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Category:Inservice/Preservice Inspection and Test Report
MONTHYEARRA-23-0011, End of Cycle 24 (H1R24) Inservice Inspection Program Owner'S Activity Report2023-01-26026 January 2023 End of Cycle 24 (H1R24) Inservice Inspection Program Owner'S Activity Report RA-22-0172, Duke Energy Progress, LLC - Supplement to Relief Request HNP-IST-004-RR1 for Inservice Testing Program Plan - Fourth Ten-Year Interval2022-06-10010 June 2022 Duke Energy Progress, LLC - Supplement to Relief Request HNP-IST-004-RR1 for Inservice Testing Program Plan - Fourth Ten-Year Interval RA-21-0200, End of Cycle 23 (H1R23) Inservice Inspection Program Owner'S Activity Report2021-08-11011 August 2021 End of Cycle 23 (H1R23) Inservice Inspection Program Owner'S Activity Report RA-21-0067, Response to Request for Additional Information - Relief Request, Service Water Pinhole Leak in a Socket Weld, Inservice Inspection Program, Fourth Ten-Year Interval2021-02-25025 February 2021 Response to Request for Additional Information - Relief Request, Service Water Pinhole Leak in a Socket Weld, Inservice Inspection Program, Fourth Ten-Year Interval RA-20-0082, Submittal of 180-Day Steam Generator Tube Inspection Report2020-04-0808 April 2020 Submittal of 180-Day Steam Generator Tube Inspection Report RA-20-0025, Cycle 22 Owner'S Activity Report2020-02-12012 February 2020 Cycle 22 Owner'S Activity Report RA-19-0206, Proposed Alternative for the Third 10-Year Inservice Inspection Program2019-04-30030 April 2019 Proposed Alternative for the Third 10-Year Inservice Inspection Program RA-18-0066, Cycle 21 Owner'S Activity Report2018-07-31031 July 2018 Cycle 21 Owner'S Activity Report HNP-17-025, Fourth Interval Lnservice Inspection Plan, Third Interval Containment Lnservice Inspection Plan, and Fourth Interval Lnservice Inspection Pressure Test Plan2017-10-23023 October 2017 Fourth Interval Lnservice Inspection Plan, Third Interval Containment Lnservice Inspection Plan, and Fourth Interval Lnservice Inspection Pressure Test Plan HNP-16-092, Relief Request I3R-16, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program, Third Ten-Year Interval2016-10-19019 October 2016 Relief Request I3R-16, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program, Third Ten-Year Interval HNP-15-064, Submits 90-day Inservice Inspection Summary Report2015-08-0505 August 2015 Submits 90-day Inservice Inspection Summary Report HNP-15-037, Relief Request I3R-15, Reactor Vessel Closure Head Nozzle Repair Technique, Response to Request for Additional Information2015-04-24024 April 2015 Relief Request I3R-15, Reactor Vessel Closure Head Nozzle Repair Technique, Response to Request for Additional Information HNP-15-034, Relief Request I3R-15 Revision and Supplement, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program - Third Ten-Year Interval2015-04-15015 April 2015 Relief Request I3R-15 Revision and Supplement, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program - Third Ten-Year Interval HNP-15-010, Relief Request I3R-15, Reactor Vessel Closure Head Nozzle Repair Technique Inservice Inspection Program - Third Ten-Year Interval2015-04-0202 April 2015 Relief Request I3R-15, Reactor Vessel Closure Head Nozzle Repair Technique Inservice Inspection Program - Third Ten-Year Interval HNP-14-099, Relief Request I3R-14, Deferral of Reactor Vessel Inspections Inservice Inspection Program - Third Ten-Year Interval Response to Request for Additional Information2014-09-0808 September 2014 Relief Request I3R-14, Deferral of Reactor Vessel Inspections Inservice Inspection Program - Third Ten-Year Interval Response to Request for Additional Information HNP-13-119, Relief Request I3R-13, Reactor Vessel Closure Head Nozzle 37, Inservice Inspection Program - Third Ten-Year Interval2013-11-22022 November 2013 Relief Request I3R-13, Reactor Vessel Closure Head Nozzle 37, Inservice Inspection Program - Third Ten-Year Interval HNP-13-071, Day Inservice Inspection Summary Report Corrections2013-06-26026 June 2013 Day Inservice Inspection Summary Report Corrections HNP-13-057, Relief Request I3R-11 Reactor Vessel