IR 05000390/2019004
| ML20043F235 | |
| Person / Time | |
|---|---|
| Site: | Watts Bar |
| Issue date: | 02/12/2020 |
| From: | Tom Stephen NRC/RGN-II |
| To: | Jim Barstow Tennessee Valley Authority |
| References | |
| IR 2019004 | |
| Download: ML20043F235 (14) | |
Text
February 12, 2020
SUBJECT:
WATTS BAR, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000390/2019004, 05000391/2019004 AND 07201048/2019001
Dear Mr. Barstow:
On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Watts Bar, Units 1 and 2. On January 14, 2020, the NRC inspectors discussed the results of this inspection with Mr. Anthony Williams and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Thomas A. Stephen, Chief Reactor Projects Branch 5 Division of Reactor Projects
Docket Nos. 05000390, 05000391 and 07201048 License Nos. NPF-90 and NPF-96
Enclosure:
As stated
REGION II==
Inspection Report
Enclosure
Docket Numbers:
05000390, 05000391 and 07201048
License Numbers:
Report Numbers:
05000390/2019004, 05000391/2019004 and 07201048/2019001
Enterprise Identifier: I-2019-001-0152
Licensee:
Tennessee Valley Authority
Facility:
Watts Bar, Units 1 and 2
Location:
Spring City, TN 37381
Inspection Dates:
October 01, 2019 to December 31, 2019
Inspectors:
W. Deschaine, Senior Resident Inspector
C. Fontana, Emergency Preparedness Inspector
J. Hamman, Resident Inspector
D. Lanyi, Senior Operations Engineer
S. Ninh, Senior Project Engineer
S. Sanchez, Senior Emergency Preparedness Inspector
J. Walker, Emergency Response Inspector
Approved By:
Thomas A. Stephen, Chief
Reactor Projects Branch 5
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Watts Bar, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000391/2019-001-00 LER 2019-001-00 for Watts Bar Nuclear Plant, Unit 2 Regarding Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed.
71153 Closed LER 05000390/2019-003-00 LER 2019-003-00 for Watts Bar Nuclear Plant, Unit 1,
Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed 71153 Closed
REPORT DETAILS
PLANT STATUS
Unit 1 began the inspection period shutdown for turbine repairs. On October 22, 2019, the unit went critical and returned to rated thermal power on October 24, 2019. Unit 1 remained at or near rated thermal power for the remainder of the inspection period.
Unit 2 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures.
External Flooding Sample (IP Section 03.04) (1 Sample)
- (1) The inspectors evaluated readiness to cope with external flooding for the following areas:
- Intake Pumping Station
- Emergency Diesel Generator Building
71111.04Q - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2, A and B motor driven auxiliary feedwater trains, while the turbine driven auxiliary feedwater train was out of service for level control valve trouble shooting and repairs on October 11, 2019.
(2)1A emergency diesel generator while 1B emergency diesel generator was out of service due to a fire in exciter cubicle on October 30, 2019.
- (3) Unit 1 & 2 Auxiliary Control Air System (ACAS) on November 5, 2019.
71111.04S - Equipment Alignment
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated system configurations during a complete walk down of the Unit 1 and 2 safety injection system on December 30, 2019.
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (1 Sample)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Auxiliary building 713.0 elevation on December 30, 2019.
71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance
Requalification Examination Results (IP Section 03.03) (1 Sample)
- (1) The licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), "Requalification Requirements," of the NRC's "Operator's Licenses." During the week of December 23, 2019, the inspector performed an in-office review of the overall pass/fail results of the individual operating examinations, the crew simulator operating examinations, and the biennial written examinations in accordance with Inspection Procedure (IP) 71111.11, "Licensed Operator Requalification Program." These results were compared to the thresholds established in Section 3.02, "Requalification Examination Results of IP 71111.11.
The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam and biennial written examination completed on November 18, 2019.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed the main control room of Unit 1 during start-up activities coming out of the forced outage on October 21 & 22, 2019.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed simulator scenario 3-OT-SRE-1006, Revision 1, which included a component cooling water pump shaft shear, followed by a hot leg loss of coolant accident with safety injection failing on October 29, 2019.
