IR 05000280/2025003
| ML25330A009 | |
| Person / Time | |
|---|---|
| Site: | Surry |
| Issue date: | 12/02/2025 |
| From: | Shawn Smith NRC/RGN-II/DORS/PB6 |
| To: | Carr E Dominion Energy |
| References | |
| IR 2025003 | |
| Download: ML25330A009 (0) | |
Text
SUBJECT:
SURRY POWER STATION - INTEGRATED INSPECTION REPORT 05000280/2025003 AND 05000281/2025003
Dear Eric S. Carr:
On September 30, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Surry Power Station. On November 21, 2025, the NRC inspectors discussed the results of this inspection with James Shell, Plant Manager, and other members of your staff. The results of this inspection are documented in the enclosed report.
Due to the temporary cessation of government operations, which commenced on October 01, 2025, the NRC began operating under its Office of Management and Budget-approved plan for operations during a lapse in appropriations. Consistent with that plan, the NRC operated at reduced staffing levels throughout the duration of the shutdown. However, the NRC continued to perform critical health and safety functions and make progress on other high-priority activities associated with the ADVANCE Act and Executive Order 14300. On November 13, 2025, following the passage of a continuing resolution, the NRC resumed normal operations.
However, due to the 43-day lapse in normal operations, the Office of Nuclear Reactor Regulation granted the Regional Offices an extension on the issuance of the calendar year 2025 inspection reports that should have been issued by November 13, 2025, to December 31, 2025. The NRC resumed the routine cycle of issuing inspection reports on November 13, 2025.
No NRC-identified or self-revealing findings were identified during this inspection.
A licensee-identified violation which was determined to be of very low safety significance is documented in this report. We are treating this violation as a non-cited violation (NCV)
consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Surry Power Station.
December 2, 2025 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Steven P. Smith, Chief Projects Branch 6 Division of Operating Reactor Safety Docket Nos. 05000280 and 05000281 License Nos. DPR-32 and DPR-37
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000280 and 05000281
License Numbers:
Report Numbers:
05000280/2025003 and 05000281/2025003
Enterprise Identifier:
I-2025-003-0031
Licensee:
Dominion Energy
Facility:
Surry Power Station
Location:
Surry, VA
Inspection Dates:
July 1, 2025, to September 30, 2025
Inspectors:
S. Battenfield, Operations Engineer
W. Deschaine, Senior Project Engineer
C. Even, Senior Project Engineer
K. Henry, Regional Governmental Liaison Officer
D. Jung, Senior Resident Inspector
A. Nielsen, Senior Health Physicist
D. Orr, Senior Project Engineer
M. Read, Senior Resident Inspector
D. Restrepo, Resident Inspector
M. Rich, Emergency Preparedness Inspector
J. Rivera, Health Physicist
J. Walker, Senior Emergency Preparedness Inspector
Approved By:
Steven P. Smith, Chief
Projects Branch 6
Division of Operating Reactor Safety
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Surry Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section: 71124.0
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Unit 1 began the inspection period at rated thermal power. On August 6, 2025, the unit experienced a reactor trip due to a spurious actuation of high consequence limiting safeguards (CLS) train B' due to a failed Hi CLS 1B relay. Following correction of the cause of the reactor trip, the unit was returned to rated thermal power on August 11, 2025.
Unit 2 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
(1)
'A' emergency service water pump (ESWP) during 'B' ESWP performance testing on July 17, 2025
- (2) Unit 1 turbine driven auxiliary feedwater pump (TDAFWP) following Unit 1 startup on August 13, 2025
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated system configurations during a complete walkdown of the Unit 2 TDAFWP system on September 4, 2025.
