IR 05000456/2019004

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Integrated Inspection Report 05000456/2019004 and 05000457/2019004
ML20027B437
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 01/24/2020
From: Hironori Peterson
NRC/RGN-III
To: Bryan Hanson
Exelon Generation Co
References
EA-16-126 IR 2019004
Preceding documents:
Download: ML20027B437 (31)


Text

January 24, 2020

SUBJECT:

BRAIDWOOD STATION, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000456/2019004 AND 05000457/2019004

Dear Mr. Hanson:

On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Braidwood Station, Units 1 and 2. On January 9, 2020, the NRC inspectors discussed the results of this inspection with Ms. M Marchionda, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No NRC-identified or self-revealing findings were identified during this inspection.

A licensee-identified violation which was determined to be of very low safety significance is documented in this report. We are treating this violation as a non-cited violation (NCV)

consistent with Section 2.3.2 of the Enforcement Policy.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Hironori Peterson, Chief Branch 3 Division of Reactor Projects

Docket Nos. 05000456 and 05000457 License Nos. NPF-72 and NPF-77

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000456 and 05000457

License Numbers:

NPF-72 and NPF-77

Report Numbers:

05000456/2019004 and 05000457/2019004

Enterprise Identifier: I-2019-004-0058

Licensee:

Exelon Generation Company, LLC

Facility:

Braidwood Station, Units 1 and 2

Location:

Braceville, IL

Inspection Dates:

October 01, 2019 to December 31, 2019

Inspectors:

R. Bowen, Illinois Emergency Management Agency

J. Bozga, Senior Reactor Inspector

J. Corujo-Sandin, Senior Resident Inspector

G. Edwards, Health Physicist

T. Go, Health Physicist

D. Kimble, Senior Resident Inspector

C. Phillips, Project Engineer

M. Porfirio, Illinois Emergency Management Agency

P. Smagacz, Resident Inspector

L. Torres, Illinois Emergency Management Agency

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Braidwood Station, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section: 71111.05Q.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000456,05000457/20 18011-01 Installed Plant Equipment Protection Against Tornado 71111.15 Closed EDG EA-16-126 Closure of EA-16-126 and Associated Enforcement Discretion Regarding Tornado Missiles Protection 71111.15 Closed

PLANT STATUS

Unit 1 began the inspection period operating at approximately 90 percent power with end-of-cycle power coast down operations in progress. On October 7, 2019, the unit was shut down for its planned 21st refueling outage (A1R21). Following completion of refueling and other maintenance activities, the reactor was restarted and taken critical on October 22, 2019, and the main electrical generator was synchronized to the power grid later that same day. The unit reached full power operation on October 27, 2019, and with the exception of minor reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, the unit remained operating at or near full power for the remainder of the inspection period.

Unit 2 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, the unit remained operating at or near full power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures during the weeks ending November 9, through December 21, 2019

External Flooding Sample (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated the licensee's readiness to cope with external flooding during the week ending December 7, 2019

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations and conducted selected alignment verifications on the following systems/equipment trains that were important to safety:

(1) The 1A Safety Injection (SI) Train while it was being credited as a mitigation system during reduced Reactor Coolant System (RCS) inventory operations during the week ending October 12, 2019
(2) The pre-staged FLEX equipment to support Unit 1 shutdown safety during reactor refueling cavity draindown and RCS reduced inventory operations during the weeks ending October 19 through October 26, 2019
(3) The 1B Auxiliary Feedwater (AF) Train while the 1A AF Train was undergoing maintenance during the week ending November 2, 2019
(4) The Unit 1 and Unit 2 Essential Service Water (SX) systems while the 2B SX Pump was undergoing scheduled maintenance during the week ending November 23, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors assessed fire protection program implementation for the issues noted and/or in the following selected plant areas:

(1) The Unit 1 Missile Shield Area, Containment 377' - 0" Elevation, Fire Zone 1.1-1 during the week ending October 12, 2019
(2) The Unit 1 Missile Shield Area, Containment 401' - 0" Elevation, Fire Zone 1.1-1 during the week ending October 19, 2019
(3) The Unit 1 Containment Annular Area, Containment 401' - 0", Fire Zone 1.1-1 during the week ending October 19, 2019
(4) The Unit 1 Diesel AF Pump Room, Auxiliary Building 383' Elevation, Fire Zone 11.4A-1 during the week ending November 2, 2019
(5) A missed compensatory fire watch for an out of service automatic CO2 fire suppression system in the Unit 2 Lower Cable Spreading Room on November 15, 2019

71111.08P - Inservice Inspection Activities (PWR) PWR Inservice Inspection Activities Sample (IP Section 03.01)

(1) The inspectors verified that the reactor coolant system boundary, steam generator tubes, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from October 7, 2019 to October 17 2019:

03.01.a - Nondestructive Examination and Welding Activities.

  • General Visual Examination (GV) of IWE Containment Liner Surfaces:

Elevation 426'-0" OMB

  • Visual Examination (VT-3) of snubber support 1RC02006BS
  • Visual examination for leakage (VT-2) of 1RC14AA
  • Visual examination for leakage (VT-2) of 1RC14AB
  • Visual examination for leakage (VT-2) of 1RC14AC
  • Visual examination for leakage (VT-2) of 1RC14AD

03.01.b - Pressurized-Water Reactor Vessel Upper Head Penetration Examination Activities.

  • Bare Metal Visual (BMV) examination of the reactor vessel upper head penetrations;

03.01.c - Pressurized-Water Reactor Boric Acid Corrosion Control Activities.

  • Boric Acid Leakage Evaluation on Component ID 1SI121B
  • Boric Acid Leakage Evaluation on Component ID 1CS020A

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Main Control Room during various activities, including Unit 1 shutdown for Refueling Outage A1R21 and subsequent restart during the weeks ending October 5 through October 26, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance activities associated with the following equipment and/or safety significant functions:

(1) The 0B Control Room Heating, Ventilation and Air Conditioning Chiller/Train maintenance during the weeks ending November 23 through December 7, 2019
(2) The 1B EDG maintenance during the weeks ending December 21 through December 28, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors reviewed and evaluated the licensee's assessment of plant risk for the following work activities:

(1) Emergent work associated with the 1C Steam Generator (SG) Power Operated Relief Valve (PORV) (1MS018C) as documented in Issue Report (IR) 4293122 during the weeks ending November 2 through November 23, 2019
(2) Emergent work associated with the 1A SG PORV (1MS018A) as documented in IR 4297820 during the weeks ending November 23, through November 30, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (3 Samples)

The inspectors evaluated the following licensee operability determinations:

(1) Closure of EA-16-126 and the associated Enforcement Discretion regarding protection against tornado missiles during the weeks ending October 12 through November 2, 2019
(2) Evaluation of 1A AF Pump operability following issues identified during testing as documented in IR 4285855 during the weeks ending October 12 through October 19, 2019
(3) Evaluation of 2B EDG operability following observation of jacket water system pressure surges during testing as documented in IR 4298842 during the weeks ending November 23 through November 30, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following permanent modifications and/or changes to the facility:

(1) Changes to the operation of the AF system to support a loss of normal feedwater during a unit startup as documented in Engineering Change (EC) 627959 during the weeks ending October 5 through December 7, 2019
(2) Enhancements to the existing Unit 1 digital control system (Westinghouse Ovation) as documented in EC 625405 during the weeks ending October 19 through December 7, 2019

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors reviewed and evaluated the following post maintenance testing activities:

(1) The Unit 1 core alignment verification following reactor refueling as documented in Work Order (WO) 4775529 during the week ending October 19, 2019
(2) Operability testing of the 1B EDG following maintenance as documented in WO 4751478 during the week ending October 19, 2019
(3) Testing of the 1A Charging (CV) Pump following maintenance as documented in WO 4751462 during the weeks ending October 19 through October 26, 2019
(4) Unit 1 digital rod position indication (DRPI) operability checks following reactor refueling as documented in WO 4781082 during the week ending October 26, 2019
(5) Unit 1 control rod drop time testing following reactor refueling as documented in WO 4820752 during the week ending October 26, 2019
(6) Functional testing of the of 0B VC Ventilation Train/Chiller following guide vane replacement as documented in WO 1929795 during the week ending November 30, 2019
(7) Operability testing of the 1B EDG following maintenance as documented in WO 4798246 during the week ending December 28, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors reviewed and evaluated Unit 1 Refueling Outage A1R21 activities from October 12 through October 26, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities:

Surveillance Tests (other) (IP Section 03.01)

(1)1BwOSR 3.3.2.9-2: Unit 1 - Train B SI manual initiation and Phase "A" Containment Isolation manual initiation surveillance during the week ending October 12, 2019 (2)2BwOSR 3.8.1.13-1: 2A EDG bypass of automatic trips surveillance during the week ending November 9, 2019

Inservice Testing (IP Section 03.01) (2 Samples)

(1) BwMP 3305-003: Main Steam Safety Valve testing using a setpoint verification device during the weeks ending October 5 through October 12, 2019 (2)1BwOSR 5.5.8.AF-4A: Unit 1 comprehensive inservice testing requirements for AF pumps during the weeks ending October 5 through October 12, 2019

Containment Isolation Valve Testing (IP Section 03.01) (2 Samples)

(1)1BwOSR 3.6.1.1-17: Primary Containment Type C local leakage rate tests for the make-up demineralizer system during the weeks ending October 19 through October 26, 2019

(2) The overall fuel cycle test results and summation of Unit 1 Primary Containment Type B and Type C local leak rates as documented in WO 4821955 during the week ending November 2, 2019

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated the site's emergency response organization during observation of the following drill activity:

(1) A graded emergency scenario for a crew of licensed operators in the station's control room simulator on November 15,

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 02.01) (1 Sample)

The inspectors evaluated radiological hazards assessments and controls.

(1) The inspectors reviewed the following:

Radiological Surveys

  • Containment 377' A1R21 Shutdown
  • Containment 401' Inside Missile Barrier
  • Containment 426' Lower Cavity Survey
  • Containment 410' Seal Table Area

Risk Significant Radiological Work Activities

  • Seal Table Activities
  • Under-vessel Activities Incore Sump
  • Reactor Head and Upper Internal

Air Sample Survey Records

  • Seal Table activities on Unit-1 401'
  • Upper Internal and Reactor Head Activities on Unit-1 426'
  • Lower Cavities on Unit-1 426'

Instructions to Workers (IP Section 02.02) (1 Sample)

The inspectors evaluated instructions to workers including radiation work permits used to access high radiation areas.

(1) The inspectors reviewed the following:

Radiation Work Packages

  • BW-01-19-00619; Undervessel Activities Incore Sump
  • BW-01-19-00614; Reactor Head and Upper Internals Move
  • BW-01-19-00649; Seal Table Room Outage Activities
  • BW-01-19-00613; Reactor Head Disassembly/Reassembly

Electronic Alarming Dosimeter Alarms

  • There were no electronic dosimeter alarms available for review during this inspection.

Labeling of Containers

  • Three or More Plastic Bags Containing Dry Active Waste (DAW) in Radwaste 401' Facility
  • Multiple Bags Containing DAW at the Upper and Lower Containment

Contamination and Radioactive Material Control (IP Section 02.03) (1 Sample)

The inspectors evaluated licensee processes for monitoring and controlling contamination and radioactive material.

(1) The inspectors verified the following sealed sources are accounted for and are intact:
  • J.L. Shepherd Model 89 Calibrator Containing 400 Ci of Cs-137 S.N.

BWS-106i

  • J.L. Shepherd Model 89 Calibrator Containing 2nd Source of 130 mCi of Cs-137 S.N. BWS-105i
  • AmBe Sealed Source in Shape of a Sphere Containing 5Ci Am-241/Beryllium S.N. BWS-102
  • Neutron Calibrator Containing 65 mCi of Cf-252 S.N. BWS-104i

Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)

The inspectors evaluated in-plant radiological conditions during facility walkdowns and observation of radiological work activities.

(1) The inspectors also reviewed the following radiological work package for areas with airborne radioactivity:
  • BW-01-19-00619; Under-vessel Activities Incore Sump
  • BW-01-19-00614; Reactor Head and Upper Internals Move
  • BW-01-19-00649; Seal Table Room Outage Activities
(1) The inspectors evaluated risk-significant high radiation area and very high radiation area controls.

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample)

(1) The inspectors evaluated radiation worker performance and radiation protection technician proficiency.

71124.02 - Occupational ALARA Planning and Controls

Radiological Work Planning (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees radiological work planning.

(1) The inspectors reviewed the following activities:
  • BW-01-19-00649; Seal Table Room Outage Activities
  • BW-01-19-00619; Under-vessel Activities
  • BW-01-19-00613; Reactor Head Disassembly/Reassembly
  • BW-01-19-00614; Reactor Head and Upper Internal Move

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Instrumentation and Equipment (IP Section 02.04) (1 Sample)

The inspectors reviewed the following radioactive effluent discharge system surveillance test results:

(1) Auxiliary Building Ventilation Test of Nuclear-Grade Activated Carbon

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage (IP Section 02.01)

The inspectors evaluated radioactive material storage.

