BYRON 2002-0051, Response to NRC Bulletin 2002-001, Reactor Pressure Vessel Head Degradation & Reactor Coolant Pressure Boundary Integrity.

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Response to NRC Bulletin 2002-001, Reactor Pressure Vessel Head Degradation & Reactor Coolant Pressure Boundary Integrity.
ML021330386
Person / Time
Site: Byron  Constellation icon.png
Issue date: 04/26/2002
From: Lopriore R
Exelon Generation Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
BL-02-001, BYRON 2002-0051
Download: ML021330386 (6)


Text

www.exeloncorp.com Exelon. N uC lear Exelon Generation Company, LLC Byron Station 4450 North German Church Road Byron, IL61010-9794 April 26, 2002 LTR: BYRON 2002-0051 File: 1.10.0101 United States Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001 Byron Station Unit 1 Facility Operating License No. NPF-37 NRC Docket No. STN 50-454

Subject:

Byron Station Unit 1 Response to NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity" On March 18, 2002, the NRC issued NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity." This bulletin requires that the following information be submitted to the NRC within 30 days after plant restart following the next inspection of the reactor pressure vessel head to identify any degradation:

- the inspection scope and results, including the location, size, and nature of any degradation detected; and

- the corrective actions taken and the root cause of the degradation.

Pursuant to 10 CFR 50.54, "Conditions of Licenses," paragraph (f), Attachment I to this letter provides the Byron Station Unit 1 30-day response. This response is due to the NRC by April 29, 2002.

VA

April 26, 2002 U.S. Nuclear Regulatory Commission Page 2 If you have any questions or desire additional information regarding this letter, please contact William Grundmann, Regulatory Assurance Manager, at (815) 406-2800.

Respectfully, ihard P. Lopriore Site Vice President Byron Nuclear Generating Station RPLJMR/dpk

Enclosures:

Attachment 1, Byron Station Unit 1 Response to NRC Bulletin 2002-01 cc: Regional Administrator - NRC Region III NRC Senior Resident Inspector - Byron Station NRC Project Manager - NRR - Byron Station Office of Nuclear Facility Safety - Illinois Department of Nuclear Safety

STATE OF ILLINOIS )

COUNTY OF OGLE )

IN THE MATTER OF EXELON GENERATION COMPANY, LLC ) Docket Numbers BYRON STATION UNIT I STN 50-454

SUBJECT:

Byron Station Unit I Response to NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity" AFFIDAVIT I affirm that the content of this transmittal is true and correct to the best of my knowledge, information and belief.

Aic&"MF:. Lo6p or Site Vice Presiden.

Byron Nuclear Generating Station Subscribed and sworn to before me, a Notary Public in and for the State above named, this (It0 day of OFFIC-'-* :2AL TRACEY L, UCK NOTARY PUBLIC OF ILLINOIS MY cOMMISSION EXPIRES 01/04

ATTACHMENT I Byron Station Unit 1 Response to NRC Bulletin 2002-01 "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity"

Attachment I Byron Station Unit I Response to NRC Bulletin 2002-01 On March 18, 2002, the NRC issued NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Pressure Boundary Integrity." This bulletin requires that the following information be submitted to the NRC within 30 days after plant restart following the next inspection of the reactor pressure vessel (RPV) head to identify any degradation:

2. Within 30 days afterplant restartfollowing the next inspection of the reactorpressure vessel head to identify any degradation,all PWR addresseesare requiredto submit to the NRC the following information:
a. the inspection scope and results, including the location, size, and nature of any degradationdetected,
b. the corrective actions taken and the root cause of the degradation.

Byron Station Unit I Response

a. the inspection scope and results, including the location, size, and nature of any degradationdetected,

Response

The following inspections were performed on the reactor pressure vessel (RPV) during refueling outage 81 R11 in March 2002:

Pre and post-outage VT-2 examinations of the accessible areas on top of the RPV head (i.e., control rod drive mechanism housings) were performed at normal reactor coolant system pressure. No evidence of leakage, boric acid residue, or degradation of material due to corrosion was identified during these inspections.

VT-1 examinations were performed on the core exit thermocouple clamp assemblies. There was no evidence of erosion, corrosion, or wear of the bolting material, and there were no instances of bolting material degradation due to corrosion. These connections, which are disassembled each refueling outage, were specifically examined for leakage by VT-2 qualified personnel during unit startup and no abnormal conditions were identified.

Approximately 20% of the bare metal RPV surface was visually inspected to confirm the inspection results of a previous leak on the reactor head vent valve discovered during refueling outage B1 R03 in 1990; no boric acid accumulation or head wastage was observed.

