IR 05000245/2015007

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IR 05000336/2015007, 05000423/2015007; on 3/30/2015 to 5/01/2015; Millstone Power Station, Units 2 and 3; Component Design Bases Inspection
ML15166A344
Person / Time
Site: Millstone  
Issue date: 06/12/2015
From: Krohn P G
Engineering Region 1 Branch 2
To: Heacock D A
Dominion Resources
References
IR 2015007
Download: ML15166A344 (46)


Text

June 12, 2015

Mr. David President and Chief Nuclear Officer Dominion Resources 5000 Dominion Blvd. Glen Allen, VA 23060-6711

SUBJECT: MILLSTONE POWER STATION UNITS 2 AND 3 - NRC COMPONENT DESIGN BASES INSPECTION REPORT 05000336/2015007 AND 05000423/2015007

Dear Mr. Heacock:

On May 1, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at the Millstone Power Station, Units 2 and 3. The enclosed inspection report documents the inspection results, which were discussed on May 1, 2015, with Mr. John Daugherty, Site Vice President, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. In conducting the inspection, the team examined the adequacy of selected components to mitigate postulated transients, initiating events, and design basis accidents. The inspection involved field walkdowns, examination of selected procedures, calculations and records, and interviews with station personnel.

This report documents three NRC-identified finding, two of which were of very low safety significance (Green) and the third was determined to be of Severity Level IV (SL IV) significance. All of the findings were determined to be violations of NRC requirements. However, because of the very low safety significance and SL IV and because they were all entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCV) consistent with Section 2.3.2.a of the NRC's Enforcement Policy. If you contest any of the NCVs in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Millstone Power Station. In addition, if you disagree with the cross-cutting aspect assigned to the findings in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector at Millstone Power Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Docket Room or from the Publicly Available Records component of NRC's document system, Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA William A. Cook for/

Paul G. Krohn,Chief Engineering Branch 2 Division of Reactor Safety Docket Nos. 50-336, 50-423 License Nos. DPR-65, NPF-49

Enclosure:

Inspection Report 05000336/2015007 and 05000423/2015007

w/Attachment:

Supplemental Information cc w/encl.: Distribution via ListServ

SUMMARY OF FINDINGS

.......................................................................................................... ii

REPORT DETAILS

REACTOR SAFETY

........................................................................................................... 1 1R21 Component Design Bases Inspection (IP 71111.21) ......................................... 1

.1 Inspection Sample Selection Process .......................................................... 1

.2 Results of Detailed Reviews

OTHER ACTIVITIES

..........................................................................................................24

4OA2 Identification and Resolution of Problems (IP 71152) ......................................24

4OA6 Meetings, including Exit ...................................................................................25

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

.................................................................................................. A-1

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED ........................................................ A-2

LIST OF DOCUMENTS REVIEWED

....................................................................................... A-2

LIST OF ACRONYMS

........................................................................................................... A-12

i Enclosure

U.S. [[]]
NUCLEA R
REGULA [[]]
TORY [[]]
COMMIS [[]]
SION [[]]
REGI [[]]

ON I

Docket Nos.: 50-336, 50-423

License Nos.:

DPR -65,

NPF-49 Report Nos.: 05000336/2015007 and 05000423/2015007

Licensee: Dominion Nuclear Connecticut, Inc. Facility: Millstone Power Station, Units 2 and 3

Location:

P.O. Box 128 Waterford,
CT 06385 Inspection Period: March 30 through May 1, 2015 Inspectors:
K. Mangan, Senior Reactor Inspector, Division of Reactor Safety (
DRS ), Team Leader
S. Pindale, Senior Reactor Inspector,
DRS [[]]
J. Ayala, Reactor Inspector,
DRS [[]]
J. Patel, Reactor Inspector,
DRS [[]]
L. McKown, Millstone Resident Inspector, Division of Reactor Projects (
DRP )
W. Sherbin,
NRC Mechanical Contractor
G. Morris,

NRC Electrical Contractor Approved By: Paul G. Krohn, Chief Engineering Branch 2 Division of Reactor Safety

ii Enclosure

SUMMAR Y
OF [[]]
FINDIN [[]]

GS IR 05000336/2015007, 05000423/2015007; 3/30/2015 - 5/01/2015; Millstone Power Station, Units 2 and 3; Component Design Bases Inspection.

The report covers the Component Design Bases Inspection conducted by a team of five

U.S. Nuclear Regulatory Commission (
NRC ) inspectors and two
NRC contractors. Two findings of very low safety significance (Green) and one Severity Level
IV [[violation were identified. The findings were considered to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process." Cross-cutting aspects associated with findings are determined using]]
IMC 0310, "Components Within the Cross-Cutting Areas." The
NRC 's program for overseeing the safe operation of commercial nuclear power reactors is described in
NUREG -1649, "Reactor Oversight Process," Revision 4, dated December 2006.
NRC [[-Identified Findings Cornerstone: Mitigating Systems Green: The team identified a non-cited violation (NCV) of Millstone Power Station Unit 2, Technical Specification (TS) 3.7.3.1 the reactor building component cooling water (RBCCW) system Limiting Condition of Operation (LCO) in that Dominion failed to maintain two loops of]]
RBCCW operable. The team found that following the identification of a degraded condition for the "C"
RBCCW pump, Dominion incorrectly concluded the loop remained operable. Specifically, the team determined that from February 4 to February 23, 2015, the
RBCCW "B" loop was inoperable because oil leakage from the "C"
RBCCW outboard pump bearing would have caused the complete loss of oil to the pump bearing, without operator compensatory action, before the "C"
RBCCW train would have completed its design basis 30-day mission time. Using

IMC 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," Section A, "Mitigating Systems, Structures or Components and Functionality," the team determined that the

finding required a detailed risk evaluation due to actual loss of function of at least a single train for greater than its

TS allowed outage time. The Region I Senior Reactor Analyst (
SRA ) identified that because the finding involved the "C"
RBCCW pump function to run for its mission time, the only accident events adversely impacted are the large break loss of coolant accident (
LLOCA ) sequences. The condition was conservatively modeled assuming an exposure period of one year with the "C"
RBCCW pump failure to run basic event set to True. The resultant change in risk was estimated at mid E-8, or very low safety significance (Green). The dominated risk sequences involve a
LLOCA with the failure of the remaining
RBCCW pumps due to common cause. Since the estimated risk increase was less than 1E-8, no additional evaluation of external events contribution or change in large early release frequency (

LERF) was required. The team concluded that this issue has a cross-cutting aspect in the Human Performance cross-cutting area of Conservative Bias: Individuals use decision-making practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. Specifically, Dominion determined that the qualitative bubbler leak rate was acceptable without evaluation against quantified operability criteria. (H.14) (Section 1R21.2.1.5)

iii Enclosure Severity Level

IV The team identified a Severity Level
IV , non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10
CFR ) 50.59, "Changes, Tests, and Experiments," in that Dominion failed to perform a written evaluation to provide the bases for determining whether a change to the facility required a license amendment. Specifically, the team identified that contrary to 10
CFR [[50.59, Dominion failed to properly evaluate operator compensatory actions to refill an oil bubbler on the "C" reactor building component cooling water (RBCCW) pump that was leaking oil at a rate that would have prevented the pump from meeting its design basis 30-day mission time. The team identified that contributing to this performance deficiency was that station procedure]]
OP -

AA-102, Attachment 1, Immediate Operability Determination Guidelines, Step 7.c., associated with the evaluation of oil and coolant leakage in order to

establish operability for this type of degraded condition, incorrectly instructs the Dominion staff that the use of compensatory actions is acceptable without performing a formal operability determination.

In accordance with the

NRC Enforcement Policy Section 6.1, the team used
IMC 0609 to inform the severity of this
10 CFR 50.59 violation. Per
IMC 0609, the team determined that the finding required a detailed risk evaluation due to actual loss of function of at least a single train for greater than its
TS allowed outage time. The Region I
SRA identified that because the finding involved the "C"
RBCCW pump function to run for its mission time, the only accident events adversely impacted are the
LLOCA sequences. The condition was conservatively modeled assuming an exposure period of one year with the "C"
RBCCW pump failure to run basic event set to True. The resultant change in risk was estimated at mid E-8, or very low safety significance (Green). The dominated risk sequences involve a

LLOCA with the failure of the

remaining

RBCCW pumps due to common cause. Since the estimated risk increase was less than 1E-8, no additional evaluation of external events contribution or change in
LERF was required. Accordingly, per Section 6.1.d of the
NRC Enforcement Policy, the severity of the violation of 10
CFR 50.59 was determined to be Severity Level
IV , as it resulted in conditions evaluated as having very low safety significance (Green) by the Significant Determination Process (

SDP).

There is no cross-cutting aspect associated with this violation as cross-cutting aspects are not assigned to traditional enforcement evaluations. (Section 1R21.2.1.5)

iv Enclosure Green: The team identified a finding of very low safety significance (Green) involving a non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10

CFR ) Part 50, Appendix B, Criterion
III [[, "Design Control," in that Dominion did not correctly evaluate the capability of 4.16 kV breakers to function properly during 3-phase bolted fault design condition. The team reviewed Millstone Unit 2 electrical distribution system analysis calculation (MP2-ENG-ETAP-04014E2), which evaluated adequacy of the circuit breakers for their interrupting rating in accordance with the Institute of Electrical and Electronics Engineers/American National Standards Institute (IEEE/ANSI) C37 series standards, and determined that Dominion's short-circuit fault current calculation did not assume the maximum plant operating voltage as a pre-fault voltage at the 4.16 kV bus and did not evaluate the plant configuration when emergency diesel generators (EDG) are operating in parallel with offsite power on the associated 4.16 kV emergency bus. The team determined this short-circuit fault current calculation was not in accordance with]]
IEEE /
ANSI [[C37 series standards and was non-conservative in some cases. Dominion entered the issue into their corrective action program and performed additional analysis to determine if the inability of the breaker to interrupt the fault current would result in the fault current affecting the other safety related bus. Dominion concluded that the other bus would not be affected. The team reviewed the analysis and determined it to be acceptable. The finding was determined to be more than minor because it was associated with the Mitigating Systems cornerstone Design Control attribute and adversely affected the cornerstone's objective and was similar to Example 3.j in Appendix E of the]]
NRC [[]]
IMC 0612. Using the
NRC [[]]
IMC "0609, "Significance Determination Process," Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," Exhibit 2, "[[Cornerstone" contains a listed "[" character as part of the property label and has therefore been classified as invalid. Screening Questions," the finding was determined to be of very low safety significance (Green). There was no crosscutting aspect assigned to the finding because it was not an indicative of current performance. (Section 1R21.2.1.7)]]
REPORT [[]]
DETAIL S 1.
REACTO R

SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R21 Component Design Bases Inspection (IP 71111.21)

.1 Inspection Sample Selection Process The team selected risk significant components for review using information contained in the Millstone Probabilistic Risk Assessment (PRA) and the

U.S. Nuclear Regulatory Commission's (

NRC) Standardized Plant Analysis Risk (SPAR) model for the Millstone Power Station. Additionally, the team referenced the Risk-Informed Inspection Notebook for the Millstone Power Station in the selection of potential components for review. In general, the selection process focused on components that had a risk achievement worth (RAW) factor greater than 1.3 or a risk reduction worth (RRW) factor greater than 1.005. The components selected were associated with both safety-related and non-safety related systems and included a variety of components such as pumps, transformers, operator actions, electrical busses, and valves.

The team initially compiled a list of components based on the risk factors previously mentioned. Additionally, the team reviewed the previous component design bases inspection (CDBI) reports (05000336/2009006 and 05000423/2009006, 05000336/2006010 and 05000423/2006010, and 05000336/2012007 and 05000423/2012007) and excluded those components previously inspected. The team then performed a margin assessment to narrow the focus of the inspection to 21 components and 5 operating experience (OE) items. The team selected one component, containment air recirculation fan, based on large early release frequency (LERF) implications. The team's evaluation of possible low design margin included

consideration of original design issues, margin reductions due to modifications, or margin reductions identified as a result of material condition/equipment reliability issues. The assessment also included items such as failed performance test results, corrective action history, repeated maintenance, Maintenance Rule (a)(1) status, operability reviews for degraded conditions,

NRC resident inspector insights, system health reports, and industry
OE. Finally, consideration was also given to the uniqueness and complexity of the design and the available defense-in-depth margins. The inspection performed by the team was conducted as outlined in
NRC Inspection Procedure (

IP) 71111.21. This inspection effort included walkdowns of selected

components; interviews with operators, system engineers, and design engineers; and reviews of associated design documents and calculations to assess the adequacy of the components to meet design basis, licensing basis, and risk-informed beyond design basis requirements. Summaries of the reviews performed for each component and OE sample are discussed in the subsequent sections of this report. Documents reviewed for this inspection are listed in the Attachment.

