IR 05000456/2006003

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IR 05000456-06-003, 05000457-06-003; Exelon Generation Company, LLC; 04/01/2006 - 06/30/2006; Braidwood Station, Units 1 & 2; Fire Protection
ML062190402
Person / Time
Site: Braidwood  
Issue date: 08/04/2006
From: Richard Skokowski
NRC/RGN-III/DRP/RPB3
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
FOIA/PA-2010-0209 IR-06-003
Download: ML062190402 (56)


Text

August 4, 2006

SUBJECT:

BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000456/2006003; 05000457/2006003

Dear Mr. Crane:

On June 30, 2006, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection results, which were discussed on June 30, 2006, with Mr. K. Polson and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, one NRC-identified finding of very low safety significance (Green) is documented in this report. The issue was determined to involve a violation of NRC requirements. Because of its very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a Non-Cited Violation in accordance with Section VI.A of the NRC Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood facility. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Richard A. Skokowski, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77 Enclosure:

Inspection Report 05000456/2006003; 05000457/2006003 w/Attachment: Supplemental Information cc w/encl:

Site Vice President - Braidwood Station Plant Manager - Braidwood Station Regulatory Assurance Manager - Braidwood Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director Licensing Manager Licensing - Braidwood and Byron Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer Chairman, Illinois Commerce Commission

SUMMARY OF FINDINGS

IR 05000456/2006003, 05000457/2006003; 04/01/2006 - 06/30/2006; Braidwood Station,

Units 1 & 2; Fire Protection.

This report covers a 3-month period of baseline inspection, an inspection in accordance with Temporary Instruction (TI) 2515/150, Reactor Pressure Vessel Head and Vessel head Penetration Nozzles, and a followup inspection of certain portions of TI 2515/165, Operational Readiness of Offsite Power and Impact on Plant Risk. The inspections were conducted by resident and inspectors based in the NRC Region III office. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Non-Cited Violation of Braidwood Facility Operating License Nos. NPF-72 and NPF-77, Condition 2.E, for failing to maintain the firewall separating the fuel handling building and the auxiliary building in accordance with the approved fire protection program. Fire dampers were required to be provided in this firewall, except where an evaluation had been performed and approved to allow a deviation. Dampers were not installed in two ventilation ducts in the firewall separating the spent fuel pool heat exchanger rooms of the fuel handling building and the Unit 1 and Unit 2 containment pipe penetration areas of the auxiliary building; also, no evaluation or exemption existed to justify this configuration. The licensee entered the issue into its corrective action program for resolution, implemented compensatory measures that included hourly fire watches.

This finding was more than minor because it affected the Mitigating Systems Cornerstone objective to ensure that external factors (i.e., fire, flood, etc) do not impact the availability, reliability, and capability of systems that respond to initiating events. The finding was of very low safety significance because the steel ventilation duct provided a minimum of 60 minutes fire endurance protection and the location of combustibles were positioned such that the unprotected duct penetration would not be subjected to direct flame impingement. (Section 1R05)

Licensee-Identified Violations

No findings of significance were identified.

REPORT DETAILS

Summary of Plant Status

Unit 1 started a gradual power coastdown on April 3, 2006, and reached about 93 percent power on April 16, 2006, when the unit was taken off line and shutdown for a refueling outage.

Unit 1 was brought critical and the generator was synchronized to the grid on May 3, 2006.

Unit 1 reached full power on May 8, 2006, and operated at or near full power for the remainder of the inspection period except that power was briefly reduced to about 95 percent on June 16, 2006, at the request of Electric Operations due to grid conditions.

Unit 2 operated at or near full power throughout the inspection period except that power was briefly reduced to about 97 percent on April 6, 2006, in order to isolate a failed open feedwater system relief valve and power was briefly reduced to about 95 percent on June 16, 2006, at the request of Electric Operations due to grid conditions.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness for Seasonal Susceptibilities

a. Inspection Scope

The inspectors reviewed the licensees seasonal preparations for operation during the summer months. This was primarily accomplished by verifying that the licensee had completed the requirements for summer readiness as documented in Exelon Nuclear Procedure WC-AA-107, Seasonal Readiness. The inspectors also reviewed the Updated Final Safety Analysis Report (UFSAR), Technical Specifications (TS) and other design-bases documents to identify those components that were susceptible to degradation from high temperatures during the summer months. The inspectors verified that the licensee had addressed these components in preparation for summer operation.

In addition, the inspectors selected the following risk-significant support systems/areas for specific review:

  • Units 1 and 2 main power transformers and bus duct cooling; and
  • auxiliary building chiller reliability.

The inspectors also reviewed several issue reports (IRs) documenting problems with bus duct fan preventive maintenance lessons learned, rescheduling of an action tracking item affecting summer readiness, and seasonal readiness peer review results to determine whether these issues were being properly addressed in the licensees corrective action program. In addition, the inspectors reviewed the licensees common cause analysis, Summer Readiness Issues, and a completed work order on high temperature equipment protection. The inspectors verified that minor issues identified during these inspections were entered into the licensees corrective action program.

Documents reviewed in this inspection are listed in the Attachment.

This review constituted two samples of this inspection requirement.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

Partial Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the accessible portions of risk-significant system trains during periods when the train was of increased importance due to redundant trains or other equipment being unavailable. The inspectors utilized the valve and electric breaker listed to determine whether the components were properly positioned and that support systems were aligned as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to determine whether there were any obvious deficiencies. The inspectors reviewed IRs associated with the train to determine whether those documents identified issues affecting train function. The inspectors used the information in the appropriate sections of the TS and the UFSAR to determine the functional requirements of the system. The inspectors also reviewed the licensees identification of and the controls over the redundant risk-related equipment required to remain in service. Documents reviewed during this inspection are listed in the Attachment.

The inspectors completed three samples of this requirement by walkdowns of the following trains:

  • 2A diesel generator (DG) electrical and mechanical line-up prior to 2B DG outage; and

b. Findings

No findings of significance were identified.

1R05 Fire Protection

Quarterly Inspection

a. Inspection Scope

The inspectors conducted fire protection walkdowns that focused on the availability, accessibility, and condition of fire fighting equipment, on the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events, with additional insights on their potential to impact equipment which could initiate a plant transient or be required for safe shutdown. The inspectors used the Fire Protection Report, Revision 21, to determine: that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The inspectors completed nine samples of this inspection requirement during the following walkdowns:

  • fuel handling building (Fire Zone 12.1-0);
  • Unit 2 non-segregated bus-duct area (Fire Zone 3.2a-2);
  • Unit 2 Division 21 engineered safety feature (ESF) switchgear room (Fire Zone 5.2-2);
  • Unit 2 Division 22 ESF switchgear room (Fire Zone 5.1-2);
  • Unit 1 Division 11 ESF switchgear room (Fire Zone 5.2-1);
  • Unit 1 Division 12 ESF switchgear room (Fire Zone 5.1-1);
  • Unit 2 Division A DG and day tank room (Fire Zone 9.2-2);
  • Unit 2 Division B DG and day tank room (Fire Zone 9.2-1); and
  • sprinkler head interference in 2B diesel oil storage tank room (Fire Zone 10.1-2).

The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program. Documents reviewed during this inspection are listed in the Attachment.

b. Findings

Failure to Maintain Fire Barrier in Accordance With Fire Protection Program

Introduction:

The inspectors identified an Non-Cited Violation (NCV) of Braidwood Facility Operating License Nos. NPF-72 and NPF-77, Condition 2.E, for failing to maintain the firewall separating the fuel handling building and the auxiliary building, in accordance with the approved fire protection program.

