Similar Documents at Salem |
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Category:Letter type:LR
MONTHYEARLR-N23-0079, Special Report 23-02-00 Pursuant to the Requirements of Salem Unit 1 Technical Specification 3.3.3.7, Action 10, for the Unit 1 Main Steam Line Rad Monitor Inoperable for Greater than Seven Days2023-12-0707 December 2023 Special Report 23-02-00 Pursuant to the Requirements of Salem Unit 1 Technical Specification 3.3.3.7, Action 10, for the Unit 1 Main Steam Line Rad Monitor Inoperable for Greater than Seven Days LR-N23-0077, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2023 & 30 Day Report for Salem Unit 1 Upflow Conversion2023-11-29029 November 2023 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2023 & 30 Day Report for Salem Unit 1 Upflow Conversion LR-N23-0072, Core Operating Limits Report Cycle 302023-11-0101 November 2023 Core Operating Limits Report Cycle 30 LR-N23-0045, and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement2023-09-0808 September 2023 and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement LR-N23-0055, Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days2023-08-0303 August 2023 Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days LR-N23-0054, In-Service Inspection Activities2023-07-26026 July 2023 In-Service Inspection Activities LR-N23-0046, Emergency Plan Document Revisions Implemented June 28, 20232023-07-10010 July 2023 Emergency Plan Document Revisions Implemented June 28, 2023 LR-N23-0005, License Amendment Request to Amend Technical Specifications (TS) 6.8.4.f for Permanent Extension of Type a and Type C Leak Rate Test Frequencies2023-06-23023 June 2023 License Amendment Request to Amend Technical Specifications (TS) 6.8.4.f for Permanent Extension of Type a and Type C Leak Rate Test Frequencies LR-N23-0035, 2022 Annual Radioactive Effluent Release Report (ARERR)2023-04-27027 April 2023 2022 Annual Radioactive Effluent Release Report (ARERR) LR-N23-0034, 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station2023-04-27027 April 2023 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station LR-N23-0033, Core Operating Limits Report Cycle 272023-04-26026 April 2023 Core Operating Limits Report Cycle 27 LR-N23-0010, License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location2023-04-21021 April 2023 License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location LR-N23-0006, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-24024 March 2023 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations LR-N23-0019, and Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums2023-03-21021 March 2023 and Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums LR-N23-0016, and Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments2023-02-28028 February 2023 and Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments LR-N23-0012, Annual Property Insurance Status Report2023-02-24024 February 2023 Annual Property Insurance Status Report LR-N23-0014, Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.7172023-02-23023 February 2023 Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.717 LR-N23-0003, Response to Requests for Additional Information Salem Unit 2 Relief Request S2-I4R-2112023-02-0101 February 2023 Response to Requests for Additional Information Salem Unit 2 Relief Request S2-I4R-211 LR-N22-0096, and Salem Generating Station, Units 1 and 2 - Request for Threshold Determination2023-01-0505 January 2023 and Salem Generating Station, Units 1 and 2 - Request for Threshold Determination LR-N22-0095, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 20222022-12-20020 December 2022 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2022 LR-N22-0094, Emergency Plan Document Revisions Implemented November 21, 20222022-12-14014 December 2022 Emergency Plan Document Revisions Implemented November 21, 2022 LR-N22-0092, Response to Final Iolb Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG2022-12-0909 December 2022 Response to Final Iolb Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG LR-N22-0091, Independent Spent Fuel Storage Installation, Report of 10 CFR 72.48 Changes, Tests, and Experiments2022-12-0202 December 2022 Independent Spent Fuel Storage Installation, Report of 10 CFR 72.48 Changes, Tests, and Experiments LR-N22-0084, Response to Final Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG (EPID L- 2022-LLA-0095)2022-11-17017 November 2022 Response to Final Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG (EPID L- 2022-LLA-0095) LR-N22-0090, Supplement to Submittal of Salem Generating Station Updated FSAR, Revision 33, 10 CFR 71.106 Review Results and 10 CFR 54.37(b) Review Results for Salem2022-11-10010 November 2022 Supplement to Submittal of Salem Generating Station Updated FSAR, Revision 33, 10 CFR 71.106 Review Results and 10 CFR 