(1) The inspectors toured the following areas:
  • Sea Vans Located and Stored Within the Protected Area
  • Radioactive Waste Storage/Processing Area (Various Locations)
  • Auxiliary Building (Various Locations)

The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers:

  • Filter Drum 0AB02FA
  • Filter Drum 0AB02FB
  • Filter Drum 1FC02F
  • Filter Drum 0AB02FA
  • Filter Drum 0AB02FB

Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample)

The inspectors evaluated the following radioactive waste processing systems and processes during plant walkdowns:

(1) Liquid or Solid Radioactive Waste Processing Systems
  • Advanced Liquid Processing System (ALPS) Located in the Radioactive Waste Area
  • Reverse Osmosis Water Processing Equipment Located in the Radioactive Waste Area

Radioactive Waste Resin and/or Sludge Discharges Processes

  • Vendor Conducted Resin Sluicing Into an Onsite Liner

Waste Characterization and Classification (IP Section 02.03) (1 Sample)

The inspectors evaluated the radioactive waste characterization and classification for the following waste streams:

(1)

  • 2018 Dry Activated Waste (DAW) Stream 10 CFR 61 Database Analysis
  • 2018 Radwaste Resin Stream 10 CFR 61 Database Analysis

Shipment Preparation (IP Section 02.04) (1 Sample)

The inspectors evaluated the following radioactive material shipment preparation processes:

(1) RWS19-003; UN2916, Radioactive Material, Type B(U) Package, 7; 0W05T Resin Liner PO676656-19 in Cask RT-100 #3

-This sample supplements inspection activities that were documented in integrated report 2019001. This constitutes one complete sample.

Shipping Records (IP Section 02.05) (1 Sample)

The inspectors evaluated the following non-excepted package shipment records:

(1)

  • RWS19-018; UN3321, Radioactive Material, Low Specific Activity (LSA-II), 7; 20' Shielded DAW Sealand
  • RWS19-003; UN2916, Radioactive Material, Type B(U) Package, 7; 0W05T Resin Liner PO676656-19 in Cask RT-100 #3
  • RWS19-004; UN2916, Radioactive Material, Type B(U) Package, 7, 0W05T Resin Liner PO676656-13 in Cask RT-100 #3
  • RWS19-012; UN2910, Radioactive Material, Excepted Package - Limited Quantity of Material,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicator information through the selected review of the submittal information listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===

(1) Unit 1 RCS Specific Activity Samples (March 2018 through June 2019)
(2) Unit 2 RCS Specific Activity Samples (March 2018 through June 2019)

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1) Unit 1 (October 1, 2018 through September 30, 2019)
(2) Unit 2 (October 1, 2018 through September 30, 2019)

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1) Radiological Effluent Occurrences Samples (July 2018 through July 2019)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program and other work documentation for potential adverse trends associated with alternating current (AC)circuit breaker trip testing during the A1R21 refueling outage during the weeks ending December 21 through December 31, 2019

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors performed an in-depth review of the licensees corrective actions for the following issue:

(1) The need for the 1C SG Feedwater Regulating Valve (1FW530) to be operated in the fully open position following power ascension after the A1R21 refueling outage, as documented in IR 4291137 during the weeks ending December 21 through December 31, 2019

71153 - Followup of Events and Notices of Enforcement Discretion Event Followup (IP Section 03.01)

(1) The inspectors reviewed and evaluated the licensee's response to the inadvertent actuation of emergency plan sirens as documented in NRC Event Notification54360 during the week ending November 2,

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71111.05Q This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Technical Specification (TS) Section 5.4.1.c requires that written procedures be established, implemented, and maintained for activities associated with the implementation of the sites Fire Protection Program. One of several procedures established by the licensee to meet this requirement was BwAP 1110-1A4, GOCAR [General Operation Condition Action Requirement] Required Compensatory Measures Action Response Carbon Dioxide Fire Suppression Systems. Revision 10 of this procedure, which was the revision active and in effect on November 15, 2019, required that a continuous fire watch be established and maintained for Fire Zone 2S-43 within the Unit 2 Lower Cable Spreading Room when the carbon dioxide suppression system associated with that fire zone was not operable.

Contrary to this requirement, on November 15, 2019, the licensee failed to implement the compensatory continuous fire watch as required by TS Section 5.4.1.c and BwAP 1110-1A4, Revision 10. Specifically, a communications error between the on-shift Operations crew and craft personnel resulted in the inadvertent securing of the continuous fire watch for Fire Zone 2S-43 for approximately 53 minutes while the carbon dioxide suppression system associated with that fire zone was not operable.

Significance/Severity: Green. The inspectors assessed the significance of the finding using Inspection Manual Chapter (IMC) 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, dated May 2, 2018. In accordance with Step 1.5 of this document, a Senior Reactor Analyst (SRA) reviewed the licensee's risk evaluation and verified the core damage frequency results were significantly less than the 1E-6/year threshold (Green).

Corrective Action References: Issue Report (IR) 42977714, Plant Barrier Impairment, BwAP 1110-1A4 Fire Watch Communication Issue

Unresolved Item (Closed)

Installed Plant Equipment Protection Against Tornado URI 05000456,05000457/2018011-01 71111.15

Description:

This Unresolved Item (URI) was identified while performing Temporary Instruction (TI)2515/191, Mitigating Strategies, Spent Fuel Pool Instrumentation and Emergency Preparedness (ML18033A711). The inspectors questioned whether the installed plant equipment which was nonconforming to the current licensing basis for protection against tornado-generated missiles, and is relied upon to implement the mitigating strategies, met the requirements of Order EA-12-049 for reasonable protection from external events.

Specifically, the inspectors were concerned about non-conforming structures, systems or components which the licensee had identified in their corrective action program (AR 2673854).

At the time of the inspection the licensee had invoked EGM 15-002, Enforcement Discretion for Tornado-Generated Missile Protection Non-compliance, which allowed the NRC to exercise enforcement discretion when an operating power plant does not comply with its current licensing basis for tornado-generated missile protection. Inspectors had previously documented the exercise of enforcement discretion in inspection reports 2016-002 (ML16209A139) and 2017-001 (ML17121A339). Enforcement Action (EA) number, EA-16-126, was tracking the use of the enforcement discretion until final corrective actions were implemented.

As discussed in the Enforcement Discretion section of this report, final corrective actions regarding EA-16-126 have been completed. The affected structures, systems and components were restored to compliance with their tornado-generated missile licensing bases. As a result, URI 05000456,05000457/2018011-01 is considered closed.