Enclosure .2 Results of Detailed Reviews .2.1 Results of Detailed Component Reviews (21 samples) .2.1.1 Unit 2, "B" High Pressure Safety Injection Pump (P41B) a. Inspection Scope The team inspected the "B" high head safety injection pump, P41B, to evaluate if it was capable of performing its design basis functions. Specifically, the team assessed the pump's ability to meet design basis head and flow requirements during design basis events. The team reviewed drawings, calculations, hydraulic analyses, procedures, system modifications, and preventive maintenance activities to determine the adequacy of high head safety injection pump performance. The team also determined whether design inputs were properly translated into system procedures and tests and reviewed completed surveillance tests to determine if the results adequately demonstrated the capability of the pump to meet design basis requirements under transient and accident conditions. In addition, the team reviewed the adequacy of water supply sources to the pump, including an assessment of the potential for vortex conditions and the ability to transfer the pump's suction during the recirculation phase of an accident. The team also performed field walkdowns to assess the material condition of the pump and supporting

equipment. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified.

.2.1.2 Unit 2, "A" Service Water Pump (SW-P-5A) a. Inspection Scope The team inspected the "A" service water (SW) pump,

SW -P-5A, to evaluate if it was capable of performing its design basis functions. Specifically, the team evaluated whether the
SW pump provided adequate flow so that the
SW system was capable of transferring the maximum heat loads, from plant primary and secondary heat source to the environment. The team reviewed applicable portions of the Updated Final Safety Analysis Report (
UFSAR ), design basis documents (DBD), and drawings to identify the design basis requirements for the pump in order to evaluate whether the pump capacity was sufficient to provide adequate flow to the safety-related components supplied by the
SW system during design basis accidents (
DBA [[). The team reviewed design calculations to assess available pump net positive suction head (NPSH), submergence requirements, worst case pump run-out conditions, and to evaluate the capability of the pump to provide required flow to supplied components under design basis conditions. The team ensured changes that impacted flow requirements to individual]]
SW system loads due to pipe replacement and modifications were properly evaluated. The team reviewed the

SW pump in-service test (IST) results and SW system flow verification tests to determine if

Enclosure adequate system flow was available. Specifically, the team reviewed pump data trends for vibration, pump differential pressure, and flow rate test results to verify acceptance criteria were met and acceptance limits were adequate. Additionally, the motor data, degraded voltage conditions, and voltage drop calculation results were reviewed to confirm that the pump motor would have sufficient voltage and power available to perform

its safety function at degraded voltage conditions. The team interviewed the system and design engineers as well as maintenance staff who supported walkdowns of the pump to

evaluate its material condition, assess the pump's operating environment, and gage the station's capability to implement inclement weather procedures. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems.

b. Findings No findings were identified. .2.1.3 Unit 2, Service Water Air Operated Valves (AOV231B and

AOV 89B) a. Inspection Scope The team inspected the emergency diesel generator (
EDG )
SW heat exchanger supply and bypass air operated valves (
AOV ),
AOV 231B and
AOV 89B, to determine whether they were capable of meeting their design basis function. Specifically, the team determined whether the valves would reposition as required to ensure
SW would be supplied to the
EDG heat exchangers following an
EDG start signal. The team reviewed the
UFSAR , the Technical Specifications (TS), the
TS Bases, and the

IST basis documents to identify the design basis requirements of the valves. The team reviewed drawings, operating and maintenance procedures, and completed maintenance records to determine whether the safety function was maintained. The team reviewed valve testing procedures and IST results, including stroke time, to verify acceptance criteria were adequate and that performance was not degrading. The team discussed design, operation, permanent modifications, and component history of the valves with engineering and operations staff to evaluate performance history and overall component

health. The team also conducted a walkdown of the valves to assess its material condition and to verify the installed configuration was consistent with plant drawings, procedures, and the design basis. Finally, the team reviewed corrective action documents to verify Dominion was identifying and correcting issues with the valve, and to verify there were no adverse trends. b. Findings No findings were identified.

Enclosure .2.1.4 Unit 2, Operator Action to Cross-tie Fire Water System to Auxilliary Feedwater a. Inspection Scope The team inspected the manual operator action that establishes an alternate source of

suction water to the auxiliary feedwater (AFW) pumps in response to a loss of the normal

AFW supply. Specifically, the team reviewed Dominion's actions to align the fire water system to supply the

AFW pump suction and the capability of the fire water system to

supply required water inventory to the

AFW system. The team selected this sample because of the extent of actions performed outside of the control room and the infrequent operation of this alignment. The team reviewed Dominion's
PRA and human reliability analysis (HRA) studies to determine when and how quickly operator actions were needed to provide the alternate
AFW supply to meet

PRA success assumptions. The team interviewed equipment operators, reviewed associated operating and alarm response procedures, walked down applicable portions of the affected systems in the plant, and observed an equipment operator simulate the in-field portions of the procedure to evaluate the ability of the operators to perform the required actions. The team also reviewed AFW and fire water system design documents to determine whether design bases were appropriately evaluated and incorporated into this system alignment. The team evaluated the available process margins based on fluid pressures and flow rates, component design values, and limiting operational parameters established in engineering

analyses and calculations. The team compared the available margins to the predicted or assumed margins in engineering analysis and calculations to verify the reasonableness of the design and operating values. Finally, the team reviewed corrective action

documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified. .2.1.5 Unit 2, "C" Reactor Building Closed Cooling Water Pump (RB-P-11C) a. Inspection Scope The team inspected the "C" reactor building closed cooling water (RBCCW) pump,

RB -P-11C, to determine whether it was capable of meeting its design basis function. Specifically, the team evaluated the ability of the

RBCCW system to provide cooling water to essential components under normal, transient, and accident conditions. The team evaluated whether the pump capacity was sufficient to provide adequate flow to the safety-related components supplied by the system during DBAs. The team reviewed drawings, calculations, hydraulic analyses, procedures, system health reports, and the

system DBD to ensure consistency with design and licensing bases requirements. Additionally, the motor data, degraded voltage conditions, and voltage drop calculation results were reviewed to confirm that the pump motor would have sufficient voltage and power available to perform its safety function at degraded voltage conditions. The team also reviewed completed pump surveillance tests to ensure pump performance and procedure acceptance criteria were consistent with system flow calculations assumptions.

Enclosure The team walked down the

RBC [[]]

CW pumps and accessible portions of the system and reviewed the system health report and maintenance records to assess Dominion's configuration control, operating environment of the pumps, and the system's overall material condition. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to

assess Dominion's ability to evaluate and correct problems. b. Findings .1 Introduction. The team identified a Green, non-cited violation (NCV) of Millstone Power Station Unit 2,

TS 3.7.3.1
RBCCW system Limiting Condition of Operation (LCO) in that Dominion failed to maintain two loops of
RBCCW operable. The team found that following the identification of a degraded condition for the "C"
RBCCW pump, Dominion incorrectly concluded the loop remained operable. Specifically, the team determined that from February 4 to February 23, 2015, the
RBCCW "B" loop was inoperable because oil leakage from the "C"
RBCCW outboard pump bearing would have caused the complete loss of oil to the pump bearing, without operator compensatory action, before the "C"
RBC [[]]

CW train would have completed its design basis 30-day mission time.

Description. The team reviewed the design of the

RBCCW system and found that the

RBCCW pumps have outboard bearing lubricating oil systems which ensure operability of

the pump by maintaining adequate oil to the bearings. The team noted that operators ensure adequate oil to the bearings by monitoring and maintaining level in an eight ounce transparent reservoir or "bubbler." The team noted that the bubbler provides makeup inventory as necessary to support pump operation through all design basis events. During operation, the pump bearing is not expected to consume significant quantities of oil. The team reviewed Condition Report (CR) 564871 dated November 9, 2014, in which Dominion identified low oil level in the "C"

RBCCW pump outboard bearing oil bubbler. The team reviewed six additional
CR s created between November 25, 2014, and March 31, 2015, in which Dominion identified that the "C"
RBCCW pump outboard oil bubbler required oil to be added to the bubbler and some cases identified oil leakage from the bubbler. The team reviewed the associated operability assessment for each
CR [[noting that the licensee concluded that the pump was operable because the actual leak rate was less than the quantified 30-day mission time leak rate acceptance criteria. However, the team's review determined that Dominion had not quantified the leak rate in any of the]]
CR s. The team reviewed control room logs,

CRs, and work orders to assess the degraded condition of the bubbler. Based on this review, the team determined that the actual leak rate was as high as 0.50 ounces per day from February 4 through February 23, 2015, and concluded that this leak rate would have resulted in the oil bubbler emptying in 2 to 8 days vice the 30-day pump mission time, without operator action to add oil. Following the team's identification of this issue, Dominion entered the issue into their corrective action program and developed a revised operability determination that concluded the pump remained operable because operators would be able to identify low oil levels in the bubbler and refill the bubbler after a DBA. Dominion's operability

Enclosure determination concluded this operator action was reasonable and consistent with Dominion's routine actions which added oil on multiple occasions between November and April. In addition, Dominion concluded the pump would be accessible post-accident. During the team review of the revised operability determination the team identified that the post-accident dose estimations for equipment environmental qualification, as well as, planned emergency operating procedure actions in the area of the pump indicate that an individual performing an oil filling evolution would receive a dose as high as 2.9 Rem within the first few hours following a

DBA , 876 mRem at approximately 2 days post-accident, and approximately 315 mRem at 8 days post-accident. The team also determined that following a
DBA operator rounds would likely be suspended for some unquantified number of days due to general post-accident dose concerns. Specifically, the team noted, in accordance with
RP -
AA -103, As Low As Reasonably Achievable (ALARA) Program, Revision 2, and
RP -
AA -106, Radiological Work Control Program, Revision 3, this level of exposure would require
ALARA committee reviews, radiation worker permits, and pre-job briefs prior to allowing entry into the pump room due to post-accident dose rates. The team also noted that the
RBCCW [[pumps do not have a low oil bearing level alarm function and that operators had not been provided specific written guidance to ensure this degraded condition was monitored and addressed post-accident. During the inspection Dominion quantified the current leakage of the "C"]]
RBC [[]]

CW pump outboard bearing oil bubbler and determined that the leakage from the lubrication system had been reduced by maintenance activities performed on February 23, 2015, which tightened the bubbler piping connections such that the outboard bearing lubrication system would support the pump 30-day mission time, without operator action. The team reviewed this analysis and found Dominion's conclusions to be reasonable. Additionally, Dominion entered the issue into their corrective action program and created a work

activity to correct the remaining leakage (CR 576963, WO 53102571327).

The team identified that bubbler levels between February 4 and February 23, 2015, were recorded between 1/8 and 3/4 full. As a result, the team determined that the observed oil levels and leak rate (calculated by the team) would have resulted in the pump oil bubbler running out of oil in two to eight days. Therefore, Dominion would likely not have been able to identify that the bubbler was out of oil in time to take compensatory actions in order to prevent pump failure. Specifically, the team concluded that Dominion's basis for operability during this time frame was not supported because the pump would not have been able to meet its 30-day mission time and operators would not have been able to identify and refill the bubbler due to radiation dose levels in the room. As a consequence, the team concluded that

TS [[]]
LCO 3.7.3.1 requiring that two
RBC [[]]

CW loops remain operable was not met between February 4 and February 23, 2015.

Analysis. The team determined that the failure of Dominion to assess the degraded condition of the

RBC [[]]

CW pump oil system and take appropriate actions in accordance

with

TS 3.7.3.1 was a performance deficiency that was reasonably within Dominion's ability to foresee and correct. Specifically, from February 4 to February 23, 2015, Dominion incorrectly concluded that the
RBCCW system was operable following the identification of the "C"
RBC [[]]

CW outboard pump bearing oil system leaking oil at a rate that would have resulted in the pump not meeting its 30-day mission time. This finding

Enclosure was more than minor in accordance with Inspection Manual Chapter (IMC) 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening," dated September 7, 2012, as it adversely affected the equipment performance attribute of the Reactor Safety Mitigating Systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the capability of the "C"

RBCCW pump train was challenged based upon Dominion's failure to ensure that "C"
RBCCW pump outboard bearing lubricating oil assembly was able to support the system design basis 30-day mission time. Using
IMC 0609, "Significance Determination Process," Attachment 4, "Initial Characterization of Findings," and
IMC [[0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," Section A, "Mitigating Systems, Structures or Components and Functionality," the team determined that the finding required a detailed risk evaluation due to actual loss of function of at least a single train for greater than its]]
TS allowed outage time. The Region I Senior Reactor Analyst (
SRA ) identified that because the finding involved the "C"
RBCCW pump failure to run for its mission time, the only accident events adversely impacted are the large break loss of coolant accident (
LLOCA ) sequences. The condition was conservatively modeled assuming an exposure period of one year with the "C"
RBCCW pump failure to run basic event set to True. The resultant change in risk was estimated at mid E-8, or very low safety significance (Green). The dominated risk sequences involve a
LLOCA with the failure of the remaining
RBCCW pumps due to common cause. Since the estimated risk increase was less than 1E-8, no additional evaluation of external events contribution or change in

LERF was required. The team used IMC 0310, "Aspects within the Cross-Cutting Areas," dated December 4, 2014, to conclude that this issue has a cross-cutting aspect in the Human Performance cross-cutting area of Conservative Bias: Individuals use decision-making practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop.

