IR 05000416/1980014

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IE Insp Repts 50-416/80-14 & 50-417/80-10 on 800603-06.No Noncompliance Noted.Major Areas Inspected:Electrical Equipment in-place Storage & Licensee Actions on Prior Items
ML19344E946
Person / Time
Site: Grand Gulf  Entergy icon.png
Issue date: 07/21/1980
From: Conlon T, Walters D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19344E943 List:
References
50-416-80-14, 50-417-80-10, NUDOCS 8009120141
Download: ML19344E946 (5)


Text

5 ississippi Power and Light Company-2-JUL 21 tgg;

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Should you have any questions concerning this letter, we will be glad to discuss them with you.

Sincerely, fuft

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C. E. Murphy, Chief

, Reactor Construction and Engineering Support Branch

Enclosure:

Inspection Report Nos. 50-416/80-14 and 50-417/80-10

REGION 11

8 101 MARIETTA ST., N.W., SUITE 3100 q

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ATLANTA, G EORGI A 30303

JUL 211980 Report Nos. 50-416/80-14 and 50-417/80-10

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Licensee: Mississippi Power and Light Company Jackson, MS Facility Name: Grand Gulf 1 and 2 Docket Nos. 50-416 and 50-417 License Nos. CPPR-118 and CPPR-119 Inspection at Gr<

Gulf site near Port Gibson, Mississippi Inspector:

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D. K.IWalters /'

'Date Signed Approved by:c j p1!rfy 7 - 3- /- 8 0 C E. Vonlon, Section Chief, RCES Branch Date Signed SUMMARY Inspection on June 3-6, 1980 Areas Inspected This routine, unannounced inspection involved 23 inspector-hours on site in the areas of in-place storage of electrical equipment; facility housekeeping; installa-tion of and quality records for safety-related 4160 volt pump motors and 480 volt valve operators; licensee actions on previously identified items.

Results Of the areas inapected, no items of noncompliance or deviations were identified.

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DETAILS 1.

Persons Contacted Licensee Employees

  • C. K. McCoy, Plant Manager
  • Y. W. Yelverton, Field QA Supervisor
  • H. D. Morgan, Construction Superintendent
  • D. L. Hun'., Plant Quality Supervisor
  • B. C. Lee, QA Representative Other Organizations Bechtel Employees
  • R. L. Scott, Project QA Manager D. D. Washburn, QA Engineer P. W. Collins, QA Engineer R. A. Valdez, QA Engineer O. B. Balis, Lead' Civil Engineer
  • Attended exit interview 2.

Exit Interview The inspection scope and findings were summarized on June 6, 1980 with those persons indicated in Paragraph I above.

3.

Licensee Acti.on on Previous Inspection Findings The below listed items were previously identified in IE inspection report 50-416/79-15 and 50-417/79-15.

a.

Unresolved item 416, 417/79-15-01, Aging effects on electrical pro-

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perties of low force pin crimps.

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Unresolved item 416,417/79-15-02, Aging effects on conductor insulation.

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Unresolved item 416, 417/79-15-03, Aging effects on connector clamp strengths.

d.

Unresolved item 416,417/79-15-04, Shield wires not pull tested.

e.

Unresolved item 416, 417/79-15-05, Environmental effects on hipot test

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results.

f.

Unresolved item 416, 417/79-15-06, Broken wire strands inside pin barrel.

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Unresolved item 416, 417/79-15-07, Evaluation of cable outer jacket damage.

h.

Unresolved item 416, 417/79-15-08, Rework of cable failing continuity check.

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Infraction 416,417/79-15-09, Failure to meet Mil-spec requirements.

In a licensee requested meeting at the Region II office which was attended by representatives of IE Region II, NRR, Mississippi Power and Light (MP&L),

General Electric, Bechtel, Pennsylvania Power and Light (PP&L) and Dupont, the licensee presented the actions to be taken to resolve and correct the above items. Items 1, 2, 3, 5, 6 and 9 are to 1,e addressed by a qualifica-tion test program conducted by General Electric (GE). The licensee has reviewed and concurred on the GE test program currently in progress.

During this inspection, the licensee stated a tentative date of September, 1980, to complete actions and resolution for all items listed above. These items will remain open pending completion of licensee corrective actions.

4.

Unresolved Items Unresolved items were not identified during this inspection.

5.

