IR 05000423/1981015
| ML20041A253 | |
| Person / Time | |
|---|---|
| Site: | Millstone |
| Issue date: | 02/01/1982 |
| From: | Elsasser T, Mattia J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20041A250 | List: |
| References | |
| 50-423-81-15, NUDOCS 8202190329 | |
| Download: ML20041A253 (7) | |
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U. S. NUCLEAR REGULATORY COMMISSION Region I Report No.
50-423/81-15 Docket No.
50-423 License No.
CPPR-113 Priority
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Category A
Licensee:
Northeast Nuclear Energy Company P. O. Box 270 Hartford, Connecticut 06101 Facility Name:
Millstone Nuclear Power Station, Unit 3 Inspection at:
Waterford, Connecticut Inspection conducted:
December 1 - 31, 1981 Inspectors:,i b 'h <
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~J.C. Mattia, Senior Resident Inspector date signed date signed date signed Approved by:
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,T. Elsasser4 Ehief,< Reactor Projects date signed Section IB, DRPI Inspection Summary:
Unit 3 Inspection on December 1 - 31, 1981 Report No. 50-423/81-15 Areas Inspected:
Routine inspection by the Resident Inspector of work activities associated with pipe erection, electrical cable raceway erection and fuel transfer canal erection. The inspector also performed plant inspection tours and reviewed licensee action on previously identified items. The inspection involved 56 inspection hours, including 2 off-shift hours by one NRC inspector.
Results:
No items of noncompliance were identified.
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9202190329 820203 PDR ADOCK 05000423 C
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' DETAILS 1.
Persons-Contacted Northeast Utilities Service Company (NUSCO)
B.' Carlson, Assistant Project Engineer (Berlin)
F. Comstock, FQA Technician K. Gray,. Construction QA Supervisor W. Langdon, Construction Engineer R. Vaccaro, QA Construction Technician-J. Powers, Licensing Engineer (Berlin)
J. Putnam, Senior Construction Engineer T. Sullivan, Resident Engineer - New Site Construction S. Toth, System Superintendent Generation Construction Stone and Webster Corporation (S&W)-
M. Bezanson, Field QC Inspector M. Hammer, QC Inspector W. MacKay, Resident Manager G. Marsh, Senior Engineer, Welding /NDE W. Orr, Senior QC Inspector M. R. Matthews, Assistant Superintendent Field QC J. Nims, Receiving and Material Controls Technician R. Reams, Materials-Supervisor R. Singh, Senior Electrical QC Engineer W. Towne, Receiving and Material Controls-Technician G. G. Turner, Superintendent, Field QC G. Wilson, Field QC Inspector Westinghouse Corporation C. Peterson, Site Representative
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The inspector also conferred with other licensee and contractor personnel l
during the course of inspection, t
2. Plant Tours L
The inspector observed work activities in progress, completed work and construction status in several areas of the plant. The inspector
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examined work for any obvious defects or noncompliance with regulatory requirem nts or license conditions.
Particular note was taken of the
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presenceIof Quality Control Inspectors and Quality Control evidence such l
as inspettion records, material identification, nonconforming material identifi3ation, housekeeping and equipment preservation. The inspector
l also ir.s}heted the various preparations for concrete operations such as:
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- fo/m erection, rebar placement (
- concrete placement concrete curing j
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N items of noncompliance were identified.
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3.
Licensee Action On Previous Inspectior Findings a.
(Closed) Unresolved item (423/81-14-03): The storage of mechanical Snubbers in warehouse was not in cccordance with vendors instruction.
S&W requested vendor to review their storage instructions and verify if the Snubbers can be stored out of original containers and without removal of the pivot pins. The vendor's reply agreed that the storage was acceptable, but suggested that the pivot pins be removed and placed in plastic bags. S&W has started a program to comply with this recommendation. The inspector observed the crafts removing some of the pivot pins from the Snubbers ard placing the pins in plastic bags, b.
(Closed) Unresolved it_m (423/81-04-01):
Conflicting storage require-ments for some Westingaouse supplied equipment. The flux mapping detectors require a level "B" storage. However, Westinghouse also requires a maximum relative humidity of 70%. Normally, when the humidity level is controlled, it is for level
"A" storage. S&W has built a plastic frame enclosure around the flux mapping system and will install a dehumidifier inside the enclosure to limit the humidity.
to 70%.
c.
