IR 05000244/1994008

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Insp Rept 50-244/94-08 on 940328-0401.No Violations Noted. Major Areas Inspected:Personnel Exposure Control & Exposure Reduction Techniques Employed During Spring 1994 Refueling Outage at Ginna NPP
ML17263A646
Person / Time
Site: Ginna Constellation icon.png
Issue date: 05/03/1994
From: Bores R, Noggle J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17263A645 List:
References
50-244-94-08, 50-244-94-8, NUDOCS 9405180041
Download: ML17263A646 (12)


Text

Report No.

Docket No.

License No.

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

5~II-

-08 50-244 DPR-18 Licensee:

Rochester Gas and Electric Co oration 89 East Avenue Rochester New York 14649 Facility Name:

Inspection At:

Robert E. Ginna Nuclear Power Plant Ontario New York Inspection Conducted:

March 28-A ril 1

4 Inspector:

J. N Approved by:

~/oalry R. Bores, ef, Facilities Radiation date Protection Section, Division of Radiation Safety and Safeguards d:

A M

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d exposure reduction techniques employed during the Spring 1994 refueling outage at the Ginna Nuclear Power Plant.

Results: 'The licensee's radiation protection organization performed effectively in providing the necessary job coverage radiation safety oversight of outage activities.

Some improvements were noted in the as low as is reasonably achievable (ALARA)program with continuing support from the engineering organization noted.

Also, the internal dosimetry tracking process was cumbersome and considered a weakness.

No safety concerns or violations of NRC regulatory requirements were identified during the inspection.

940S180041 940506 PDR ADOCK OS000244

PDR

DETAILS 1.0 ivi l

n h

r a

n Elec ri i n

~ S. Adams, Superintendent Support Services

  • T. Alexander, Manager, Nuclear Assurance
  • J. Bement, Radiation Protection Operations Lead Technician

~ A. Harhay, Manager, Radiation Protection and Chemistry N. Kiedrowski, Senior Instructor, Radiation Protection

  • K. Lang, Health Physicist

~ F. Mis, Health Physicist

~ J. St. Martin, Director, Operating Experience

  • R. Watts, Corporate Radiation Protection

~ J. Widay, Plant Manager 1.2 P r nnel

.o T. Moslak, Senior Resident Inspector

~ Denotes attendance at the exit meeting on April 1, 1994.

Qnyo~g This inspection was an announced safety inspection of the Ginna Nuclear Power Plant radiation control program during the Spring 1994 refueling and maintenance outage.

3.0 1 I ifi Im I

In rFII I m 244-2-2 The licensee had identified two instances where faulty valve lineups resulted in the inability of the licensee to obtain containment air and containment recirculation fan condensate samples.

The NRC inspector requested a licensee review of radiation protection sampling procedures to evaluate the need for more specific valve lineup instructions to preclude other similar events from occurring.

The licensee completed this review and revised the instruction accordingly.

The inspector reviewed the revisions.

Procedure PC-24, Rev. 14, describes the liquid sampling setup requirements.

This procedure has been revised to include specific valve numbers and the discrete steps necessary to perform the liquid sampling.

Signoffs were included to indicate that correct valve lineups were completed.

Allliquid sampling procedures, including the containment air condensate sampling procedure, were revised to incorporate reference to Procedure PC-24 for proper valve lineups.

These revisions have also been incorporated into the training program.

This item is now close.0 r

ni n

The licensee's radiation protection organization normally consists of 30 personnel of whom 6 were long-term contractors.

During this outage, an additional 61 contract HP personnel were hired.

The HP staff was supervised by 8 RG&B HP technicians to provide 24-hours/day leadership over the contract HP technician workforce.

Adequate manpower resources were available to accomplish the outage activities in a safe manner.

The previous HP Operations Foreman retired and was replaced by a fullyqualified HP lead technician who had previous experience writing special work permits (SWPs)

and supervising HP technicians.

No deficiencies with regard to radiation safety personnel resources were noted.

5.0 T inin lifi n

The licensee has issued an incentive-based three-year contract for HP technician services.

This new initiative implemented for this outage willinclude the 1996 steam generator replacement outage.

The HP contractor was asked to propose a percentage of the contract for performance-based adjustment based on the utilityevaluation report developed after each outage.

The "at risk" percentage could be increased or decreased by 100% depending on the performance rating.

The categories to be rated include: HP technician performance, budget, coordination, and schedule parameters.