Description:

On April 12, 2006, during a routine fire protection walkdown of the fuel handling building, the inspectors noted that ventilation ducts in the 3-hour firewall between the spent fuel pool heat exchanger room and the auxiliary building did not appear to have fire dampers installed. The inspectors questioned the fire protection system engineer regarding the state of the ventilation ducts in that area and their apparent lack of dampers. As a result, the licensee performed an independent walkdown and confirmed that fire dampers were not installed in the ventilation ducts of the firewall separating the spent fuel pool heat exchanger rooms of the fuel handling building and the Unit 1 and Unit 2 containment pipe penetration areas of the auxiliary building. This was inconsistent with Section 2.3.12.1 of the Fire Protection Report, which described the fire area analysis for the fuel handling building and stated that fire dampers were provided in the firewall separating the fuel handling building and the auxiliary building.

The inspectors reviewed the Fire Protection Report and did not identify any existing deviations allowing for the existence of this condition. The inspectors also reviewed Braidwood Stations Generic Letter 86-10 Evaluation, Fire Protection Evaluation for Fire Zones 11.3-1/12.1-0 and 11.3-2/12.1-0 Boundaries to Demonstrate Separation Equivalent to Branch Technical Position CMEB 9.5-1, C5.b(2), which was performed in response to the issue. The inspectors took into consideration the fact that the licensees evaluation presented evidence in support of the ability of the existing condition to prevent the spread of fire from one zone to the other. Specifically referenced was ComEd Nuclear Design Information Transmittal MSD-97-021, dated December 17, 1997, which documented the ability of steel ventilation ducts and supports of a similar design to act as an effective fire barrier for a period of 60 minutes.

The licensee entered the damper issue into their corrective action program for resolution, implemented compensatory measures that included hourly fire watches.

Analysis:

The inspectors determined that the licensees failure to maintain the firewall between the fuel handling building and the auxiliary building in accordance with the approved fire protection program was a performance deficiency warranting a significance determination. Furthermore, the issue was considered more than minor because the finding affected the attribute of protection against external factors (i.e. fire)of the Mitigating Systems Cornerstone. The inspectors assessed the finding using Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process, and determined the finding to be of very low safety significance (Green). The finding was of very low safety significance because the steel ventilation ducts would provide a minimum of 60 minutes fire endurance protection, and the fixed fire ignition sources and combustibles were positioned such that the degraded barrier would not be subject to direct flame impingement.

Enforcement:

Braidwood Stations Operating License Condition 2.E stated, in part, that The licensee shall implement and maintain in effect all provisions of the approved fire protection program as described in the UFSAR. Section 9.5.1 of the UFSAR stated that The design bases, system descriptions, safety evaluation, inspection and testing requirements, personnel qualification, and training are described in Reference 1 [the Fire Protection Report]. Section 2.3.12.1 of the Fire Protection Report stated, in part, that Fire dampers are provided in the fire wall separating the fuel handling building and the auxiliary building. Contrary to the above, the licensee failed to have installed dampers in the firewall separating the spent fuel pool heat exchanger rooms of the fuel handling building and the Unit 1 and Unit 2 containment pipe penetration areas of the auxiliary building since original construction. Because this issue was entered into the corrective action program as IR 477902, and the finding was of very low safety significance, this violation was being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000456/2006003-01; 05000457/2006003-01, Failure to Maintain Fire Barrier in Accordance with Fire Protection Program.

1R06 Flood Protection Measures

External Flooding Review

a. Inspection Scope

The inspectors reviewed Braidwoods flood analysis and design basis documents to identify design features important to external flood protection, and reviewed the external flood protection measures in place to prevent or mitigate effects of the probable maximum flood and the probable maximum precipitation. This included a general area walkdown of the outdoor plant area and perimeter to assess the condition and readiness of the various plant drainage system components to perform their function during a probable maximum flood or probable maximum precipitation scenario.

The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program. This review represented one annual inspection sample. Documents reviewed during this inspection are listed in the

.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

Annual Review

a. Inspection Scope

The inspectors reviewed the licensees program for maintenance and testing of risk-important heat exchangers in the component cooling water system. Specifically, the review included the program for performance testing and analysis of the Unit 1 component cooling water heat exchanger when RH system shutdown cooling was established during the shutdown and subsequent cooldown to Mode 5. The inspectors observed the physical condition of the heat exchanger and performance testing apparatus and reviewed previous performance trend data to validate that the frequency of cleaning and testing was sufficient to detect degradation prior to loss of heat removal capabilities below design requirements; that the inspection results were appropriately categorized against pre-established engineering acceptance criteria, including the impact of tubes plugged on the heat exchanger performance; and that the licensee had developed adequate acceptance criteria for bio-fouling controls. This review represented one inspection sample. Additional documents reviewed are listed in the

.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection (ISI) Activities

.1 Piping Systems ISI

a. Inspection Scope

From April 17, 2006, through May 5, 2006, the inspectors conducted a review of the implementation of the licensees ISI program for monitoring degradation of the reactor coolant system boundary, and the risk significant piping system boundaries for Unit 1.

The inspectors selected the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Section XI required examinations and Code components in order of risk priority as identified in Section 71111.08-03 of the inspection procedure, based upon the ISI activities available for review during the onsite inspection period.

For the following two types of nondestructive examination (NDE) activities the inspectors:

  • observed ultrasonic test examination (UT) of the following welds to evaluate compliance with the ASME Code Section XI requirements and to verify that indications and defects (if present) were dispositioned in accordance with the ASME Code Section XI:
  • pressurizer shell-to-nozzle weld (N4A), nozzle inner radius, and upper shell welds (8E and 9D);
  • reviewed dye penetrant examination report for a penetration-to-pipe weld (1SI-21-09) to evaluate compliance with the ASME Code Section XI and Section V requirements and to verify that indications and defects (if present)were dispositioned in accordance with the ASME Code Section XI requirements.

The inspectors reviewed relevant indications (leakage) identified during a Code visual examination (VT)-2 from the previous outage at the excess letdown heat exchanger flanges to determine if the licensees corrective actions and extent of condition reviews were in accordance with the ASME Code Section XI requirements.

The inspectors reviewed pressure boundary weld records for replacement of a 2 inch diameter safety injection system check valve (1SI-8819D) completed during the previous refueling outage, to determine if the welding acceptance and preservice examinations (e.g., pressure testing, visual, dye penetrant, and weld procedure qualification tensile tests and bend tests) were performed in accordance with ASME Code Sections III, V, IX, and XI requirements.

The inspectors performed a review of ISI related problems that were identified by the licensee and entered into the corrective action program, conducted interviews with licensee staff, and reviewed licensee corrective action records to determine if:

  • the licensee had described the scope of the ISI related problems;
  • the licensee had established an appropriate threshold for identifying issues;
  • the licensee had evaluated industry generic issues related to ISI and pressure boundary integrity; and
  • the licensee implemented appropriate corrective actions.

The inspectors performed these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action documents reviewed by the inspectors are listed in the Attachment to this report.

The reviews as discussed above counted as one inspection sample.

b. Findings

No findings of significance were identified.

.2 Pressurized Water Reactor Vessel Head Penetration (VHP) ISI

a. Inspection Scope

The inspectors did not perform a review of this procedure section (reduction in one inspection sample), because it is not required to be implemented until after completion of Temporary Instruction (TI) 2515/150, Reactor Pressure Vessel Head and Vessel Head Penetration Nozzles. Note that TI 2515/150 was implemented during this inspection.

b. Findings

No findings of significance were identified.

.3 Boric Acid Corrosion Control (BACC) ISI

a. Inspection Scope

From April 16, 2006, through April 27, 2006, the inspectors reviewed the Unit 1 BACC inspection activities conducted pursuant to licensee commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary.