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Number 3 emergency diesel generator (EDG) room, fire area 8, elevation 27 feet - 6 inches, on July 16, 2025
- (2) Charging pumps, Unit 1 auxiliary building, fire area 17, elevation 13 feet and elevation 2 feet, on July 18, 2025
- (3) Unit 2 safeguards complex, fire area 20, elevations 27 feet - 6 inches and 11 feet - 6 inches, on August 1, 2025
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the onsite fire brigade training and performance during an announced fire drill on August 19, 2025.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the main control room (MCR) during Unit 1 reactor trip due to spurious train B Hi CLS system actuation on August 6, 2025.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the simulator during a licensed operator requalification training involving vital bus offsite power lost due to reserve station service transformer lockout, and large break loss of coolant accident (LOCA) inside containment on July 29, 2025.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Partial)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
(1)
(Partial) Unit 1 heat trace panel that supports hydrogen analyzer found not energized on August 19, 2025 (Condition Report [CR] 1298739)
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Medium risk plan review during train B of spent fuel pool cooling on July 30, 2025
- (2) Medium risk plan review prior to the input/output (I/O) amplifier card replacement in Unit 2 rod control cabinet on July 31, 2025
- (3) High risk plan review during train B Hi CLS relay replacement in Unit 1 CLS cabinet number 1 on August 7, 2025
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) CR1295193, 1-FW-P-2, Unit 1 TDAFWP, outboard bearing low oil pressure during surveillance testing on July 1, 2025
- (2) CR1295657, 2-SW-P-10B, Unit 2 charging pump service water (CPSW) pump, flow transient during CPSW check valve (1-SW-108) maintenance on July 8, 2025
- (3) CR1296765, 2-EE-PI-227, number 2 EDG fuel system number 1 outlet pressure, reads incorrectly on July 21, 2025
- (4) CR1298780, corrosion on stud/nuts for inlet flange to self-cleaning strainer that supports main control room chillers on August 22, 2025
- (5) CR1301871, letdown ion exchanger differential pressure exceeded 80 pounds with 1-CH-I-3B, 3B deborating demineralizer, in service on September 26, 2025
71111.24 - Testing and Maintenance of Equipment Important to Risk
The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:
Post-Maintenance Testing (PMT) (IP Section 03.01) (6 Samples)
(1)1-IPT-CLS-HIHI-LGC-8.5B, Consequence Limiting Safeguards Logic Train B (Hi-Hi CLS), following Hi-Hi CLS relay replacement on July 2, 2025 (Work Order [WO]
===38204373574)
- (2) PMT-CMP-OP-01, Component In-Service Visual Leak Test, following number 2 EDG fuel filter pressure gauge replacement on July 21, 2025 (WO 38204374933)
(3)0-OP-SW-002, Emergency Service Water Pump 1-SW-P-1B, following 1B ESWP maintenance package on July 21, 2025 (WO 38204356516)
(4)0-OPT-EG-009, Number 3 Emergency Diesel Generator Major Maintenance Operability, following 6-year and 18-month planned maintenance on August 15, 2025 (WO 38204341144)
(5)2-OPT-RX-005, Control Rod Assembly Partial Movement, following Unit 2 rod control cabinet I/O amplifier card reseating on August 19. 2025 (WO 38204375428)
(6)2-PT-18.8, Charging Pump Service Water Performance, following Unit 2 B CPSW pump preventative maintenance on August 21, 2025 (WO 38204328385)
Surveillance Testing (IP Section 03.01)===
(1)0-OSP-AAC-001, Quarterly Test of 0-AAC-DG-OM, Alternate Alternating Current Diesel Generator, on July 7, 2025 (2)1-OPT-EG-001, Number 1 Emergency Diesel Generator Quarterly Performance Test, on July 28, 2025 (3)1-OPT-CH-003, Charging Pump Operability and Performance Test for 1-CH-P-1C, on July 11, 2025 (4)2-IPT-CLS-HI-LGC-8.4A, Consequence Limiting Safeguards (Hi-Train A), on September 16, 2025
71114.04 - Emergency Action Level and Emergency Plan Changes
Inspection Review (IP Section 02.01-02.03) (1 Sample)
- (1) The inspectors evaluated submitted Emergency Action Level (EALs), Emergency Plan, and Emergency Plan Implementing Procedure changes during the week of July 21, 2025. This evaluation does not constitute NRC approval.
71114.06 - Drill Evaluation
Additional Drill and/or Training Evolution (1 Sample)
The inspectors evaluated:
- (1) The inspectors observed a licensed operator training evolution in the MCR simulator that contributed to the Emergency Response Organization Performance Indicators on August 26, 2025. Events included vital bus offsite power lost due to reserve station service transformer lockout, and large break LOCA inside containment requiring containment spray manual start.
71114.07 - Exercise Evaluation - Hostile Action (HA) Event
Inspection Review (IP Section 02.01 - 02.11) (1 Sample)
- (1) The inspectors evaluated the biennial emergency plan exercise during the week of July 22, 2025. The scenario began with a simulated report from the field that a hostile action was occurring outside the protected area, thus meeting the criteria for declaration of an Alert. Subsequently, simulated adversaries breached the protected area and engaged site security, and a Site Area Emergency was declared. As the scenario progressed, a simulated explosion occurred near low-head safety injection piping. The percussive force caused check valves to fail, allowing reactor coolant system leakage and causing fuel damage, which resulted in increasing radiation levels. When effluent radiation levels reached a prescribed threshold, conditions for a General Emergency were met, and the Offsite Response Organizations demonstrated their ability to implement emergency actions.
71114.08 - Exercise Evaluation - Scenario Review
Inspection Review (IP Section 02.01 - 02.04) (1 Sample)
- (1) The inspectors reviewed and evaluated in-office, the proposed scenario for the biennial emergency plan exercise at least 30 days prior to the day of the exercise.
