discussed and reviewed relevant corrective action

issues (ARs/CRs), reviewed generic operations event data, probabilistic risk data, and

discussed issues with system engineers. Operational event information was evaluated

by the inspectors in its use in MR functions. The inspectors selected WOs, and MR

assessments, and other corrective action documents of systems recently removed from

10 CFR 50.65 a(1) status and those in a(2) status for some period to assess the

justification for their status. The documents were compared to the sites MR program

criteria, and the MR a(1) evaluations and rule related data bases.

Routine Maintenance

For the equipment issues described in work documents listed below, the inspectors

reviewed the licensees implementation of the Maintenance Rule (10 CFR 50.65) with

respect to the characterization of failures, the appropriateness of the associated

Maintenance Rule a(1) or a(2) classification, and the appropriateness of the associated

a(1) goals and corrective actions. The inspectors evaluated licensee work controls or

practices to assess whether these activities contributed to the degraded performance or

condition. The inspectors also reviewed operations logs and licensee event reports to

verify unavailability times of components and systems, if applicable. Licensee

performance was evaluated against the requirements of Procedure ADM-NGG-0101,

Maintenance Rule Program. The inspectors also reviewed deficiencies related to the

work activities listed below to verify that the licensee had identified and resolved

deficiencies in accordance with Procedure CAP-NGGC-0200, Corrective Action.

7

Enclosure

AR 110705110705Actuation of the Unit 2 high pressure coolant injection system

steam exhaust rupture discs during the performance of testing

following a system maintenance outage

AR 110948110948Radioactive waste effluent radiation monitor alarmed and

automatically secured detergent drain tank discharge

b. Findings

Introduction. A Green NCV was identified for failure to position a Unit 2 HPCI system

valve as required by a clearance order following maintenance activities.

Description. During the performance of Unit 2 HPCI system testing following

maintenance activities on November 12, 2003, the HPCI system automatically isolated

on a primary containment Group 4 isolation signal as a result of high pressure as

measured between the two (series mounted) turbine exhaust line rupture discs. High

turbine exhaust pressure resulted in a HPCI turbine trip, exhaust rupture disc failures,

and the actuation of the HPCI room carbon dioxide system due to the resultant room

high temperatures. The licensee found that the high turbine exhaust pressure was

caused by the turbine exhaust line to suppression pool stop check valve (2-E42-F021)

improperly being left in the closed position following the completion of maintenance

activities earlier that day. Following damage assessment and repairs caused by the

event, the HPCI system was declared operable on November 16, 2003.

The licensee determined the root cause to be the failure of auxiliary operators

performing the restoration lineup to properly check that valve 2-E41-F021 was in the

open position in accordance with plant practices. They failed to position the valve in the

open position in accordance with system restoration Clearance Order 60551.

Administrative Procedure 0AO-013, Plant Equipment Control, Revision 9, directs

operators to first stroke a valve in the close direction, and then return the valve to the

fully open position, when checking valves in the open position. Valve 2-E41-F021 has an

impacting type handwheel which allows the valve to be positioned with the aid of valve

handwheel inertia. The auxiliary operators were unfamiliar with this valve operational

feature and, as a result, were unsuccessful in moving the valve stem when they

attempted to turn the handwheel without the aid of impact. The operators deduced that

the valve was already in the open position based on the inability to turn the valve in the

open direction and the appearance that the valve was open based on valve stem

position.

In addition, the licensees investigation revealed other human performance-based

problems including: 1) one auxiliary operator performing the check did not attend the

prejob brief; 2) the prejob brief was limited in scope leaving the attending auxiliary

operator uncertain of valve locations, which contributed the position check being

performed concurrently; and 3) the auxiliary operators did not consult supervision when

they performed the check concurrently, versus independently, which was also not in

accordance with licensee expectations. The licensee planned corrective actions to

address the identified issues.

8

Enclosure

Analysis. The failure to position HPCI system valve 2-E41-F021 in accordance with

Clearance Order 60551 following maintenance activities is greater than minor because it

is associated with system configuration control and affected the mitigating availability of

the HPCI system. This finding was determined to be of very low safety significance

(Green) because the HPCI system was returned to an operable status within the TS

allowed outage time. The finding was related to the cross-cutting aspect of Human

Performance because the cause was determined to be due to plant operators using

improper techniques in verifying the valves position. Other contributing causes

including operator knowledge deficiencies of valve operation, failure to perform an

independent check of valve position, and the pre-job briefs limited scope were also

related to Human Performance.

Enforcement. Technical Specification 5.4.1.a. requires that written procedures shall be

implemented covering applicable procedures recommended in Regulatory Guide 1.33,

Appendix A, November 1972. Regulatory Guide 1.33 requires written procedures for

equipment control (e.g., locking and tagging). Equipment control Clearance Order

60551 required HPCI system valve 2-E41-F021 (turbine exhaust line to suppression

pool stop check valve), to be in the open position following maintenance activities on the

HPCI system on November 12, 2003. Contrary to Clearance Order 60551, valve 2-E41-

F021 was left in the closed position following the completion of maintenance activities on

November 12, 2003. Because this failure to follow Clearance Order 60551 is of very low

safety significance and has been entered into the licensees corrective action program

(AR 110705110705, this violation is being treated as an NCV, consistent with Section VI.A of

the NRC Enforcement Policy: NCV 05000324/2003006-01, Failure to Position HPCI

System Valve in Accordance with Clearance Order.