Negative incentive would come out of the contractor company's profit margin.

Positive incentive would be directed to both the contractor company and the HP technicians.

This is viewed as a good initiative that encourages high performance and penalizes the contractor company for poor performance.

The inspector reviewed selected contractor resumes and training qualifications to ensure the minimum requirements of ANSI 18.1-1971 were met for HP technicians responsible forjob coverage and the radiological protection of the workers.

In all cases, the criteria were met.

No discrepancies were noted.

The contractor HP training program was accomplished in one week beginning with an initial HP screening examination provided through the Middle Atlantic Nuclear Training Group (MANTG). Successful completion of this examination was indicated by achieving greater than or equal to 80%.

The licensee provided a second chance for a technician who failed the examination by offering the technician an opportunity to pass another test version.

Two test failures resulted in rejection of the HP technician from employment.

One individual was rejected due to this reason.

The licensee also accepts successful test results within a two-year period from another MANTGparticipating utility. Also, ifan individual is certified by the National Registry of Radiation Protection Technologists (NRRPT), the screening examination requirement is waived.

After completion of the initialHP screening examination,

16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> of classroom training was provided on site specific HP procedures.

Job coverage related on the job training (OJT) signoffs were required within a 30-month period to complete the HP technician qualification program.

The inspector reviewed select HP contractor personnel and verified that the above training requirements were completed.

In general, the contractor HP technician training appeared to be adequate.

6.0 i 'ni n

The inspector reviewed the licensee's radiological incident reports (RIRs) to evaluate management oversight of radiological events at the station.

The licensee recorded eight RIRs for 1994.

There were two incidents that had potential safety significance relative to high radiation area entry.

These involved the non-issuance of alarming dosimeters for high radiation area entries.

In one case, there was no actual high radiation area present although the entrance to the "A" reactor coolant system loop area was conservatively posted as a high radiation area.

The posting was precautionary since the radiation levels in this area were dependent on changes in the steam generator water level.

The HP staff was cognizant of the steam generator water level and the radiation levels at the time of the event.

In the other case, constant HP coverage was provided for entry into an RCS loop area, meeting the Technical Specification requirement for high radiation area entry.

The special work permit (SWP), however, required issuance of alarming dosimeter without specifying constant HP coverage.

The inspector reviewed with the licensee the conditions surrounding each event and was satisfied that in each case, the licensee exercised control over the areas.

However, attention to detail with regard to postings and improvements in SWP briefings was needed.

The licensee had made these assessments, improved radiological postings, and reinforced with the HP staff, the need to verify SWP compliance prior to the beginning of work.

The inspector noted a contributing problem with regard to proper issuance of alarming pocket dosimeters.

At the alarming dosimeter issue point, the HP staff was not checking the SWPs to ensure who was required to have an alarming dosimeter and who had one for data comparison purposes only. The staff health physicists stated that with the adoption of the new access control system, scheduled for Pall of 1994, everyone entering the RCA would be issued an alarming dosimeter and this contributing problem willno longer be a concern.

The other RIRs recorded minor station radiological occurrences of low safety significance.

The inspector determined that the licensee's review of the RIRs was thorough and effective actions have been implemented to prevent recurrences.

In general, the licensee had a low frequency of safety significant radiological events.

Management oversight of radiological problems was effectiv o xrR io The licensee reported 193.1 person-rem for 1993, which included 156 person-rem for the 1993 refueling outage.

This compares favorably with the previous three years:

347 person-rem for 1990; 328 person-rem for 1991; and 261 person-rem for 1992.

Compared with other U.S. pressurized water reactors (PWRs), the annual exposure history at Ginna remains higher than the average.

For 1994, the licensee estimates 160 person-rem with a goal of 140 person-rem from outage exposures.

At the time of this inspection (day 28 out of a 39-day scheduled outage), the licensee had accumulated 104.2 person-rem versus the pro-rated estimate of 114.6 person-rem.

The licensee's station exposures have demonstrated a good moderately downward trend.

The permanent ALARAgroup staff includes a staff Health Physicist and an ALARA technician.

During the preparation and performance of this outage, the HP Department provided additional staffing for the ALARAgroup to include three ALARAtechnicians while upgrading the permanent ALARAtechnician to a lead ALARAtechnician position. In addition, field engineering supplied part-time assistance of an engineer for the second consecutive outage to support the shielding requests generated by the ALARAgroup.

Noted improvements in the ALARA performance were observed during this inspection.