Corrective Action Reference(s): AR 04109224 - "NRC URI - Tornado Missile Protection for Installed Equipment" AR 02673854 - "Non-Conforming Conditions Identified - Tornado Missiles"

Enforcement Discretion Enforcement Action EA-16-126: Closure of EA-16-126 and Associated Enforcement Discretion Regarding Tornado Missiles Protection 71111.15

Description:

On June 10, 2015, the NRC issued Regulatory Issue Summary (RIS) 2015-06, Tornado Missile Protection, (ML15020A419) and Enforcement Guidance Memorandum (EGM) 15-002, "Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance" (ML15111A269). The RIS focused on the requirements regarding tornado-generated missile protection and required compliance with the facility-specific licensing basis. The EGM provided guidance to allow the NRC staff to exercise enforcement discretion when an operating power plant licensee did not comply with the current license basis for tornado-generated missile protection.

On May 25, 2016, the licensee documented several identified non-conformances related to tornado missile protection in their corrective action program (AR 02673854). In addition, the licensee discussed their intent to request to use the enforcement discretion, afforded by EGM 15-002, and discussed the actions required to comply with the provisions in the EGM.

Inspectors documented the exercise of enforcement discretion in the baseline quarterly reports 2016-002 (ML16209A139) and 2017-001 (ML17121A339). Enforcement Action (EA)number, EA-16-126, was assigned to administratively track the use of enforcement discretion until final corrective actions were implemented.

Corrective Actions: By letter dated February 1, 2018, (ML18036A227), as supplemented by letters dated July 9, 2018, (ML18036A227) and August 3, 2018, (ML18215A421) the licensee submitted a license amendment request to revise their licensing bases regarding protection from tornado-generated missiles. As part of the amendment process the licensee committed to protecting the reactor water storage tanks (RWSTs) hatches from tornado-generated missiles. The licensee installed the committed physical protection via Engineering Change 618920, Tornado Missile Protection for Refueling Water Storage Tank Roof Hatches.

On November 8, 2018, the NRC issued license amendment No. 199 to NPF-72, amendment No. 199 to NPF-77 and its associated safety evaluation report (ML18291A980). Based on its evaluation the NRC approved Braidwood Station, Units 1 and 2, to revise the Updated Final Safety Analysis Report (UFSAR) to incorporate the TORMIS computer Code as the methodology used for assessing tornado-generated missile protection of specific unprotected plant structures, systems and components and to describe the results of the site-specific tornado hazard analysis as described in the licensees application and safety evaluation.

Corrective Action References: AR 02673854 - "Non-Conforming Conditions Identified - Tornado Missiles" AR 04014784 - "1Q17 LIV - Lack of Adequate Tornado Missile Protection" AR 04217133 - "DBAI - Global Effects of Missile Impact on RWST Hatch Cover"

Enforcement:

Based on the licensees corrective actions described above no additional violations were identified, the enforcement discretion afforded by EGM 15-002 is no longer required and EA-16-126 is considered closed.

The disposition of this issue closes URI: 05000456,05000457/2018011-01.

Observation: Steam Generator 1C Main Feedwater Regulating Valve, 1FW530, Required to be Operated in the Fully Open Position 71152 The inspectors performed a detailed review of IR 4291137, 1FW530 Full Open Following Power Ascension. The issue involved the need for the licensee to operate the 1C Steam Generator (SG) Main Feedwater Regulating Valve (FRV), 1FW530, in the fully open position to provide adequate feedwater flow to the 1C SG at full power following return of Unit 1 to operation after the licensees October 2019 A1R21 refueling outage. This condition stemmed from the fact that the associated main feedwater check valve in that line, 1FW079C, did not open to the expected position for the full power operating condition and additional open travel on 1FW530 was required to compensate for the additional flow resistance in the line.

The failure of the 1FW079C check valve to move to the expected open position for full power operation appears to be a design issue associated with the FW079 series check valves in the stations main feedwater lines. Similar issues have been observed from time to time by the licensee with various FW079 series check valves going back a number of years. In 2018 when an analogous condition occurred on the 1B SG main feedwater line, the inspectors reviewed the licensees operability and functionality evaluation for the 1FW079B check valve being more closed than expected for the full power operating condition and did not identify any findings or violations of NRC requirements. (Reference: Braidwood Station, Units 1 and 2 - NRC Integrated Inspection Report 05000456/2018003 and 05000457/2018003; ADAMS Accession Number: ML18304A205). Consequently, for this detailed Problem Identification and Resolution inspection sample, the inspectors focused on assessment of the licensees corrective actions taken to date and those planned going forward.

At Braidwood Stations sister facility, Byron Station, the licensee replaced the FW079 series main feedwater check valves several years ago with check valves of a different design in order to alleviate the condition at that facility. In reviewing the licensees corrective actions for this most recent condition at Braidwood Station, the inspectors noted that one of the actions within the licensees corrective action program (CAP) tasked licensees engineering organization with evaluating the modification performed at Byron Station for potential use at Braidwood. In addition, the licensee established corrective actions to evaluate possibly increasing the speed of the running turbine-driven main feedwater pumps to force the 1C SG FRV to close somewhat. This, however, would also impact the other three Unit 1 FRVs, which are presently operating as desired. Lastly, the licensee has developed an adverse condition monitoring plan in accordance with station procedures and processes to monitor the condition, with trigger points for additional analysis and/or actions should the condition degrade.

The FRVs are intended to be able to modulate to adjust SG level as necessary during plant operation. The overall safety significance of the issue comes down to an increased risk of SG level instability if a second Unit 1 FRV were to reach the fully open position with 1FW530 already needing to be fully open to ensure proper main feedwater flow to the 1C SG.

Following their review, the inspectors concluded that the licensees actions taken in accordance with their CAP were reasonable given the overall safety significance of the issue.

The inspectors did not identify any findings or violations of NRC requirements in the course of their review.

Observation: Potential Trend in Molded Case Circuit Breaker Trip Testing Issues 71152 The inspectors performed a review of plant issues, particularly those entered into the licensees corrective action program (CAP), associated with problems encountered during MCCB trip testing that was accomplished as part of the licensees Unit 1 A1R21 refueling outage. During their review, the inspectors noted that there had been several MCCB testing issues encountered by the licensee. In each of the six cases noted, the subject MCCB was subsequently evaluated as being capable of adequately tripping if required. Four of the cases involved MCCBs not tripping within their specified tolerances. These MCCBs were evaluated by licensee engineering and determined to be capable of adequately tripping if required and capable of maintaining proper breaker coordination. One issue involved an MCCB that could not be reset following successful trip testing, and one involved an MCCB that had to have its testing sequence aborted when technicians identified some minor signs of smoke coming from the breaker. The MCCB that tripped but could not be reset was subsequently replaced by the licensee prior to Unit 1 restart. The MCCB that had its testing aborted was removed from service and sent to an offsite testing facility where its testing was completed within tolerances; the breaker was replaced, however, due to the minor signs of smoke noted by licensee technicians during its initial testing sequence.