Specifically, Dominion determined that the qualitative bubbler leak rate was acceptable without evaluation against quantified operability criteria. (H.14) Enforcement. Millstone Unit 2,

TS 3.7.3.1 states, in part, "Two reactor building closed cooling water loops shall be
OPERAB LE." Contrary to the above, from February 4, 2015, through February 23, 2015, Dominion failed to maintain the "B"
RBCCW loop operable as the "C"
RBCCW pump outboard bearing was leaking oil at rate which would have only supported 2 to 8 days of the 30-day mission time. Dominion restored compliance with the
LCO following maintenance on February 23, 2015. Because this issue is of very low safety significance (Green) and Dominion restored compliance with the
TS [[]]
LCO and entered this issue into their corrective action program (
CR 576963), this finding is being treated as an
NCV consistent with the
NRC Enforcement Policy Section 2.3.2. (NCV 05000336/2015007-01, Reactor Building Closed Cooling Water System Pump Oil Leakage Results in Technical Specification Inoperability) .2 Introduction. The team identified a Severity Level
IV ,

NCV of 10 CFR 50.59, "Changes, Tests, and Experiments," in that Dominion failed to perform a written evaluation to provide the bases for determining whether a change to the facility required a license

Enclosure amendment. Specifically, the team identified that contrary to

10 CFR 50.59, Dominion failed to properly evaluate compensatory actions to refill an oil bubbler on the "C"
RBCCW pump following identification of an oil leak that would have prevented the pump from meeting its design basis 30-day mission time. The team identified that contributing to this performance deficiency was that station procedure
OP -
AA [[-102, Attachment 1, Immediate Operability Determination Guidelines, Step 7.c., incorrectly instructs the Dominion staff that the use of compensatory actions for oil and coolant leaks is acceptable without performing a formal operability determination. Description. During the team's review of actions taken by Dominion to address a degraded condition associated with oil leakage from the "C"]]
RBCCW pump bearing, the team identified that Dominion did not perform a 10
CFR 50.59 screening or safety evaluation prior to implementing the compensatory measures credited for maintaining operability of the "C"
RBCCW pump. Specifically, following identification by the team that the observed oil leakage prevented the pump from meeting its 30-day mission time, Dominion credited operators, through the use of procedure,
MP 2701F, Lubrication, Attachment P011, Reactor Building Closed Cooling Water Pump Lubrication Information Sheet, Revision 005-03, to add oil to the "C"
RBCCW pump outboard bearing post-accident, in order to maintain operability of the train. The team observed that Dominion used
OP -AA-102, Operability Determination, Attachment 1, Revision 12, to evaluate the use of the interim compensatory action in order to restore operability of the
RBCCW train. However, prior to implementing the compensatory action to ensure pump operability, a 50.59 screen/evaluation was not performed. The team conducted a detailed review of Dominion's process for determining operability as implemented in accordance with
OP -AA-102. The team determined the procedure directs operators to determine the impact on
TS structure, system, and component (
SSC [[) operability for a degraded, non-conforming, or unanalyzed condition using guidance provided in Attachment 1, Immediate Operability Determination Guidelines. The team noted that the Attachment allows the use of compensatory actions and associated procedural guidance to maintain the operability of]]
SSC s without performing a formal operability evaluation. Specifically,
OP -AA-102, Attachment 1, Immediate Operability Determination Guidelines, Step 7.c. states: "IF the oil / coolant level in the
SSC can be maintained during its mission time by replenishment and meets all the following criteria,
THEN the equipment is operable and
NO [[]]
OD evaluation is required. Non-complex evolution capable of being performed by on-shift operators Can be accomplished with equipment in operation Replenishment frequency required with
SSC in operation is greater than every 24 hours The area is accessible during the design events requiring
SSC operation
IF all of the requirements above can
NOT be met
THEN an

OD evaluation is required."

Enclosure The team reviewed the Millstone licensing basis and found that the use of compensatory actions, such as operator actions or proceduralized maintenance activities, to maintain safety related

SSC s operable was not part of the Millstone licensing basis. Specifically, the
UFSAR does not discuss the use of operator compensatory actions to maintain safety related system operability. In addition, the team found that a 50.59 evaluation was not performed when Revision 1 of procedure
OP -
AA -102 was first implemented (July 13, 2007), and that no subsequent
10 CFR 50.59 evaluations have been performed by Dominion to evaluate the use of compensatory actions, per this procedure, since that time. The team's review of
OP -AA-102 identified that multiple sections of the procedure state when implementing compensatory actions verify a
10 CFR 50.59 review is completed in accordance with procedure
CM -AA-400,
10 CFR 50.59, and 10
CFR 72.48, "Changes, Tests, and Experiments," Revision 4. The team reviewed
CM -
AA -400 and found that the implementing procedure is used to determine if a change to the facility would require a license amendment prior to implementation. The team noted that
OP -
AA -102, Attachment 1, Section 7.c. directs personnel to exit the operability determination evaluation process when determining the basis for operability for some oil or coolant leakage conditions. As a result,
CM -
AA -400 would not be entered and, therefore, a
10 CFR [[50.59 review would not be performed to assess the use of procedure changes and associated compensatory actions that are being credited to restore the operability of safety related equipment with this type of degradation. As discussed in Section .2.1.5.1 above, the team determined that it was not reasonable to conclude that the compensatory action being credited to address the]]
RBCCW oil leak would have been successful, due to the significant expected post-accident dose operators would have been exposed to for both identifying and replenishing the low lubricating oil condition of the "C"
RBCCW pump bearing during a postulated
DBA. Dominion entered this condition for evaluation within their corrective action program (CR 577964). On May 5, 2015, Dominion implemented a standing order,
SO -15-010, reinforcing 10
CFR 50.59 regulatory requirements. Analysis. The team determined that the failure to perform a written evaluation which provided the bases for the determination that operator compensatory actions did not require a license amendment was a violation of
10 CFR 50.59(d)(1). Specifically, Dominion failed to provide bases for not applying for a license amendment for the implementation of an interim compensatory measure, in lieu of an automatic design feature to maintain the capability of a
TS [[]]
SSC to meet its design basis mission time. Because this performance deficiency impacted the ability of the
NRC to perform its regulatory function, the team evaluated the issue using the traditional enforcement process. In accordance with The
NRC Enforcement Manual, Revison 9, Part
II , Enforcement of
10 CFR 50.59 and Related

FSAR, Sections 2.1.3.E.1 and 2.1.3.E.6, this violation was determined to be more than minor because Dominion failed to conduct a 10 CFR 50.59 screen or evaluation that, if performed, would likely have concluded that the change or operator compensatory actions would have required Commission review and approval prior to implementation.

Enclosure In accordance with the

NRC Enforcement Policy Section 6.1, the team used
IMC 0609 to inform the severity of this
10 CFR 50.59 violation. As previously discussed in Section .2.1.5.1, the team determined that the finding required a detailed risk evaluation due to actual loss of function of at least a single train for greater than its
TS allowed outage time. The Region I
SRA identified that because the finding involved the "C"
RBCCW pump failure to run for its mission time, the only accident events adversely impacted are the
LLOCA sequences. The condition was conservatively modeled assuming an exposure period of one year with the "C"
RBCCW pump failure to run basic event set to True. The resultant change in risk was estimated at mid E-8, or very low safety significance (Green). The dominated risk sequences involve a
LLOCA with the failure of the remaining
RBCCW pumps due to common cause. Since the estimated risk increase was less than 1E-8, no additional evaluation of external events contribution or change in
LERF was required. Accordingly, per Section 6.1.d of the
NRC Enforcement Policy, the severity of the violation of
10 CFR 50.59 was determined to be Severity Level

IV, as it resulted in conditions evaluated as having very low safety significance (Green) by the SDP.

There is no cross-cutting aspect associated with this violation as cross-cutting aspects are not assigned to traditional enforcement evaluations. Enforcement. Title 10 CFR 50.59, "Changes, Tests, and Experiments," Section (d)(1) states, in part, "The licensee shall maintain records of changes in the facility, of changes in procedures, and of tests and experiments made pursuant to paragraph (c) of this section. These records must include a written evaluation which provides the bases for the determination that the change, test, or experiment does not require a license amendment

pursuant to paragraph (c)(2) of this section."

10 CFR [[50.59(c)(1)(ii) states, in part, that a licensee may make changes in the procedures as described in the final safety analysis report (as updated), without obtaining a license amendment pursuant to Section 50.90 only if the change does not meet any of the criteria in paragraph (c)(2) of this section. Title 10]]
CFR [[50.59(c)(2)(ii) requires, in part, that a licensee shall obtain a license amendment pursuant to Section 50.90 prior to implementing a proposed change if the change would result in more than a minimal increase in the likelihood of occurrence of a malfunction of an]]
SSC important to safety previously evaluated in the final safety analysis report (as updated). Millstone Unit 2 final safety analysis report (as updated) Section 9.4 describes the

RBCCW system. Contrary to the above, between February 4 and February 23, 2015, Dominion implemented a change in procedures as described in the final safety analysis report and did not include a written evaluation that provided the

bases for the determination that the change did not require a license amendment pursuant to paragraph (c)(2). Specifically, Dominion credited the operator compensatory action of manually refilling oil leaking from the "C"

RBCCW pump outboard bearing lubricating oil assembly as maintaining the operability of the degraded "C"
RBCCW pump under postulated
DBA conditions. However, Dominion did not perform an evaluation, which would have determined that this change would result in more than a minimal increase in the likelihood of occurrence of a malfunction of an
SSC important to safety previously evaluated in the final safety analysis report (as updated) and would, therefore, require a license amendment. The team identified that Dominion procedure
OP -

AA-102, Attachment 1, Immediate Operability Determination Guidelines, Step 7.c. improperly allows Dominion staff to change the facility through the use compensatory actions to

Enclosure maintain safety related

SSC operability, without evaluating this change pursuant to 10
CFR 50.59(c)(2). Dominion prevented the use of that portion of procedure
OP -
AA -102 following the inspection and until properly revised. This violation is being treated as an
NCV , consistent with Section 2.3.2 of the Enforcement Policy because it was Severity Level
IV and was entered into the Dominion corrective action program (CR 577964). (NCV 05000336/05000423/2015007-02, Failure to Provide
10 CFR 50.59 Evaluation Associated with Implementation of Operability Determination Procedure) .2.1.6 Unit 2, "A" Containment Air Recirculation Fan Unit (F14A) a. Inspection Scope The team inspected the "A" containment air recirculation (
CAR [[) fan unit, F14A, and associated cooler to assess whether they were capable of meeting their design basis function. Specifically, the team evaluated if the equipment was capable of removing heat from the containment during certain design basis events. The team reviewed drawings, calculations, hydraulic analyses, containment analysis, and the system]]
DBD to determine the
CAR fan design and licensing bases requirements. The team evaluated if Dominion ensured, through testing and flow balance measurements of the
RBCCW system, that the flow needed to meet heat removal requirements, assumed in containment temperature and pressure response calculations, were being met for the
CAR unit. The team also reviewed fan flow test results to determine whether the fan was capable of meeting air flow requirements assumed in the containment analysis. The team verified that the
CAR fan surveillance testing was performed consistent with
TS requirements. The team also performed a visual examination of control room
CAR fan controls and 480Vac breakers at associated load centers. The team verified breaker overcurrent protective relay set-points were established that ensured the
CAR fan motor and electrical bus were adequately protected and that the
CAR unit was not subject to spurious tripping. Additionally, the team reviewed electrical diagrams associated with breaker and fan controls, and piping and instrument diagrams associated with containment ventilation and the
RBCCW system to ensure all components of the
CAR [[unit were appropriately included in a test or maintenance program. Finally, the team reviewed corrective action documents and system health reports, and interviewed system and design engineers to determine whether there were any adverse operating trends or existing issues affecting]]

CAR unit reliability and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified.

.2.1.7 Unit 2, 4kv AC Electric Bus (24C)

a. Inspection Scope The team inspected the 4160 volts, alternating current (Vac) vital bus, 24C, to determine whether it was capable of performing its design basis function. The team reviewed the

UFSAR ,

DBDs, and electrical distribution calculations including load flow, voltage drop, transient, and short-circuit analysis. This review was performed to evaluate the adequacy

Enclosure and appropriateness of design assumptions, to evaluate whether bus capacity was exceeded, and to assess if bus voltages remained above minimum acceptable values under design basis conditions. The team reviewed the design and test results for automatic and manual transfers of alternating current (AC) power sources to determine whether they satisfied the design basis timing requirements. The team also reviewed the electrical overcurrent, undervoltage, and ground protective relay settings for selected circuits to evaluate whether the trip set points interfered with the ability of the supplied equipment to perform its safety function but were also set to provide adequate bus protection. The loss of voltage and degraded voltage relay surveillances, calibration results, and set point calculations were also reviewed to verify that they satisfied the requirements of the associated

TS [[s. Additionally, the team reviewed system maintenance test results, interviewed system engineers, and conducted field walkdowns to verify that equipment alignment, nameplate data, and breaker positions were consistent with design drawings, and to assess the material condition of the bus. Finally, the team reviewed corrective action documents and system health reports and interviewed system and design engineers to determine whether there were any adverse operating trends or existing issues affecting bus reliability and to assess Dominion's ability to evaluate and correct problems. b. Findings Introduction. The team identified a Green]]
NCV of
10 CFR Part 50, Appendix B, Criterion
III [[, "Design Control," in that, Dominion did not correctly evaluate the capability of 4.16 Kilovolts (kV) breakers to function properly during a severe fault condition. The team found the prospective fault currents on 4.16 kV load breakers would exceed the circuit breaker symmetrical interrupting rating of]]
250 MVA during a 3-phase bolted fault design condition. The team determined that this condition existed for multiple breakers on 24C and 24D emergency buses of Dominion's Millstone Nuclear Power Station Unit 2. Description. The team reviewed Dominion's
UFSAR and found that Section 8.2.2.2 describes 4.16 kV load breakers as having fault current interrupting capability of
250 MVA. The team also reviewed
GE drawing
GEZ -6105, "Power Circuit Breaker Specification for Type
AM [[Circuit Breakers Mounted in Vertical Lift Metal Clad Equipment" and determined the installed breakers are rated in accordance with the Institute of Electrical and Electronics Engineers/American National Standards Institute (IEEE/ANSI) C37.06 with ratings as follow: 250 3-phase]]
MVA class, 4.16 kV voltage class, 4.76 kV maximum voltage, and 36000A maximum symmetrical interrupting capability at 1.24 voltage range factor (K factor). The team then reviewed Millstone Unit 2 electrical distribution system analysis calculation (

MP2-ENG-ETAP-04014E2). This calculation evaluated Millstone Unit 2 electrical load flow, motor starting study, transient study, and short-circuit analysis. The team noted that the short-circuit analysis was performed to evaluate adequacy of the circuit breakers for their interrupting rating and the analysis evaluated different plant configurations such as power to the vital busses from the reserve station service transformer (RSST) feed, and normal station service transformer (NSST). The calculation was also used to evaluate operating scenarios such as reactor operation in Mode 1, Mode 6, and DBA scenarios.