1R13

Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed the licensees implementation of 10 CFR 50.65 (a)(4)

requirements during scheduled and emergent maintenance activities. The inspectors

reviewed the effectiveness of risk assessments performed prior to changes in plant

configuration for maintenance activities (planned and emergent). The review was

conducted to verify that, upon unforseen situations, the licensee had taken the

necessary steps to plan and control the resultant emergent work activities. The

inspectors reviewed the applicable plant risk profiles, work week schedules, and

maintenance WOs for the following OOS equipment or conditions, and the documents

listed in the Attachment:

WO 59720

Service water intake structure bay cleaning

AR 108100108100EDG 4 inoperable due to failed low lubricating oil pressure switch

relay (2-DG4-LPSCR)

WO 473659

Vital battery 1B-1 declared inoperable due to low voltage on cell

  1. 10 during Work Week 41

AR 110705110705Unit 2 HPCI system steam exhaust rupture disc failure and

restoration to operable status

9

Enclosure

AR 110399110399Elevated integrated core damage probability on Unit 2 due to

reactor feed pump speed control system power supply sensitivity

to voltage fluctuations

AR 105246105246Unit 2 power reduction to repair main condenser tube leak

WO 464194

Repair motor-driven fire pump breaker compartment

To assess the licensees identification and resolution of problems, the inspectors

reviewed AR 112681112681associated with inconsistent risk evaluations for EDG wipedowns,

and AR 112544112544which documented issues associated with risk reduction compensatory

actions during the implementation of modifications on the Unit 2 reactor feed pump

speed control system.

b. Findings

No findings of significance were identified.

1R14

Operator Performance During Non-Routine Plant Evolutions and Events

a. Inspection Scope

The inspectors reviewed or observed the operating crews performance during the

following unplanned transient/abnormal conditions to verify the response to the event

was in accordance with procedures and training. Operator logs, plant computer data,

and associated operator actions were reviewed as well as the procedures listed in the

Attachment.

Operating crew performance and reactivity management during portions of the

Unit 2 down power and power escalation to repair a main condenser tube leak

occurring September 23-25, 2004.

Unit 2 reactor scram due to failure of the main generator exciter occurring on

November 4, 2003. Plant response to the failure resulted in the load shedding of

various plant loads, the tripping of the reactor feed pumps, and the loss of the

normal decay heat removal heat sink (main condenser) due to the receipt of a

primary containment isolation of Group 1 (i.e., main steam line isolation).

Operating crew performance and reactivity management during portions of the

Unit 2 control rod pull to criticality following repairs to the main generator exciter

on November 7, 2003.

Unit 2 HPCI system primary containment isolation and fire protection system

activation occurring on November 12, 2003. The transient resulted in challenges

to operators including unexpected isolation indications. Additionally, adverse

atmospheric conditions in the reactor building required deferral of fire protection

compensatory measures.

10

Enclosure

b. Findings

No findings of significance were identified.

1R15

Operability Evaluations

a. Inspection Scope

The inspectors reviewed the operability evaluations associated with the following six

issues, which affected risk significant systems or components, to assess as appropriate:

1) the technical adequacy of the evaluations; 2) the justification of continued system

operability; 3) any existing degraded conditions used as compensatory measures; 4) the

adequacy of any compensatory measures in place, including their intended use and

control; and 5) where continued operability was considered unjustified, the impact on TS

limiting conditions for operations (LCOs) and the risk significance. In addition to the

reviews, discussions were conducted with the applicable system engineer regarding the

ability of the system to perform its intended safety function. The inspectors reviewed the

documents listed in the Attachment.

AR 70787

Unit 2 residual heat removal system loop B pressurization due to

leakage past inboard low pressure coolant injection isolation valve

(2-E11-F015B)

AR 109435109435Vital battery 1A-2, cracked positive plate discovered cell #50

AR 110037110037Unit 2 standby gas treatment train A failure to start as required

following the Unit 2 reactor scram occurring on November 4, 2003

AR 105510105510Foreign material found in EDG 4 inter-cooler end cap

AR 111812111812Unit 2 residual heat removal system pipe support (2-E11-34FH88)

broken

AR 110948110948Radioactive waste radiation monitor Hi-Hi alarm received while

discharging the detergent drain tank

To assess the licensees identification and resolution of problems, the inspectors

reviewed AR 109291109291 associated with the loss of standby liquid control loop B squib

valve continuity on Unit 2, while working in the A loop circuit.

b. Findings

No findings of significance were identified.

11

Enclosure

1R16

Operator Work-Arounds (OWAs)

a. Inspection Scope

Selected OWAs

The inspectors reviewed the status of OWAs for Units 1 and 2 to verify that the

functional capability of the system or operator reliability in responding to an initiating

event was not affected. The review was to evaluate the effect of the OWA on the

operators ability to implement abnormal or emergency operating procedures during

transient or event conditions. The inspectors compared licensee actions to the

requirements of Procedure 0OI-01.08, Control of Equipment and System Status and

held discussions with operations personnel related to the OWAs reviewed.

The OWAs reviewed were:

1093

Interlock between reactor building doors 402 and 403 is broken

1028

Low pressure core injection line is pressurizing due to reactor coolant

inleakage

Cumulative Effects Review

The inspectors reviewed the cumulative effects of all identified operator work-arounds

and their: 1) impact on the reliability, availability, and potential for misoperation of the

effected systems; 2) potential for increasing an initiating event frequency; and 3) impact

on the ability of operators to respond in a correct and timely manner to a plant transient

and accident. Aggregate impacts of the identified work-arounds on each individual

operator watch station were also reviewed.

The inspectors held discussions with the OWA coordinator and reviewed the OWA

database to determine their cumulative effects. The effect of the work-arounds on

reliability, availability, and potential misoperations of the systems involved were

reviewed. The inspectors reviewed the OWAs on Unit 1 and Unit 2 to verify that no

increase in initiating event frequency occurred and that the OWA could not affect

multiple mitigating systems. The cumulative effects of OWAs on operators correct and

timely response to plant transients and accidents were also reviewed by the inspectors.

b. Findings

No findings of significance were identified.