Following their review, the inspectors queried the licensee regarding the number and nature of the testing issues observed, specifically asking about whether or not the scope and nature of the issues was comparable to prior refueling outage testing campaigns. The licensee entered the potential trend with A1R21 MCCB issues into their CAP as Issue Report (IR) 4305858. The licensees initial evaluation of their MCCB testing data from previous refuel outages did not indicate that this most recent MCCB testing campaign issues represented anything unusual.

The inspectors did not identify any findings or violations of NRC requirements in the course of their review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 9, 2020, the inspectors presented the integrated inspection results to Ms. M Marchionda, Site Vice President and other members of the licensee staff.
  • On October 11, 2019, the inspectors presented the radiation protection baseline inspection results to Ms. M. Marchionda, Site Vice President and other members of the licensee staff.
  • On October 17, 2019, the inspectors presented the Inservice Inspection inspection results to Ms. M. Marchionda, Site Vice President and other members of the licensee staff.
  • On November 20, 2019, the inspectors presented the URI 2018011-01 (FLEX) and EA 16-126 (Tornado Missile Discretion) Closures inspection results to Mr. R. Schliessmann, NRC Coordinator, and other members of the licensee staff.
  • On December 5, 2019, the inspectors presented the Radiation Protection Inspection Results inspection results to Mr. J. Keenan, Plant Manager and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

Resulting from

Inspection

4301787

NRC ID: Unit 1 Auxiliary Building Roof Drains Plugged

2/05/2019

Miscellaneous

Letter

20 Winter Readiness Certification

2/13/2019

Procedures

0BwOA ENV-1

Adverse Weather Conditions Unit 0

23

0BwOS XFT-A1

Unit Common Freezing Temperature Equipment Protection

Surveillance

0BwOS XFT-A2b

Unit Common Station Heat Area Heaters Freezing

Temperature Equipment Protection Surveillance

0BwOS XFT-A3

Unit Common Cold Weather Surveillance

0BwOS XFT-A4

Unit Common Freezing Temperature Equipment Protection

Inside Surveillance

0BwOS XFT-A5

Unit Common Freezing Temperature Equipment Protection

of Out Building Surveillance

OP-AA-102-102

General Area Checks and Operator Field Rounds

OP-AA-108-111-

1001

Severe Weather and Natural Disaster Guidelines

OP-BR-102-102-

1001

Augmented Operator Field Rounds

WC-AA-107

Seasonal Readiness

71111.04Q Drawings

ECCS-1

Training Document - Emergency Core Cooling System

Drawing

Procedures

1BwFSG-14

Shutdown Reactor Coolant System (RCS) Makeup

BwOP AF-E1

Electrical Lineup - Unit 1 Operating

BwOP AF-M1

Operating Mechanical Lineup Unit 1

BwOP SX-E1

Electrical Lineup - Unit 1 Essential Service Water System

Operating

BwOP SX-E2

Electrical Lineup - Unit 2 Essential Service Water System

BwOP SX-M1

Operating Mechanical Lineup Unit 1

BwOP SX-M2

Operating Mechanical Lineup Unit 2

OP-BR-FX-1004

Medium Head FLEX Pump Operating Guideline

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.05Q Corrective Action

Documents

297714

Plant Barrier Impairment, BwAP 1110-1A4 Fire Watch

Communication Issue

11/15/2019

Fire Plans

No. 1; Fire Zone

1.1-1

Containment 377'-0" Elevation; Unit 1 Containment Missile

Shield Area

No. 2; Fire Zone

1.1-1

Containment 401'-0" Elevation; Unit 1 Containment Missile

Shield Area

No. 5; Fire Zone

1.2-1

Containment 377'-0" Elevation; Unit 1 Annular Area

No. 6; Fire Zone

1.2-1

Containment 401'-0" Elevation; Unit 1 Annular Area

No. 9; Fire Zone

1.3-1

Containment 426'-0" Elevation; Unit 1 Containment Upper

Area

Miscellaneous

Transient

Combustible

Permit 618

Reactor Head Stand Area

10/07/2019

Transient

Combustible

Permit 619

ROV Control Point for Head Lift

10/07/2019

Transient

Combustible

Permit 629

RCP Motor Replacement

01/07/2019

Transient

Combustible

Permit 630

Pipefitters Working RCP Motor

10/07/2019

Procedures

BwAP 1110-1

Fire Protection Program System Requirements

BwAP 1110-1A4

GOCAR [General Operation Condition Action Requirement]

Required Compensatory Measures Action Response Carbon

Dioxide Fire Suppression Systems

BwAP 1110-3

Plant Barrier Impairment Program

BwOP PBI-1

Plant Barrier Impairment Program Pre-Evaluated Barrier

Matrix

CC-AA-201

Plant Barrier Control Program

71111.05Q Procedures

ER-AA-600-1069

High Risk Fire Area Identification

ER-BR-600-1069

Site List of High Risk Fire Areas - Braidwood Unit 1 and

Unit 2

OP-AA-201-004

Fire Prevention for Hot Work

OP-AA-201-007

Fire Protection System Impairment Control

OP-AA-201-008

Pre-Fire Plan Manual

OP-AA-201-009

Control of Transient Combustible Material

71111.08P

Corrective Action

Documents

202190

Unable to Complete Final Review for ASME XI Repair

Replacement

2/11/2018

286524

04-OSP-X A1R21 Snubber 1CV41036S Degraded Req's

Replacement

10/09/2019

287141

06-OSP-A A1R21 Snubber Operation Test Failure

1RC02006AS

10/11/2019

287143

06-OSP-A A1R21 Snubber Operation Test Failure

1RC02006BS

10/11/2019

287727

10-OSP-A (ISI) Constant Spring Can 1FW05024C FOUND

OOT

10/13/2019

287731

10-OSP-A (ISI) Variable Spring Can 1CV16034V FOUND

OOT

10/13/2019

287815

10-OSP-X Defer ASME Section XI Support Exam

1CC13045X (ISI)

10/14/2019

287816

10-OSP-X Defer ASME Section XI Support Exam on

1SX16019V (ISI)