54.37(b) Review Results for Salem LR-N22-0065, Submittal of Relief Request Associated with the Fourth Inservice Inspection (ISI) Interval Limited Examinations2022-09-27027 September 2022 Submittal of Relief Request Associated with the Fourth Inservice Inspection (ISI) Interval Limited Examinations LR-N22-0074, Emergency Plan Evacuation Time Estimate2022-09-15015 September 2022 Emergency Plan Evacuation Time Estimate LR-N22-0066, License Amendment Request (LAR) to Relocate Technical Specifications (TS) Requirements for Reactor Head Vents to the Technical Requirements Manual (TRM)2022-08-31031 August 2022 License Amendment Request (LAR) to Relocate Technical Specifications (TS) Requirements for Reactor Head Vents to the Technical Requirements Manual (TRM) LR-N22-0063, Spent Fuel Cask Registration2022-08-10010 August 2022 Spent Fuel Cask Registration LR-N22-0068, In-Service Inspection Activities - 90-Day Report2022-08-10010 August 2022 In-Service Inspection Activities - 90-Day Report LR-N22-0012, License Amendment Request to Amend the Technical Specifications to Revise and Relocate the Reactor Coolant System Pressure and Temperature Limits and Pressurizer Overpressure Protection System Limits to a Pressure and Temperature2022-08-0707 August 2022 License Amendment Request to Amend the Technical Specifications to Revise and Relocate the Reactor Coolant System Pressure and Temperature Limits and Pressurizer Overpressure Protection System Limits to a Pressure and Temperature LR-N22-0062, Spent Fuel Cask Registration2022-07-21021 July 2022 Spent Fuel Cask Registration LR-N22-0006, License Amendment Request (LAR) to Amend Salem Unit 1 and Unit 2 Technical Specifications (TS) to Extend the Allowed Outage Time for an Inoperable Emergency Diesel Generator from 72 Hours to 14 Days2022-06-29029 June 2022 License Amendment Request (LAR) to Amend Salem Unit 1 and Unit 2 Technical Specifications (TS) to Extend the Allowed Outage Time for an Inoperable Emergency Diesel Generator from 72 Hours to 14 Days LR-N22-0051, License Amendment Request to Relocate Technical Specification Facility/Unit Staff Qualification Requirements to Quality Assurance Topical Report2022-06-22022 June 2022 License Amendment Request to Relocate Technical Specification Facility/Unit Staff Qualification Requirements to Quality Assurance Topical Report LR-N22-0044, Emergency Plan Document Revisions Implemented November, 20212022-05-19019 May 2022 Emergency Plan Document Revisions Implemented November, 2021 LR-N22-0043, Core Operating Limits Report - Cycle 292022-05-0909 May 2022 Core Operating Limits Report - Cycle 29 LR-N22-0041, 2021 Annual Radioactive Effluent Release Report (Rerr)2022-04-28028 April 2022 2021 Annual Radioactive Effluent Release Report (Rerr) LR-N22-0040, 2021 Annual Radiological Environmental Operating Report2022-04-28028 April 2022 2021 Annual Radiological Environmental Operating Report LR-N22-0039, Emergency Plan Document Revisions Implemented March 24, 20222022-04-21021 April 2022 Emergency Plan Document Revisions Implemented March 24, 2022 LR-N21-0052, Request for Relief from ASME Code Defect Removal for Service Water Buried Piping2022-04-0707 April 2022 Request for Relief from ASME Code Defect Removal for Service Water Buried Piping LR-N22-0023, Guarantees of Payment of Deferred Premiums2022-03-21021 March 2022 Guarantees of Payment of Deferred Premiums LR-N22-0022, Response to Request for Additional Information Relief Request S1-14R-210, Alternative Examination of Welds2022-03-21021 March 2022 Response to Request for Additional Information Relief Request S1-14R-210, Alternative Examination of Welds LR-N22-0017, Submittal of 2021 Annual Report of Fitness for Duty (FFD) Performance Data2022-02-25025 February 2022 Submittal of 2021 Annual Report of Fitness for Duty (FFD) Performance Data LR-N22-0016, Radiological Survey of Site Property to Be Used for Offshore Wind Port Facility2022-02-24024 February 2022 Radiological Survey of Site Property to Be Used for Offshore Wind Port Facility LR-N22-0013, In-Service Inspection Activities - 90-Day Report2022-02-10010 February 2022 In-Service Inspection Activities - 90-Day Report LR-N22-0007, Request for Exemption from Specific Requirements of 10 CFR Part 26, Fitness for Duty Programs2022-01-0505 January 2022 Request for Exemption from Specific Requirements of 10 CFR Part 26, Fitness for Duty Programs LR-N21-0061, Annual Report of Specific Activity Analysis - TS 6.9.1.5c2021-12-0909 December 2021 Annual Report of Specific Activity Analysis - TS 6.9.1.5c LR-N21-0083, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2021 & 30 Day Report for Salem Unit 2 Upflow Conversion2021-11-24024 November 2021 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2021 & 30 Day Report for Salem Unit 2 Upflow Conversion LR-N21-0078, Hope and Creek Generating Station, Supplement to License Amendment Request to Revise Technical Specifications (TS) to Delete Definitions Found in 10 CFR Part 20 and Delete Figures of the Site and Surrounding Areas from TS2021-11-18018 November 2021 Hope and Creek Generating Station, Supplement to License Amendment Request to Revise Technical Specifications (TS) to Delete Definitions Found in 10 CFR Part 20 and Delete Figures of the Site and Surrounding Areas from TS LR-N21-0066, Submittal of Relief Request Associated with the Fourth Inservice Inspection (ISI) Interval Limited Examinations2021-11-10010 November 2021 Submittal of Relief Request Associated with the Fourth Inservice Inspection (ISI) Interval Limited Examinations 2023-09-08