12

Enclosure

1R17

Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed a permanent plant modification documented in Engineering

Change (EC) 46822 that modified the Unit 2 reactor feed pump speed control system

with a digital speed control system. One purpose of the review was to verify that the

modification met the design bases and the design assumptions. Another purpose was

to verify that modification implementation did not impair emergency/abnormal operating

procedure actions and key safety functions. The inspectors also reviewed the

modification to verify that unintended system interactions would not occur, and that no

additional failure modes were introduced.

b. Findings

Introduction. An unresolved item (URI) was identified for an inadequate design review

of a modification implemented on the Unit 2 reactor feed pump speed control system.

This is a URI pending completion of the SDP.

Description. During the Spring 2003 Unit 2 outage, the licensee implemented a

modification to the reactor feed pump speed control system. This modification, EC 46822, replaced the existing mechanical-hydraulic speed control system with a digital

speed control system (Woodward TMR 5009). During investigation as to the cause of

the reactor feed pumps tripping during the November 4, 2003 reactor trip, (See Section

40A3.2) the licensee determined that a trip of both reactor feed pumps would occur

following Unit 2 turbine trips. The licensee found that the digital speed control system

power supplies (two auctioneered for each reactor feed pump) were designed to sense

a fault condition within one cycle of abnormal supply voltages. The power supplies

would fault, and thus cease to supply output power, if incoming voltage was sensed

greater than 132 volts (AC) or less than 88 volts (AC). Simultaneous faults in the power

supplies would result in the reactor feed pump tripping.

The speed control system power supplies ultimately receive power from the 2C and 2D

Buses. These buses are provided with an automatically initiated, automatically

executed, quick, dead bus transfer. The scheme is capable of quickly transferring each

bus section and its loads from the normal source (Unit Auxiliary Transformer) to the

preferred source (Startup Auxiliary Transformer) in the event of a loss of the normal

power source or unit/turbine trip. This transfer results in the buses being disconnected

from both voltage sources for a period of between one and five cycles, per the UFSAR.

The licensee concluded that there was a high probability that reactor feed pump speed

control power supplies would fault during the period that the 2C and 2D are

disconnected from both voltage sources due to the sensitivity of the power supplies to

detect abnormally low voltage (i.e., less than 88 volts for 1 cycle). As a result, the

reactor feed pumps would trip following unit/turbine trips and during certain voltage

transients on the 2C and 2D Buses. The licensees evaluation of the modification failed

to recognize this vulnerability.

13

Enclosure

The licensee implemented compensatory work risk measures because of the resultant

elevated integrated core damage probability introduced by the reactor feed pump speed

control system vulnerabilities. The licensee promptly initiated corrective actions (AR

110399) and developed a modification to supply the reactor feed pump control system

with an uninterruptible power source.

On December 7, 2003, the licensee completed the modifications to the reactor feed

pump speed control system, which eliminated the vulnerabilities introduced by EC 46822. The licensee also plans to include uninterruptible power sources to the reactor

feed pump governors planned to be modified on Unit 1 in the Spring 2004 refueling

outage.

Analysis. The inadequate design review of the Unit 2 reactor feed pump speed control

system modification (EC 46822) affects the Initiating Events and Mitigating System

cornerstones. This issue is greater than minor because if left uncorrected, it would

increase the likelihood of initiating events caused by a loss of reactor feed pumps

following transients and affect the reliability and functional capability of the reactor feed

pumps to mitigate events. The condition existed since Unit 2 startup on April 6, 2003

until completion of a modification to install an uninterruptible power source to the system

on December 7, 2003. The dominant core damage sequence of the Significance

Determination Process Phase 2 analysis was Transients without Power Conversion

System. Because the finding increased the likelihood of transients with loss of reactor

feed pumps and because the reactor feed pumps would not be available to mitigate

events, the Phase 2 analysis determined that this finding has potential safety

significance greater than very low significance.

Enforcement. No violation of regulatory requirements occurred because the reactor

feed pumps are not classified as safety-related and the UFSAR does not credit the

reactor feed pumps for abnormal operating occurrence or accident mitigation. This

issue is unresolved pending determination of the safety significance and is identified as

URI 05000324/2003006-02, Unit 2 Reactor Feed Pump Speed Control System

Modification.

1R19

Post-Maintenance Testing

a. Inspection Scope

For the post maintenance tests and maintenance activities listed below, the inspectors

reviewed the test procedure and witnessed the testing and/or reviewed test records to

confirm that the scope of testing adequately verified that the work performed was

correctly completed, and that the test demonstrated that the affected equipment was

capable of performing its intended function and was operable in accordance with TS

requirements. The inspectors reviewed the licensees actions against the requirements

in Procedure 0PLP-20, Post Maintenance Testing Program. Documents reviewed are

listed in the Attachment.

14

Enclosure

WO 474971

Repair EDG 4, lubricating oil low pressure switch relay (2-DG4-

LPSCR)

WO 245950

Unit 1A nuclear service water pump discharge check valve

refurbishment

WO 464194

Repair motor-driven fire pump breaker/compartment

WO 469646

Repair EDG 2 jet assist solenoid valve (2-DG2-6552-2)

b. Findings

No findings of significance were identified.

1R22

Surveillance Testing

a. Inspection Scope

Routine Surveillance Testing

The inspectors either observed surveillance tests or reviewed test data for the risk

significant SSC surveillances, listed below, to verify the tests met TS surveillance

requirements, UFSAR commitments, in-service testing (IST), and licensee procedural

requirements. The inspectors assessed the effectiveness of the tests in demonstrating

that the SSCs were operationally capable of performing their intended safety functions.

The inspectors reviewed the documents listed in the Attachment.