Closure Head Nozzles Lnservice Inspection Program - Third Interval2013-05-22022 May 2013 Relief Request I3R-11 Reactor Vessel Closure Head Nozzles Lnservice Inspection Program - Third Interval HNP-12-091, Day Inservice Inspection Summary Report2012-09-0505 September 2012 Day Inservice Inspection Summary Report HNP-12-018, Day Inservice Inspection (ISI) Summary Report Corrections2012-04-11011 April 2012 Day Inservice Inspection (ISI) Summary Report Corrections HNP-11-045, 180-Day Steam Generator Tube Inspection Report2011-05-0505 May 2011 180-Day Steam Generator Tube Inspection Report HNP-11-017, 90-Day Inservice Inspection (ISI) Summary Report2011-02-10010 February 2011 90-Day Inservice Inspection (ISI) Summary Report HNP-09-095, Response to Request for Additional Information Regarding Relief Requests 2R1-018, 2R1-019, 2R1-020, 2R1-021, 2R1-022, 2R2-009, 2R2-010, & 2R2-011 for the Second 10-Year Inservice Inspection Program2009-09-24024 September 2009 Response to Request for Additional Information Regarding Relief Requests 2R1-018, 2R1-019, 2R1-020, 2R1-021, 2R1-022, 2R2-009, 2R2-010, & 2R2-011 for the Second 10-Year Inservice Inspection Program ML0923103532009-08-27027 August 2009 Correction to 10-Year Inservice Inspection Interval Enumerated in Relief Request 13R-02 Issued on April 30, 2009 HNP-09-076, 90-Day Inservice Inspection (ISI) Summary Report2009-08-0606 August 2009 90-Day Inservice Inspection (ISI) Summary Report HNP-08-067, Supplement to Third Interval Inservice Inspection Relief Request 13R-02 Submittal2008-06-19019 June 2008 Supplement to Third Interval Inservice Inspection Relief Request 13R-02 Submittal ML0804600932008-02-0808 February 2008 RFO13 90 Day Inservice Inspection (ISI) Summary Report ML0813304642008-01-30030 January 2008 Rev. 0 to PEN02.G03, Shearon Harris Nuclear Plant ISI Program Plan, Third 10-Year Inspection Interval. Cover to Page 8-2 ML0813304652008-01-30030 January 2008 Rev. 0 to PEN02.G03, Shearon Harris Nuclear Plant ISI Program Plan, Third 10-Year Inspection Interval. Attachment 1: Welds & Supports Schedule ML0813304662008-01-30030 January 2008 Rev. 0 to PEN02.G03, Shearon Harris Nuclear Plant ISI Program Plan, Third 10-Year Inspection Interval. Page 288 to End HNP-07-179, 90-Day Inservice Inspection (ISI) Summary Report2008-01-18018 January 2008 90-Day Inservice Inspection (ISI) Summary Report HNP-07-145, Inservice Inspection Relief Request 1, Summary of Ultrasonic Examinations of Preemptive Weld Overlays for Pressurizer Nozzle Locations Containing Alloy 600 Materials2007-10-22022 October 2007 Inservice Inspection Relief Request 1, Summary of Ultrasonic Examinations of Preemptive Weld Overlays for Pressurizer Nozzle Locations Containing Alloy 600 Materials HNP-07-143, Inservice Inspection Relief Request 1 Re Weld Overlay Repair Stress Analysis Summary2007-10-19019 October 2007 Inservice Inspection Relief Request 1 Re Weld Overlay Repair Stress Analysis Summary HNP-07-042, Revision of the Relief Request from ASME OM Code Inservice Testing Requirements for the Third Ten-Year Interval Plan2007-03-22022 March 2007 Revision of the Relief Request from ASME OM Code Inservice Testing Requirements for the Third Ten-Year Interval Plan HNP-06-141, Relief Request from ASME OM Code Inservice Testing Requirements for the Third Ten-Year Interval Plan2006-12-18018 December 2006 Relief Request from ASME OM Code Inservice Testing Requirements for the Third Ten-Year Interval Plan HNP-06-091, Relief Requests from ASME Code Inservice Testing Requirements to Allow Online Disassembly of Certain Check Valves2006-09-0707 September 2006 Relief Requests from ASME Code Inservice Testing Requirements to Allow Online Disassembly of Certain Check Valves HNP-06-081, Submittal of Inservice Inspection Summary Report for Harris Nuclear Plant2006-08-10010 August 2006 Submittal of Inservice Inspection Summary Report for Harris Nuclear Plant HNP-05-088, One-Year Special Report - Steam Generator Tube Inservice Inspection Results2005-08-0101 August 2005 One-Year Special Report - Steam Generator Tube Inservice Inspection Results HNP-05-018, Inservice Inspection Summary Report2005-02-15015 February 