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (4 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 1 and 2, Function 082-B, Emergency Diesel Generator (a)(1) Evaluation
- (2) Unit 1 Function 235-B 120 Vital Instrument Power (a)(1) Evaluation
- (3) CR 1556229, Steam Generator #3 Level Control valve, 2-LCV-003-172, stroke time failure on May 22, 2019
- (4) Watts Bar Nuclear Plant Units 1 and 2 Maintenance Rule Program (a)(3) Periodic Evaluation
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Risk assessment for week of October 15, with the 1B emergency diesel generator out of service due to a fire in the exciter cubicle
- (2) Risk assessment for week of October 28, with the 1B motor driven auxiliary feedwater pump out of service for planned maintenance
- (3) Risk assessment for week of November 4, with the A train auxiliary air compressor out of service for planned maintenance
- (4) Risk assessment for week of November 18, with the 1A-A emergency diesel generator (EDG) out of service for planned maintenance
- (5) Risk assessment for week of December 8, with the Unit 1 Main Steam Loop 4 Pressure Transmitter (1-PT-1-27B) tagged out due to a steam leak and the 1B residual heat removal pump out for planned maintenance
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (6 Samples)
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Operability determination for CR 1561235, failure of lubricating oil pump discharge pressure gauge for 1B-B motor driven auxiliary feedwater pump
- (2) Immediate determination of operability for CR 1556746, failure of emergency diesel generator 2A-A room heater
- (3) Immediate determination of operability for CR 1556562, abnormal sound in emergency diesel generator engine 2A2 lubrication oil circulation pump
- (4) Operability determination for CR 1556571, received window 60-A auxiliary feedwater pump electronic overspeed trip or trouble multiple times
- (5) Immediate determination of operability for CR 1541453, excessive seal leakage on E-B essential raw cooling water pump
- (6) Immediate determination of operability for CR 1555289, failure of the Unit 2 turbine-driven auxiliary feedwater pump overspeed trip linkage
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)
The inspectors evaluated the following temporary or permanent modifications:
- (1) Permanent modification design change notice 63820, Addition of a new safety-related auxiliary control air subsystem swing air compressor and air dryer skid
- (2) WBN-1-2019-001-001, Temporarily replace flexible hose on 1-PT-1-27B sensing line with a Swagelok fitting to repair a steam leak on December 12, 2019
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)
The inspectors evaluated the following post maintenance tests:
- (1) WO 120841664, 2-SI-3-16, 18 Month Channel Calibration of Steam Generator 3 Turbine Driven Auxiliary Feed Water Level Control Loop 2-LPL-3-172, following repairs to 2-LCV-003-0172-A on October 11, 2019
- (2) WO 120858219, 1-TRI-85-1, Reactivity Control Systems Movable Control Assemblies (Modes 3, 4 AND 5) following circuit card replacement on October 21, 2020
- (3) WO 120878153, 1-SI-3-907-B Valve Position Indication (Train B) Auxiliary Feedwater System, following solenoid replacement on 1-LCV-3-148A on October 29, 2019
- (4) WO 120289270, post maintenance test run of lubricating oil pump for 1B-B motor driven auxiliary feedwater pump following lube oil pump replacement on October 29, 2019
- (5) WO 120846057, emergency diesel generator 1B voltage regulator tuning and postmaintenance testing following the replacement all 3 linear reactors and damaged cables located in the 1B emergency diesel generator exciter cubicle on October 18, 2019
- (6) WO 120928508, 0-SI-82-11-A Monthly Diesel Generator Start and Load Test DG 1A-A following emergency diesel generator outage on November 22, 2019
- (7) WO 120603491, Postmaintenance testing following replacement of the safety injection pump 1A room cooler coil on October 2, 2019
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated a Unit 1 forced outage due to a unit trip caused by a #2 main feedwater regulating valve failure from August 31, 2019 to October 23, 2019.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01)
- (1) WO 118180277, 0-SI-82-7, 10 Year Diesel Generator Interdependence Test
- (2) WO 118180277, 0-SI-82-17-A, 184 Day Fast Start And Load Test Diesel Generator 1A-A following Interdependence Test
- (3) WO 120452206, 2-SI-3-901-A, Auxiliary Feedwater Pump 2A-A Quarterly Performance Test
- (4) WO 120482998, 2-SI-99-10-B, 62 Day Functional Test of SSPS Train B and Reactor Trip Breaker B
RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)
- (1) WO 120450906, 2-SI-68-32 Reactor Coolant System Water Inventory Balance
71114.01 - Exercise Evaluation
Inspection Review (IP Section 02.01-02.11) (1 Sample)
- (1) The inspectors evaluated the biennial emergency plan exercise during the week of November 4, 2019. The exercise scenario simulated an earthquake felt onsite and met the criteria for declaration of an Unusual Event. An aftershock caused the 2B residual heat removal pump to trip and subsequently led to the declaration of an Alert on Unit 2. A loss of condenser vacuum forced the operators to trip the Unit 1 reactor, thereby causing a chain of events that eventually led to a loss of all feedwater and created conditions for declaring a Site Area Emergency. As part of the simulated event response, the operators manually activated safety injection, which in turn created another chain of events that ultimately led to containment pressurization with failure of the containment protection systems. Once radiation levels reached a prescribed threshold, the conditions for a General Emergency were met, and the Offsite Response Organizations were able to demonstrate their ability to implement emergency actions.