Maintenance Surveillance Test 2MST-DG22R, EDG 4 Trip Bypass Logic Test

Periodic Test 2PT-01.7, Heatup/Cooldown Monitoring, following Unit 2 reactor

trip on November 4, 2003

Periodic test 0PT-20.3, Local Leak Rate Testing, performed on Unit 2 low

pressure coolant inboard injection valve (2-E11-FO15B)

Periodic Test 0PT-12.3.2.B, Number 2 Diesel Generator Starting Air Valve

Operability Test

Inservice Surveillance Testing

The inspectors reviewed the performance of Periodic Test 0PT-09.2, High Pressure

Coolant Injection System Operability Test, performed on Unit 2. The inspectors

evaluated the effectiveness of the licensees American Society of Mechanical Engineers

(ASME)Section XI testing program to determine equipment availability and reliability.

The inspectors evaluated selected portions of the following areas: 1) testing procedures;

2) acceptance criteria; 3) testing methods; 4) compliance with the licensees IST

program, TS, selected licensee commitments, and code requirements; 5) range and

accuracy of test instruments; and 6) required corrective actions. The inspectors also

assessed any applicable corrective actions taken.

b. Findings

No findings of significance were identified.

15

Enclosure

1R23

Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed Plant Operating Manual 0PLP-22, Temporary Changes, to

assess implementation of the below listed temporary modifications. The inspectors

reviewed these temporary modifications to verify that the modifications were properly

installed and whether they had any effect on system operability. The inspectors also

assessed drawings and procedures for appropriate updating and post-modification

testing. Documents reviewed are listed in the Attachment.

ECs 5597 & 45694 - Review temporary shielding installation on the residual heat

removal (RHR) and primary containment systems

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP2

Alert and Notification System Testing

a. Inspection Scope

The inspectors ascertained the licensees commitments with respect to the testing and

maintenance of the alert and notification system (ANS), which comprised 36 sirens in

the ten-mile-radius emergency planning zone (31 in Brunswick County, 5 in New

Hanover County). The inspectors evaluated the design of the ANS, the licensees

methodology for testing the system, and the adequacy of the testing program design.

Assessment of the program as actually implemented included review of siren test

records (with an emphasis on identification of any repetitive individual siren failures),

system changes during the past two years, procedures for periodic preventative

maintenance (including post-maintenance testing), and a sample of corrective actions

and their effectiveness for siren failures and issues. The review of this program area

encompassed the period January 2002 through November 2003. Licensee procedures,

records, and other documents reviewed within this inspection area are listed in the

Attachment.

b.

Findings

No findings of significance were identified.

16

Enclosure

1EP3 Emergency Response Organization (ERO) Augmentation

a.

Inspection Scope

The inspectors identified the licensees commitments with respect to timeliness and

numbers of personnel for staffing emergency response facilities (ERFs) in the event of

an emergency declaration at Alert or higher. The licensees automated paging system

and manual backup system for call-out of ERO personnel were reviewed to determine

whether they would support staff augmentation in accordance with the criteria for ERF

activation timeliness. Methodologies for testing the primary and backup systems for

augmenting the ERO were reviewed and discussed with cognizant licensee personnel.

The inspectors also reviewed and discussed the changes to the augmentation system

and process during the past two years. The inspectors reviewed records of the last off-

hour ERO augmentation drill which involved actual travel to the plant and activation of

ERFs (conducted on April 23, 2003). Records of ERO pager tests (the backup system

for ERO notification) were reviewed. Follow-up activities for a sample of problems

identified through augmentation testing were evaluated to determine whether

appropriate corrective actions were implemented. Licensee procedures, records, and

other documents reviewed within this inspection area are listed in the Attachment.

b.

Findings

No findings of significance were identified.

1EP4 Emergency Action Level (EAL) and Emergency Plan Changes

a.

Inspection Scope

The inspectors reviewed a selected sample of changes made to the Emergency

Response Plan (ERP) since the last inspection in this program area (conducted in

November 2002) against the requirements of 10 CFR 50.54(q) to determine whether

any of the changes decreased ERP effectiveness. The subject changes, which were

incorporated in ERP Revisions 60, 61, and 62, did not include modifications to the

emergency action levels (EALs). The inspectors reviewed documentation of the

licensees 10 CFR 50.54(q) screening evaluations for Revisions 60 and 62. Licensee

procedures, records, and other documents reviewed within this inspection area are

listed in the Attachment.

b.

Findings

No findings of significance were identified.

17

Enclosure

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

a.

Inspection Scope

The inspectors evaluated the efficacy of licensee programs that addressed weaknesses

and deficiencies in emergency preparedness. The procedure governing the plant

corrective action program was reviewed for applicability to the Emergency Preparedness

Program. Since the last inspection of this program area (conducted in November 2001),

one emergency declaration (a Notification of Unusual Event [NOUE]) was made by the

licensee, as a result of the projected threat from Hurricane Isabel on September 16,

2003. The inspectors reviewed event documentation to assess the adequacy of

implementation of ERP requirements, as well as the licensees self-assessment of ERO

performance during the event. The inspectors evaluated selected drill scenarios and

associated critiques to determine whether the licensee had properly identified failures to

implement regulatory requirements and planning standards. A sample of weaknesses

and deficiencies identified by means of these licensee processes was evaluated to

determine whether corrective actions were effective and timely. Licensee procedures,

records, and other documents reviewed within this inspection area are listed in the

Attachment.

b. Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors sampled licensee submittals for the Units 1 and 2 performance indicators

(PIs) listed below for the period October 2002 through September 2003. To verify the

accuracy of the PI data reported during that period, PI definitions and guidance

contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 2, were used to confirm the reporting basis

for each data element.