Independent Inspection Effort (Units 1 & 2)

The facility housekeeping in the Unit I auxiliary building and control building in the ESF switchgear areas was observed. Although debris was observed, ' the amounts were not excessive for construction and testing activities in progress..The in-place storage of unit 2 safety-related switchgear identified below was observed:

Auxiliary Building Switchgear (Elevation 119)

1.

480 volt motor control center (MCC) 26B11 2.

480 volt load center (LC) 2'3B3 3.

480 volt LC 26BB1 4.

480 volt LC 25BA3 Control Building Switchgear (Elevation Ill)

1.

4160 volt switchgear panel 25AA 2.

480 volt MCC 27B11 The auxiliary building switchgear was covered with internal space heaters energized.

The control building switchgear room was heated, and the i

switchgear was observed to have sufficient protection (e.g.,

glass on

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maters and relays covered) for the construction and testing activities in progress.

Within the areas inspected, no items of noncompliance or deviations were identifie,

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Electrical (Components and Systems I) Observation of Work and Work

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Activities and Review of Quality Records The inspector selected Load Sequencing and Shedding panel number Q1H22P331 and Diesel Generator 21 Control panel number Q1H22P115 for inspection.

Installation instructions and inspection requirements are provided in Work Plan and Inspection Records (WP&IR) which are prepared in accordance with Bechtel procedure WP/P-1, " Establishment, Control and Implementation of the Construction Work Plan / Procedure Program". The inspector reviewed WP&IR number Q1H22-S-25A111-YO3 for panel P331 and W2&IR nshar Q1H22-P-12133-YO4 for panel P115. Panel installations were observed to be in accordance with the following Bechtel drawings.

Number Title C-0602A, R14 Unit 1 & 2 control Building Area 25A Reinforced Concrete, Floor Plan at El.111'-0" M-0013, R11 Equipment Location, Control Building Plan at El.93'-0",

111'-0",133'-0" & El.148'-0", Units 1 & 2-FSXE-028-06068, R7 Grounding Plan, Control Bldg El 93'-0" and 111'-0",

Units 1 & 2 M-1026, R12 Equipment Location, Diesel Generator Building, Unit 1 C-1506C, R7 Unit 1 Diesel Gen. Bldg Area 12, Reinforced Concrete

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Sections and Details E-1610, R3 Grounding Plans, Diesel Generator Building, Area 12, Unit 1 The Material Receiving Instruction and Inspection Report (MRI&IR) number 330E and the vendor certificate of compliance were reviewed for panel P331.

Both in-place panels were observed to be located in accordance with the above drawings.

Within the areas inspected, no items of noncompliance or deviations were identified.

Observation of Work and Work 7.

Electrical (Components and Systems II)

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Activities and Review of Quality Records The safety-related components identified below were selected for inspection.

Component Number High Pressure Core Spray (HPCS)

Q1E22C001 Pump Motor Standby Service Water (SW) Pump B Q1P41C001B-B Motor-

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e g-4-Reactor Heat Removal (RHR) Pump A Q1E12C002A-A Motor SSW Pump A Discharge Valve Motor Q1P41F001A-A Operator PSW to SSW Intetie Valve Motor QSP41F189-B Operator RHR A Shutdown Cooling Isolation Q1E12F009-B Valve McLur Operator RWCU Isolation Valve Motor Operator Q1G33F040-B The installation of 4160 volt SSW pump B motor was inspected for compliance with the requirements of WP&IR number 129-M, and the installation of 4160 volt RHR pump A motor was inspected for compliance with WP&IR number Q1E12-C-07093-Y0A. Quality documentation reviewed included MRI&IR number NSSS-E22-IUC for the HPCS pump motor, MRI&IR number 129-M for the SSW pump B motor, MRI&IR number NSSS-S12-IUC for the RER pump B motor, and vendor certifications for all three pump motors. Although the installation of the HPCS pump motor was observed and appeared to meet requirements, the installa-tion was not verified against the WP&IR requirements.

The installations of the 480 volt m,.or operators for valves Q1P41F001A-A and QSP41F189-B were inspected for compliance with the valve Installation Card requirements.

The installation of motor operators for valves Q1G33F040-B and Q1E12F009-B was not observed due to the status of prepara-tions - for performance of the containment drywell integrity test (instru-mentation alignments were complete and containment lighting had been removed). Quality documentation reviewed included MRI&IR number 044 for valve operator Q1I41F001A-A, MRI&IR number 039 for valve operator Q1E12F009-B, and vendor certifications for valve operators Q1P41F001A and Q1E12F009-B.

Within the areas inspected, no items of noncompliance or deviations were identified.

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