(Closed)
Construction deficiency (423/81-00-02): The licensee reported to NRC on February 24, 1981, that a potential significant deficiency involving the use of welding procedures in containment fabrication for an application where they had not been qualified. The inspector reviewed S&W documents relating to this matter and noted that a May 28, 1981, letter addressed to the licensee stated that after completing their evaluation they determined it was.not a reportable significant deficiency. The inspector discussed his concerns with this and other significant deficiencies with licensee representatives from the Berlin Office.
It appears that many outstanding items such as 50.55(e) and Part 21 are not being addressed in a reasonable time period. The licensee has since issued a letter dated December 17, 1981, to the NRC stating that they have concluded that this item is not a significant deficiency and are also in the process of reviewing and replying to other outstanding 50.55(e) and Part 21 items, d.
(Closed) Violation (423/81-11-01): The inspector reviewed the corrective actions taken to prevent the use of uncontrolled copies of design documents by crafts for safety related work activities. The following are the specific actions taken by the licensee:
- Notices were placed on reproduction machines (Xerox, IBM, etc.)
stating " Documents not to be used for construction".
- S&W conducted periodic in-process verification inspections to ascertain that uncontrolled copied design documents were not used by crafts. Verifications conducted on September 1, 8 and 9, 1981 were reviewed.
- Training on control of level I design documents was conducted on 9/15 & 16/81 for construction, engineering and QC personnel.
- S&W memorandum dated September 14, 1981, outlined several corrective actions taken to prevent the use of uncontrol.ied machine copied docu-ments.
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(Closed) Violation (423/81-09-01): S&W had initiated Engineering Design and Coordination Reports (E&DCR) which did not fulfill the procedure requirements; specifically E&DCR F-S-2683 and PS-S-1004 were incorrectly processed. The inspector reviewed the licensee actions to correct the specific violation and also their actions to prevent it trom recurring. The following items were reviewed:
- E&DCR P-S-3812 was issued to supercede PS-S-1004 and identify a change to S&W Specification C-999.
- Addendum No. 1 to Specification C-999 was issued on October 29,1981, to incorporate the concrete repair procedure and update the control change status.
- SSW Engineering Quality Assurance performed an audit, which sanpled 87 issued E&DCR's. The audit did not find an infonnation type E&DCR which had supplemented or superceded a previou; E&DCR.
- S&W Project Procedure NEAM 38, Revision 6, issued September 22,1981, requires that supplementing E&DCR's are to be used only when it is not practical to issue an E&DCR to completely replace the previous E&DCR.
- The S&W Engineering Assurance Procedure 6.5 Revision 0, is now implemented, and provides details for revising E&DCR's.
- A requirement has been placed upon the Project E&DCR Coordinator to review all revisions and addenda to specifications to ensure that all outstanding E&DCR's are properly listed.
4.
Safety Related Piping Erection a. The following weld joints located in the ESF Building were inspected to verify compliance with the applicable specification, welding procedure and ASME Code requirements:
(1) Weld Joint 3QSS-008-33-2 Field Weld No, 4 was a completed weld joint, but radiography revealed three areas where the root weld insert was not fully consumed. The inspector observed the weld repair being performed in accordance with weld technique sheet W12F, Revision 2.
The weld data card for this weld joint was also reviewed.
I (2) Weld Joint 3FWA-008-86-3 Field Weld No. 3 was approximately 3/4 finished. The inspector verified that the welding was in accordance with weld technique sheet W210, Revision 2.
A review of the weld data card was also conducted.
(3) Weld Joints 3CCP-018-556-3, Field Weld Nos. 4, 36-1 & 35-1, were in final stages of welding. The inspector verified that the welding was in accordance with weld technique sheet W20W, Rev. 3.
The weld history card for both weld joints was reviewed for compliance with the applicable S&W QA Procedur.
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(4) Weld Joint 3CCP-01'. 7-3 Field Weld No. 32-1 was approximately one-half completed.