Reactor Safety Cornerstone

Reactor Coolant System Specific Activity

Reactor Coolant System Leak Rate

A sample of plant records and data was reviewed and compared to the reported data to

verify the accuracy of the PIs. The licensees corrective action program records were

also reviewed to determine if any problems with the collection of PI data had occurred.

Documents reviewed are listed in the Attachment.

18

Enclosure

Emergency Preparedness Cornerstone

  • Emergency Response Organization (ERO) Drill/Exercise Performance
  • ERO Drill Participation
  • Alert and Notification System Reliability

For the specified review period, the inspectors examined data reported to the NRC,

procedural guidance for reporting PI information, and records used by the licensee to

identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO

drill and exercise performance through review of a sample of drill and event records.

The inspectors reviewed selected training records to verify the accuracy of the PI for

ERO drill participation for personnel assigned to key positions in the ERO. The

inspectors verified the accuracy of the PI for alert and notification system reliability

through review of a sample of the licensees records of periodic system tests. The

inspectors also interviewed the licensee personnel who were responsible for collecting

and evaluating the PI data. Licensee procedures, records, and other documents

reviewed within this inspection area are listed in the Attachment.

b.

Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution

a. Inspection Scope

The inspectors performed an in-depth annual sample review of a selected AR to

determine whether conditions adverse to quality were addressed in a manner that was

commensurate with the safety significance of the issue. The inspectors reviewed the

actions taken to verify that the licensee had adequately addressed the following

attributes:

Complete, accurate, and timely identification of the problem

Evaluation and disposition of operability and reportability issues

Consideration of previous failures, extent of condition, generic or common cause

implications

Prioritization and resolution of the issue commensurate with the safety

significance

Identification of the root cause and contributing causes of the problem

Identification and implementation of corrective actions commensurate with the

safety significance of the issue

The following issue and associated corrective actions were reviewed:

AR 110705110705Actuation of the Unit 2 high pressure coolant injection system

steam exhaust rupture discs during the performance of testing

following a system maintenance outage

19

Enclosure

b. Findings and Observations

No findings of significance were identified.

4OA3 Event Follow-up

.1

All Oscillation Power Range Monitors (OPRMs) Declared Inoperable

a. Inspection Scope

On October 5, 2003, the licensee received a 10 CFR 21 notification from General

Electric that the Units 1 and 2 OPRMs have the potential for numerous, unexpected

confirmation count resets in the event of a reactor power instability condition, and were

therefore inoperable. The inspectors reviewed the licensee actions to verify proper

response in accordance with plant TS. The inspectors also reviewed the initial 10 CFR 50.72 notification to assess for appropriate reporting with established criteria.

b. Findings

No findings of significance were identified.

.2 Unit 2 Reactor Scram

a. Inspection Scope

The inspectors reviewed the licensees action in response to a Unit 2 main turbine trip

and reactor scram due to main generator loss of field that occurred on November 4, Unit

2. The loss of field was caused by the failure of the main generator alternator

brush/collector ring. During the scram all safety systems operated properly with the

exception of the 2A standby gas treatment train failing to start, the isolation of

containment isolation group 1 (main steam isolation), and the trip of the reactor feed

pumps. The licensee determined momentary degraded voltage on the AC emergency

buses (about 40% of rated) caused the relays associated with the group 1 isolation

(resulting in a loss of normal decay heat removal) and standby gas treatment fire

protection features to drop out. For further discussion of the trip of the reactor feed

pumps, see Section 1R17. In addition, the inspectors reviewed Operating Instruction

(OI) 0OI-01.06, Post Trip Review to verify the initial data gathering, equipment response

and post-trip review were conducted in accordance with the procedure requirements.

The inspectors also reviewed the initial 10 CFR 50.72 notification to verify proper

reporting with established criteria. The licensee entered this event into their corrective

action program as AR 109923109923 Licensee personnel performance is discussed in Section

1R14.

b. Findings

No findings of significance were identified.

20

Enclosure

.3 HPCI Exhaust Rupture Disc Failures

a. Inspection Scope

The inspectors reviewed the licensees response to a Unit 2 HPCI system isolation and

room fire protection actuation occurring on November 12, 2003. The actuations

occurred in response to the HPCI turbine exhaust line rupture discs actuating during

system testing. See Section 1R12.1 for further discussion of the rupture discs

actuating. The inspectors reviewed the initial 10 CFR 50.72 notification to verify proper

reporting with established criteria. The licensee entered this event into their corrective

action program as AR 110705110705

b. Findings

No findings of significance were identified.

.4 New Hanover County Sirens

a. Inspection Scope

The inspectors reviewed the licensees actions in response to the New Hanover County

emergency sirens not responding from the county emergency operations center on

November 12, 2003. The sirens were subsequently tested from the Emergency Offsite

Facility. The cause was determined to be due to radio frequency interference. Testing

to demonstrate the sirens could be successfully initiated from the county facility was

completed. The inspectors reviewed the licensees 10 CFR 50.72 notification against

established reporting criteria. The licensee entered the event into the corrective action

program as AR 110623110623

b. Findings

No findings of significance were identified.

4OA4 Cross Cutting Aspects of Findings

Section 1R12 describes a finding for the failure to position a HPCI system valve in

accordance with a clearance order following maintenance activities. The finding is

related to the cross-cutting aspect of Human Performance because the cause was

determined to be due to plant operators using improper techniques in verifying the

valves position. Other contributing causes including operator knowledge deficiencies of

valve operation, failing to perform an independent check of valve position, and the pre-

job briefs limited scope were also related to Human Performance.