The inspectors observed the licensee conducting a walkdown of borated systems within the Unit 1 containment outside the missile barrier. The scope of this walkdown included a bare metal visual examination of the reactor vessel closure head and vessel head penetrations from access doors on the service structure. The inspectors observed the licensee during these examinations to evaluate compliance with licensee BACC program requirements and 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action requirements. In particular, the inspectors performed this observation to determine if the licensee focused BACC inspections on locations where boric acid leaks can cause degradation of safety significant components and to determine if degraded or non-conforming conditions were properly identified in the licensees corrective action system.

The inspectors reviewed corrective actions and evaluations performed for boric acid found on reactor coolant system connected piping and components to confirm that corrective actions were consistent with requirements of Section XI of the ASME Code and 10 CFR Part 50, Appendix B, Criterion XVI, and that the minimum Code required section thickness had been maintained for the affected components. In particular, this review focused on licensee corrective actions (reference IR 480489) implemented in response to identification of boric acid deposits on insulation and at four heater tube locations on the bottom of the Unit 1 pressurizer.

The documents reviewed during this inspection are listed in the Attachment to this report. The reviews as discussed above counted as one inspection sample.

b. Findings

No findings of significance were identified.

.4 Steam Generator (SG) Tube ISI

a. Inspection Scope

From April 21, 2006, through April 27, 2006, the inspectors performed an on-site review of SG tube examination activities conducted pursuant to TS and the ASME Code Section XI requirements.

The NRC inspectors observed acquisition of eddy current test (ET) data, interviewed ET data analysts, observed in-situ pressure testing of degraded tubes and reviewed documents related to the SG ISI program to determine if:

  • in-situ SG tube pressure testing screening criteria and the methodologies used to derive these criteria were consistent with the Electric Power Research Institute (EPRI) TR-107620, SG In-Situ Pressure Test Guidelines;
  • in-situ pressure testing performance criterial were met for degraded tubes tested in SG A and SG B;
  • the in-situ SG tube pressure testing screening criteria were properly applied in terms of SG tube selection based upon evaluation of the list of tubes with measured/sized flaws;
  • the numbers and sizes of SG tube flaws/degradation identified was bound by the licensees previous outage Operational Assessment predictions;
  • the SG tube ET examination scope and expansion criteria were sufficient to identify tube degradation based on site and industry operating experience by confirming that the ET scope completed was consistent with the licensees procedures, plant TS requirements and EPRI 1003138, Pressurized Water Reactor SG Examination Guidelines, Revision 6;
  • the SG tube ET examination scope included tube areas which represent ET challenges such as the tubesheet regions, expansion transitions, and support plates;
  • the licensee identified new tube degradation mechanisms;
  • the licensee implemented repair methods which were consistent with the repair processes allowed in the plant TS requirements;
  • the licensee primary-to-secondary leakage (e.g., SG tube leakage) was below the detection threshold during the previous operating cycle;
  • the licensee did an evaluation for unretrievable loose parts;
  • the ET probes and equipment configurations used to acquire data from the SG tubes were qualified to detect the known/expected types of SG tube degradation in accordance with Appendix H, Performance Demonstration for Eddy Current Examination, of EPRI 1003138, Pressurized Water Reactor SG Examination Guidelines, Revision 6; and
  • the licensee identified deviations from ET data acquisition or analysis procedures.

The inspectors performed a review of SG ISI related problems that were identified by the licensee and entered into the corrective action program, conducted interviews with licensee staff and reviewed licensee corrective action records to determine if:

  • the licensee had described the scope of the SG related problems;
  • the licensee had established an appropriate threshold for identifying issues;
  • the licensee had evaluated industry generic issues related to SG tube integrity; and
  • the licensee implemented appropriate corrective actions.

The inspectors performed these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action documents reviewed by the inspectors are listed in the Attachment to this report.

The reviews as discussed above counted as one inspection sample.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

Quarterly Review of Testing/Training Activity

a. Inspection Scope

The inspectors observed operating crew performance during an evaluated simulator out-of-the-box scenario involving multiple solid state protection system input bistable failures requiring plant shutdown, with subsequent fuel failure during unit ramp down.

The inspectors evaluated crew performance in the following areas:

  • clarity and formality of communications;
  • ability to take timely actions in the safe direction;
  • prioritization, interpretation, and verification of alarms;
  • procedure use;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • group dynamics.

Crew performance in these areas was compared to licensee management expectations and guidelines.

The inspectors verified that the crew completed the critical tasks listed in the simulator guide. The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed the licensee evaluators to determine whether they also noted the issues and discussed them in the critique at the end of the session. Documents reviewed are listed in the Attachment.

This review constituted one sample of this inspection requirement.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

Routine Inspection

a. Inspection Scope

The inspectors reviewed the licensees overall maintenance effectiveness for selected plant systems. This evaluation consisted of the following specific activities:

  • observing the conduct of planned and emergent maintenance activities where possible;
  • reviewing selected IRs, open work orders, and control room log entries in order to identify system deficiencies;
  • reviewing licensee system monitoring and trend reports;
  • attending various meetings throughout the inspection period where the status of maintenance rule activities was discussed;
  • a partial walkdown of the selected system; and
  • interviews with the appropriate system engineer.

The inspectors also reviewed whether the licensee properly implemented Maintenance Rule, 10 CFR 50.65, for the chosen systems. Specifically, the inspectors determined whether:

  • performance problems constituted maintenance rule functional failures;
  • the system had been assigned the proper safety significance classification;
  • the system was properly classified as (a)(1) or (a)(2); and
  • the goals and corrective actions for the system were appropriate.

The above aspects were evaluated using the maintenance rule program and other documents listed in the Attachment. The inspectors also verified that the licensee was appropriately tracking reliability and/or unavailability for the systems.

The inspectors completed two samples in this inspection requirement by reviewing the following systems:

  • 0A and 0B control room ventilation trains subsequent to a fuse failure resulting in a maintenance rule functional failure; and
  • Unit 1 and Unit 2 main power systems subsequent to an increasing trend in licensee identified main power transformer deficiencies.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensees management of plant risk during emergent maintenance activities or during activities where more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety-significant equipment. The inspections were conducted to determine whether evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate.

The licensees daily configuration risk assessment records, observations of operator turnover and plan-of-the-day meetings, and observations of work in progress, were used by the inspectors to verify that; the equipment configurations were properly listed; protected equipment were identified and were being controlled where appropriate; work was being conducted properly; and significant aspects of plant risk were being communicated to the necessary personnel. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program.

In addition, the inspectors reviewed selected issues, listed in the Attachment, that the licensee encountered during the activities, to determine whether problems were being entered into the corrective action program with the appropriate characterization and significance.

The inspectors completed six samples by reviewing the following activities:

  • delayed return to service of 1B DG following pushrod replacement;
  • 1B RH train outage due to overhaul of recirculation sump isolation valve operator 1SI8811B;
  • Unit 0 component cooling water heat exchanger outage, which results in dual unit yellow risk condition;
  • 2B DG outage for periodic engine and generator overhaul; and
  • 2A CS pump mechanical seal replacement following gross leakage during initial post maintenance testing.

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Evolutions and Events

a. Inspection Scope

The inspectors completed one sample by observing and/or reviewing operator performance during the Unit 2 25B feedwater heater drain cooler relief valve failure on April 6, 2006.

The inspectors observed the control room response, interviewed plant operators and reviewed plant records including control room logs, operator turnovers, and IRs. The inspectors verified that the control room operators response was consistent with station procedures and that identified discrepancies were captured in the corrective action program.