Enclosure During this review, the team found that the assumptions used in this design analysis for calculating short-circuit fault currents were not in accordance with

IEEE /
ANSI [[C37 series design standards and were non-conservative, in some cases. Specifically, the team found that the analysis did not assume the maximum plant operating voltage (4284 Vac versus 4144 Vac assumed) at the 4.16 kV bus in Mode 1 and did not consider the plant configuration when]]
EDG s are operating in parallel with offsite power on the associated 4.16 kV emergency bus which is the system lineup during the monthly
TS [[surveillances. Following identification of the issue, Dominion revised the analysis to evaluate the capability of the affected safety related breakers to function properly during a worst case 3-phase bolted fault, including a case where the evaluation assumes 4284 Vac bus voltage and the]]
EDG [[is paralleled with offsite power. Dominion found that the result of this analyzed case showed that the prospective fault currents exceeded the breaker maximum symmetrical interrupting capability. To address this deficiency, Dominion entered this issue in their corrective action program under]]
CR [[576783. Dominion performed single failure analysis for this configuration to determine whether the breaker fails to interrupt the fault on one bus, and/or would the fault current affect the other safety related bus. Dominion concluded that the other bus would not be affected. The team reviewed the analysis and agreed with the assessment. Analysis. The team determined that Dominion's failure to correctly evaluate adequacy of the circuit breakers for their interrupting rating in accordance with]]
IEEE /
ANSI [[C37 series standards was a performance deficiency that was reasonable within Dominion's ability to foresee and prevent. The finding was more than minor because it adversely affected design control performance attribute of the mitigating system cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. This issue was similar to example 3.j in Appendix E of the]]
NRC [[]]

IMC 0612. Specifically, Dominion used non-conservative pre-fault bus voltage and did not consider the plant configuration where EDG synchronized in parallel configuration to the bus as an input to

the design analysis.

The team assessed this finding in accordance with

IMC 0609, "Significance Determination Process," Attachment 4, "Initial Characterization of Findings," and

IMC 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," Section A, "Mitigating Systems, Structures or Components and Functionality," and determined that the finding was of very low safety significance (Green) because the performance deficiency resulted in a non-conforming condition that did not result in loss of operability or functionality of the 4.16 kV system. Specifically, Dominion performed additional analysis and breaker and relay coordination study to show that breaker failure to interrupt the fault on one 4.16 kV bus did not affect the redundant 4.16 kV bus.

The team determined that the finding did not have a cross-cutting aspect because this performance deficiency was not indicative of Dominion's current performance. The team noted that this error existed since the issuance of Revision 1 of the calculation in January 2009. Enforcement. The team identified a violation of

10 CFR Part 50, Appendix B, Criterion

III, "Design Control," which states, in part, measures shall be established to assure that

Enclosure applicable regulatory requirements and the design basis are correctly translated into specification, drawings, procedures, and instructions. These measures shall include provisions to assure that appropriate quality standards are specified and included in design documents and that deviations from such standards are controlled. The design control measures shall provide for verifying or checking the adequacy of design, such as by the use of alternate or simplified calculational methods. Contrary to the above, between January 2009 and April 15, 2015, calculation

MP 2-
ENG -ETAP-04014E2 did not evaluate the circuit breaker interrupting capability in accordance with
IEEE /

ANSI C37

series standards. Specifically, Dominion did not assume correct voltage at the 4.16 kV bus and did not include a case where the

EDG [[was synchronized parallel with the bus which resulted in an inadequate evaluation of the 4kv bus and circuit breaker design which resulted in lower fault current being analysed. Dominion revised the calculation during the inspection. Because the finding was of very low safety significance and has been entered into Dominion's corrective action program (]]
CR 576783), this violation is being treated as an
NCV consistent with Section 2.3.2 of the
NRC [[Enforcement Policy. (NCV 05000336/2015007-01, Inadequate Evaluation of Circuit Breaker Interrupting Capability) .2.1.8 Unit 2 480 Volt Bus (22E) a. Inspection Scope The team inspected the 480 Vac vital bus, 22E, to determine whether it was capable of performing its design basis function. The team reviewed the]]
UFSAR ,

DBDs and electrical distribution calculations including load flow, voltage drop, short-circuit, and electrical protection coordination. This review evaluated the adequacy and

appropriateness of design assumptions, evaluated if bus capacity was exceeded and determined whether bus voltages remained above minimum acceptable values under design basis conditions. The team reviewed the electrical overcurrent protective relay settings for the supply and selected breakers at the load center to verify that the trip set points would not interfere with the ability of supplied equipment to perform their safety function yet ensuring the trip set points provided for adequate load center protection. The control logic design drawings of the 4kV supply breaker to vital bus 22E were reviewed to verify adequate breaker closing and opening circuit interlocks. Additionally, the team reviewed system maintenance test results, interviewed system engineers, and conducted field walkdowns to verify that equipment alignment, nameplate data, and breaker positions were consistent with design drawings and to assess the material condition of the bus. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess

Dominion's ability to evaluate and correct problems.

b. Findings No findings were identified.

Enclosure .2.1.9 Unit 2, 4kV to 480V transformer (24C1-1X) a. Inspection Scope The team inspected the 4160 Vac to 480 Vac transformer, 24C1-1X, to determine whether it was capable of performing its design basis function. The team reviewed the system one-line diagram, nameplate data, and design basis descriptions to verify that the loadings on 480 Vac substation transformer and the associated 4160 Vac and 480 Vac circuit breakers were within the corresponding transformer and switchgear design ratings. The team reviewed the design assumptions and calculations related to the short-circuit currents, voltage drops, and protective relay settings associated with the equipment to determine whether the output voltage was adequate and the settings were appropriate to meet design requirements. The team also reviewed a sample of completed maintenance activities and test results to evaluate if the high and low voltage cable feeders had sufficient capacity to supply the current and voltage requirements of the 480 Vac substation during normal and accident conditions. Finally, the team reviewed corrective action documents and system health reports, and interviewed system and design engineers to determine whether there were any adverse operating trends or existing issues affecting bus reliability and to assess Dominion's ability to evaluate and correct problems.

b. Findings No findings were identified.

.2.1.10 Unit 2, Inverter 2 (3VDA-INV2) a. Inspection Scope The team inspected the 120 Vac vital inverter,

3VDA -

INV2, to determine whether it was capable of performing its design basis function. The team reviewed the system loading

documentation to determine the design basis for maximum load and evaluated if the inverter vendor ratings were adequate to meet the design basis requirements. The team also reviewed calculations to evaluate whether the inverter provided the 120 Vac system loads with adequate voltage for design basis conditions. The team reviewed the operating and surveillance procedures to verify 120 Vac system voltage limits were correctly incorporated. Additionally, the team reviewed the inverter qualification testing to evaluate if component breakers provided for adequate clearing for the 120 Vac system branch circuits during fault conditions. The team completed a walkdown to assess the inverters material condition and to evaluate if the installation was in accordance with manufacturer instructions. Finally, the team reviewed corrective action documents and system health reports, and interviewed system and design engineers to determine whether there were any adverse operating trends or existing issues affecting the busses reliability and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified.

Enclosure .2.1.11 Unit 3, Service Water Motor-Operated Valve (MOV-71A) a. Inspection Scope The team inspected the

SW valve,
MOV [[-71A, to determine if it was capable of performing its design basis functions. Specifically, the team determined if the valve would reposition to isolate the turbine plant closed cooling water system, as required upon receipt of an engineered safety features actuation signal, to ensure adequate flow was available to the]]
SW system. The team reviewed the
UFSAR ,
TS s,
TS Bases, and the
IST basis documents to identify the design basis requirements of the valve. The team also reviewed periodic motor-operated valve (

MOV) diagnostic test results and stroke-timing test data to verify acceptance criteria were met. The team evaluated whether the

MOV safety functions, performance capability, and design margins were adequately monitored and maintained in accordance with
NRC Generic Letter 96-05 guidance. The team reviewed the
MOV [[weak link calculation to ensure the ability of the valve to remain structurally functional while stroking under design basis conditions. The team verified that the valve analysis used the maximum differential pressure expected across the valve during worst case operating conditions. Additionally, the team reviewed motor data, degraded voltage conditions, and voltage drop calculation results to confirm that the]]
MOV [[would have sufficient voltage and power available to perform its safety function at degraded voltage conditions. The team discussed the design, operation, and component history of the valve with engineering and operations staff and conducted a walkdown of the valve to assess its material condition of the valve and determine if the installed configuration was consistent with plant drawings, procedures, and the design basis. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified. .2.1.12 Unit 3, "A" Recirculation Spray Pump (3]]
RSS *P1A) a. Inspection Scope The team inspected the "A" containment recirculation spray system (RSS) pump,
3RSS [[*P1A, to determine whether it was capable of meeting its design basis function. The team reviewed calculations, operating procedures, test procedures, recent pump test results, and interviewed system and design engineers in order to evaluate the capability of the]]
RSS pump to perform its required function under limiting operating conditions. The team also reviewed minimum and maximum flow calculations, as well as
NPSH and vortex calculations to determine the adequacy of the pump's suction sources. The team reviewed system operating procedures to ensure they were consistent with the design requirements. The team also reviewed pump
IST procedures, test results, and trends in test data to evaluate pump performance. Additionally,
IST acceptance criteria were reviewed to verify appropriate correlation to accident analyses requirements. The team reviewed the

TS requirements associated with the recirculation spray pump and verified

Enclosure test results met

TS [[requirements. The team reviewed motor data, degraded voltage conditions, and associated voltage drop calculation to determine whether the pump motor would have sufficient voltage available to perform the intended safety function at degraded voltage conditions. Finally, the team performed a walkdown of the pump and associated equipment, interviewed station personnel, and reviewed recent]]

CRs, system health reports, and maintenance history to determine the overall condition of the pump,

whether there were any adverse operating trends, and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified.

.2.1.13 Unit 3, "B" Motor Driven Auxiliary Feedwater Pump (AFW-P9B)

a. Inspection Scope The team inspected the "B" motor-driven

AFW pump,
AFW -P9B, to determine if it was capable of meeting its design basis functions. Specifically, the team evaluated whether the pump was capable of providing adequate flow to the steam generators during
DBA s. The team reviewed the
AFW system hydraulic model and the design basis hydraulic analysis/calculations to verify that required total developed head (TDH),
NPSH , and pump run-out conditions had been properly evaluated under all
DBA conditions. The team reviewed system operating procedures to ensure they were consistent with the design requirements. The team also reviewed pump
IST procedures, test results, and trends in test data to determine if pump performance was consistent with design basis assumptions and verified

IST acceptance criteria were appropriately correlated to accident analyses requirements. Seismic design documentation was reviewed to evaluate whether pump design was consistent with limiting seismic conditions. Additionally, the motor data, degraded voltage conditions, and voltage drop calculation results were reviewed to confirm that the pump motor would have sufficient voltage and power available to perform the intended safety function at degraded voltage conditions. The team also conducted a detailed walkdown of the pump and support systems to determine the material condition of the components and to ensure adequate configuration

control. Finally, the team reviewed corrective action documents and system health reports to evaluate whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified.