71114.04 - Emergency Action Level and Emergency Plan Changes
Inspection Review (IP Section 02.01-02.03) (1 Sample)
- (1) The inspectors evaluated submitted Emergency Action Level, Emergency Plan, and Emergency Plan Implementing Procedure changes during the week of November 4, 2019. This evaluation does not constitute NRC approval.
71114.06 - Drill Evaluation
Drill/Training Evolution Observation (IP Section 03.02) (2 Samples)
The inspectors evaluated:
- (1) The residents observed the site emergency response to a training drill which involved a turbine trip, without an immediate reactor trip, followed by a steam generator tube rupture leading to a general emergency declaration on October 9, 2019.
- (2) The residents observed the site emergency response to a training drill which involved a loss-of-coolant accident with a failure of the containment sump recirculation valves to open, on October 30, 2019. The scenario also involved the site emergency response organization using the severe accident mitigation guidelines to try and restore core cooling.
71114.08 - Exercise Evaluation Scenario Review
Inspection Review (IP Section 02.01 - 02.04) (1 Sample)
- (1) The inspectors reviewed and evaluated in-office, the proposed scenario for the biennial emergency plan exercise at least 30 days prior to the day of the exercise.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
EP01: Drill/Exercise Performance (IP Section 02.12)===
- (1) EP01: Drill & Exercise Performance for the period October 1, 2018, through September 30, 2019.
EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)
- (1) EP02: Emergency Response Organization Drill Participation for the period October 1, 2018, through September 30, 2019.
EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)
- (1) EP03: Alert & Notification System Reliability for the period October 1, 2018, through September 30, 2019.
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Excessive water found in the 2B motor driven auxiliary feedwater pump outboard bearing oiler due to outboard pump seal leaking a stream of water impacting outboard bearing housing (CR 1444650).
71153 - Followup of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)
The inspectors evaluated the following licensee event reports (LERs):
- (1) LER 05000390/2019-003-00, Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed (ADAMS accession: ML19294A010). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.
- (2) LER 05000391/2019-001-00, Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed (ADAMS accession: ML19199A085). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.
Personnel Performance (IP Section 03.03) (1 Sample)
- (1) The inspectors evaluated a Unit 1 solid state protection system (SSPS) circuit card failure, with an unexpected reactor trip bypass breaker failure during SSPS troubleshooting, and the licensees performance in response to this issue, on December 31,
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants Operation of an Independent Spent Fuel Storage Installation at Operating Plants
- (1) The inspectors evaluated the licensees activates related to long-term operation and monitoring of their independent spent fuel storage installation.
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On January 14, 2020, the inspectors presented the integrated inspection results to Mr.
Anthony Williams and other members of the licensee staff.
- On November 7, 2019, the inspectors presented the Emergency Preparedness Exercise Inspection inspection results to Mr. Tony Williams and other members of the licensee staff.