The inspectors verified that minor issues identified during this inspection were entered into the licensees corrective action program. Documents reviewed as part of this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors evaluated plant conditions and selected IRs for risk-significant components and systems in which operability issues were questioned. These conditions were evaluated to determine whether the operability of components was justified. The inspectors compared the operability and design criteria in the appropriate section of the UFSAR to the licensees evaluations presented in the IRs and documents listed in the Attachment to verify that the components or systems were operable. The inspectors also conducted interviews with the appropriate licensee system engineers and conducted plant walkdowns, as necessary, to obtain further information regarding operability questions. Documents reviewed as part of this inspection are listed in the

.

The inspectors completed three samples by reviewing the following operability evaluations and conditions:

  • repeated cracking of reactor containment fan cooler (RCFC) turning vanes;
  • elevated spent fuel pool temperature conditions.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance testing activities associated with important mitigating systems, barrier integrity, and support systems to ensure that the testing adequately demonstrated system operability and functional capability. The inspectors used the appropriate sections of the TS and UFSAR, as well as the Work Orders for the work performed, to evaluate the scope of the maintenance and to determine whether the post-maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. The inspectors determined whether the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. The activities were selected based on their importance in demonstrating mitigating systems capability and barrier integrity. Documents reviewed as part of this inspection are listed in the Attachment.

Six samples were completed by observing post-maintenance testing of the following components:

  • 1B DG start-up subsequent to engine pushrod replacement;
  • 1SI8811B valve automatic actuation testing subsequent to motor operator maintenance;
  • 1MS018D 1D SG power operated relief valve stroke testing subsequent to valve work outage;
  • Unit 0 component cooling water heat exchanger leak check and operation subsequent to piping replacement of tube side vent lines;
  • 2A component cooling water pump ASME run subsequent to pump motor replacement and re-balance; and
  • 2B DG fast start and engine power factor testing subsequent to 6 year engine and generator overhaul.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 1 refueling outage, conducted April 16 - May 3, 2006, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth.

During the refueling outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program. Documents reviewed during the inspection are listed in the Attachment. This inspection constituted one sample.

This inspection included:

  • initial walkdown of containment to look for evidence of reactor coolant system leakage and other discrepancies;
  • review of licensee configuration management, including maintenance of defense-in-depth commensurate with the Outage Safety Plan for key safety functions and compliance with the applicable TS when taking equipment out of service;
  • observation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing;
  • review of the installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and an accounting for instrument error;
  • review of the licensees controls over the status and configuration of electrical systems to ensure that TS and outage safety plan requirements were met, and controls over switchyard activities;
  • review of the licensees controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system;
  • monitoring reactor water inventory controls including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss;
  • monitoring the licensees controls over activities that could affect reactivity;
  • observation and review of refueling activities, including fuel handling;
  • observation and review of startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the primary containment to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing; and
  • monitoring and review of licensee identification and resolution of problems related to refueling outage activities.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed surveillance testing activities associated with important mitigating systems, barrier integrity, and support systems to ensure that the testing adequately demonstrated system operability and functional capability. The inspectors used the appropriate sections of the TS and UFSAR to determine whether the surveillance testing was performed adequately and that operability was restored. The inspectors determined whether the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. The activities were selected based on their importance in demonstrating mitigating systems capability, barrier integrity and the initiating events cornerstone. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program. Documents reviewed as part of this inspection are listed in the Attachment.

Six samples were completed by observing and evaluating the following surveillance tests:

  • OB fire protection pump flow and pressure test;
  • 2B DG slave relay 611B fast start and engine overspeed testing; and

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the installation of temporary storage tanks for liquid radwaste processing.

For the above modification, the inspectors reviewed the associated design change paperwork, performed a walkdown of the tanks and associated piping; observed the transfer of liquid radwaste to the tanks and discussed radiological and environmental controls with applicable engineering, operations, and radiation protection staff. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program. Those documents reviewed during this inspection are listed in the Attachment. This review constituted one sample of this inspection requirement.

b. Findings

No findings of significance were identified, however, a minor violation associated with this temporary modification was described in Section 4OA2.2 of this report.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed licensee performance during one crew emergency preparedness drill on the simulator and one site emergency preparedness drill on the simulator and Technical Support Center for a total of two samples. The inspectors observed event classification, notification, and development of protective action recommendations, manning of the emergency response facilities, and turnover of command and control. The inspectors also observed portions of the post drill critiques to determine whether their observations were also identified by the licensee evaluators and reviewed documents listed in the Attachment to determine whether deficiencies were entered into the licensees corrective action system.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstones: Occupational Radiation Safety and Public Radiation Safety 2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone

a. Inspection Scope

The inspectors discussed performance indicators with the radiation protection staff and reviewed data from the licensees corrective action program to determine if there were any performance indicator occurrences in the occupational exposure cornerstone that had not been reported or reviewed. The inspector limited this review to incidents occurring since the last inspection in this area, (June 2005). The inspectors verified that minor issues identified during this inspection were entered into the licensees corrective action program. Documents reviewed during this inspection are listed in the

. This review represented one sample.

b. Findings

No findings of significance were identified.

.2 Plant Walkdowns, Observation of Radiological Access Controls and Radiation Work

Permits

a. Inspection Scope

The inspectors selected several radiologically significant activities for further review.

These activities included those having significant total exposure estimates and/or being performed in high radiation or potential airborne areas in the plant. Selected work packages and radiation work permits (RWPs) were reviewed to determine if appropriate controls (i.e., surveys, postings and barricades) were being used. This review represented one sample.

The inspectors performed a walkdown of radiological controlled areas in the auxiliary building and Unit 1 containment, to observe whether licensee surveys were complete and accurate and whether radiological areas were properly posted. For selected activities, the inspectors reviewed RWPs, and observed ongoing work to determine if areas of significant radiological concern, (such as hot spots or higher dose rate areas)were properly identified. Several workers were also interviewed to verify that they understood the RWP requirements and radiological conditions in their work area. This review represented one sample.

The inspectors performed a walkdown of selected high radiation areas and all areas currently being controlled as a locked or very high radiation area. This walkdown included the auxiliary building and Unit 1 containment, but not the Unit 2 containment.

Specifically, the inspectors observed whether postings and barriers were properly used to control access to these areas. The inspectors also selectively observed whether electronic dosimetry was properly used by workers in these areas and, through interviews, whether the workers were aware of the dosimetry alarm setpoints and access control requirements. Site TSs and the following station procedures were used as standards for the appropriate barriers and controls:

  • RP-AA-376, Radiological Postings, Labeling, and Markings, Revision 1; and
  • RP-AA-376-1001, Radiological Posting, Labeling, and Marking Standard, Revision 3.

This review represented one sample.

The inspectors reviewed the following activities and evaluated the radiological controls to determine whether workers were adequately protected against airborne contamination:

  • reactor cavity decontamination;
  • under pressurizer weld examination and No.15 heater removal; and

These activities were selected as they had the potential for workers to receive an internal exposure of greater than 50 millirem committed effective dose equivalent. The inspectors reviewed the associated as-low-as-is-reasonably-achievable (ALARA) plans and RWPs, and observed work activities to evaluate whether engineering controls, (such as high efficiency particulate air filtration and respirators) were appropriately considered and used. Field observations were also used to verify that air samplers were appropriately placed and operational. Documents reviewed are listed in the Attachment.

This review represented one sample.

b. Findings

No findings of significance were identified.

.3 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed a recently completed licensee self-assessment that focused on high radiation area controls and reviewed condition reports generated since the last inspection (June 2005), related to access control or high radiation area incidents, to determine if identified problems were being entered into the licensees corrective action program. This review represented one sample.

Issue reports related to access controls or high radiation area incidents were reviewed to determine if they were being properly evaluated. Specifically, the issue reports were reviewed against the following criteria:

  • initial problem identification and screening;
  • disposition of potential operability/reportability issues;
  • evaluation of safety significance and/or risk;
  • identification of cause; and
  • implementation of corrective actions.

