IR 05000324/1980026

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IE Insp Repts 50-324/80-26 & 50-325/80-29 on 800601-30. No Noncompliance Noted.Major Areas Inspected:Control Room Observations,Unit 1 Refueling Operations,Review of Plant Logs,Tour of Vital Areas & Physical Security
ML19344F530
Person / Time
Site: Brunswick  
Issue date: 07/23/1980
From: Kellogg P, Ouzts J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19344F491 List:
References
50-324-80-26, 50-325-80-29, NUDOCS 8009150375
Download: ML19344F530 (3)


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UNITED STATES

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101 MARIETTA sT., N.W., sulTE 3100 j

V ATLANTA, GEORGIA 30303 g

Report Nos. 50-324/80-26 and 50-325/80-29 Licensee: Carolina Power and Light Company

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411 Fayetteville Street Raleigh, NC 27602 Facility Name: Brunswick Units 1 and.2 Docket Nos. 50-324 and 50-325 License Nos. DPR-62 and DPR-71 Inspection at Brunswie site near So hpo t, NC Inspector:

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J. E. Ouztk

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V Date $ip,ned Approved by:

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P. J. Kelfoggg h io lei, xUNS Branch D/t6 Sig'ned o

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SUMMARY Inspection on June 1-30, 1980 Areas Inspected This routine announced inspection involved 104 inspector-hours onsite in the areas of control room observations, Unit I refueling operations, review of plant logs, tour of vital areas, physical security, radiation protection, beusekeeping and cleanliness, fire protection, review and followup on licensee event reports.

Unit 1 Areas Inspected This routine inspection by the resident inspector involved 54 manhours of inspec-tion time onsite in the nine areas identified above.

Unit 1 Findings Of the nine areas inspected, no apparent items of noncomplinace or deviations were identified.

Unit 2 Areas Inspected This routine inspection by the resident inspector involved 50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br /> of inspection

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time onsite in the nine areas identified above.

Unit 2 Findings Of the nine areas inspected, no apparent items of noncomplinace or deviations were observed.

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1009150375

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bk DETAILS 1.

Persons Contacted

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Licensee Employees A. C. Tollison,' Plant General Manager J. M. Brown, Operations Manager K. E. Enzor,. Maintenance Supervisor, I&C G. T. Milligan, Maintenance Manager J. A. Padgett, QA and Safety Director W. M. Tucker, Administrative and Technical Manager L. V. Wagoner, Engineering Supervisor Other licensee emplovees contacted included three technicians, twelve oper-ators, eight securit) force members, and two office personnel.

Other Organizations Army Corps of Engineers - Wilmington, North Carolina - F. Yelverton called regarding oil spill analysis for Cape Fear River.

  • Attended exit interview 2.

Exit Interview The inspection scope and findings were summarized on June 13 and 27, 1980, with those persons indicated in Paragraph 1 above.

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Licensee Action on Previous Inspection Findings Not inspected.

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Unresolved Items Unresolved items were not identified during this inspection.

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The resident inspector conducted plant tours, performed surveillance of plant operations and inspected plant conditions as identified below:

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Control Room Observations b.

Unit 1 Refueling Floor Refueling Operations c.

Operator Log Review d.

Tour of Vital Areas e.

Physical Security Protection f.

Radiation Protection g.

Fire Protection h.

Housekeeping and Cleanliness

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Acceptance Criteria-The inspector used one 'or more _of the following sources of acceptance cri-

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teria for evaluating the'above areas inspected:

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.10.CFR 50, Appendix "B"

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10 CFR 20 c.

. Technical Specification d.

ANSI N45.2.3 (1971)

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ANSI N18.7 0972)

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Regulatory Guiles-g.

Safe Security Plan h.

Quality Assurance Program

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