Similar Documents at Salem |
---|
Category:Licensee 30-Day Written Event Report
[Table view] Category:Written Event Report (30 or 60 day)
MONTHYEARLR-N23-0055, Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days2023-08-0303 August 2023 Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days LR-N21-0083, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2021 & 30 Day Report for Salem Unit 2 Upflow Conversion2021-11-24024 November 2021 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2021 & 30 Day Report for Salem Unit 2 Upflow Conversion ML0333606682003-11-24024 November 2003 Special Report 03-002 Re Condenser Off Gas Monitor Being Inoperable for Greater than Seven Days ML19031A9121997-02-25025 February 1997 LER 1977-009-01 for Salem Unit 1 No. 12 Containment Fan Coil Unit Inoperable ML19031B1781977-02-25025 February 1977 LER 1977-010-01 for Salem, Unit 1 No. 12 Containment Fan Coil Unit Inoperable ML19031B0621977-02-24024 February 1977 LER 1977-011-01 and LER 1977-013-01 for Salem Unit 1 Industrial Waste Was Discharged from the Treatment Area When the Ph Was Outside the Range of 6~5 to 8.5 ML19031B1791977-02-15015 February 1977 LER 1977-006-01 for Salem Unit 1 #12 Reactor Coolant Flow Channel 1 Inoperable ML19031A9151977-02-15015 February 1977 LER 1977-007-01 for Salem Unit 1 No. 12 Steam Generator Steam Flow Channel II Inoperable ML19031B0631977-02-15015 February 1977 LER 1977-008-01 for Salem Unit 1 No. 13 Steam Generator Steam Flow Channel I Inoperable ML19031A9161977-02-0707 February 1977 LER 1977-004-01 for Salem, Unit 1, #13 Auxiliary Feed Pump Fail to Start ML19031B5731977-02-0101 February 1977 LER 1976-029-01 for Salem Unit 1 Phase III Test Procedure ML19031A8271977-01-31031 January 1977 LER 1977-005-01 for Salem, Unit 1, Hydraulic Line Flange on Nos. 11 and 12 Main Steam Isolation Valves and Subsequent Violation of Technical Specification 3.0.3 ML19031B0641977-01-28028 January 1977 LER 1976-031-01 for Salem, Unit 1, Boron Injection Tank Inoperable ML19031B0651977-01-28028 January 1977 LER 1977-001-01 for Salem, Unit 1, Containment Pressure Protection, Channel II, PT-948C, Inoperable ML19031B0671977-01-28028 January 1977 LER 1977-002-01 for Salem, Unit 1, Pipe Failure on Letdown Vent Line ML19031B5741977-01-28028 January 1977 LER 1976-030-01 for Salem Unit 1 No. 11 and No. 12 Boric Acid Storage Tanks Inoperable ML19031B1801977-01-19019 January 1977 LER 1976-028-42 for Salem, Unit 1 Radioactive Spill and Unauthorized Release ML19031B0681977-01-14014 January 1977 LER 1976-026-01 for Salem, Unit 1, Boron Injection Tank Inoperable ML19031A7621977-01-14014 January 1977 LER 1976-020-01 for Salem, Unit 1 High Reactor Coolant System Chlorides ML19031B1811977-01-14014 January 1977 LER 1976-025-01 for Salem Unit 1 Reduction of Shutdown Margin During Special Test Exceptions ML19031A9191977-01-0404 January 1977 LER 1976-024-01 for Salem, Unit 1, Failure of Radiation Monitoring System Channel Rlla, Containment/Plant Vent Air Particulate Monitor ML19031A5471977-01-0404 January 1977 LER 1976-017-01 for Salem, Unit 1 Inoperable Personnel Air Lock - Elevation 100' ML19031A9201977-01-0303 January 1977 LER 1976-016-01 for Salem Unit 1 Improper Use of Test Leads ML19031A9181976-01-0707 January 1976 LER 1976-021-01 for Salem, Unit 1, Boron Injection Tank Inoperable 2023-08-03
[Table view] |
Text
t Y- PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 LRN-03-0477 PSEG NuclearLLC United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Special Report 311/03-002 Salem Unit 2 Facility Operating License DPR-75 Docket No. 50-311 This special report is being submitted pursuant to the requirements of Salem Unit 2 Technical Specification (TS) 3.3.3.1 Radiation Monitoring Instrumentation" Action b, due to the condenser off gas monitor (2R15) being inoperable for greater than 7 days.
On November 10, 2003 at 0810 hours0.00938 days <br />0.225 hours <br />0.00134 weeks <br />3.08205e-4 months <br />, TS 3.3.3.1 was entered when Salem Unit 2 entered Mode 4 from its thirteenth (2R13) refueling outage. TS 3.3.3.1, Action b requires that With one or more radiation monitoring channels inoperable, take the ACTION shown in Table 3.3-6." Action 26 of Table 3.3-6 requires that within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> the preplanned alternate method of monitoring the appropriate parameter(s) be initiated, and (a) the inoperable channel be restored to operable within 7 days, or (b) to prepare and submit a Special Report to the Commission pursuant to Specification 6.9.2 within 14 days following the event outlining the action taken, the cause of the inoperability and the plans and schedule for restoring the system to OPERABLE status.
As stated above, the channel became inoperable when Unit 2 entered Mode 4 and condenser vacuum could not be established. Condenser vacuum could not be established due to delays during the generator shaft and exciter alignment. Condenser vacuum was established on November 18, 2003 and the 2R15 action statement was terminated.
Should there be any questions regarding this matter please contact E.H. Villar at 856-339-5456.
Sincerely a ager - Salem 952168 REV. 7/99
NOV 2 4 2003 Document Control Desk LRN-03-0477 C Administrator- Region I United States Nuclear Regulatory Commission 474 Allendale Road King of Prussia, PA 19406
/EHV