This review also considered whether recurring events or adverse trends were properly evaluated and addressed. Documents reviewed are listed in the Attachment. This review represented one sample.

b. Findings

No findings of significance were identified.

.4 Radiation Worker Performance and Radiation Protection Technician Proficiency

a. Inspection Scope

During job performance observations the inspectors evaluated radiation worker performance with respect to stated RWP work requirements. Specifically, whether workers were aware of the radiological hazards present and whether they were properly utilizing those controls implemented to protect against such hazards. This review represented one sample.

During walkdowns of the auxiliary building and Unit 1 containment, the inspectors evaluated radiation protection technician performance. Specifically, the inspectors determined if technicians adequately covered work activities, performed radiological surveys and briefed workers on radiological conditions. The inspectors also interviewed several technicians to verify that RWP requirements were well understood. This review represented one sample.

Documents reviewed as part of this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

2OS2 As-Low-As-Is-Reasonably-Achievable Planning and Controls (71121.02)

.1 Radiological Work Planning

a. Inspection Scope

The inspectors reviewed the following Unit 1 work activities to determine the efficacy of the licensees ALARA planning:

  • reactor head disassembly/reassembly;
  • snubber removal, inspection and testing;
  • scaffold staging, building and removal;
  • pressurizer boric acid inspection and cleaning; and
  • replacement of the No. 15 pressurizer heater.

These activities were selected based on their estimated total exposure, potential for significant radiological conditions (airborne, work in high radiation areas, etc.) and potential for emergent activities. The inspectors used the guidance contained in licensee procedures RP-AA-400, ALARA Program, Revision 3 and RP-AA-401, Operational ALARA Planning and Controls, Revision 5, as the criteria for the review.

The inspectors evaluated whether the RWPs were consistent with the associated ALARA plans for the above activities. In particular, whether electronic dosimeter dose and dose rate alarm setpoints were appropriate given the expected work area radiological conditions. Additionally, the inspectors noted whether engineering controls credited in the ALARA plan were appropriately captured in the RWP. The inspectors also observed whether the RWP and ALARA plan requirements were properly communicated during pre-job briefings. This review represented one sample.

The inspectors compared the actual dose received against the estimated dose for the above ALARA plans. These comparisons were made to gauge the accuracy of the licensees dose estimates based on knowledge of the work activity. Specifically, whether the licensee properly used previous work history and/or information from other work groups (such as man-hour estimates) in dose estimates. The inspectors also reviewed work-in-progress and post job reviews. Reasons for inconsistencies between the actual and intended dose were discussed with radiation protection staff to determine whether the differences resulted from radiation controls or job planning. This review represented one sample.

The inspectors evaluated the licensees dose reduction strategies utilized in the above ALARA plans. In particular, whether shielding from water filled components and piping, job scheduling and coordination with shielding and scaffold installation and removal were considered. Temporary shielding requests were also evaluated with respect to dose rate reduction, along with engineering shielding responses follow-up. Documents reviewed are listed in the Attachment. This review represented one sample.

b. Findings

No findings of significance were identified.

.2 Job Site Inspection and ALARA controls

a. Inspection Scope

Electronic dose reports from workers involved in the activities reviewed under Section

.1 above, were reviewed to determine if there were any significant exposure variations.

Specifically, these variations were evaluated to determine if they were caused by poor ALARA work practices or by differences in job skill assignments. These evaluations also consisted of observing selected work activities to monitor worker performance.

Documents reviewed are listed in the Attachment. This review represented one sample.

b. Findings

No findings of significance were identified.

.3 Source Term Reduction and Control

a. Inspection Scope

The inspectors reviewed the source term reduction actions implemented by the licensee for the Unit 1 refueling outage. These actions included hydrogen peroxide addition, reactor coolant filtration and hydrolazing. The effectiveness of these actions were, in part, evaluated by comparing the observed average plant dose rates from the current outage to historical trends. The effectiveness of these actions on those work activities observed by the inspectors were also considered. The plant source term (including input mechanisms) and overall mitigation strategies were discussed with radiation protection staff. Documents reviewed are listed in the Attachment. This review represented one sample.

b. Findings

No findings of significance were identified.

.4 Declared Pregnant Workers

a. Inspection Scope

The inspectors reviewed the licensees program for monitoring the exposure of declared pregnant workers. This program was described in RP-AA-270, Prenatal Radiation Exposure, Revision 3. The inspectors determined whether the program was consistent with the requirements of 10 CFR 20.1208. There were no declared pregnant workers during this assessment period. Documents reviewed are listed in the Attachment. This review represented one sample.

b. Findings

No findings of significance were identified.

.5 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the following licensee self-assessments:

  • source term reduction, dated June 2004; and
  • SG outage ALARA report for A2R11, dated Spring 2005 The inspectors also reviewed condition reports generated since the last inspection (June 2005), related to ALARA planning or source term reduction, to determine if identified problems were being entered into the licensees corrective action program.

This review represented one sample.

The inspectors determined if identified problems were being entered into the corrective action program for resolution. This included dose significant work-in-progress and post-job reviews of exposure performance. This review represented one sample.

Issue reports related to the ALARA program were reviewed to determine if they were being properly evaluated. Specifically, the issue reports were reviewed against the following criteria:

  • initial problem identification and screening;
  • disposition of potential operability/reportability issues;
  • evaluation of safety significance and/or risk;
  • identification of cause; and
  • implementation of corrective actions.

This review also considered whether recurring events or adverse trends were properly evaluated and addressed. This review represented one sample.

Documents reviewed as part of this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems (71122.01)

Tritiated Liquid Discharge Storage, Monitoring, and Remediation

a. Inspection Scope

As discussed previously in Inspection Reports 05000456/2005010; 05000457/2005010; Section 4OA3.1, and 05000456/2006002; 05000457/2006002; Section 4OA3.1, the inspectors continued to monitor the licensee activities resulting from previous inadvertent leaks of tritiated liquid from the blowdown line to the Kankakee River. This inspection was not considered a complete sample. The inspection activities included completion or review of the following:

Temporary Storage of Liquid

  • results of licensee fixed rear axil container (FRAC) tank inspections;
  • safety evaluation of installation of FRAC tanks; and
  • several walkdowns of FRAC tank installation and transfer hoses.

Mitigation of Previous Spills

  • disposal of water from vacuum breaker vaults and off-site cistern;
  • installation of concrete bottoms and waterproof membranes in vacuum breaker vaults;
  • installation of isolation/throttle valve at river end of blowdown line;
  • tie-in of pond pumping pipe to blowdown line in vacuum breaker #2 vault;
  • installation and testing of vacuum breaker vault leakage alarms;
  • installation and testing of pond pump;
  • installation and testing of the pond pumping composite sampler;
  • implementation of state injunction order;
  • response to vacuum breaker water alarms;
  • startup and operation of pond pumping system;
  • procedures for obtaining composite samples of pumped pond water; and
  • several inspections of vacuum breaker vaults during pumping operations.

Response to New Spills

  • 25B drain cooler relief valve lift on April 6, 2006;
  • small spill from auxiliary boiler test line on May 15, 2006;
  • procedures for monitoring waste water discharges to the cooling lake; and
  • procedures for spill notification.