Enclosure .2.1.14 Unit 3. Demineralized Water Storage Tank (3FWA-TK1) a. Inspection Scope The team inspected the demineralized water storage tank (DWST),

3FWA -
TK [[1, to determine if it was capable of meeting its design basis function. Specifically, the team evaluated whether the tank was adequately designed to provide the required quantity of water during design basis events. The team reviewed the design, testing, inspection, and operation of the]]
DWST and associated tank level instruments to evaluate whether the tank could perform its design basis function as the water source for the
AFW [[pumps. Specifically, the team reviewed design calculations, drawings, and vendor specifications (including tank sizing and level uncertainty analysis, and pump vortex calculations) to evaluate the adequacy and appropriateness of design assumptions and operating limits. Seismic design documents were reviewed to evaluate whether]]
DWST [[design assumptions were consistent with limiting seismic conditions. The team interviewed system and design engineers, reviewed instrument test records, and tank inspection results to determine whether maintenance and testing was adequate to ensure reliable operation. Additionally, the review evaluated whether those activities were performed in accordance with regulatory requirements, industry standards, and vendor recommendations. The team also interviewed system and design engineers and conducted a walkdown of the tank area to assess the material condition of the]]
DWST [[and associated instrumentation. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified. .2.1.15 Unit 3, "A" Service Water Pump (3-SWP-P1A) a. Inspection Scope The team inspected the "A"]]
SW pump, 3-

SWP-P1A, to determine whether the pump was capable of performing its design basis function. Specifically, the team evaluated whether

the pump could provide an adequate supply of cooling water flow to safety-related components during abnormal and accident conditions. Additionally, the team evaluated the ability of the system to respond to several beyond

DBA [[s credited in Millstone's risk analysis. The team assessed the system hydraulic calculations to ensure the pump provided adequate cooling to safety-related components. The team also verified that design requirements for flow and pressure were properly translated into]]

IST acceptance criteria and evaluated pump IST performance to determine if there was any degradation in pump performance. Seismic design documentation was reviewed to determine

whether pump design was consistent with limiting seismic conditions. The team reviewed the SW pump submergence requirements and available submergence to ensure the pump was capable of fulfilling its safety function at the maximum flowrate assumed and lowest intake level. The team also reviewed design documentation to verify pump motor design was consistent with limiting environmental conditions and evaluate the required

Enclosure capacity for the brake horsepower required by the pump to determine if the pump motor would operate as required. In addition the team reviewed the 4160 Vac system load flow calculation to confirm adequate voltage would be available at the motor terminals during operation. The inspectors also reviewed the motor overcurrent relay setting calculation, relay settings, and recent overcurrent relay calibration tests to evaluate whether the protective relays would provide for reliable motor operation at design basis minimum voltage conditions. The team conducted a detailed walkdown of the pump and discussed the

SW [[pump operation and performance with the engineering staff to assess the material and environmental conditions, and to verify that the installed configuration was consistent with system drawings, and the design and licensing bases. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings No findings were identified. .2.1.16 Unit 3, "B" Safety Injection Pump (3]]

SIH*P1B) a. Inspection Scope The team inspected the "B" high head safety injection pump, 3SIH*P1B, to determine if it was capable of performing its design basis function. Specifically, the team assessed the ability of the pump to provide required system head and flow requirements for injection

into the reactor coolant system during design basis events through the review of the

UFSAR , drawings,

DBDs, and procedures. The team determined whether design inputs were properly translated into system procedures and tests, and reviewed completed surveillance tests to determine if the results adequately demonstrated pump operability. Additionally, the motor data, degraded voltage conditions, and voltage drop calculation results were reviewed to confirm that the pump motor would have sufficient voltage and

power available to perform its safety function at degraded voltage conditions. The team also reviewed the adequacy of water supply sources to the pump including an assessment of the potential for vortex conditions. The team also performed field walkdowns and interviewed system engineers and operators to assess the material condition of the pump and supporting equipment as well as the capability to implement design basis event procedures. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings

No findings were identified.

Enclosure .2.1.17 Unit 3, "C" Charging Pump (3CHS*P3C) a. Inspection Scope The team inspected the "C" charging pump,

3CHS [[*P3C, to determine whether it was capable of performing its design basis function. Specifically, the team assessed the ability of the pump to provide required system head and flow requirements for injection into the reactor coolant system during normal operation and design basis events through the review of the]]
UFSAR , drawings,
DBD [[s, and procedures. The team reviewed a sample of surveillance test results to verify that pump performance met the acceptance criteria and to ensure that the acceptance criteria were consistent with the design basis. The team reviewed calculations for suction resource vortexing during design basis injection conditions as well as]]

NPSH requirements and post modification testing analyses

associated with pump rotating element replacement. The team discussed the design, operation, and corrective maintenance of the pump with engineering and operations staff as well as performed a walkdown of the pump to gain an understanding of the capability of the site to implement normal, abnormal, and emergency operating procedures,

component performance history, and overall component health. Finally, the team reviewed corrective action program entries, maintenance activities, and system health

reports to determine whether there were any adverse operating trends and to assess Dominion's ability to identify, correct, and prevent equipment reliability concerns. b. Findings No findings were identified. .2.1.18 Unit 3, "B" Emergency Diesel Generator - Electrical (3B) a. Inspection Scope The team inspected the "B"

EDG 3B to determine whether it was capable of meeting its design basis function. Specifically, the team reviewed calculations for both static and transient loading to determine whether the

EDG had sufficient capacity and capability to

supply the required accident loads. The team reviewed one-line diagrams for the

EDG , the vendor manuals, nameplate rating data, and the

EDG load study to ensure that the EDG was operated consistent with its rating and capable of operating under the worst case design basis loading conditions. The team also reviewed the generator electrical protective relaying scheme including drawings, calculations, calibration records, and procedures to determine whether the generator was adequately protected and whether its output breaker was subject to spurious tripping. Additionally, the team reviewed maintenance schedules, procedures, and completed work records to determine whether

the

EDG was being properly maintained and reviewed completed surveillances to determine whether the diesel was being tested in accordance with the
TS s. The team reviewed the design and testing of the
EDG sequencer, confirmed the accident loading of the
EDG was within the
EDG rating, and reviewed the interlocks and sequence timing to confirm they were correctly represented on the control schematics of the selected safety-related pumps. The team also interviewed station engineers and performed walkdowns of the Unit 3

EDGs to assess the material condition of equipment. Finally, the

Enclosure team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems.

b. Findings No findings were identified.

.2.1.19 Unit 3, 480 Volt Bus 32R Transformer (34D4-1X) a. Inspection Scope The team inspected the 4160-480 Vac transformer, 34D4-1X, to determine whether it was capable of meeting its design basis function. Specifically, the team evaluated if the transformer had adequate capability to provide required power to supplied 480 volt bus and associated equipment. The team reviewed load calculations to determine the design basis maximum load and reviewed the bus load center equipment vendor ratings to ensure they were in conformance with the design basis. The team reviewed surveillance tests to verify the acceptance criteria satisfied design basis load requirements and

transformer protection settings. The team also reviewed the coordination/protection calculation for the transformer incoming line and load side breakers for design basis load

flow conditions and transformer protection and coordination to ensure breaker set points were adequate to protection equipment and to ensure that the spurious tripping did not occur. Additionally, the team interviewed plant engineers and performed a walkdown of the transformer to assess the material condition of the equipment. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Dominion's ability to evaluate and correct problems. b. Findings

No findings were identified. .2.1.20 Unit 3, 480 Volt Vital Load Center (32T)

a. Inspection Scope The team inspected the 480 Vac vital load center, 32T, to determine whether it was capable of performing its design basis function. The team reviewed electrical distribution calculations including load flow, voltage drop, short-circuit, and electrical protection coordination. This review evaluated the adequacy and appropriateness of design

assumptions, determined whether load center capacity was exceeded, and evaluated if voltages remained above minimum acceptable values under design basis conditions. The team reviewed the electrical overcurrent protective relay settings for the supply and selected breakers at the load center to verify that the trip set points would not interfere with the ability of supplied equipment to perform their safety function yet provide for adequate load center protection. The team also reviewed system maintenance test results, interviewed system and design engineers, and conducted field walkdowns to

Enclosure verify that equipment alignment, nameplate data, and breaker positions were consistent with design drawings and to assess the material condition of the load center. Finally, the team reviewed corrective action documents and system health reports, and interviewed system and design engineers to determine whether there were any adverse operating trends or existing issues affecting the busses reliability and to assess Dominion's ability to

evaluate and correct problems. b. Findings

No findings were identified. .2.2 Review of Industry Operating Experience and Generic Issues (5 samples) The team reviewed selected

OE issues for applicability at the Millstone Power Station. The team performed a detailed review of the
OE issues listed below to verify that Dominion had appropriately assessed potential applicability to site equipment and initiated corrective actions when necessary. .2.2.1
NRC Information Notice 2009-10, Transformer Failures - Recent Operating Experience a. Inspection Scope The team reviewed Dominion's response to

NRC Information Notice (IN) 2009-10, "Transformer Failures - Recent Operating Experience" and found the site was not aware of this specific IN. However, the team noted that Dominion had already replaced all the large power transformers on Unit 2 and the main transformer on Unit 3. Replacement of the remaining large power transformers at Unit 3 were in the site's long term plans. b. Findings

No findings were identified. .2.2.2

NRC Information Notice 2012-01, Seismic Considerations - Principally Issues Involving Tanks a. Inspection Scope The team assessed Dominion's applicability review and disposition of
NRC [[]]
IN 2012-01, "Seismic Considerations - Principally Issues Involving Tanks." The

IN was issued to inform licensees of operating experience related to inadequate seismic analyses of safety related tanks associated with stored inventory and interaction with non-seismic systems, structures, or components. The team interviewed station engineers and performance improvement group staff and reviewed operating experience program administrative guidance and corrective action program entries concerning the implementation of the operating experience program to determine Dominion's expectations and standards for the evaluation and mitigation potential vulnerabilities identified via external operating

experience. The team interviewed station engineers as well as reviewed seismic

Enclosure analyses and maintenance procedures for safety related tanks to assess Dominion's response to the seismic to non-seismic concerns identified in the IN. b. Findings No findings were identified.

.2.2.3 NRC Information Notice 2012-14, Motor-Operated Valve Inoperable Due to Stem-Disc Separation a. Inspection Scope

The team reviewed Dominion's response to

NRC [[]]
IN 2012-14, "Motor-Operated Valve Inoperable Due to Stem-Disc Separation." This notice informed licensees about operating experience involving an
MOV that failed at the connection between the valve stem and disc and the
NRC 's expectations regarding licensee actions/programs to ensure the completeness of operability determinations for
MOV s. The team reviewed Dominion's applicability review and disposition of
NRC lN 2012-14 and the
MOV and
IST Programs at Millstone, as they related the issues identified in this
IN. The team reviewed the associated corrective action program document,

CR 521814, which addressed questions regarding the incorporation of Joint Owner's Group threshold valve factors in determining the operability of MOVs and discussed the bases for valve factors

implemented at Millstone. The team also reviewed Millstone's test program to verify conformance with testing requirements and reviewed

IST procedures to assess the adequacy of methods for accurately determining valve functionality. Finally, the team reviewed actions during the inspection that addressed how weaknesses in documenting the adequacy of their

IST procedures review were addressed. b. Findings

No findings were identified. .2.2.4

NRC Information Notice 2013-05, Battery Expected Life and Its Potential Impact on Surveillance Requirements a. Inspection Scope The team reviewed Dominion's response to
NRC [[]]
IN 2013-05, "Battery Expected Life and its Potential Impact on Surveillance Requirements." The
NRC issued this
IN to inform the licensees about issues involving licensee's nonconservative technical specifications regarding surveillance requirements for direct current (
DC ) power systems due to reduction in battery life. The team reviewed Dominion's response and associated documents that were used to disposition this
IN. Specifically, the team reviewed Dominion's battery sizing calculations and verified that the calculation used correct aging factor of 1.25 in accordance with

IEEE 485 standard. This aging factor ensures that frequencies for performing TS surveillances, specifically those associated with

Enclosure performance and modified performance discharge testing, are conservative when batteries reach 85 percent of expected life.

b. Findings No findings were identified. .2.2.5

NRC Information Notice 2012-06, Ineffective Use of Vendor Technical Recommendations a. Inspection Scope The team reviewed Dominion's response to
NRC [[]]
IN 2012-06, "Ineffective Use of Vendor Technical Recommendations." This notice informed licensees about operating experience regarding ineffective use of vendor technical recommendations. The team reviewed Dominion's disposition of
NRC lN 2012-06 by evaluating Dominion's associated corrective action program document,
OEE 001481. Additionally, the team evaluated the actions to address performance gaps in their program identified by Dominion's following their review of the

IN. In addition, the team selected specific vendor communications/updates to determine whether the updates were appropriately reviewed

and incorporated into the required document (e.g., vendor manual, station procedures, etc.). b. Findings No findings were identified. 4.

OTHER [[]]
ACTIVI TIES
4OA 2 Identification and Resolution of Problems (

IP 71152) a. Inspection Scope The team reviewed a sample of problems that Dominion had previously identified and entered into the corrective action program. The team reviewed these issues to verify an appropriate threshold for identifying issues and to evaluate the effectiveness of corrective actions. In addition, CR written on issues identified during the inspection, were reviewed to verify adequate problem identification and incorporation of the problem into the corrective action system. The specific corrective action documents that were sampled and reviewed by the team are listed in the Attachment. b. Findings No findings were identified.

Enclosure 4OA6 Meetings, including Exit On May 1, 2015, the team presented the inspection results to Mr. John Daugherty, Site Vice President, and other members of the Millstone Power Station staff. The team reviewed proprietary information, which was returned to Dominion at the end of the

inspection. The team verified that no proprietary information was documented in the report.