21

Enclosure

4OA6 Meetings, Including Exit

On December 18, 2003, the resident inspectors presented the inspection results to

Mr. C. J. Gannon and other members of his staff. The inspectors confirmed that

proprietary information was not provided or examined during the inspection.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meets the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

10 CFR 50.74 requires in part that each licensee shall notify the commission in

accordance with section 50.4 within 30 days of the following in regard to a licensed

operator or senior operator ... (c) permanent disability or illness as described in 10CFR 55.25 of this chapter. Contrary to this, in June of 2001 a licensed operator had a

change in medical condition as described in ANSI/ANSA 3.4-1983, that was not reported

to the commission within 30 days. This finding was identified by the licensee during an

audit of medical records in April 2003. The NRC was notified of this finding in a letter

dated April 21, 2003. The licensed individual was administratively restricted to no solo

operation on April 4, 2003. The finding is of very low safety significance because

records indicate that the individual did not stand solo watch while performing licensing

duties after the change in medical condition occurred. This issue is documented in

licensee correction action request number 8992.

ATTACHMENT : SUPPLEMENTAL INFORMATION

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

E. Atkinson, Supervisor - Emergency Preparedness

A. Brittain, Manager - Security

E. Conway, Senior Nuclear Security Specialist

W. Dorman, Manager - Nuclear Assessment

C. Elberfeld, Lead Engineer, Technical Support

C. Gannon, Site Vice President (former Director - Site Operations)

J. Gawron, Training Manager

D. Hinds, Plant General Manager (former Engineering Manager)

J. Keenan, Past Site Vice President

D. Makosky, Lead Nuclear Security Specialist

W. Noll, Director - Site Operations (former Plant General Manager)

E. ONeil, Manager - Site Support Services

E. Quidley, Manager - Outage and Scheduling

H. Wall, Manager - Maintenance

M. Williams, Manager - Operations

NRC Personnel

P. Fredrickson, Chief, Reactor Projects Branch 4, Division of Reactor Projects Region II

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000324/2003006-02

URI

Unit 2 Reactor Feed Pump Speed Control System

Modification (Section 1R17)

Opened and Closed

05000324/2003006-01

NCV

Failure to Position HPCI System Valve in Accordance with

Clearance Order (Section 1R12)

Closed

NONE

Discussed

NONE

2

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Plant Operating Manual (POM), Volume VII, Operating Instruction 0OI-01.03, Non-Routine

Activities

POM, Volume XII, Preventive Maintenance, 0PM-HT001, Preventive Maintenance on Plant

Freeze Protection and Heat Tracing System

System Description SD-53, Freeze Protection and Heat Tracing System

Section 1R04: Equipment Alignment

Procedures

Administrative Procedure ADM-NGGC-0106, Configuration Management Program

Implementation

POM, Volume III, 2OP-10, High Pressure Coolant Injection System Operating Procedure

POM, Volume III, 1OP-43, Service Water System Operating Procedure

POM, Volume III, 2OP-16, Reactor Core Isolation Cooling System Operating Procedure

Section 1R05: Fire Protection

Procedures

POM, Volume XIX, Prefire Plan, 1PFP-RB and 2PFP-RB, Reactor Building Prefire Plans

POM, Volume XIX, Prefire Plan, 0PFP-DG, Diesel Generator Building Prefire Plans

Reports

Analysis No. BNP-E-9.004, Safe Shutdown Analysis Report

Section 1R06: Flood Protection Measures

Miscellaneous Documents

UFSAR section 3.4.1, Protection From External Flooding

UFSAR section 3.4.2, Protection From Internal Flooding

Design Basis Document (DBD)-106, Hazards Analysis

DBD-105, Postulated Pipe Failure

BNP Maintenance Rule a(1) System Action Plan For Site Cables Within Manholes (system

5259)

Maintenance Rule Expert Panel Meeting Minutes System 5259 (11/19/02 - 11/19/03)

3

Work Orders

47043, Functional test of flood status level switches for DG 1 and 2 fuel oil tank rooms

47102, Functional test of flood status level switches for DG 4 fuel oil tank room

45871, Functional test of DG 1 pipe trench level switches

45867, Functional test of DG 2 pipe trench level switches

172678,Functional test of DG 4 pipe trench water level switches

46974, Functional test of service water intake structure level switch

46091, Functional test of flood status level switches (Unit 1 core spray (CS) rooms, residual

heat removal (RHR) rooms, and high pressure coolant injection (HPCI) room)

180508, Functional test of flood status level switches (Unit 2 CS rooms, RHR rooms, and HPCI

room)

Corrective Action Documents

54376, DG1 jacket water cooler service water supply valves leak by

66048, Functional test of diesel generator building cell trench flood level switches