RADIATION SAFETY
71124.06 - Radioactive Gaseous and Liquid Effluent Treatment
Walkdowns and Observations (IP Section 03.01) (3 Samples)
The inspectors evaluated the following radioactive effluent systems during walkdowns:
- (2) Liquid radwaste discharge pathway, through effluent monitor 1-RRM-RE-131
Sampling and Analysis (IP Section 03.02) (3 Samples)
Inspectors evaluated the following effluent samples, sampling processes and compensatory samples:
(1)1-GW-RM-130B, Process vent noble gas monitor, compensatory sampling, July 31, 2023 (2)1-SW-RM-120, Circulating water discharge monitor, compensatory sampling, September 19 - September 20, 2024 (3)1-VG-RM-131B, Ventilation vent 2 gaseous effluent monitor, sample line configuration
Dose Calculations (IP Section 03.03) (2 Samples)
The inspectors evaluated the following dose calculations:
- (1) L-20250604-118-B, liquid waste release permit
- (2) G-20250601-142-C, Gaseous release permit
71124.07 - Radiological Environmental Monitoring Program
Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated environmental monitoring equipment and observed collection of environmental samples.
Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the implementation of the licensees radiological environmental monitoring program.
GPI Implementation (IP Section 03.03) (1 Sample)
- (1) The inspectors evaluated the licensees implementation of the Groundwater Protection Initiative (GPI) program to identify incomplete or discontinued program elements.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===
- (1) Unit 1 (October 1, 2023, through December 31, 2024)
- (2) Unit 2 (October 1, 2023, through December 31, 2024)
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)
- (1) Unit 1 (October 1, 2023, through December 31, 2024)
- (2) Unit 2 (October 1, 2023, through December 31, 2024)
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)
- (1) Unit 1 (October 1, 2023, through December 31, 2024)
- (2) Unit 2 (October 1, 2023, through December 31, 2024)
PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)
- (1) May 10, 2024, through July 15, 2025
EP01: Drill/Exercise Performance (DEP) Sample (IP Section 02.12) (1 Sample)
- (1) July 1, 2024, through March 31, 2025 EP02: Emergency Response Organization (ERO) Drill Participation (IP Section 02.13) (1 Sample)
- (1) July 1, 2024, through March 31, 2025 EP04: Emergency Response Facility and Equipment Readiness (ERFER) (IP Section 02.14) (1 Sample)
- (1) July 1, 2024, through March 31, 2025
===71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03) (1 Partial)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
(1)
(Partial) Units 1 and 2 TDAFWP surveillance test failures (CR1284152, 1280548, and 1283327)71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Follow-up (IP Section 03.01)===
- (1) The inspectors evaluated Unit 1 reactor trip due to the spurious Hi CLS actuation and licensees response on August 6, 2025. Per IMC 0309, Reactive Inspection Decision Basis for Power Reactors, the NRC considered whether this inspection sample should be the subject of a reactive inspection and determined that a reactive inspection was not necessary, as documented in ML25237A179.
INSPECTION RESULTS
Licensee-Identified Non-Cited Violation 71124.06 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Violation: Technical Specification 6.4 N(1) requires effluent monitor surveillance to be performed in accordance with the methodology in the ODCM. Attachment 2 of the ODCM requires that 1-SW-RM-120, Unit 1 circulating water discharge monitor, be calibrated on an 18-month frequency. Contrary to this, on June 24, 2024, the grace period for the most recent 18-month cycle expired without calibration being performed. The delays were due to a calibration source that had decayed below the point of usability, and a technical evaluation (TE) that incorrectly determined it was acceptable to extend the calibration out for an additional 6 months. Licensee staff identified the error in September of 2024, initiated compensatory sampling, and performed a causal evaluation. With assistance from the radiation monitor vendor, the licensee was able to perform a calibration on September 19, 2024, however the detector was found to be out of tolerance and had to be replaced.
Significance/Severity: Green. The finding was part of the licensee's effluent release program, but it did not represent a failure to implement the program and did not involve any release of radioactive material into the environment.
Corrective Action References: CR 1261927 and CR
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On November 21, 2025, the inspectors presented the integrated inspection results to James Shell, Plant Manager, and other members of the licensee staff.
- On July 17, 2025, the inspectors presented the radiation protection inspection results to James Shell, Plant Manager, and other members of the licensee staff.