Attachment

ATTACH [[]]
MENT [[]]
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]
CONTAC T Dominion Personnel
D. [[Dougherty, System Engineer D. Lowell, System Engineer D. MacNeill, Engineering Supervisor D. Russo, System Engineer D. Scott, System Engineer H. Williamson, Unit 2 Shift Manager Operations J. Barile, System Engineer J. Daugherty, Vice President J. Plourde, System Engineer J. Price, Supervisor Mechanical Maintenance K. Deslandes, Design Engineering Supervisor K. Wallace, System Engineer L. Salyards, Licensing Engineer J. Powers, Engineering L. Loomis, System Engineer M. Fiala, System Engineer M. Legg, Corporate Mechanical Engineer, M. Marino, Corporate Mechanical Engineering Supervisor M. Vezina, System Engineer P. Amdola, Seismic Engineer R. Acquaro, Shift Manager R. Deconto, Consulting Engineer R. Patel, Design Engineer R. Shauffler, Corporate Mechanical Engineer R. Van Steengergen,]]

MOV Program Owner S. Saulter, Mechanical Maintenance Technician S. Smith, Manager Operations S. Stanley, Director of Nuclear Engineering T. Cleary, Licensing Engineer T. Perkins, Unit 2 Unit Supervisor Operations W. Chestnutt, Unit 2 Supervisor Nuclear Shift Operations W. Saputo, System Engineer

Attachment

LIST [[]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED [[]]
AND [[]]
DISCUS [[]]
SED Open and Closed 05000336/2015007-01
NCV Reactor Building Closed Cooling Water System Pump Oil Leakage Results in Technical Specification Inoperability (Section 1R21.2.1.5) 05000336/411/2015007-02
SLIV Failure to Provide
10 CFR 50.59 Evaluation for Interim Action Associated with Implementation of Operability Determination Procedure (Section 1R21.2.1.5) 05000336/2015007-023
NCV Inadequate Evaluation of Circuit Breaker Interrupting Capability (Section 1R21.2.1.7)
LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]
ED Calculations & Engineering Evaluations00-059,
MP 3
SW System
NPSH Evaluation, Revision 1 02-0600,
MP 3
PM Change Request (
RSS Pumps), Revision 0 03705-US(B)-359, Recirculation Spray Pump Performance, Revision 0 03705-US(B)-361, Containment
RSS and
SI System Hydraulic Analysis, Revision 3 07077-US(B)-002, Maximum Containment Water Level During
LOCA , Revision 0 08-
ENG -04393M3,
AFW System,
NPSH Margin Given Pump Suction Alignment to
CST , Revision 0 12179-526, Stress Analysis of Demineralized Water Storage Tank, Revision 1 12179-
HYD -H39, Design of Vortex Suppressor for the
QSS Tank
QSS *TK1, Revision 1 12179-NM(B)-534-IE, Millstone Unit 3 Refueling Water Storage Tank Design and Analysis, Revision 1, and Change Notice 1, Revision 1 and Change Notice 2, Revision 1 12-ENG-04355M2,
HPSI Pump Comprehensive
IST [[Acceptance Criteria, Revision 0 151E, Panel Loading for Class 1E and Non-Class 1E Channels 1-4, Revision 01 178E, 5 kV and 8 kV Power Cable Temperature under Fault Conditions, Revision 2 183E, Effect of Sil-Temp Wrap on Cable Ampacity, dated 10/04/1985 195E, Verify Cable Selection for 9.9 kV and 4.16 kV Loads, dated 8/27/85 211E, Voltage Verification for 120V Vital bus Circuits Class 1E, Revision 01 25203-ER-98-0103, Design Inputs for]]
MP 2
ECCS System Analysis, Revision 0 84-065-00753GE, 480V Breaker Overcurrent Trip Device, Revision 2 90-094-01076M3, Target Thrust Torque for
3SWP *
MOV 71A,
3SWP *
MOV 71B, Revision 5 91-004-288E2, Primary Penetration Protection Study (Unit 2), Revision 00, Changes 1- 6, 8 92-030-1311E2, Emergency Bus Undervoltage Setpoint Analysis, Revision 1 92-079,
NPSH Requirements and
NPSH Available for
MP 2
SWS Pumps, Revision 1 93C2799-C-008, Millstone Unit 2 Seismic Capacity of Refueling Water Storage Tank, Revision 0 94103-C-08, Weak Link Seismic Assessment for
MOV s 3
SWP *MOV71A/B, Revision 3 96-001, Empirical Adjustment of
MP 3
SW Model to 1995 Flow Test Data, Revision 3 96-067, Aux. Feedwater System Comprehensive Flow Analysis, Revision 3 97-120,
MP 2

CAR Unit Performance with Design Fouling, Revision B

Attachment 97-CAR-01916M2, Containment Air Recirculation System Original Design Data, Revision 0 97-CAR-01917M2, Containment Air Recirculation System, Air Flow Rate and Throw Distance through Fusible Link Plates, Revision 0 97-ENG-01774-E2, Battery Sizing, Revision 2 97-ENG-01912E2, Millstone Unit 2 4.16 Switchgear Relay Settings, Revision 0, Change 4, through Addendum 23 98-ENG-02568M2,

RBCCW Pump Acceptance Curve for
TS Section 4.7.3.1, Revision 01 C14.1460, Lateral Supports for Service Water Pumps, Revision
0 CN -
TA -06-101, Millstone Unit
3 SPU Program
IGOR /RETRAN Base Deck, Revision
1 DM 2 00-0200-09, Temporary Credit for Local Manual Action Outside Control Room,
RWST Purification Subsystem, dated 5/17/12
DM 2-00-0135-09, New O/C Relay for P41A/B/C Motors
DM 2-01-0135-09, Move Test Point for New O/C Relay for P41A/B/C Motors
DM 3-00-0127-08, Power Uprate Effect on
RCP Operation
DM 3-00-0206-09,
MCC Starter Replacement, dated 7/21/10
DM 3-02-0983-97, Addition of New Drawing for Orifice Plates 3
RSS *RO40A-D, dated 3/6/98
ENG 97-122,
ECCS System Analysis, Revision
3 ETE -
CEE -2014-1006,
MPS 3 Auxiliary Feedwater Pump Quarterly and Comprehensive
IST Flow Test Requirements, Revision
0 ETE -
CME -2014-1010,
MP 3, 'A' Service Water Pump Performance Evaluation Based on Data from
SPROC [[]]
OPS 14-3-001, Revision 107
ENG -01912E2, Millstone Unit 2 4.16
KV Switchgear Relay Settings, Revision 0
GSI -191-ECCS-04150M3, Post-LOCA Transport Evaluation for
GSI -191 Resolution, Revision 1
GSI -191-ECCS-04162M2, Post
LOCA Debris Transport Evaluation, Revision 1
GSI -191-ECCS-04364M3,
RSS Pump
NPSH with
ECCS Strainer and Debris Bed, Revision 1 M22502022-01643-C2, Calculation for
RWST Pipe Support 5-2-22, Revision 0 M3-05003, Replacement of
ECCS Sump Strainer per Generic Letter 2004-02, Revision 0 M3-06006, Unit 3 Vital Inverters Replacement, Revision 0 M3-98-008, Containment Recirculation Pump Pressure Drop at Inboard Seal Cavity, Revision 1
MIL 2-34325-AR-001, Hydraulic Performance of Containment Sump Strainers, Revision
1 MP 2-
ENG -ETAP-04014E2,
MP 2 Electrical Distribution System Analysis, Revision 3
MP 3-12-01171, Millstone Unit
3 BDB Integrated
FLEX Strategy, Electrical Connection, Revision 008
MP 3-
CALC -ENG-067R, Maximum Cable Lengths for Continuous Duty Motors, Revision
1 MP 3-
CALC -ENG-195E, Unit 3 Verification of Cable Size for 6.9 and 4.16 kV Loads, Revision
1 MP 3-
CALC -ENG-195R, Unit 3 Verification of Cable Size for 6.9 and 4.16 kV Loads, Revision
0 MP 3-
ENG -ETAP-04125E2,
MP 3 Electrical Distribution System Analysis, Revision 3
MP 3-ENG-ETAP-04125E3,
MP 3 Electrical Distribution System Analysis, Revision 0
MP 3-ENG-ETAP-04125E3,
MP 3 Electrical Distribution System Analysis, Revision 0
NL -033, Millstone 3 Emergency Generator Loading & Starting
KVA , dated 3/19/2015
NL -035, 480 V Emergency Load Center Bus Tie Cable Ratings, Revision
0 NSP -098-
FWA ,
DWST Level Setpoint and Loop Uncertainty, Revision 2
PA 84-065-753GE,
AC 480 V Load Center 22E/22F Relay Settings, Revision 2 S-M2
CNT -04325S2, Gothic Containment Analysis Models for
MP 2, Revision 0
SP -M3-EE-10118,
MP 3 Vital Inverter System Replacement, Revision 008-01
SP -M3-EE-321, Control of Electrical Setpoints, Revision
02 US (B)-294,
NPSH Available for
ECCS Pumps, Revision 6
US (B)-295,
RW [[]]

ST Draw-Down Rates and Switchover Levels, Revision 8

Attachment W3-517-981RE, Millstone 3 Emergency Operating Procedure (EOP) Setpoint Documentation, Revision 9 U3-M3-E-0333, Specification for Millstone Unit 3 - Environmental Conditions for Equipment Qualification, Revision 8 Corrective Action Condition Reports M3-98-0264 578418* 578186* 578094* 578021 577964* 577517

577352 576963* 576954* 576894* 576849* 576783* 576769 576681 576672* 576668* 576660* 576658* 576653* 576586* 576087* 575949 575859* 575795

575715 575386 574885 574298 571810 570890 569843 567464 566235 565930 565623 564871 564728 564534 564145 564063 562815 562524 561251

555200 553357 552620 546641 546553 546392 546145 545333 543044 542534 541482 539885 533729 527366 522948 521814 515688 515402 512399 512342 507496 506375 505514 492266 484281 483716 479997 477001 473152 461213 455671 448364 446274 438997 435062 433907 425265 422481 417346 411945 322563 242390 08-01442 001481

CR written as a result of this inspection Design and Licensing Basis Documents 25212-
MP 3-SFR, Millstone Unit 3 Safety Functional Requirements Manual, Revision 6
3DBS -
BOP -001, Design Basis Summary for
MP 3 Service Water System, Revision 2 3
DBS -NSS-003, Design Basis Summary for the Containment
RSS , Revision 1
DBS -2308, High Pressure Safety Injection System, Revision
1 DBS -2326A, Design Basis Summary - Service Water System, Revision 1
DBS -2330A, Design Bases Summary - Reactor Building
CCW System, Revision 0
DCR M3-07001,
MP 3 A & C Charging Pump Rotating Assembly Replacement, dated 10/22/10
DBS -NSS-001, Design Bases Summary -
AFW System, Revision 1
DBS -2313A, Design Bases Summary - Containment Air Recirculation and Cooling System, Revision
0 DBS -
BOP -001, Design Bases Summary - Service Water System, Revision
2 DM 3-00-0015-08, Addition of Vent Valve Upstream of Valve 3
SIH *MV8835, dated 5/27/07
EQR 113-01, Equipment Qualification Record
RBCCW Pumps, Revision
5 EQR 115-4-1, Millstone Unit 3 Equipment Qualification Record Charging Pumps, Revision 1 M3-
EV -07-0036, New Design Information for
MP 3 Charging Pump (

CHS*P3C) Rotating Assembly Upgrades, dated 10/22/10 Millstone Unit 2 Technical Specifications, dated 4/18/14 Millstone Unit 2 Updated Final Safety Analysis Report, Revision 32

Millstone Unit 3 Technical Specifications, dated 7/11/14 Millstone Unit 3 Updated Final Safety Analysis Report, Revision 27.2

Attachment U2-IST-ISTBDM,

MP 2
IST Basis Document, Revision 4 U3-24-IST-ISTBD,
MP 3
IST Basis Document, Revision 3-14-001 Drawings 1201170-E-25203-30001-A, Main Single Line Diagram, Revision 0 1201170-E-25203-30001-B, Main Single Line Diagram, Revision 0 1201171-E-25212-300001,
MP 3 Main One Line / Phasing Diagram, Revision 0 12179-
EC -30F, Demineralized Water Storage Tank, Foundation Yard Tankage, Revision 7 12179-EC-14T, Outline
CW Pump House, Revision 6 12179-
EM -8B, Circ and Service Water Pump House, Revision 11 25212-20406, Sht. 1, Containment Recirculation Pump
3RSS [[*P1A Seal Piping, Revision 2 25203-24014, Containment Ventilation, Revision 2 25212-25031, Sht. 1, Yard Piping, Revision 8 D-74-413, Richmond Engineering Company Demineralized Water Storage Tank, Revision 14 25212-30004, Main One Line Diagram 4160 Norm & Emergency Buses, Revision 20 25203-30108, Sht. 5, Millstone Unit #2 4160V System Relay Settings, Revision 3 25203-26005, Sht. 3, Condensate Storage and]]
AFW , Revision 60 25203-26011, Sht. 1, Fire Protection, Revision 57 25203-26008, Sht. 3, Service Water to Vital
AC Switchgear Cooling Coil and
AC [[Chillers, Revision 33 25203-26008, Sht. 2, Piping & Instrument Diagram Service Water, Revision 113 25203-26015, Sht. 2, High Pressure Safety Injection Pumps, Revision 46 25203-26015, Sht. 1, Low Pressure Safety Injection System, Revision 45 25203-26022, Sht. 3,]]
RBCCW System Containment Spray Pump and Safety Injection Pump Seal Coolers, Revision 14 25203-26022, Sht. 2,
RBCCW System Spent Fuel Pool and Shut-down Heat Exchangers, Revision 26 25203-26022, Sht. 1,
RBCCW System