The use of permanently installed lead shielding was noted inside of the containment vessel.

Both the regenerative heat exchanger and the pressurizer spray line had been shielded with heat resistant Amertex lead blankets that were approved for use during containment operating conditions.

This allows for elimination of the installation and removal resources associated with the temporary outage shielding approach and can also be of benefit during routine containment power entry inspections.

The ALARAshield package format was completely revised and greatly improved over the previous outage, Previously the shield packages measured contact dose rates and did not focus on the work area dose rate reduction.

The latter is applicable to the reduction of personnel exposures while performing work. The inspector noted that now each shield package contained a dose rate goal for the shielding that reflected near background values.

Therefore, ifthe initial shield design did not meet the stated shield package goal, further shielding efforts could be made to ensure fullexposure reduction potential was attained.

This was an improved approach over that used during previous outages.

The inspector reviewed all twelve shield packages utilized during the outage.

They included:

"A" sump and incore detector area, pressurizer spray line, top of pressurizer block valves, a valve located on the "B" RCP platform,

"B" crossover piping, reactor head thermocouples and conoseal area, general purpose moveable shield racks, regenerative heat exchanger, primary sample delay coil, steam generator hand holes, and an auxiliary building drain line. The approved shield design packages were worth approximately 9,000 pounds of shielding that was

estimated to save up to 68 person-rem.

The actual shielding used and actual exposure savings attained would be expected to be somewhat lower than these ideal values, however, this does provide an indication of a moderate level of effort and performance of the ALARAgroup in reducing outage personnel exposures.

The ALARAgroup has developed an outage exposure tracking system based on the Plan-A-Log outage schedule.

This schedule provided estimated exposure tracking as a function of the scheduled work during the outage.

This was an improvement over the previous straight-line estimation as a function of time previously used, which estimated the exposure for the outage and assumed a straight line accumulation with time throughout the outage.

The new method accounts for the timing of various specific jobs and reflects the estimated exposure expenditures for each day.

The actual exposure expenditures were tracked and compared to the estimate to determine ifoverall personnel exposures were remaining ALARA.

The inspector questioned the accuracy of tracking actual exposures against the originally scheduled exposures, when actual work completion varies from the original schedule.

gf the workscope did not follow the original schedule, but was worked more slowly or more quickly, then the exposure accumulation would not be expected to follow the original exposure estimate schedule.) Ifthe Plan-A-Log outage schedule tracking, which reported the actual completion status of each job on a shiftly basis, was also to the exposure tracking estimate, schedule variations could be accomodated in the tracking to provide accurate comparisons of work completed versus exposure expended.

This would allow for the timely identification and correction for exposure overruns.

Notwithstanding, the inspector determined that the current ALARA estimation and tracking method was very good and provided a good measure of exposure oversight during this outage.

The inspector reviewed ALARAProcedure RP-ALA-Shield, Rev. 0, "Control of Temporary Lead Shielding".

This procedure provided an acceptable methodology for the safe application of temporary shielding on plant systems.

Opportunity exists to expand the scope of this procedure or develop additional procedures to include the analysis of exposure reduction possibilities and include cost versus benefit analysis evaluations.

Improvement in these areas would provide better formulation of exposure reduction problems for engineering evaluation and allow the licensee to make appropriate resource commitments based on defensible ALARAdecisions.

The inspector also reviewed Procedure A-1.6.1, Rev. 16,"ALARAJob Reviews".

This procedure indicates the various review levels required based on the exposure estimated to complete a job. This procedure requires worker attendance at ALARA prejob review briefings for jobs expected to result in significant exposure.

The inspector questioned the licensee as to how work was controlled so that only workers who attended the ALARAprejob briefing were allowed to work on a SWP.

The staff Health Physicist indicated that there was currently no mechanism to ensure attendance

at an ALARAprejob briefing was met.

However, the staff Health Physicist indicated that the alarming dosimeter computer network software under evaluation could provide this capability and stated that this provision would be considered during dosimetry system development and implementation.

In general, the inspector determined that steady improvements have been made in the ALARAprogram performance, but areas for growth still exist in meeting the exposure reduction challenges of Ginna Station.

8.0 x

r nr

The inspector reviewed the major outage work areas of the plant and made the following observations.

The refueling cavity was successfully decontaminated (a previous weakness) through a vendor-supplied hydrolasing service, although occasional airborne radioactivity areas resulted during the outage.

This allowed the reduction in respirator use for most of the refueling activities.