10/14/2019

Miscellaneous

2410146-02

Eductor 1A Spray Add Suct Check VLV

06/22/2018

2731397-02

Bonnet Thermal Relief Valve for 1SI8811B

06/22/2018

NDE Reports

A1R21-PT-001

Reactor Head Surface Penetration 69

10/12/2019

A1R21-UT-007

RCP Main Flange Bolt (01-24)

10/13/2019

A1R21-UT-034

Main Steam Pipe to Elbow Weld 1-MS-02-24

10/17/2019

A1R21-UT-035

Main Steam Elbow to Pipe Weld 1-MS-02-25

10/17/2019

A1R21-UT-036

Main Steam Pipe to Elbow Weld 1-MS-02-26

10/17/2019

A1R21-UT-040

Main Steam Elbow to Pipe Weld 1-MS-02-32

10/17/2019

A1R21-UT-041

Main Steam Elbow to Pipe Weld 1-MS-02-29

10/17/2019

A1R21-UT-042

Main Steam Elbow to Pipe Weld 1-MS-02-27

10/17/2019

A1R21-UT-043

Main Steam Pipe to Elbow Weld 1-MS-02-28

10/17/2019

SN-19-0034

Pipe Support 1RC02006BS

10/10/2019

SN-19-0041

Pipe Support 1RC02006AS

10/10/2019

Procedures

ER-AA-335-002

Liquid Penetrant (PT) Examination

ER-AA-335-015-

2013

VT-2 Visual Examination in Accordance with ASME 2013

ER-AA-335-018

Visual Examination of ASME IWE Class MC and Metallic

Liners of IWL Class CC Components

ER-AA-335-031

Ultrasonic Examination of Austenitic Piping Welds

ER-AA-335-037

Ultrasonic Examination of Studs and Bolts

ER-AA-335-1008

Code Acceptance & Recording Criteria for Nondestructive

(NDE) Surface Examination

ER-AP-335-001

Bare Metal Visual Examination for Nickel Alloy Materials

EXE-PDI-UT-2

Ultrasonic Examination of Austenitic Pipe Welds in

Accordance with PDI-UT-2

EXE-PDI-UT-5

Straight Beam Ultrasonic Examination of Bolts and Studs in

Accordance with PDI-UT-5

Work Orders

04775229-01

1CV8396B Is Spraying from Diaphragm Between Body and

Bonnet

04/20/2018

71111.11Q Procedures

1BwGP 100-4

Power Decension

OP-AA-101-111-

1001

Operations Standards and Expectations

OP-AA-101-113

Operator Fundamentals

OP-AA-101-113-

1006

4.0 Crew Critique Guidelines

OP-AA-103-102

Watch-Standing Practices

OP-AA-103-102-

1001

Strategies for Successful Transient Mitigation

OP-AA-103-103

Operation of Plant Equipment

OP-AA-104-101

Communications

OP-AA-108-107-

1002

Interface Procedure Between BGE/COMED/PECO and

Exelon Generation (Nuclear/Power) for Transmission

Operations

OP-AA-111-101

Operating Narrative Logs and Records

OP-AA-300

Reactivity Management

71111.12

Corrective Action

Documents

4149917

Oil Slinger Ring Not Installed on 0A and 0B VC Chillers

06/24/2018

297028

Degradation on 0B VC Chiller Condenser Head Flange

Faces

11/13/2019

297481

Rejectable NDE Indication 0WO01CB Outlet Flange

11/15/2019

Procedures

ER-AA-310-1002

Maintenance Rule Functions - Safety Significant

Classification

ER-AA-320

Maintenance Rule Implementation per NEI 18-10

ER-AA-320-1001

Maintenance Rule 18-10 - Scoping

ER-AA-320-1003

Maintenance Rule 18-10 - Failure Definitions

ER-AA-320-1004

Maintenance Rule 18-10 - Performance Monitoring and

Dispositioning Between (a)(1) and (a)(2)

Work Orders

1917679

Replace 0TS-WO207 - Chiller 0WO1CB Hot Gas Bypass

Temperature Switch

11/24/2019

29795

0WO01CB: Replace Guide Vanes

11/13/2019

4609716

0WO01CB Condenser PM and Eddy Current Testing

11/12/2019

4802125

Oil Slinger Ring Not Installed on 0A and 0B VC Chillers -

Disassemble / Take Measurements / Reassemble Chiller

11/14/2019

71111.13

Corrective Action

Documents

287867

09-OSP-A: 1C Steam Generator PORV Hydraulic Reservoir

Level Low

10/15/2019

288936

13-OSP-A: Annunciator 1-15-C10, Steam Generator 1C

PORV Trouble

10/18/2019

293122

1-/15-C10, Steam Generator 1C PORV Trouble - 1MS018C

Hydraulic Fluid Low

10/31/2019

297820

1-15-A10: Steam Generator 1A PORV Trouble - Accumulator

Pressure Low

11/16/2016

Corrective Action

Documents

Resulting from

Inspection

295505

1MS018C Lost Paperwork for Hydraulic Fill Evolution

11/07/2019

Procedures

1BwOSR

3.6.3.5.MS-1

Main Steam System Containment Isolation Valve Stroke

Surveillance

ER-AA-600

Risk Management

ER_AA-600-1042

On-Line Risk Management

MA-AA-716-004

Conduct of Troubleshooting

OP-AA-108-117

Protected Equipment Program

WC-AA-101-1006

On-Line Risk Management and Assessment

Work Orders

4970682

1MS018C Add Oil to PORV (Unscheduled Maintenance)

11/08/2019

71111.15

Corrective Action

Documents

2673854

Non-Conforming Conditions Identified - Tornado Missiles

05/25/2016

4014784

1Q17 LIV - Lack of Adequate Tornado Missile Protection

05/25/2017

4109224

NRC URI - Tornado Missile Protection for Installed

Equipment

2/28/2018

285855

2-OSP: 1A Auxiliary Feedwater Pump Breaker did not

Close During ATWS (Anticipated Transient Without Scram)

Testing

10/08/2019

298842

2B DG EMG Stop Due to Abnormal JW Surging

11/20/2019

Drawings

M-152, Sheet 14

Manufacturers Supplemental Diagram of Diesel Generator

Jacket Water Schematic Units 1 & 2

V

Procedures

1BwOS ATWS-

R1

Unit 1 Anticipated Transient Without Scram Mitigation

System Refueling Outage End to End Surveillance

2BwOSR 3.8.1.2-

Unit 2B Diesel Generator Operability Surveillance

BwOP AF-5

Motor-Driven Auxiliary Feedwater Pump 'A' Startup on

Recirculation

BwOP DG-11

Diesel Generator Startup and Operation

BwOP DG-11T2

Diesel Generator Operating Log

ER-AA-600-1012

Risk Management Documentation

OP-AA-106-101-

1006

Operational Decision Making Process

OP-AA-108-111

Adverse Condition Monitoring and Contingency Planning

OP-AA-108-115

Operability Determinations (CM-1)