RBCCW Pumps and Heat Exchangers, Revision 45 25203-26022, Reactor Building Closed Cooling Water System Containment Air Recirculation and Coolant Unit, Revision 27 25203-26028, Containment and Enclosure Building Ventilation, Revision 47 25212-26933, Sht. 2, Service Water, Revision 89 25212-26904, Sht. 1, Chemical and Volume Control, Revision 54 25212-26904, Sht. 4, Chemical & Volume Control, Revision 30 25212-26930, , Feedwater System, Revision 48 25212-26933, Sht. 4, Service Water, Revision 45 25212-26904, Sht. 1, Chemical and Volume Control, Revision 54 25212-26905, Sht. 1, Charging Pump Sealing and Lubrication, Revision 23 25212-26916, Sht. 4, EDG "B" Starting Air System, Revision 7 25212-26912, Sht. 1, 2 and 3, Low Pressure Safety Injection, Revision 50, 23 and 38 25212-26913, Sht. 2, High Pressure Safety Injection, Revision 41 25212-26911, Fuel Pool Cooling & Purification System, Revision 37 25212-26913, Sht. 1, High Pressure Safety Injection, Revision 32 25212-26916, Sht. 3, Emergency Diesel Generator "B" Starting Air System, Revision 20 25212-26914, Sht. 1, Safety Injection Pump and Neutron Shield Tank Cooling Systems, Revision 18 25212-26915, Sht. 1, Quench Spray and Hydrogen Recombiners, Revision 37

Attachment 25203-28108, Sht. 26, Logic Diag.-Diesel Gen. Cooling Water Heater Exch. Supply & Bypass Valves, Revision 8 25203-28115, Sht. 22, Pump Recirculation Header Stop Valves, Revision 3 25203-28150, Sht. 1, Engineered Safety Logic, Revision 9 25203-28150, Sht. 3, Engineered Safety Logic Sequencer, Revision 6 25203-28150, Sht. 2B, Engineered Safety Logic, Actuated Equipment Tabulation, Revision 6 25212-28457, Sht. 11, Logic Diagram Containment Recirculation, Revision 11 25212-28457, Sht. 10, Logic Diagram Containment Recirculation, Revision 11 25212-29004, Sht. 11, Hayward Tyler

24 VSN [[Vertical Pump, Revision N 25212-29023, Sht. 1, Refueling Water Storage Tank, Revision 24 25212-29023, Demineralized Water Storage Tank, Revision 21 25212-29044, Sht. 19, Tandem Package Shaft Seal, Revision E 25212-29041, Motor Driven Aux. Feedwater Pump, Revision H 25203-29126, Sht. 28, Pressure Relief Damper, Revision A 25212-29190, Sht. 24, Orifice Plates,]]
RSS Pump Discharge, Revision A 25212-30078,
125 VDC One Line Diagram Batteries 308B-1& 301B-2, Revision 33 25212-30047, Sht. 2, 480V
MCC One Line Diag Rod Control Area, Revision 49 25203-30052, Sht. 2, Schematic Diagram 480 V Unit Substation 22E (B05), Revision 5 25212-30061,
480 VAC [[]]
MCC One Line Diagram Control Building, Revision 35 25203-30099, Sht. 23, 480 V Load Center Circuit Breaker Settings, Revision 5 25203-30099, Sht. 20, 480 V Load Center Circuit Breaker Settings, Revision 6 25203-29641, Containment Building
HVAC ,
CAR Fans F14A/B/C/D, Revision 3 25212-30076, One Line Diagram
125VDC &120
VAC Distr Sys-Cmpst, Revision 31 25212-30082,
120 VAC One Line Diagram Vital Bus
II &
IV , Revision 29 25203-30001, Main Single Line Diagram, Revision 40 25203-30005, Single Line Meter & Relay Diagram, Revision 21 25212-30001, Main One Line / Phasing Diagram
PWR "Distr Sys Composite, Revision 26 25203-30044, Sht. 17, Schematic Diagram 4.16KV Bus 24C, Revision 11 25203-30044, Sht. 16, Schematic Diagram 4.16KV Bus 24C, Revision 8 25203-30044, Sht. 4, Schematic Diagram 4.16KV Bus 24C, Revision 8 25203-30044, Sht. 1, Schematic Diagram [[power source" contains a listed "[" character as part of the property label and has therefore been classified as invalid. Bus 24C, Revision 5 25203-30044, Sht. 3, Schematic Diagram 4.16KV Bus 24C, Revision 2 25203-30044, Sht. 2, Schematic Diagram 4.16KV Bus 24C, Revision 2 25203-30034, Sht. 1, Logic Diagram, Diesel Generator & Diesel Bkr. Control, Revision 13 25212-30241, Sht. 1, Emergency Generator Starting Air System Air Compressor Control, Revision 5 25203-32002, Sht. 56, C Containment Air Recirc Fan F14C, Revision 6 25212-32001, Sht.]]
5CJ , Service Water Pump 3
SW *P1A, Revision 20 25203-32022, Sht. 55, "A" Containment Air Recirc Fan F14A, Revision 6 25203-32003, Sht. 33, Containment Air Recirculation Fan F14A
CB 22E6-2, Revision 5 25212-32001, Sht. 5
CN , Unit No.
3 CNTMT Recirc Pump, Revision 14 and 17 25212-32001, Sht. 5
CU , Unit No. 3 Charging Pump P3C, Revision 14 25212-32001, Sht.
5DK , Safety Injection Pump P1B, Revision 14 25203-32005, Sht. 30, Reserve Station Service Transformer, Revision 7 25212-32001, Sht. 5
CV , Charging Pump P3C (Swing), Revision 12 25203-32023, Sht. 42, Vital Switchgear Room Cooling Fan F51, Revision 15 25203-32002, Sht. 14, Millstone Unit 2 4.16
KV Tie Feeder Bkr, Revision 6 25203-32002, Sht. 13, Millstone Unit 2 4.16

KV Tie Feeder Bkr, Revision 6

Attachment 25203-32002, Sht. 1, 4.16KV Main Feeder Bkr., Revision 12 25203-32002, Sht. 2, 4.16KV Main Feeder Bkr., Revision 11 25212-32001, Sht.

5DY , Millstone Nuclear Power Station - Unit No. 3 Stm Gen Aux Fdwtr
PP Mot Driven P1B, Revision 14 25203-32013, Sht. 22, Millstone Unit 2 Diesel Eng.
CW Ht. Exch. Supply
SV -FV6397 (2-SW-89B) & Bypass Valve
SV -
FV [[6342 (2-SW-231B), Revision 13 25203-32008, Sht. 6, Containment Spray Pump P43A, Revision 11 25203-32013, Sht. 5, Service Water Pump P5A, Revision 14 25203-32008, Sht. A, Control Switch Development, Revision 11 25203-32008, Sht. B, Limit Switch Development, Revision 6 25203-32008, Sht. 3, High Pressure Safety Injection Pump P41B, Revision 14 25203-32015, Sht. 3, Reactor Building Closed Cooling Water Pump, Revision 17 25203-32022, Sht. 1, Cnmt. Air Recirc. Fan]]
MF 14A Control, Revision 15 25203-39005, Sht. 51A,
MCC For Load Center B5, Revision 3 25203-39005, Sht. 51C, Millstone Unit 2 Containment Air Recirculation Fan, Revision 5 25212-39241, Sht. 189, Emergency Generator Load Sequencing, Rev 8 25212-39622, Sht. 65, Schematic
25 KVA Inverter 125
VDC [[]]
120VAC 1 60
HZ [[, dated 5/09/2006 25212-39427, Sht. 127, Sequencer Electrical Schematic, Revision D 25212-39427, Sht. 118, Sequencer Electrical Schematic, Revision B 25212-39427, Sht. 116, Sequencer Electrical Schematic, Revision B 25212-39427, Sht. 106, Sequencer Electrical Schematic, Revision C B-30869, Seal Piping Schematic, Revision C 25203-211173, Containment Floor Plan, Revision 4 25203-32008, Sht. 54, Minimum Flow Isolation]]
SOV [[]]
SI 659 (2-SI-659), Revision 11 Functional, Surveillance and Modification Acceptance Testing
EN 21063A, Rectangular Duct Traverse Data Sheet,
CAR Fan F14A Slow Speed, dated 11/10/12 3622.2-2, Comprehensive pump test results for
FWA P1B, performed 11/10/14
SP 3626.3-017, Service Water Train 'A' Valve Position Verification Test, performed 10/28/14
SP 3606.1,
RSS Pump
3RSS *P1A Operational Readiness Test, performed 11/2/14
SP 3608.2, Safety Injection Pump B Quarterly IST Pump Test, performed 1/7/15
SP 3604A.4, 3
CHS *P3C Biennial
IST Comprehensive Pump Test, performed 10/17/14
SP [[]]
3604A. 3, 3
CHS *P3C Quarterly
IST Pump Test (Two Charging Pumps Aligned for Service), performed 3/11/15
SP 2612A-003, A Service Water Pump and Facility 1 Discharge Check Valve
IST , performed 1/19/15
SP 2612A-005, A Service Water Pump Comprehensive Pump Test, performed 11/1/14
3SWP *
MOV 71A Open and Closed Stroke Time Results, performed 2011 through
2015 SP 2612D, 2-
SW -3.2A, 2-SW-178C, 2-SW-97B, 2-SW-89B, 2-SW-231B, Stroke and Timing
IST , performed 12/7/14
SP 2403BB, Facility
2 ESAS [[]]
UV ,
RSST and Sequencer Calibration and Functional Test, performed 4/20/15
SP 2403BA, Facility
1 ESAS [[]]
UV ,
RSST and Sequencer Calibration and Functional Test, performed 4/7/15
SP 2613H-001, Facility
2 ESF Integrated Test Data Sheet, performed 4/29/14
SP 2613G-001, Facility
1 ESF Integrated Test Data Sheet, performed 10/11/12

SP2613G-001, Facility 1 ESF Integrated Test Data Sheet, performed 4/7/14

Attachment

MPS -2 A
SW Pump and Motor
IST Data, from 2/2/11 through 1/19/15
MPS -2 C
RBCCW Pump and Motor
IST Data, from 1/11/11 through 2/23/15
MPS -3 B
SIH Pump and Motor
IST Data, from 2/9/11 through 1/7/15
MPS -3 C
CHS Pump and Motor
IST Data, from 1/11/11 through 12/13/14 3626.4-1, Quarterly Pump Test for
SWP P1A, performed 3/17/15 3622.2-1, Quarterly pump test results for
FWA P1B, performed 1/26/15
EN 31154, External Tank Inspection Data Sheet, performed 2/17/14 M30406056,
RSS Heat Exchanger
3RSS -E1A Inspection, performed 4/23/04
OP 2308,
HPSI System Valve Alignment, Facility 2, performed 4/29/14
SP 3646A.15-001, Train A
ESF with
LOP Test, performed 10/24/14
SP 2604
AO ,
HPSI Pump Inservice Testing, performed 1/22/14
SP [[]]
2604AR ,
HPSI Comprehensive Pump Testing, performed 4/11/14
SP 3606.8,
RSS Valve Stroke Time Test - Train 'A,' performed 3/11/15
SP 3626.3-016,
EGLS 'A'
3SWP *71A Output Relay Test, performed 12/22/14
SP 3626.3-019,
3SWP *71A,
TPCCW [[]]
HX [[]]
SW Supply, Stroke Test, performed 12/26/14
SP 3646A.15, Train 'A' Loss of Power Test, performed 10/27/14
SP [[]]
3646A. 17, Train 'A'
ESF with
LOP , performed 10/12/11 and 10/27/14
SP [[]]
3646A. 18, Train B
ESF with
LOP Test, performed 10/11/11 and 4/16/13
SP 3670.1, Mode 1 - 4 Weekly Control Room Rounds, dated 3/28/15, 4/4/15 and 4/11/15
SP 2611B-002, C
RBCCW Pump
IST , performed 2/23/15
SP 2611B-003, C
RBCCW Comprehensive Pump Test, performed 2/4/15 Miscellaneous 120062C, 120 Vac Electrical Distribution, Revision 5 14210106/9, Letter, Sulzer Pumps to Northeast Utilities Energy Co.,
RSS Pump Seals, dated 1/9/98 282-025-001, Letter,
MPR Assoc. to Northeast Utilities Energy Co.,
RSS Pump Seals, dated 12/12/97 7604-E-4, Technical Specification for Metal Clad Switchgear, Revision 7 7604-E-6, Specification for 480 V Load Center Unit Substations, Revision 5 7604-M-501, F14 Fan Data Sheet, Revision
2 CM -M3-
STI -101, Att. 1, Technical Specification Surveillance Test Interval List, Revision
3 DCN [[]]
DM 2-00-0061-07,
RBCCW Pump Lube Oil Bubbler Volume Increase (Seismic Report Only), Revision 0
MP 2-10-01106, Removal of Bus 24G, Revision
11 DM 3-00-0019-13, Correction of Cover Gasket Part Number for 3
EGO *STR2A/2B, dated 2/26/13
DM 3-00-0028-13, Torqueing Technique, Diesel Exhaust Valve Cage Hold-Down Nuts, dated 2/27/13