In addition, stairs were installed in the cavity to allow safer access for cavity workers than the conventional vertical ladder.

Alarming pocket dosimeters were issued to all high radiation area workers as well as select work groups of the outage workforce.

The licensee was collecting data to compare with pocket ion chamber data and thermoluminescent dosimeter data.

After the ALNOR alarming dosimeters are evaluated, they willbe used for all workers entering the radiological controlled area (RCA) and the pocket ion chamber use will be discontinued.

This is expected to occur during the Fall of 1994.

Radwaste minimization has been effective.

Launderable tarpaulins, cloth bags, and rags have replaced herculite, plastic bags and masslin cloths.

Reusable pressurized spray cans were used for dispensing a decontamination solvent instead of the throw away aerosol cans.

In 1993, 15,000 ft'fradwaste was generated which resulted in 1,600 ft'isposal volume after segregation and incineration.

During steam generator nozzle dam removal, the inspector noted that the audio/video communications allowed for excellent coverage of manway entries.

The entire steam generator platform was not monitored by the video monitors, however, and the platforms were controlled as high radiation areas and the SWP required continuous HP coverage of this area.

During the nozzle dam removal work, three workers were on the platforms and the inspector noted that the video cameras did not provide coverage of all workers.

The RPM agreed that this area could be improved.

Another area for improvement involved the difficultyof installing the steam generator manway inserts.

These heavy steel plates were manually lifted to slightly above shoulder height.

This activity had to be repeated several times with some degree of difficulty during this outage because of alignment difficulties and lack of an appropriate

lifting/alignment device.

These constitute minor improvement possibilities that could be made, however, Ginna continues to provide a very successful steam generator maintenance program.

The HP training staff was temporarily rotated into HP positions during the outage performing the following duties:

sample counting, SWP review, dosimetry, and CO, blast decontamination coordinator.

This was in response to a previous INFO finding that reported a gap between the training curriculum and the actual HP plant practices.

The HP control points were well staffed to coordinate and provide oversight of outage activities. A good level of surveys and job coverage oversight was maintained.

An adequate level of air samples (approximately 30) were taken per day during the outage with a relatively high number of airborne radioactivity results associated with the refueling cavity work area, steam generator maintenance, and pressurizer component maintenance.

Appropriate respiratory protection of the workers was generally prescribed for this work, however the high number of airborne radioactivity air sample results provided a significant demand on the internal dosimetry tracking program.

The current internal dosimetry tracking program involved correlation of high activity air sample data with SWP sign-in sheet entry times to establish air sample based intake assignments.

This manual correlation and calculation required the dosimetry staff and operational HP staff to separately provide their reviews followed by a senior level health physicist to review and approve the completed internal dosimetry tracking package for each completed SWP.

This method of tracking was not always accurate and not timely with respect to outage requirements.

This tracking system was previously reported as being inaccurate and not current in a previous inspection report. At that time, the inspector pointed out inaccuracies in the air sample calculations and numerous transcription errors in the various forms used.

The licensee has improved the accuracy of air sample calculations with the institution of a computer program to provide this function. The rest of the manual administrative internal tracking system remains weak to meet current outage demands.

This is viewed as a process weakness.

The licensee stated that the tracking system process would be reevaluated and appropriate changes to improve its accuracy and timeliness would be made.

'RC Inspection No. 50-244/92-05, conducted on April27 - May 1, 1992

Ini i ve The design of a new improved personnel access to the restricted area has been approved.

This new design is intended to economize the personnel travel path and increase the accessibility for HP interface for all personnel entering the radiological controlled area of the plant.

The reconstruction of the existing plant space is expected to be completed by the end of 1994.

The current design was reviewed by the inspector and was viewed as an improvement and a good initiative.

The radiation protection and chemistry procedure upgrade project was begun in 1993 and was expected to revise all of the subject procedures (approximately 400) during a three-year period.

The upgrade project was to bring the procedures in line with a substantially revised and improved procedure writer's guide.

During 1993, all of the radiation protection and chemistry staff were trained on the new procedure writer'

guide and 34 procedures were rewritten to satisfy the new 10 CFR 20 requirements.

In 1994, 137 procedures are currently targeted for revision.

This procedure upgrade project is viewed as a good initiative. The inspector willreview the revised procedures in future inspections.

lD.D The inspector met with licensee representatives at the end of the inspection, on April 1, 1994.

The inspector reported the inspection results and the licensee acknowledged the inspection findings.