Work Orders

1956941

Unit 1 ATWS (Anticipated Transient Without Scram)

Refueling Outage Testing

04/09/2018

1956941

Unit 1 ATWS [Anticipated Transient Without Scram]

Refueling Outage Testing

04/09/2018

71111.18

Corrective Action

Documents

272924

EC 627959 Follow-Up Actions for Auxiliary Feedwater

Procedure Changes

08/19/2019

280595

CDO - Inadequate 50.59 Review for EC 625405

09/12/2019

Engineering

Changes

25405

Unit 1 Ovation Post N-Outage Backfit

27959

Auxiliary Feedwater System Operation to Support a Loss of

Normal Feedwater During a Unit Startup

Procedures

EC 625405-1

Braidwood Station N+1 Outage Mod Acceptance Test (MAT)

71111.19

Corrective Action

Documents

299555

0WO01CB Chiller Tripped

11/24/2019

Operability

Evaluations

BwVP 500-14

Core Alignment Verification

Procedures

1BwOS RD-3

Shutdown Rod Insertion Limit During Approach to Criticality

Surveillance

1BwOS TRM

3.1.k.1

Unit 1 Digital Rod Position Indication (DRPI) Operability

Verification Prior to and During Rod Drop Testing

1BwOSR 3.1.7.1

Digital Rod Position Indication (DRPI) Operability Checkout

1BwOSR

3.8.1.19-2

1B Diesel Generator ECCS Sequencer Surveillance

1BwOSR 3.8.11-

1B Diesel Generator Loss of ESF Bus Voltage with No SI

Signal

1BwOSR

5.5.8.CV-4A

Group A IST Requirements for 1A Centrifugal Charging

Pump (1CV01PA) and Check Valve 1CV8480A Stroke Test

BwISR 3.1.4.3.a

Rod Drop Time (Automatic)

NF-AA-330-1001

Core Verification Guideline

OU-AP-230

Newton Core Gap Alignment Data Acquisition for Byron and

Braidwood

Work Orders

1966510

1B Diesel Generator 24 Hour Load Test and ECCS

Surveillance

10/26/2019

4709143

Functional Run of 0WO01CB Following Control Panel Relay

Replacements

11/24/2019

4751413

1CV01PA Disassemble, Inspect & Clean Gearbox Oil Filter

10/16/2019

4751462

Check Shaft Driven Oil Pump Drive Mechanism

10/16/2019

475147B

1B Diesel Generator Loss of ESF Buss Voltage with No SI

Signal

10/16/2019

4775529

Core Alignment Verification - Unit 1

10/16/2019

4781082

Unit 1 Digital Rod Position Indication (DRPI) Operability

Checkout

10/21/2019

4790778

Change Oil in Motor Bearings and Take Sample

10/16/2019

4798246

Perform 2 Year Inspection of Diesel Generator

2/15/2019

20752

Unit 1 Automatic Rod Drop Time Surveillance

10/21/2019

4875703

1SC-DG250B Replace DG Governor Actuator

2/15/2019

4897408

Digital Rod Position Indication (DRPI) Surveillance During

Rod Drop Testing

10/21/2019

71111.20

Corrective Action

Documents

286018

2 DC Ground

10/08/2019

286592

Unexpected Toggling of Alarm SR S/D Flux High

10/10/2019

289506

Mode 3 Entry with LCO 3.0.4B Requirements

10/20/2019

289892

Active Water Leak in Unit 1 Seal Table Room

(Clean/Tighten)

10/21/2019

Corrective Action

Documents

Resulting from

Inspection

285795

NRC ID: BWOP RC-4 Improvement Opportunity

10/07/2019

Procedures

1BwGP 100-1

Plant Heatup

1BwGP 100-3

Power Ascension 5% to 100%

1BwGP 100-5

Plant Shutdown and Cooldown

1BwOS TRM

2.5.b.1

Unit 1 - Containment Loose Debris Inspection

BwAP 1450-1

Access to Containment

BwGP 100-2

Plant Startup

BwOP DG-1

Diesel Generator Alignment to Standby Condition

BwOP RC-4

Reactor Coolant System Drain

BwVS 500-6

Low Power Physics Test Program

BwVS TRM

3.1.h.1

Core Reload Sequence and Verification

HU-AA-1211

Pre-Job Briefings

LS-AA-119

Fatigue Management and Work Hour Rules

MA-AA-716-1008

Reactor Services: Refuel Floor FME Plan

OP-AA-108-108

Unit Restart Review

OP-AA-108-110

Evaluation of Special Tests or Evolutions

71111.22

Corrective Action

Documents

1BwOSR

5.5.8.AF-4A

Unit One Comprehensive Inservice Testing (IST)

Requirements for 1A Auxiliary Feedwater Pump

284962

1MS015A Did Not Pass As Found Testing

10/04/2019

286889

06-OSP-X: Safety Injection Full Flow Testing Post

Calibration Unsatisfactor

10/10/2019

Procedures

1BwOSR 3.3.2.9-

Unit One - Train B Safety Injection Manual Initiation and

Phase "A" Containment Isolation Manual Initiation

Surveillance

1BwOSR 3.6.1.1-

Primary Containment Type C Local Leakage Rate Test of

Make-Up Demineralizer System

1BwVSR 3.6.1.25

Summation of Type "B" & "C" Tests for Acceptance Criteria

2BwOSR

3.8.1.13-1

2A Diesel Generator Bypass of Automatic Trips Surveillance

2BwOSR 3.8.1.2-

2A Diesel Generator Operability Surveillance

BwMP 3305-003

Main Steam Safety Valve Testing Using Setpoint Verification

Device

BwOP DG-11

Diesel Generator Startup and Operation

BwOP GD-12

Diesel Generator Shutdown

Work Orders

1961853

IST - Unit 1 Local Leak Rate Test WM 190/191 for

Containment Penetration No. 30

10/18/2019

1966521

Unit 1 Train B SI Signam Manual Initiation and Phase A

Containment Isolation Manual Initiation

10/07/2019

4787030

2DG01KA Bypass of Automatic Trips Not with Slave Start

11/06/2019

4795683

IST-Unit 1 AF Pumps Comprehensive Full Flow Test and

Equipment Response Time

10/05/2019

21955

Unit 1 Local Leak Rate Test Summation for Type "B" & "C"