Page 1 of 2

Attachment I

b. the corrective actions taken and the root cause of the degradation.

Response

There were no corrective actions taken or root cause investigations performed as no RPV degradation was identified.

Page 2 of 2

Text

www.exeloncorp.com Exelon. N uC lear Exelon Generation Company, LLC Byron Station 4450 North German Church Road Byron, IL61010-9794 April 26, 2002 LTR: BYRON 2002-0051 File: 1.10.0101 United States Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001 Byron Station Unit 1 Facility Operating License No. NPF-37 NRC Docket No. STN 50-454

Subject:

Byron Station Unit 1 Response to NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity" On March 18, 2002, the NRC issued NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity." This bulletin requires that the following information be submitted to the NRC within 30 days after plant restart following the next inspection of the reactor pressure vessel head to identify any degradation:

- the inspection scope and results, including the location, size, and nature of any degradation detected; and

- the corrective actions taken and the root cause of the degradation.

Pursuant to 10 CFR 50.54, "Conditions of Licenses," paragraph (f), Attachment I to this letter provides the Byron Station Unit 1 30-day response. This response is due to the NRC by April 29, 2002.

VA

April 26, 2002 U.S. Nuclear Regulatory Commission Page 2 If you have any questions or desire additional information regarding this letter, please contact William Grundmann, Regulatory Assurance Manager, at (815) 406-2800.

Respectfully, ihard P. Lopriore Site Vice President Byron Nuclear Generating Station RPLJMR/dpk

Enclosures:

Attachment 1, Byron Station Unit 1 Response to NRC Bulletin 2002-01 cc: Regional Administrator - NRC Region III NRC Senior Resident Inspector - Byron Station NRC Project Manager - NRR - Byron Station Office of Nuclear Facility Safety - Illinois Department of Nuclear Safety

STATE OF ILLINOIS )

COUNTY OF OGLE )

IN THE MATTER OF EXELON GENERATION COMPANY, LLC ) Docket Numbers BYRON STATION UNIT I STN 50-454

SUBJECT:

Byron Station Unit I Response to NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity" AFFIDAVIT I affirm that the content of this transmittal is true and correct to the best of my knowledge, information and belief.

Aic&"MF:. Lo6p or Site Vice Presiden.

Byron Nuclear Generating Station Subscribed and sworn to before me, a Notary Public in and for the State above named, this (It0 day of OFFIC-'-* :2AL TRACEY L, UCK NOTARY PUBLIC OF ILLINOIS MY cOMMISSION EXPIRES 01/04

ATTACHMENT I Byron Station Unit 1 Response to NRC Bulletin 2002-01 "Reactor Pressure Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity"

Attachment I Byron Station Unit I Response to NRC Bulletin 2002-01 On March 18, 2002, the NRC issued NRC Bulletin 2002-01, "Reactor Pressure Vessel Head Degradation and Reactor Pressure Boundary Integrity." This bulletin requires that the following information be submitted to the NRC within 30 days after plant restart following the next inspection of the reactor pressure vessel (RPV) head to identify any degradation:

2. Within 30 days afterplant restartfollowing the next inspection of the reactorpressure vessel head to identify any degradation,all PWR addresseesare requiredto submit to the NRC the following information:
a. the inspection scope and results, including the location, size, and nature of any degradationdetected,
b. the corrective actions taken and the root cause of the degradation.

Byron Station Unit I Response

a. the inspection scope and results, including the location, size, and nature of any degradationdetected,

Response

The following inspections were performed on the reactor pressure vessel (RPV) during refueling outage 81 R11 in March 2002:

Pre and post-outage VT-2 examinations of the accessible areas on top of the RPV head (i.e., control rod drive mechanism housings) were performed at normal reactor coolant system pressure. No evidence of leakage, boric acid residue, or degradation of material due to corrosion was identified during these inspections.

VT-1 examinations were performed on the core exit thermocouple clamp assemblies. There was no evidence of erosion, corrosion, or wear of the bolting material, and there were no instances of bolting material degradation due to corrosion. These connections, which are disassembled each refueling outage, were specifically examined for leakage by VT-2 qualified personnel during unit startup and no abnormal conditions were identified.

Approximately 20% of the bare metal RPV surface was visually inspected to confirm the inspection results of a previous leak on the reactor head vent valve discovered during refueling outage B1 R03 in 1990; no boric acid accumulation or head wastage was observed.

Page 1 of 2

Attachment I

b. the corrective actions taken and the root cause of the degradation.

Response

There were no corrective actions taken or root cause investigations performed as no RPV degradation was identified.

Page 2 of 2