88221, Storm drain basin overboard valves open due to weather

94558, Pump unplugged allowing floor area to flood

98218, Oil and water leak on floor of heater drain pump room Unit 1

Procedures

0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings

0AOP-13.0, Operation During Hurricanes

0MST-Flood11Q, Flood Protection Intake Canal Level Channel Functional

0OP-47, Floor and Equipment Drain System Operating Procedure

Alarm Response Procedures

1(2)APP-UA-01 3-8, SW INTAKE STRC SUMP LEVEL HI-HI

1(2)APP-UA-28 3-5, SW INTAKE STRUCTURE FLOOD LVL HI

1(2)APP-UA-24 6-8, INTAKE CANAL FLOOD LEVEL HI

1(2)APP-UA-06 3-3, DRAINAGE BASIN TROUBLE

1(2)APP-UA-12 2-1, NORTH CS RM FLOOD LEVEL HI

1(2)APP-UA-12 1-1, NORTH CS RM FLOOD LEVEL HI-HI

1(2)APP-UA-12 2-3, SOUTH CS RM FLOOD LEVEL HI

1(2)APP-UA-12 1-3, SOUTH CS RM FLOOD LEVEL HI-HI

1(2)APP-UA-12 2-2, NORTH RHR RM FLOOD LEVEL HI

1(2)APP-UA-12 1-2, NORTH RHR RM FLOOD LEVEL HI-HI

1(2)APP-UA-12 2-4, SOUTH RHR RM FLOOD LEVEL HI

1(2)APP-UA-12 1-4, SOUTH RHR RM FLOOD LEVEL HI-HI

1(2)APP-UA-12 2-5, HPCI ROOM FLOOD LEVEL HI

1(2)APP-UA-12 1-5, HPCI ROOM FLOOD LEVEL HI-HI

1(2)APP-UA-28 3-6, DG NO 1 FUEL TNK RM FLOOD LVL HI

1(2)APP-UA-28 3-7, DG NO 2 FUEL TNK RM FLOOD LVL HI

1(2)APP-UA-28 3-8, DG BLDG BASEMENT FLOOD LVL HI

1(2)APP-UA-28 4-5, DG BLDG VALVE PIT FLOOD LVL HI

1(2)APP-UA-28 4-6, DG NO 3 FUEL TNK RM FLOOD LVL HI

4

1(2)APP-UA-28 4-7, DG NO 4 FUEL TNK RM FLOOD LVL HI

1(2)APP-UA-28 5-6, TURB BLDG PIPE TUNNEL FLOOD LVL HI

1(2)APP-UA-28 5-7, TURB BLDG PIPE TUNNEL FLOOD HI-HI

1(2)APP-UA-28 5-8, DG NO 1 PIPE TRENCH FLOOD LEVEL HI

1(2)APP-UA-28 5-9, DG NO 2 PIPE TRENCH FLOOD LEVEL HI

1(2)APP-UA-28 6-8, DG NO 3 PIPE TRENCH FLOOD LVL HI

1(2)APP-UA-28 6-9, DG NO 4 PIPE TRENCH FLOOD LVL HI

Section 1R07: Heat Sink Performance

Procedures

POM, Volume X, OMST-DG501R3, Emergency Diesel Generators 72 Month Inspection

Work Order

WO 453062-01, 2-DG4-ENG Turbocharger Intercooler Cover

Section 1R11: Licensed Operator Requalification

Procedures and Logs

POM, Volume I, Book 3, Training Program Procedure 0TPP-200, Licensed Operator Continuing

Training Program

Conduct of Examinations, TAP - 403, Rev. 6

Initial Licensing and Continued Training - Annual/Biannual Examination Development, TAP-411

License Activation and Maintenance; 0OI-01.05, Rev. 10

Licensed Operator Continued Training Program, TAP - 200, Rev. 2

Logs Recent Changes to BNP Simulator Logs

Medical Records

Operation Logs

Reactivation Records

Reactivity Anomaly Check; OPT-14.5.2, Rev. 34

Simulator Change Reports

Simulator Operation and Maintenance, TAP-412, Rev. 0

Simulator Service Request (SSR)

Simulator Test Procedure; STP-SS-002; 50% Power Steady State Comparison, Rev. 9

Simulator Program, OTPP-206, Rev. 1

Training Administration Procedure (TAP) 409, Conduct of Simulator Training and Evaluation

U1 Core Model Upgrade Report (B1C14)

U2 Core Model Upgrade Report (B2C16)

5

Section 1R12: Maintenance Effectiveness

Corrective Action (CR/AR) Reports

5051, instrument air repetitive MPFFs

5120, MSIV 1A PMG MR A(1)

22366, missed A(1) Assessment for system 5045

46853, isolated-phase bus system is not monitored in accordance with plan

46855, missed unavailability events

46857, three functional failures not logged in the MR data base

46861, AR investigation of improperly answered MR functional failure question

47884, coupling failed on Unit 1 service air dryer

48428, system 3080 has a condition monitoring criteria that was not being monitored

48432, scoping for Nuclear Boiler Instrumentation not adequate for assigning functional failures

48443, a missed functional failure in system 1080 was identified

54595, binding of transmitter 2-B21-LT-N024B-2

58722, 1-B21-F022B would not pressurize

71058, 1-iso-ph-cool-fan-2 tripped

86919, 2-B21-F028A would not pressurize

Administrative Procedures

NGGC-ADM-0101, Maintenance Rule Program, Rev. 16

Miscellaneous

BNP-PSA-056, PSA Evaluation of Maintenance Rule Performance Criteria, Unit 0, Rev. 0

Self Assessment Report 27639, dates July 23-26, 2001

Self Assessment Report 27639, dates July 22-25, 2002

1R13: Maintenance Risk Assessments and Emergent Work Evaluation

Procedures

POM, Volume 0AI-81, Water Chemistry Guidelines

Procedure OAP-025, BNP Integrated Scheduling

Technical Requirements Manual (TRM) 5.5.13, Configuration Risk Management Program

1R14: Operator Performance During Non-Routine Evolutions and Events

Procedures

Emergency Operating Procedure, 2EOP-01-RSP, Reactor Scram Procedure

POM Volume IV, General Operating Procedure, 0GP-2, Approach to Criticality and

Pressurization of the Reactor

6

Section 1R15: Operability Evaluations

Procedures

POM, Volume X, 0MST-BATT11Q, Batteries, 125 VDC, Quarterly Operability Test

POM, Volume XII, 0MMM-055, Cleanliness and Flushing Requirement

Section 1R19: Post Maintenance Testing

Procedures

POM, Volume X, OPT-34.1.1.0, Fire Pump Test (Motor-Driven and Engine-Driven)

POM, Volume X, 1PT-24.1-1, Service Water Pump and Discharge Valve Operability Test

POM, Volume X, 2MST-DG22R, DG-4 Trip Bypass Logic Test

POM, Volume XII, 0MMM-055, Cleanliness and Flushing Requirements

POM, Volume XII, 0MMM-015, Operation and Inspection of Cranes and Material Handling