In addition, the inspectors attended and presented information at several meetings, hosted by the licensee, for interested community members, and accompanied public officials on tours of the affected areas. The inspectors also obtained numerous split water samples from the licensee and sent them to an independent laboratory for analysis. The inspectors verified that minor issues identified during this inspection were entered into the licensees corrective action program. Documents reviewed as part of this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified, however, a minor violation associated with temporary modification that installed the FRAC tanks was described in Section 4OA2.2 of this report.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

Cornerstone: Mitigating Systems

The inspectors reviewed the document listed in the Attachment to verify that the licensee had correctly reported Performance Indicator data, in accordance with the criteria in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 2. The data reported by the licensee was compared to a sampling of control room logs, IRs, Licensee Event Reports, and other sources of data generated since the last verification. The inspectors completed two samples by reviewing the following Performance Indicators:

  • Unit 1 safety system functional failures from July 1, 2004, through March 31, 2006; and
  • Unit 2 safety system functional failures from July 1, 2004, through March 31, 2006.

Cornerstone: Barrier Integrity

The inspectors reviewed the documents listed in the Attachment to verify that the licensee had correctly reported Performance Indicator data, in accordance with the criteria in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 2. The data reported by the licensee was compared to a sampling of control room logs, chemistry records, surveillance records, and other sources of data generated since the last verification. The inspectors verified that minor issues identified during this inspection were entered into the licensees corrective action program. The inspectors completed four samples by reviewing the following Performance Indicators:

b. Findings

No findings of significance were identified.

Note that this inspection covered data reported for about 2 years since the inspection requirement was waived in 2005.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to determine whether they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action program as a result of the inspectors observations are generally denoted in the Attachment. These activities were part of normal inspection activities and were not considered separate samples.

b. Findings

No findings of significance were identified.

.2 Annual Sample - Issues Related to Temporary Storage of Liquid Radioactive Waste

Introduction The inspectors reviewed the adequacy of the licensees corrective actions, prioritization, and evaluation of issues related to the onsite, temporary storage of liquid radioactive waste. The liquid was being stored in temporary tanks commonly referred to as FRAC tanks. Temporary storage was required following the suspension of routine liquid radioactive waste discharges after discovery of leaks from the circulating water blow down line. The issues associated with the blowdown line leaks, including the discovery, licensee actions, and the results of an NRC inspection are documented in NRC Inspection Reports 05000456/2005010, 05000457/2005010, 05000456/2006002, 05000457/2006002, 05000456/2006008(DRS) and 05000457/2006008(DRS). The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program. Those documents reviewed during this inspection are listed in the Attachment. This activity completed one sample.

Observations The inspectors assessed the licensees evaluation, including the review performed in accordance with 10 CFR Part 50.59, Changes, Tests and Experiments. The inspectors determined that the licensees conclusion, This activity does not need NRC approval prior to implementation, was appropriate. The inspectors assessment also determined that the installation of the FRAC tanks did not comply with Regulatory Guide 1.143, Revision 0, however the licensee had already reached that conclusion prior to the onsite portion of this inspection.

On April 13, 2006, the licensees Nuclear Oversight group determined that Revision 0 of the 10 CFR 50.59 review failed to address Regulatory Guide 1.143. The observation was documented in the licensees corrective action system and subsequent revisions to the 10 CFR 50.59 review did address Regulatory Guide 1.43.

The original 10 CFR 50.59 review failed to recognize that the commitment to follow Regulatory Guide 1.143, Revision 0, was explicitly described in the UFSAR and therefore the guidance contained in the regulatory guide needed to be addressed.

Based on the inspectors review, it was determined that the initial 10 CFR 50.59 review was inadequate since it failed to address the commitment to Regulatory Guide 1.143.

The safety significance of the noncompliance with Regulatory Guide 1.143 was minor because the licensees revision to the 10 CFR 50.59 that addressed Regulatory Guide 1.143 concluded that NRC approval was still not required. Specifically, the licensees revision to the 10 CFR 50.59 review addressed the aspects of the regulatory guide that were not being met. The new 10 CFR 50.59 provided sufficient basis or compensatory actions to conclude that the installation of the temporary storage tanks did not require prior NRC approval in accordance with 10 CFR 50.59. The inspectors reviewed the revised 10 CFR 50.59 evaluation and acknowledged that the licensee appropriately determined that prior NRC approval was not required. Therefore, this issue constituted a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the Enforcement Policy.

.3 Semiannual Review to Identify Trends

a. Inspection Scope

The inspectors performed a review of the licensees Corrective Action Program (CAP)and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment and corrective maintenance issues but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1. An issue report trend review focused on systems important to risk according to the licensees probabilistic risk assessment model was performed for main power, component cooling water, instrument/service air, circulating water, switchyard, essential service water, reactor cooling, auxiliary feedwater, pressurizer, and safety injection systems. The review also included issues documented outside the normal CAP including focus area self assessments, corrective maintenance backlog reports, common cause analysis reports, component status reports, and maintenance rule assessments. The inspectors review nominally considered the 6-month period of January through June 2006, although some examples expanded beyond those dates when the scope of the trend warranted. The inspectors compared and contrasted their results with the results contained in the licensees mechanisms for identifying and correcting trends. Corrective actions associated with a sample of the issues identified by the licensee were also reviewed for adequacy.

Specific documents reviewed are listed in the Attachment.

b.

Assessment and Observations Overall the inspectors review noted that the licensee aggressively identified trends through diverse means. System level trends were routinely identified by system engineering through the sites CAP. Programmatic trends were generally identified in a timely manner by nuclear oversight, operations, or engineering through the focus area self assessment process or via the CAP. The inspectors daily issue report review along with the documents reviewed specifically for this sample did not indicate the existence of a trend not previously identified by the licensee.

4OA5 Other Activities

.1 Reactor Pressure Vessel Head and VHP Nozzles (TI 2515/150)

a. Inspection Scope

On February 11, 2003, the NRC issued Order EA-03-009 (ADAMS Accession Number ML030410402). This order required examination of the reactor vessel closure head (RVCH) and associated VHP nozzles to detect primary water stress corrosion cracking (PWSCC) of VHP nozzles and corrosion of the vessel head. The purpose of TI 2515/150, Reactor Pressure Vessel Head and Vessel Head Penetration Nozzles, was to implement an NRC review of the licensee's head and VHP nozzle inspection activities required by NRC Order EA-03-009.

The inspectors performed a review in accordance with TI 2515/150 of the licensees procedures, equipment, and personnel used for examinations of the RVCH and VHP nozzles to confirm that the licensee met requirements of NRC Order EA-03-009 (as revised by NRC letter dated February 20, 2004). The results of the inspectors review included documentation of observations in response to the questions identified in TI 2515/150.

From April 19, 2006, through April 24, 2006, the inspectors performed a review of the licensees RVCH inspection activities completed in response to NRC Order EA-03-009.

This review included:

  • observation of the licensee personnel conducting automated UT and ET of VHP nozzle locations from the on-site data acquisition trailer;
  • interviews with NDE personnel performing examinations of the RVCH and VHP nozzles from an on-site trailer;
  • certification records of NDE personnel performing examinations of the RVCH and VHP nozzles;
  • UT and ET examination procedures used for examinations of the RVCH and VHP nozzles;
  • procedures used for identification and resolution of boric acid leakage from systems and components above the vessel head;
  • the licensees procedures and corrective actions for boric acid leakage; and
  • UT and ET examination records for the RVCH and VHP nozzles.

The inspectors conducted these reviews to confirm that the licensee performed the vessel head examinations in accordance with requirements of NRC Order EA-03-009, using procedures, equipment, and personnel qualified for the detection of PWSCC in vessel VHP nozzles and detection of vessel head wastage.

From April 17, 2006, through April 26, 2006, the inspectors reviewed the licensees VHP nozzle susceptibility ranking calculation to:

  • verify that appropriate plant-specific information was used as input;
  • confirm the basis for the head temperature used by licensee; and
  • determine if previous VHP cracks had been identified, and if so, documented in the susceptibility ranking calculation.