2005 Inservice Inspection Summary Report HNP-04-076, One Year Special Report, Steam Generator Tube Inspection Results2004-05-0707 May 2004 One Year Special Report, Steam Generator Tube Inspection Results HNP-03-081, Inservice Inspection Summary Report2003-08-13013 August 2003 Inservice Inspection Summary Report HNP-02-051, Part 2 of 2, Shearon Harris Nuclear Power Plant, Inservice Inspection Summary Report, Class 2 Through End2002-04-0101 April 2002 Part 2 of 2, Shearon Harris Nuclear Power Plant, Inservice Inspection Summary Report, Class 2 Through End HNP-01-170, Inservice Inspection Summary Report for Harris Nuclear Plant2002-01-24024 January 2002 Inservice Inspection Summary Report for Harris Nuclear Plant 2023-01-26
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Progress Energy AUG 0 12005 Serial: HNP-05-088 U.S. Nuclear Regulatory Commission ATTENTION: Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT, UNIT NO. 1 DOCKET NO. 50-400/LICENSE NO. NPF-63 ONE-YEAR SPECIAL REPORT STEAM GENERATOR TUBE INSERVICE INSPECTION RESULTS Ladies and Gentlemen:
In accordance with Technical Specification 4.4.5.5.b of the Harris Nuclear Plant (HNP), Carolina Power and Light Company doing business as Progress Energy Carolinas, Inc., provides the attached Special Report, which transmits the results of the steam generator (SG) tube inservice inspections performed during the May 2004 mid-cycle outage. provides the Special Report.
Please refer any question regarding this submittal to Mr. Dave Corlett at (919) 362-3137.
Sincerely, D. H. Corlett Supervisor - Licensing/Regulatory Programs Harris Nuclear Plant DHC/jpy
Attachment:
- 1. Summary of the HNP May 2004 Mid-Cycle Outage Steam Generator (SG)
Tube Inservice Inspection Results C:
Mr. R. A. Musser, NRC Senior Resident Inspector Mr. C. P. Patel, NRC Project Manager Dr. W. D. Travers, NRC Regional Administrator Progress Energy Carolinas, Inc.
\O1' Harris Nuclear Plant P.O. Box 165 New Hill, NC 27562
4 atr mr-z-H~r Attachment 1 to SERIAL: HNP-05-088 SHEARON HARRIS NUCLEAR POWER PLANT, UNIT NO. 1 DOCKET NO. 50-400/LICENSE NO. NPF-63
.; ONE-YEAR SPECIAL REPORT.,,
STEAM GENERATOR TUBE INSERVICE INSPECTION RESULTS Summary of the HNP May 2004 Mid-Cycle Outage Steam Generator (SG) Tube Inservice Inspection Results Technical Specification 4.4.5.5.b of the Harris Nuclear Plant (HNP) requires the complete results of the steam generator (SG) tube inservice inspection shall be submitted in a Special Report within 12 months following completion of the inspection. The Special Report shall include:
- 1. Number and extent of tubes inspected.
- 2. Location and percent of wall-thickness penetration for each indication of an imperfection, and
- 3. Identification of tubes plugged.
The second inservice inspection of the SG following replacement was performed in a mid-cycle outage and completed on May 14, 2004.
- 1. Number and extent of tubes inspected:
SG UC':
Number of Tubes Number of Tubes Extent of Tubes Available for Inspected Inspected Inspection 6,3048 1,268bTube end to opposite
___ ____ ___ ____ ___tu be en d Notes: a. The number of tubes available for inspection accounts for the three tubes that were plugged as noted In Item 3 (Identification of tubes plugged) below.
- b. The number of tubes inspected includes the six tubes inspected as part of the repair due to loose parts damage.
- 2. Location and percent of wall-thickness penetration for each indication of an imperfection:
No recordable eddy current testing (ECT) indications with wall-thickness penetration were identified from the results of this inservice inspection.
Page Al-I of 2
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Attachment 1 to SERIAL: HNP-05-088 SHEARON HARRIS NUCLEAR POWER PLANT, UNIT NO. 1 DOCKET NO. 50-400/LICENSE NO. NPF-63 ONE-YEAR SPECIAL REPORT STEAM GENERATOR TUBE INSERVICE INSPECTION RESULTS
- 3. Identification of tubes plugged:
SG "A":
One tube plugged (pre-service): R106C85 SG "B":
One tube plugged (pre-service): RI 14C73 SG "C":
Three tubes plugged due to loose parts damage (identified prior to performing this inservice inspection): R01 C120, R02C121, and R03C120 Page Al-2 of 2