Equipment

POM, Volume XII, 0CM-VCK506, Technocheck Check Valves

Section 1R22: Surveillance Testing

Procedures

POM, Volume X, 0PT-20.7B, Pressure Isolation Valve Leak Rate Test in Conjunction with RPV

Pressure Test

Section 1R23: Temporary Plant Modifications

Engineering Service Requests

ESR 00-00291, Rev. 0, Radioactive Floor Drains System

ESR 00-00291, Rev. 1, Fuel Pool Cooling & Supplemental Cooling

Sections 1EP2 - 1EP5: Reactor SafetyEmergency Preparedness

Plans and Procedures

BNP Siren Preventative Maintenance Checklist (no effective date or procedure number)

BNP Maintenance and Testing of Sirens - Customer/Supplier Agreement, 06/27/2003

CAP-NGGC-0200, Corrective Action Program, Rev. 9

Emergency Response Plan, Rev. 60 (effective 02/19/2003), Rev. 61 (effective 06/03/2003),

and Rev. 62 (effective 07/31/2003)

0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,

and General Emergency, Rev. 9

0PEP-02.6.21, Emergency Communicator, Rev. 42

0PEP-02.6.26, Activation and Operation of the Technical Support Center, Rev. 13

0PEP-02.6.27, Activation and Operation of the Emergency Operations Facility, Rev. 15

0PEP-03.8.2, Personnel Accountability and Evacuation, Rev. 16

7

0PEP-04.2, Emergency Facilities and Equipment, Rev. 27

0PEP-04.3, Performance of Training, Exercises, and Drills, Rev.16

0PEP-04.7, Brunswick Emergency Notification (Automated Telephone) System, Rev. 4

REG-NGGC-0010, 10 CFR 50.59 and Selected Regulatory Reviews, Rev. 5

Siren Control System Manual (Motorola document, June 1999)

Records and Data

BNP Siren Preventative Maintenance Checklists dated 11/05/2002 (sirens 27, 28, 29)

and 07/07/2003 (siren 10)

CP&L Brunswick Steam Electric Plant Siren System Test Reports for biweekly silent tests

(01/10/2002 - 12/01/2003), quarterly growl tests (01/07/2002, 04/08/2002, 07/08/2002,

10/07/2002, 01/13/2003, 04/14/2003, 07/17/2003, 10/13/2003) and annual full-volume

tests (11/06/2002, 11/12/2003)

Critique Report on 04/23/2003 Augmentation Drill, 04/25/2003

09/17/2003 NOUE Critique Report-Hurricane Isabel, 10/24/2003

Records of ERO pager tests, 01/2002 - 11/2003 (performed monthly through 06/2003,

then quarterly)

REG-NGGC-0010, Attachment 2, 10 CFR 50.54(q) Emergency Preparedness Program

Evaluation for ERP Rev. 60 (ID No. 03-0170) and Rev. 62 (ID No. 03-1007)

Unit 2 Operator Log for September 16-18, 2003

Audits and Self-Assessments

Nuclear Assessment Section (NAS) Assessment No. B-EP-02-01, Emergency Preparedness

Assessment, 01/06/2003

Self-Assessment No. AR 79474, Emergency Preparedness Response to Security Events

(conducted 06/23-26/2003)

Self-Assessment No. AR 79476, Evaluate Effectiveness of 2003 EP Team Training Drill Cycle

(conducted 10/27-30/2003)

Action Requests (Corrective Action Documents)

Action Request (AR) 79138, NAS Assessment No. B-EP-02-01 identified examples where

positions were staffed with non-qualified individuals, 12/10/2002

AR 00083236, CPLDOSE problems on Control Room computers, 01/30/2003

AR 00083532, ERO suspensions due to lapsed qualifications, 02/03/2003

AR 00085594, EP drill weakness: Alternate EOF competes for equipment use, 02/15/2003

AR 00091046, Brunswick Emergency Notification System unavailable, 04/21/2003

AR 00095497, EP drill 05/27/2003: Items for management consideration, 06/06/2003

AR 00100005, EP drill 07/15/2003: TSC weakness, 07/17/2003

AR 00110343. Hurricane Isabel: Items for management consideration, 11/04/2003

AR 00110623, Failure of New Hanover sirens during full volume testing, 11/12/2003

AR 00112517, Alert and Notification System process enhancement, 12/04/2003

AR 00112518, Alternate EOF augmentation goals, 12/04/2003

AR 00112529, Evaluate documenting offsite assembly area locations, 12/04/2003

8

Section 4OA1: Performance Indicator Verification

Procedures

POM, Vol. VII, 1OI-03.1, Control Operator Daily Surveillance Report

POM, Vol. VII, 2OI-03.1, Control Operator Daily Surveillance Report

Reactor coolant radiochemistry logs

Records and Data

CP&L Brunswick Steam Electric Plant Siren System Test Reports for biweekly silent tests

(01/10/2002 - 12/01/2003), quarterly growl tests (01/07/2002, 04/08/2002, 07/08/2002,

10/07/2002, 01/13/2003, 04/14/2003, 07/17/2003, 10/13/2003) and annual full-volume

tests (11/06/2002, 11/12/2003)

Documentation packages (scenario/time line/event notification forms/critique report) for ERO

drills on 10/15/2002 and 05/27/2003

Documentation packages (event notification forms/evaluator critique) for Licensed Operator

Continuing Training drills on 02/23/2003, 06/09/2003, 06/16/2003, 06/23/2003, and 06/30/2003

EPL-001, Emergency Phone List, 09/30/2003

ERO participation rosters (source record) for 05/27/2003 drill

Section 4OA3: Event Followup

Procedures

POM, Volume VII, Operating Instructions 0OI-01.07, Notifications, Rev. 11