The documents reviewed by the inspectors in conducting this inspection are listed in the to this report.

b.

Observations Summary: At of the end of operating cycle No. 12, the Braidwood Unit 1 vessel head was at 2.2 effective degradation years (EDY), which is in the low susceptibility ranking category as described in NRC Order EA-03-009. To meet the inspection requirements of Order EA-03-009, the licensee completed automated UT and ET examinations for each of the 78 VHP nozzles and head vent line. The licensee identified nine vessel head penetrations with minor limitations in the volumetric examination coverage below the J-groove weld required by Order EA-03-009. Additionally, at the inside surface of VHP nozzle No. 74 a surface anomaly was identified, which limited examination coverage in an area above the J-groove weld. The inspectors were also concerned that the disrupted metal area at the inside surface of VHP nozzle No. 74 may require further evaluations to determine if it could facilitate the onset of PWSCC. Following restart of Unit 1, the licensee intended to request relaxation from the Order to accept the VHP nozzles with limited examinations.

Overall, the inspectors concluded that the licensee had completed an examination of the reactor vessel head using methods which were consistent with the requirements of Order EA-03-009. The inspectors responses and conclusions to specific questions identified in TI-2515/150 related to the quality of personnel, procedures, and equipment used to perform the vessel head examination are discussed below. The inspectors could not independently confirm the ability of some of the NDE techniques to detect PWSCC. This condition reflected a lack of industry or vendor qualified techniques and did not represent a deviation from NRC Order EA-03-009, which did not specify qualification or demonstration standards for the NDE techniques used. Additionally, the inability to identify PWSCC within the J-groove weld is consistent with the requirements of Order EA-03-009, which does not require examination of the J-groove welds when UT of the nozzle base material has been completed.

Evaluation of Inspection Requirements In accordance with the reporting requirements contained within TI 2515/150, Revision 3, the inspectors evaluated and answered the following questions:

a.

For each of the examination methods used during the outage, was the examination:

1. Performed by qualified and knowledgeable personnel?

Yes. The licensees vendor NDE staff that performed the automated UT and ET examinations were certified to a level II or level III for these examinations. The licensee vendor certified their NDE staff in accordance with vendor Procedures WDP-9.2, Qualification and Certification of Personnel in Nondestructive Examination and accepted subcontracted NDE staff qualified to different recommended practices which met industry standard ANSI/ASNT CP-189-1991 ASNT Standard for Qualification and Certification of Nondestructive Testing Personnel.

2. Performed in accordance with demonstrated procedures?

Yes. The licensees vendor performed automated UT and ET of VHP nozzles in accordance with Procedure WDI-UT-010, Intraspect Ultrasonic Procedure for Inspection of Reactor Vessel Head Penetrations, Time of Flight Ultrasonic, Longitudinal Wave, and Shear Wave, Revision 12. The vendor performed these examinations from the inside nozzle surface using probes which contained UT and ET equipment configurations which were consistent with those used during vendor mockup testing. This procedure identified a number of UT probes which could be used for this examination, but it did not identify the specific probes or equipment settings which had been demonstrated. For the Braidwood Unit 1 vessel head examination, the inspectors verified that the vendor used UT probes, frequencies, and angles that were consistent with that used in the demonstration.

The licensees vendor had demonstrated an earlier version of procedure WDI-UT-010 on mockup VHP nozzles which contained cracks or simulated cracks as documented in EPRI MRP-89, Materials Reliability Program Demonstrations of Vendor Equipment and Procedures for the Inspection of Control Rod Drive Mechanism Head Penetrations. The inspectors reviewed the summary of changes up through Revision 12 of Procedure WDI-UT-010 from Revision 3, which had been demonstrated as documented in EPRI MRP-89, to ensure that any equipment configuration changes did not affect flaw detection capability.

Additionally, the inspector reviewed the vendors technical justifications for changes in equipment configurations (e.g., changes in cable length, or eddy current probe frequencies) that could affect detection capability. These supporting vendor technical documents reviewed during this inspection are listed in the Attachment to this report.

3. Able to identify, disposition, and resolve deficiencies and capable of

identifying the PWSCC and/or head corrosion phenomena described in Order EA-03-009?

Automated UT/ET of VHP Nozzles Equipped with a Thermal Sleeve Yes. The licensees vendor examined the 55 sleeved control rod drive VHP nozzle base metal using a Trinity Blade Probe from the inside surface of the nozzles. The Trinity Blade Probe contained a time-of-flight-diffraction UT transducer, a zero degree UT transducer, and an ET coil designed to optimize detection of both circumferential and axial oriented flaws. The UT portion of this probe was also configured to detect leakage paths in the shrink fit region between the VHP nozzle tube and the reactor vessel head material. The licensees vendor had detected PWSCC in VHP nozzles at Beaver Valley Unit 1 as documented in PVP2004-2555, Advanced Nondestructive Examination Technologies for Alloy 600 Components, using this examination technique. The licensee had also detected simulated flaws in VHP mockups as documented in EPRI MRP-89 using this technique. Therefore, the inspectors concluded that this examination would have been effective for detection of PWSCC in the Braidwood Unit 1 VHPs.

Automated UT/ET of VHP Nozzles without a Thermal Sleeve Yes. The licensees vendor examined the 23 unsleeved control rod drive VHP nozzle base metal using a rotating probe from the inside surface. This probe contained time-of-flight-diffraction UT transducer pairs, zero degree UT transducers, and ET coils designed to optimize detection of both circumferential and axial oriented flaws. The UT portion of this probe was also configured to detect leakage paths in the shrink fit region between the VHP nozzle tube and the reactor vessel head material. The licensees vendor had detected PWSCC in VHP nozzles at Beaver Valley Unit 1 as documented in PVP2004-2555, Advanced Nondestructive Examination Technologies for Alloy 600 Components, using this examination technique. The licensee had also detected simulated flaws in VHP mockups as documented in EPRI MRP-89 using this technique. Therefore, the inspectors concluded that this examination would have been effective for detection of PWSCC in the Braidwood Unit 1 VHPs.

Vent Line Penetration ET Unknown. The licensees vendor used probes containing an array of ET coils to examine the inside of the head vent line and vent line VHP nozzle J-groove weld. This technique had been used on a vendor mockup and on a calibration standard which both contained electric discharge machined notches. Because this demonstration did not include actual or closely simulated PWSCC type flaws, the inspectors could not independently confirm that this examination would have been effective at detection of PWSCC. Additionally, this equipment was not equipped with ET probes which could detect outside diameter initiated circumferentially oriented cracking.

VHP Nozzle J-Groove Welds No. The licensees vendor examinations of the VHP nozzle base material were not designed to detect PWSCC contained entirely within the VHP nozzle J-groove welds. Based upon a review of vendor equipment performance capability on simulated cracks documented in EPRI MRP-89, the UT techniques generally could not consistently detect cracking until it had reached 10 percent or greater depth into the VHP nozzle thickness. Therefore, the inspectors concluded that these examinations would not be effective at identification of PWSCC flaws located entirely within the J-groove weld. However, the licensee did implement a demonstrated UT technique intended to identify evidence of leakage behind a VHP nozzle caused by through-wall cracking of the J-groove weld.

b.

What was the physical condition of the reactor vessel head (e.g., debris, insulation, dirt, boron from other sources, physical layout, viewing obstructions)?

The licensee was not required by the NRC Order EA-03-009 to conduct a qualified visual examination of the Braidwood Unit 1 vessel head during this refueling outage. Although not required by the Order, the licensee performed an inspection of the bare metal head to meet the stations boric acid program and VHP nozzles through the access doors in the service structure. Based upon this inspection, the licensee did not identify any indication of boric acid leakage from sources above the vessel head. The inspectors observed the head during this inspection and did not observe any evidence of boric acid leakage. The inspectors noted some areas of minor staining on the VHP nozzles which the licensee had noted during prior inspections.

c.