[Table view] Category:Licensee 30-Day Written Event Report
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Text
PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 0 PSEG NuclearLLC OCT 0 2 2006 Technical Specification 6.9.2 LR-N06 - 0405 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 SALEM GENERATING STATION UNIT NO. 2 FACILITY OPERATING LICENSE DPR-75 DOCKET NO. 50-311
Subject:
Special Report 311106-002 Main Steam Line Discharge Monitors (R46s) Inoperable Greater Than Seven (7) Days This special report is being submitted pursuant to the requirements Salem Unit 2 Technical Specification (TS) 3.3.3.1 Action b, and 26. TS 3.3.3.1 requires one main steam line discharge monitor per line to be Operable in Modes 1 - 4. With less than the required detectors operable, Action 26 of Table 3.3-6 requires that within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> the pre-planned alternate method of monitoring the appropriate parameter(s) be initiated, and: (1) either the inoperable channel be restored to Operable within 7 days of the event, or (2) prepare and submit a Special Report to the Commission pursuant to Specification 6.9.2 within 14 days following the event outlining the actions taken, the cause of the inoperability and the plans and schedule for restoring the system to Operable.
On September 19, 2006, plant personnel commenced performance testing of the Chilled Water System in accordance with the Inservice Testing of Chilled Water Valves procedure. At approximately 0205 hours0.00237 days <br />0.0569 hours <br />3.38955e-4 weeks <br />7.80025e-5 months <br />, Salem Unit 2 control room operators entered TS 3.3.3.1 upon isolating the Chilled Water to the main steam line radiation monitors (2R46A-E). Additionally, in accordance with the TS action statement requirements, Radiation Protection personnel were notified of the requirements to establish the pre-planned alternate method of monitoring the appropriate parameters.
95-2168 REV. 7/99
OCT 0 2 2006 Page 2 Document Control Desk LR-N06-0405 Subsequently, during the surveillance testing, the Chilled Water outlet check valve 2CH260 failed its performance test. Maintenance personnel opened, inspected and cleaned the valve with a post maintenance test to be performed during system restoration.
Additionally, it was noted that the Chilled Water inlet isolation valve 2CH253 did not close on low Chilled Water system pressure as designed. Investigation and troubleshooting by Maintenance/l&C personnel revealed that a defective pressure switch caused the failure of the 2CH253 valve to fully close.
Maintenance/l&C personnel unsuccessfully tried to calibrate the pressure switch and replacement of the switch could not be accomplished because the component was not maintained in inventory. Efforts to obtain a replacement part prior to the seven-day expiration date of the action statement were unsuccessful due to the required lead-time from the vendor.
Currently, PSEG is in process of repairing the subject valves, and it is expected that the TS action statement will be terminated by October 31, 2006.
There was no safety consequences associated with the inoperability of the R46 detectors. The pre-planned alternate of monitoring the appropriate parameter(s) was initiated within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Implementation of the pre-planned alternate method of sampling provides reasonable assurance that any increase in activity will not go undetected.
There are no commitments made in this document. Any actions or dates discussed in this submittal represent intended or planned actions. They are described to the NRC for the NRC's information and are not regulatory commitments.
Should there be any questions regarding this matter please contact E. H. Villar 856-339-5456.
Sincerely, Thomas P. Joyce Salem Site Vice President
,o OCT 0 2 2006 Page 3 Document Control Desk LR-N06-0405 C Administrator- Region I United States Nuclear Regulatory Commission 474 Allendale Road King of Prussia, PA 19406 USNRC Senior Resident Inspector - Salem (X24)
Mr. K. Tosch, Manager IV Bureau of Nuclear Engineering PO Box 415 Trenton, NJ 08625