The inspector observed the actual welding and verified that the ;;quirements of weld technique sheet W21H, Revision 2, were adhered to. The weld data card was also reviewed.
(5) The inspecto _ooserved the cutting of pipe spool and also the machining of the end weld preps for a field modification in accord-ance with S&W Construction Revision Notice CCP-523-002.
No violations were identified for the above items.
b. The following weld joints located in the containment building were inspected to verify compliance with welding and installation procedures:
(1) The inspector observed the installation and fit-up of spool piece 3SIL-5-6-1-1 for weld joint 3RCS-010-132-1 Field Weld No. 11.
The rigging and handling of the spool piece was in accordance with the applicable S&W QA documents.
(2) Weld Joint 3RCS-031-8-1 Field Weld No. 5 was approximately one-quarter completed. The inspector observed the actual welding and verified that the requirements of weld technique sheet W13B, Revision 3, were adhered to. The weld data card was also reviewed.
(3) Weld Jcints 3RCS-029-7-1 Field Weld No. 4 and 3RCS-029-6-1 Field Weld No. 2 were in the process of being welded. The inspector verified that the welding was in accordance with weld technique sheet W138, Revision 3.
The weld history and weld shrinkage data was reviewed to verify compliance with the QA documents.
(4) Weld Joint 3SIH-003-26-1 Field Weld No. 7 was recently completed and ready for liquid penetratant (LP) examination. The inspector visually inspected the completed weld prior to LP examination to determine compliance with ASME Code. The inspector also observed the LP examination to verify compliance with Procedure QAD 9.32.
The inspector also reviewed the S&W Field QC inspector's qualifications for performing this examination.
No violations were identified for the above items.
c. The inspector observed the welding of weld joints 3FWA-008-86-3 Field Weld Nos. 3 & 4 located in the auxiliary building. These weld joints were approximately one-half complete. The inspector also verified that the welding was in accordance with weld technique sheet W21U, Revision 2, and that the weld data cards were acceptable.
No violations were identified, a
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5.
Installation Of Containment' Air Purge System The inspector observed the fit-up and welding of a 42" valve (CTV-338)
to containment penetration No. 86. This weld joint is identified as CI-HVU-1A Field Weld No. 2.
The inspector verified that the welding requirements specified in welding technique sheet No. W11B, Revision 1, and the fit-up requirements specified in Procedure W200C and E&DCR No. FM-6645, were being adhered to. An inspection of-the weld data card was also conducted.
No violations were identified.
6.
Erection Of Fuel Transfer Canal In Fuel Building The inspector observed the fit-up and welding of the fuel transfer canal sections. There are two welding technique sheets W76C, Rev. 1 (fillet weld) and W76M, Rev. 0 (butt weld) for this installation. The inspector inspected to insure that the fit-up alignment, root opening and minimum preheat met the procedure requirements. When verifying that the welding technique sheets were the current revision, the inspector noted that-Revision 1 of W76M was issued on September 23, 1981. The inspector approached S&W on this condition, and they informed the inspector that if the welding is in process and none of the essential variables of welding are changed, the welding is allowed to continue with older revision. The inspector verified that the S&W site welding engineer had notated that the Revision 1 of W76M did not change the essential
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variables. The inspector also compared the specific changes of Revision 0 with Revision 1, and agreed with the welding engineer's conclusion.
No violations were identified.
7.
Erection Of Raceways In Control Building a) The inspector observed the welding of several seismic conduit supports in the control building. These supports are depicted on Drawing FSK-CS-710-42L-1. The welding requirements were specified in weld technique sheet W70G, Revision 4 and Drawing ES77A-4.
No violations were identified.
b) The inspector inspected several completed seismic conduit support welds that have been accepted by S&W Quality Control Inspectors.
The specific items inspected are as follows and on Drawing EE-34KT-1:
Support No.
Location (Cable Spreading Room)
AVC 343A - C 343B Elev.
27'-7" 29'-5"
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"B-30'-3"
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- C 346A 25'
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- C 346A 28'
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- C 346A 30'-3"
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No violations were identified.
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7-8.
' Management Meetings ~'
At periodic intervals during!the course of this inspection, meetings were held with'. senior plant management to: discuss the scope and findings
.of this. inspection.
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