DM3-00-0053-14, Diesel VTM Update for Air Start Check Valve Styles, dated 10/6/14 Dominion Cable Schedule (Millstone), dated 4/16/15 Dominion System Health Stacked Report, Q4, 2013

Dominion System Health Stacked Report, Q4,

2014 EPRI [[]]
TR 3002000557, Aging Management Program Guidance for Medium Voltage Cable Systems for Nuclear Power Plants, Revision
1 ER -96-0362, Seismic Concern For Buckets on
MCC & 480 V Swgr. When Left In-Out Position, Revision
0 ETE -
CEE -2015-1005, Response to
CR 577517 for Unit 2

CAR Fan F14C, dated 4/24/15 Hayward Tyler Memo, Millstone Unit 3 Intake Structure Level Requirements, dated 12/7/90

Attachment Hayward Tyler Memo, Millstone Unit

3 NPSHR 24
VSN Pumps, dated 9/2/92
IEEE Std. 400.2,
IEEE Guide for Field Testing of Shielded Power Cable Systems Using Very Low Frequency (VLF) (less than 1 Hz), dated
2013 IEEE /
ANSI C37.010,
IEEE Application Guide for
AC High-Voltage Circuit Breakers, dated
2005 IEEE /
ANSI C57.140,
IEEE Guide for the Evaluation and Reconditioning of Liquid Immersed Power Transformers, dated 2006
IEEE /ANSI C57.94,
IEEE Recommended Practice for Installation and Maintenance of Dry Type Power Transformers, dated 1982
IHE -00-C, In-House Electrical System, Revision
9 ISO -
NE , Att. C, Nuclear Plant Transmission Operations - List of
NPIR s, Revision 17.1 LaSalle Hydraulic Laboratory Hydraulic Model Study of the Circulating Water Pump Installation, dated June 1982 M3-
EV -970195, Short Circuit Performance of 4/0 Aluminum Cable above 240 deg. C, dated 11/26/97 Maintenance Rule Basis Document (MP2
HPSI ), dated 9/5/08 Maintenance Rule Basis Document (
MP 3
RSS ), dated 3/18/13 Maintenance Rule Basis Document (
MP 3
SW ), dated 9/12/08
MP 2 Response to
RAI Regarding Resolution of Issues Related to
NRC Generic Letter 96-06, dated 1/12/99
MP 2-14-01061, Increase 2-
SW -231A/B Closing Stroke Time, dated 7/29/14
MP 3-
DE -97-1644, Letter, Northeast Nuclear Energy to Sulzer-Bingham,
RSS Pumps, dated 12/18/97
NCR 398-047, Drawing Requirements vs. Actual Machined Components, dated 3/8/98
PDS 9906, Final Results For the Simulated Life Cycle Management Evaluation of D6A15A1 Grease in Magne-Blast Circuit Breakers, dated 5/11/99
SAR 001947, Inservice Testing Program, Pumps and Valves, dated 10/18/12 Specification No. 2412.300-253, Insulated 1,000 V Power cable, dated 11/16/73 Specification Number 7604-M-506, Containment and Safeguards Ductwork, Revision
9 SP -
ME [[-668, Millstone Unit 2 - Piping Class Sheets, Revision 6 System Health Report, Q4-2014, Millstone Unit 2 - 2326A Service Water System Health Report, Q4-2014, Millstone Unit 2 - 2330A Reactor Building Component Cooling Water System Health Report, Q4-2014, Millstone Unit 3 - 3304A, B, C, 3330D Chemical and Volume Control System Health Report, Q4-2014, Millstone Unit 3 - 3308, 3308E High Head Safety Injection (SIH) Operating Procedures]]
AOP 2580, Degraded Voltage, Revision 003-06
AOP 3560, Loss of Service Water, Revision
9 AOP 3577, Loss of Normal and Offsite Power to "A" 4.16 kV Emergency Bus, Revision 002-01
EN 31173, Refueling Water Storage Tank or Boron Recovery Tank Silica Cleanup using Reverse Osmosis, Revision 002-00
EOP 2532, Loss of Coolant Accident, Revision 031-01
EOP 2536, Excess Steam Demand, Revision 26
EOP 2541, Appendix 18, Simultaneous Hot and Cold Leg Injection, Revision 000-01
EOP 2541, Appendix 7,
TDAFW Pump Abnormal Startup, Revision 000-01
EOP 2541, Appendix 9, Aligning Firewater to
AFW , Revision 000

EOP 35 - E-0, Reactor Trip or Safety Injection, Revision 029

Attachment

EOP 35 -
ES -1.3, Transfer to Cold Leg Recirculation, Revision
016 EOP 35 -
GA -4, Transfer
AFW Pump Suction and Fill
DWST , Revision
1 EOP 3501, Loss of All
AC Power, Revision 014-06
OP 2201, Plant Heatup, Revision 033-07
OP 2313A, Containment Air Recirculating and Cooling System, Revision
9 OP 2347A, Reserve Station Service Transformer, 15G-22S, Revision 011-02
OP 3306, Containment Recirculation Spray System, Revision
009 OP 3322,
AFW System, Revision
21 OP 3326, Service Water System, Revision 24
OP 3346A, Emergency Diesel Generator, Revision 025-06
OP -
AA -102, Operability Determination, Revision
12 OP -
AA -102-1001, Development of Technical Basis to Support Operability Determination, Revision
9 SP 3646A.18, Train B
ESF With
LOP Test, Revision 019-02
SP [[]]
3646A. 2, Emergency Diesel Generator "B" Operability Test, Revision 019-07

SP 3670.1, Control Room and PEO Surveillance, Revision 012-09

Procedures C

PT 1407A,
AMETEK Inverter Meter Calibration, dated 4/10/07 C
PT 1410, 5kV and 8 kV Cable Tests, Revision 001-03 C
PT 1410A,
VLF (Very Low Frequency)
AC Hi-Pot Testing, Revision 001-004 C
PT 1411B, Load Center Transformer Test, Revision 001-01
CM -AA-STI-101, Risk Informed Technical Specification Surveillance Frequency Control Program, Revision
1 CM -M3-
STI -101, Att. 1, Surveillance Frequency Control Program, Revision 3 EN 31084, Operating Strategy for Service Water System at Millstone Unit 3, Revision 7
ER -
AA -CBL-103, Evaluation and Testing of Medium Voltage Cables, Revision
2 ER -
MP -BDB-FLD-1, Beyond Design Basis Project, Walkdowns of Flood Protection and Mitigation Features, Revision
1 IC 3471A01,
SBO [[]]
UPS Testing, Revision 002-03
MP 2701J-092G, Dampers and Blowout Doors, Revision
1 MP 2703A5, Unit 2 Service Water Pump Overhaul, Revision 014-01
MP 2703B5, Reactor Building Closed Cooling Water Pump Overhaul, Revision 010-04
MP 2720D8,
CAR Fan Overhaul, Revision
4 MP 2721C, Protection and Restoration of Service Water Pump and Strainer Motor During a Postulated Maximum Hurricane, Revision 008-02
MP 3470KA, Service Water Pump Maintenance, Revision 3
MP 3718
AB , Repair of Bonnet Type Gate and Globe Valves, Revision 005-07
MP -24-
BKR -REF00, Circuit Breaker Maintenance Program, Revision
6 MP 3781
AH , Calibration Check/Calibration of Vital
AMETEK , Revision 001-02
PI -AA-100-1007, Operating Experience Program, Revision
12 SP 2604
AO ,
HPSI Pump In-Service Testing, Revision 002-02,
SP [[]]
2604AR ,
HPSI Comprehensive Pump Testing, Revision 001-04
SP 2625A,
LPSI Injection Valve Operability Test, Revision 000-01
SP 3443E20, Train B
ESFAS Time Response, Revision 001-01
SP 3448E12,
EGLS Auto Test Train B, Revision 000-02
SP 3448E41, Train B - Diesel Sequencer Actuation Logic Test, Revision 005-01

SP 3448E52, Diesel Sequencer Train B Actuation Timer Test, Revision 004-03

Attachment

SP 3606.1, Containment
RSS Pump
3RSS *P1A Operational Readiness Test, Revision 015-08
SP 3626.3, Service Water Train B Valve Position Indication Verification Test, Revision 001-04
SP 3646A.15, Train 'A' Loss of Power Test, Revision 018-02
SP [[]]
3646A. 17, Train 'A'
ESF with
LOP , Revision 018-02
SP 3446C01,
AMSAC Calibration (
ATWS Mitigation System Actuation Circuitry), Revision 003-03
SP 3446C11,
AMSAC Operability Test (ATWS Mitigation System Actuation Circuitry), Revision
003 SP -M2-
EE -332,
MP 2 Environmental Conditions for Equipment Qualification, Revision 5
SP [[-M3-EE-269, Electrical Design Criteria, Revision 3 W3-517-981RE, Millstone 3 Emergency Operating Procedure (EOP) Setpoint Documentation, Revision 9 Vendor Technical Manuals 252030815-003, Installation, Operation and Maintenance of Reactor Containment Fans and Coolers, Revision 5 25203-365-011, Installation, Operation and Maintenance of]]
HPSI Pumps, Revision 3 25212-044-001, Installation, Operation and Maintenance of Containment Recirculation Pumps, Revision 6 25212-164-001A, Installation and Service Manual, Pratt
MKII Rubber Seat Butterfly Valve, Revision 0 25212-676-001, Limitorque
SMB /
SB Series, Installation and Maintenance, Revision 10 25215-056-002,
AMETEK Solid State Controls Instruction/Technical Manual for Inverters, Revision 2 Brochure 12-1029, C&D Technologies High Rate Max Valve Regulated Lead Acid Battery Brochure 12-120, C&D Technologies
UPS Valve Regulated Lead Acid Battery
GEH -1753J, Time Overcurrent Relays
GEH -1788L, Time Overcurrent Relays
GEI -90890A,
AKD -5 PowerMaster Low Voltage Drawout Switchgear
GEK -34053G, Time Overcurrent Relays
GEK -34054H, Time Overcurrent Relays
GEZ -6105, Specs - Type
AM Power Circuit Breaker
IBXFI -00,
ABB Instruction Bulletin, Installation/Maintenance Instructions, Indoor Dry Type Transformers
IPS -927, Conax Design Qualification Report For Electric Penetration Assemblies, Revision B Vendor Technical Manual, Assembly and Disassembly Instructions for

NOVA 90 H-2 Series Actuator, Revision 1

Work Orders M398-02773 53M20704526 53M20608738 53M20608739 53M20707131 53M30704152 53M30711716 53M20706137 53M30707783 53M30707784 53M20603819 53M20604145 53M20608738 53M20805888 53M30402412 53M30407267 53M30505735 53M30600960 53M30804628 53M30112160 53M30703941 53M20608731 53M20805762 53M30741820 52102476775

53102239224 53102258576 53102291633 53102292008 53102292021 53102292025 53102292287 53102293198 53102293895

53102341598 53102341721 53102341972 53102343959 53102356674

53102428628

Attachment 53102428644 53102431095 53102431419 53102431605 53102468528

53102471726 53102472248 53102475480 53102475817 53102477128

53102477811 53102480484

53102497034 53102575801

53102576950 53102586738 53102592183 53102597292 53102602203

53102629898 53102630848 53102633000 53102633254 53102638516 53102659590 53102691543 53102739170 53102759184

53102763807 53102767039 53102774564

53102780448 53102795379 53102816030 53192431605 53520707359

LIST [[]]
OF [[]]
ACRONY [[]]
MS [[]]
AC Alternating Current
ADAMS Agencywide Documents Access and Management System
AFW Auxiliary Feedwater
ALARA As Low As Reasonably Achievable
ANSI American National Standards Institute
AOV Air Operated Valve
CAR Containment Air Recirculation
CCW Component Cooling Water
CDBI Component Design Bases Inspection
CFR Code of Federal Regulations
CR Condition Report
DBA Design Basis Accident
DBD Design Basis Document
DC Direct Current
DRP Division of Reactor Projects
DRS Division of Reactor Safety
DWST Demineralized Water Storage Tank
EDG Emergency Diesel Generator
HRA Human Reliability Assessment
IEEE Institute of Electrical and Electronics Engineers
IMC Inspection Manual Chapter
IN Information Notice
IP Inspection Procedure
IST In-Service Test kV Kilovolt
LCO Limiting Condition of Operation
LERF Large Early Release Frequency
LLOCA Large Break Loss of Coolant Accident
MOV Motor Operator Valve
NCV Non-cited Violation
NPSH Net Positive Suction Head
NRC Nuclear Regulatory Commission
NSST Normal Station Service Transformer
OE Operating Experience

PRA Probabilistic Risk Assessment

Attachment

RAW Risk Achievement Worth
RBCCW Reactor Building Component Cooling Water Rem Roentgen Equivalent Man
RRW Risk Reduction Worth
RSS Recirculation Spray System
RSST Reserve Station Service Transformer
SDP Significance Determination Process
SLIV Severity Level
IV [[]]
SPAR Standardized Plant Analysis Report
SRA Senior Reactor Analyst
SSC Structure, System and Components
SW Service Water
TDH Total Dynamic Head
TS Technical Specification
UFS [[]]
AR Updated Final Safety Analysis Report Vac Volts, Alternating Current