THIRD PARTY REVIEWS
Inspectors reviewed the World Association of Nuclear Operators (WANO) report that was issued for Watts Bar in March 2018.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
60855.1
Procedures
0-SI-79-2
Dry Cask Storage Log
Revision 7
Corrective Action
Documents
Condition Reports 1564591, 1562311, 1562302, 1556745, 156746
Miscellaneous
3-OT-STG-084A
Flood Mode Boration Makeup System Student Training
Guide
Revision 8
N3-84-4001
System Description for Flood Mode Boration Makeup
System
Revision 6
Procedures
0-PI-OPS-1-FP
Freeze Protection
Miscellaneous
WBN-SDD-N3-
63-4001
System Description, Safety Injection System
Revision 35
Procedures
1,2-SOI-63.01
System Operating Instruction for the Safety Injection System
Revision 19
71111.05Q Fire Plans
AUX-0-713-01
Pre-Fire Plan for Aux Building 713.0 Elevation
Revision 1
AUX-0-713-02
Pre-Fire Plan for Aux Building 713.0 Elevation
Revision 3
AUX-0-713-03
Pre-Fire Plan for Aux Building 713.0 Elevation
Revision 4
Miscellaneous
Component Deficiency Evaluation 1633
Watts Bar Nuclear Plant Maintenance Rule Expert Panel
Meeting Minutes
11/14/2019
14-PAR-WBN
WBN Maintenance Rule Program Fourteenth Periodic
Evaluation Assessment Report 10CFR50.65(a)(3)
Revision 0
Procedures
NPG-SPP-03.4
Maintenance Rule Performance Indicator Monitoring,
Trending, and Reporting
Miscellaneous
Operator's Risk Report
11/18/2019
Procedures
1-PI-OPS-1-PE
Protected Equipment
NPG-SPP-
09.11.1
Equipment Out of Service Management
Corrective Action
Documents
Condition Report
1561235, 1556562, 1322853, 1541453, 1454816, 1555289
Miscellaneous
SDD-N3-3B-4002
Auxiliary Feedwater System Unit 1 / Unit 2
Revision 29
SDD-N3-82-4002
Standby Diesel Generator System Unit 1 / Unit 2
WBN-SDD-N3-
67-4002
Essential Raw Cooling Water System, System 67
Revision 37
WBN-VTD-1075-
0080
Vendor Manual
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Procedures
1-SI-0-2B-01
0700-1900 Shift and Daily Surveillance Log Mode 1
Work Orders
Work Orders
20289270
Engineering
Changes
DCN-63820
Addition of a new safety-related Auxiliary Control Air
Subsystem (ACAS) swing air compressor and air dryer skid
Revision B
WBN-1-2019-
001-001
Temporarily replace flexible hose on 1-PT-1-27B sense line
with a Swagelok fitting to repair a steam leak
Revision 0
Corrective Action
Documents
Condition Reports 1558700, 1567851
Procedures
0-SI-82-11-A
Monthly Diesel Generator Start and Load Test DG 1A-A
1-SI-3-907-B
Valve Position Indication Verification (Train B) Auxiliary
Feedwater System
1-TRI-85-1
Reactivity Control Systems Movable Control Assemblies
(Modes 3, 4 AND 5)
2-SI-3-16
Month Channel Calibration of Steam Generator 3 Turbine
Driven Auxiliary Feed Water Level Control Loop 2-LPL-3-172
2-SI-3-908
Valve Full Stroke Exercising During Plant Operation Turbine
Driven Auxiliary Feedwater
Work Orders
20603491
Replacement of the safety injection pump 1A room cooler
coil
10/02/2019
20846057
Replacement all 3 linear reactors and damaged cables
located in the 1B EDG exciter cubicle
10/18/2019
Work Orders
20319939, 120841664, 120858219, 120878153,
20193806, 120928508
Corrective Action
Documents
Condition Report
1555433
Procedures
0-SI-82-17-A
184 Day Fast Start And Load Test Diesel Generator 1A-A
following Interdependence Test
0-SI-82-7
Year Diesel Generator Interdependence Test
2-SI-3-901-A
Auxiliary Feedwater Pump 2A-A Quarterly Performance Test
Revision 10
2-SI-68-32
Reactor Coolant System Water Inventory Balance
Revision 5
2-SI-99-10-B
Day Functional Test of SSPS Train B and Reactor Trip
Breaker B
Revision 11
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Miscellaneous
Watts Bar Nuclear Plant Integrated Training Drill packet
10/09/2019
2019 Watts Bar Nuclear September Training Drill packet
10/30/2019
Corrective Action
Documents
Condition Reports 1518719, 1284060, 1545537
Miscellaneous
0-IMI-101
Instrument Maintenance Planning and Work Activity
Guidelines
Revision 1
0-MI-MVV-003-
001.00
Maintenance Instruction for Fisher Main Feedwater
Regulating Valve Maintenance
Revision 19
WBN-2-MVOP-
0003-0048
PM Work Instructions
Revision 1
Procedures
NPG-SPP-09.20
Vendor Manual Control
Revision 8
NPG-SPP-2.5
Vendor Manual Control
Revision 0
NPG-SPP-22.500
Operating Experience Program
Revision 4