- On July 24, 2025, the inspectors presented the emergency preparedness inspection results to David Wilson, Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Corrective Action
Documents
Resulting from
Inspection
CR 1300045
NRC questions regarding auxiliary feedwater system
09/05/2025
11548-FM-064A -
Sheet 4 of 6
Flow/Valve Operating Numbers Diagram Main Steam
System Surry Power Station Unit 2
Revision 59
Drawings
11548-FM-068A -
Sheet 3 of 4
Flow/Valve Operating Numbers Diagram Feedwater System
Surry Power Station Unit 2
Revision 73
0-OPT-SW-001
Emergency Service Water Pump 1-SW-P-1A
2-OP-28A
Main Steam System Valve Alignment
Revision 24
2-OP-FW-001A
Auxiliary Feedwater System Valve Alignment
Revision 8
2-OP-FW-008
Resetting Turbine Driven AFW Pump Overspeed Trip and
Throttle Valve
Revision 5
Procedures
SDBD-SPS-AFW
System Design Basis Document for Auxiliary Feedwater
System
Revision 32
CR 1296626
NRC identified - Fire Strategy Discrepancy
07/18/2025
CR 1296631
NRC questioned charging pump seal area posting
07/18/2025
Corrective Action
Documents
Resulting from
Inspection
CR 1299492
NRC identified fire drill critique item
08/28/2025
0-FS-FP-123
Diesel Generator Room Number 3 Elevation 27 Feet - 6
Inches
Revision 2
1-FS-FP-157
Charging Pumps - Unit 1 Auxiliary Building Elevation 13 Feet
- 0 Inches and 2 Feet - 0 Inches
Revision 3
2-FS-FP-140
Safeguards Basement - Unit 2 Elevation 11 Feet - 6 inches
Revision 3
Fire Plans
2-FS-FP-141
Safeguards Spray Side - Unit 2 Elevation 27 Feet - 6 Inches
Revision 2
Procedures
RQ-25.6-SP-1
25 Cycle 25.6 Sim Exam
Revision 0
Procedures
Operational Risk Assessment
Revision 27
Corrective Action
Documents
Resulting from
Inspection
CR 1298587
NRC identified mark number typo in 0-OPT-EG-009
08/17/2025
Procedures
Surry Emergency
Surry Emergency Action Level Matrix
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Action Level
Matrix
Surry Emergency
Action Level
Technical Basis
Document
Surry Emergency Action Level Technical Basis Document
Surry Emergency
Plan
Surry Emergency Plan
VPAP-2802
Notifications and Reports
Procedures
RQ-25.6-SP-1
25 Cycle 25.6 Sim Exam
Revision 0
Procedures
EP-AA-CSD-311
Interface with Off-site Incident Command
Rev 2
CA 1261927
Level of Effort Evaluation
10/25/2024
CR 1261927
Calibration source (Ba-133, SN 339A) strength below reqd
for calibration of the 01-SW-RM-120
06/13/2024
CR 1269294
1-SW-RM-120 Calibration not IAW the ODCM requirements
09/19/2024
Corrective Action
Documents
CR 1273152
Alarm setpoint for 2-SW-RM-220 needs evaluated IAW 0-
HPS-RMSS-001
10/21/2024
Procedures
Surry Power Station - Equipment Important to Emergency
Response
Revision 31
CR 1218540
22 Meteorological Data recovery rate < 90%
2/01/2023
CR 1224716
Entered AP-35.01 Radioactive liquid release control
04/16/2023
CR 1233055
Leak of contaminated water near 2-CS-36 (B RWST cooler
inlet isolation)
07/13/2023
Corrective Action
Documents
CR 1295308
24 Meteorological Data recovery rate < 90%
07/02/2025
Corrective Action
Documents
Resulting from
Inspection
CR 1296565
Non-functional groundwater monitoring well
07/17/2025
Procedures
0-IPM-MM-PR0-
001
Primary Meteorological Tower Instrumentation Calibration
Rev. 10
204236171
Piping Repair / Replacement, Water Table extraction Well
(Deep), 01-PL-PIEZ-P51-PIPE
05/15/2025
Work Orders
204358683
PM/CAL Primary Met Tower Instrumentation
03/19/2025
71151
Corrective Action
CR1239515
TSC Full Staff ERO position below preferred depth (EPC)
10/02/2023
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
CR1241484
Quarterly TSC Battery Checks Unacceptable
10/23/2023
CR1252705
TSC missing and tampered with items
03/06/2024
CR1257470
TSC video wall not working properly
04/23/2024
CR1265011
Five (5) ERO members did not attend nor have
replacements for SJUL24 TD on 7/23/24
07/24/2024
CR1265066
Surry NRC ENS line had no dial tone during SJUL24TD
07/25/2024
CR1267462
Primary Met tower upper wind direction point unavailable
08/27/2024
CR1273137
Differences between NAPS and SPS target power levels for
secondary plant issues.
10/21/2024
Documents
CR1293950
Backup MET tower wind direction indication is responding
differently than the primary MET tower.
06/12/2025