Tests

10/20/2019

4851024

IST - Main Steam Safety Valve Test for

1MS013S/014S/015S/016S/017S

10/03/2019

4971355

2A Emergency Diesel Generator Monthly

11/06/2019

71114.06

Procedures

EP-AA-1000

Standardized Radiological Emergency Plan

EP-AA-1001

Radiological Emergency Plan Annex for Braidwood Station

LS-AA-2100

Monthly Data Elements for NRC Reactor Coolant System

(RCS) Leakage

71124.01

Calculations

BW-01-19-00513

Airborne Radioactivity Calculation Worksheet; U-1 426'

Inside Cavity

10/09/2019

BW-01-19-00619

Airborne Radioactivity Calculation Worksheet U-1 377' In-

Core Sump

10/07/2019

BW-01-19-00641

Airborne Radioactivity Calculation Worksheet U-1

Containment 426' Reactor Head

10/11/2019

BW-01-19-00649

Airborne Radioactivity Calculation Worksheet U-1 401' Seal

Table

10/08/2019

Procedures

RP-AA-460

Controls for High and Locked High Radiation Areas

Radiation

Surveys

054691

Containment 426' Lower Cavity

10/07/2019

054692

Containment 401' Inside Missile Barrier

10/07/2019

054699

Containment 426' Upper Cavity

10/07/2019

054705

Containment 377 Outside Missile Barrier

10/07/2019

958270

Containment 390' A&D Steam Generator Platform

10/07/2019

958270

Containment 390' Steam Generator B&C Platform

10/07/2019

Radiation Work

Permits (RWPs)

BW-01-19-00615

Reactor Cavity Work

71124.02

ALARA Plans

BW-01-19-00613

Reactor Head Disassembly/Reassembly

BW-01-19-00614

Reactor Head and Upper Internal Move

BW-01-19-00619

Under-vessel Activities

BW-01-19-00649

Seal Table Room Outage Activity

71124.06

Miscellaneous

Sample ID

0VA05FA

Radioiodine Test Report

07/06/2018

Sample ID

0VA05FB

Radioiodine Test Report

07/06/2018

Sample ID

0VA05FC

Radioiodine Test Report

07/06/2018

Sample ID

0VA05FD

Radioiodine Test Report

06/15/2018

Sample ID

0VA05FE

Radioiodine Test Report

06/15/2018

Sample ID

0VA05FF

Radioiodine Test Report

06/15/2018

Work Orders

01937904 01

Auxiliary Building Vent Stack Wide Range Gas Monitor Full

Calibration

05/11/2018

71124.08

Corrective Action

Documents

AR 04148257

Spent Resin Pump 0WX79MA Does Not Rotate

06/18/2018

AR 04193272

Brine Tank Booster Pump Degraded

11/09/2018

AR 04229135

0WX05DB Radwaste Demin is Leaking

03/13/2019

AR 04277770

Resin Not Available For The 1CV01DA De-Boration Bed

Sluice

09/09/2019

Corrective Action

Documents

Resulting from

Inspection

AR 04065270

NRC Open Item From Inspection Regarding RW Resin Resin

Sampling

10/20/2017

Engineering

Changes

0000623825

TCCP To Restore 0WX889-XA Interlocks to Allow Water

Processing Through 0W889 and 0WX890

04/10/2018

Miscellaneous

CFR 61 Primary Filter Waste Stream Analysis

01/14/2019

CFR 61 Radwaste Resin Analysis

2/03/2018

CFR 61 Dry Activated Waste (DAW) Analysis

01/29/2019

Procedures

RW-AA-100

Process Control Program for Radioactive Wastes

Self-Assessments AR 04214019

NRC Inspection IP 71142.08 Radioactive Solid Waste

Processing and Radioactive Material Handling, Storage and

Transportation

07/11/2019

Shipping Records RWS19-003

0WX05T Resin Liner PO676656-19 in Cask RT-100 #3

03/05/2019

RWS19-004

0WX05T Resin in Liner PO676656-13 in Cask RT-100 #3

03/12/2019

RWS19-012

B-25s of Grossly Dewatered Resin

07/18/2019

RWS19-014

Resin Liner PO683742-17 in Cask

09/25/2019

71151

Miscellaneous

LS-AA-2090

Monthly Data Element for NRC Reactor Coolant System

Specific Activity

03/2018 -

06/2019

LS-AA-2150

Monthly Data Elements for NRC RETS/ODCM Radiological

Effluent Occurrences

07/2018 -

07/2019

NRC

Performance

Indicator Data

Barrier Integrity - RCS Identified Leakage

10/01/2018 -

09/30/2019

Procedures

LS-AA-2001

Collecting and Reporting of NRC Performance Indicator Data 15

71152

Corrective Action

Documents

0699328

1FW079B Check Valve Further Closed Than Expected

11/14/2007

4141563

Ovation Alarm Associated with 1FW520

05/26/2018

4165777

1FW079B Check Valve Further Closed Than 1FW079A, C,

and D

08/20/2019

287309

08-OSP-A A1R21 ODEN 1AP27E-D1 Fail to Reset

(1VX01C) Test

10/12/2019

287313

A1R21 ODEN 1AP27E-C4F (1RY8000B) Tripped Out of

Tolerance Low

10/12/2019

287314

A1R21 ODEN 1AP23E-G4F (OSX165B) Tripped Out of

Tolerance

10/12/2019

287316

ODEN 1AP23E-G4R (0SX165B) Tripped Out of Tolerance

10/12/2019

287396

09-OSP-A A1R21 ODEN 1AP28E-D4 Did Not Trip

10/13/2019

287492

08-OSP-R A1R21 ODEN 1AP32E-D5 (1OG084) Tripped Out

of Tolerance

10/13/2019

291137

1FW1137 Full Open Following Power Ascension

10/25/2019

291137

1FW530 Full Open Following Power Ascension

10/25/2019

298999

Trend IR - Breaker Deficiencies in Breaker Refurbishments

11/21/2019

4305858

Trend IR for A1R21 ODEN Testing

2/23/2019

Procedures

NO-AA-10

Quality Assurance Topical Report (QATR)

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program (CAP) Procedure

PI-AA-125-1001

Root Cause Analysis Manual

PI-AA-125-1003

Corrective Action Program Evaluation Manual

71153

Corrective Action

Documents

287444

11-OSP-A: Preliminary Data - Manufacturing Defect on

1FW520 Digital Valve Controller Relay

10/13/2019

292282

Inadvertent Siren Activation of Will County Sirens

10/29/2019