Could small boron deposits, as described in the Bulletin 01-01, be identified and characterized?

Not applicable. The licensee performed a volumetric examination of the reactor from under the vessel head during the refueling outage and did not perform a qualified bare metal visual examination as discussed above.

d.

What material deficiencies (i.e., cracks, corrosion, etc.) were identified that required repair?

None.

e.

What, if any, impediments to effective examinations, for each of the applied methods, were identified (e.g., centering rings, insulation, thermal sleeves, instrumentation, nozzle distortion)?

The licensee identified physical limitations (due to RVCH and VHP nozzle design configurations) to completing the extent of the examination coverage required by NRC Order EA-03-009. Specifically, the licensee could not meet the NRC Order EA-03-009, requirement IV.C.(5)(i) to perform ultrasonic testing to at least 1 inch below the toe of the J-groove weld for 9 VHP nozzles. The extent of coverage achieved below the toe of the J-groove weld for these VHP nozzles was less than 1 inch due to the short distance that these nozzles extended below the J-groove welds and/or the presence of threads on the outside surface of these nozzles. Because these nonvisual examinations were completed earlier than required under the NRC Order EA-03-009, the licensee did not need to rely on the inspection results to remain in compliance with the NRC Order prior to restart. To remain in compliance with the NRC Order, the licensee intended to request relaxation from the NRC Order EA-03-009 requirements for these VHP nozzles with limitations after restart and before the next refueling outage.

The licensee also identified an area above the J-groove weld in VHP nozzle No. 74, which could not be examined with UT or ET probes due to an irregular surface condition. The licensee conducted a video probe assisted visual examination, which revealed scoring and metal disruption at the inside surface of this penetration. Based upon ET data the inspectors estimated that an area of disrupted material existed that was approximately 10 degrees (0.25 inches) in circumferential extent and 0.6 inches in height. The licensee believed that this area was caused by galling of the inside surface when a spring clip became wedged against the thermocouple housing during maintenance activities which occurred at least 12 years ago. The inspectors were concerned that the metal disruption could serve to make this area of VHP nozzle No. 74 more susceptible to PWSCC. The licensee intended to address the lack of coverage for this area during a relaxation request from the NRC Order EA 03-009 and intended to document the nozzle limitations and the surface condition of VHP nozzle No. 74 in their corrective action system.

f.

What was the basis for the temperatures used in the susceptibility ranking calculation, were they plant-specific measurements, generic calculations, (e.g., thermal hydraulic modeling, instrument uncertainties), etc.?

NRC Order EA-03-009 required licensees to calculate the susceptibility category of the reactor head to PWSCC-related degradation. The susceptibility category in EDY establishes the basis for the vessel head examination schedule and scope. In May of 2005, the licensee calculated the EDY for the Braidwood Unit 1 reactor head as documented in work order 0070306. In this calculation, the licensee used the formula required by NRC Order EA-03-009 and determined the EDY for the vessel head for several operating cycles. Based upon this calculation, at the end of operating cycle No.12, the Braidwood Unit 1 reactor vessel head was predicted to reach 2.2 EDY, which placed it in the low susceptibility category.

The NRC Order EA 03-009 Section IV.A required This calculation shall be performed with best estimate values for each parameter at the end of each operating cycle for the RVCH that will be inservice during the subsequent operating cycle. Contrary to this requirement, as documented in Work Order 0070306, the licensee used estimated data for reactor power level and cycle length approximately 11 months prior to the end of operating cycle No. 12.

The licensee entered this issue into the corrective action system (AR 00483826)and re-performed this calculation on April 29, 2006. This issue was considered a violation of NRC Order EA-03-009 of minor significance, because the revised calculation did not affect the original 2.2 EDY estimate and hence did not affect the head examination requirements.

NRC Order EA-03-009, required the licensee to have used best estimate values for the vessel head temperature in the EDY calculation. From the design average reactor coolant system temperature, the licensee calculated a cold leg temperature applicable to each operating cycle and applied this value as representative of vessel head temperature for the EDY calculation. The licensee considered the cold leg temperature representative of operating head temperature because of the coolant bypass flow channels in the vessel head which allowed the inlet flow to the reactor vessel to pass along the vessel head (e.g., cold leg temperature). The licensee concluded that this design feature applied to the Braidwood Unit 1 vessel head based upon information in Westinghouse Letter CA-RPV-076, Confirmatory Measurement of Upper Head Temperature for Byron Class Plants, and WCAP 11444, Thot Reduction Reactor Vessel Evaluation.

g.

During non-visual examinations, was the disposition of indications consistent with the guidance provided in Appendix D of this TI? If not, was a more restrictive flaw evaluation guidance used?

Not applicable. The licensee did not identify any indications for which required a flaw evaluation.

h.

Did procedures exist to identify potential boric acid leaks from pressure-retaining components above the vessel head?

Yes. Procedure ER-AP-331-1001, BACC Inspection Locations, Implementation and Inspection Guidelines, contained general walkdown inspection requirements.

This procedure required BACC inspections after plant shutdown during each scheduled refueling outage by VT-2 examiners. To meet the requirements of NRC Order EA-03-009, the licensee performed a direct visual inspection of the RVCH through access doors in the service structure in accordance with this procedure. The licensee did not identify any boric acid leaks from pressure-retaining components above the vessel head during this inspection.

i.

Did the licensee perform appropriate follow-on examinations for boric acid leaks from pressure retaining components above the vessel head?

Not applicable. The licensee did not identify any boric acid leaks from pressure retaining components above the vessel head during the current refueling outage.

c. Findings

No findings of significance were identified.

.2 Operational Readiness of Offsite Power and Impact on Plant Risk (TI 2515/165)

This TI was completed and documented in Inspection Report 05000456/2006002; 05000457/2006002, Section 4OA5. During this inspection period the NRC requested followup information regarding the status of one operating procedure that was still in draft during the last inspection. The inspectors determined that the procedure had been issued on April 7, 2006.

.3 World Association of Nuclear Operators Peer Review Report Review

The inspectors and the NRC Branch Chief reviewed the final report, dated June 6, 2006, for the World Association of Nuclear Operators plant assessment conducted in December 2005.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. K. Polson and other members of licensee management at the conclusion of the inspection on June 30, 2006. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

Interim exit was conducted for TI 2515/150, and ISI activities with Mr. K. Polson and other members of licensee management at the conclusion of the inspection on April 27, 2006. The inspectors returned proprietary information reviewed during the inspection and the licensee confirmed that none of the potential report input discussed was considered proprietary.

An interim exit meeting was conducted for the access control to radiologically significant areas program and the ALARA planning and controls program with Mr. J. Moser on April 28, 2006.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Polson, Site Vice President
G. Boerschig, Plant Manager
D. Ambler, Regulatory Assurance Manager
G. Bal, Engineering Programs Manager
B. Casey, Engineering Programs, ISI
M. Cichon, Licensing Engineer
T. DAntonio, Project Manager
H. Do, Engineering Programs, Corporate
G. Dudek, Operations Director
J. Gosnell, Tritium Team
A. Haeger, Tritium Team
J. Moser, Radiation Protection Manager
M. Sears, Steam Generator Program Manager
M. Smith, Engineering Director

Nuclear Regulatory Commission

R. Skokowski, Chief, Reactor Projects Branch 3

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000456/2006003-01;
05000457/2006003-01 NCV Failure to maintain fire barrier in accordance with fire protection program (Section 1R05)

Discussed

None.

LIST OF DOCUMENTS REVIEWED