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MONTHYEARML0810800382008-04-0808 April 2008 Brunswick, Shearon Harris, H.B. Robinson, Crystal River, Request for Extension of 3-Month Response to Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems. Project stage: Request ML0813100152008-05-22022 May 2008 Response to Extension Request for Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems Project stage: Other ML0816505982008-09-25025 September 2008 Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems, Proposed Alternative Course of Action Project stage: Other BSEP 09-0079, Post-Outage Supplemental Response to Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems2009-07-27027 July 2009 Post-Outage Supplemental Response to Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems Project stage: Request BSEP 09-0130, Response to Request for Additional Information Regarding Generic Letter 2008-01 (NRC TAC Nos. MD7802 and MD7803)2009-12-21021 December 2009 Response to Request for Additional Information Regarding Generic Letter 2008-01 (NRC TAC Nos. MD7802 and MD7803) Project stage: Response to RAI BSEP 10-0089, Post-Outage Supplemental Response to Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling Decay Heat Removal, and Containment Spray Systems2010-07-22022 July 2010 Post-Outage Supplemental Response to Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling Decay Heat Removal, and Containment Spray Systems Project stage: Supplement 2008-09-25
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Category:Letter type:BSEP
MONTHYEARBSEP 19-0012, Submittal of 2018 Sea Turtle Annual Report2019-01-17017 January 2019 Submittal of 2018 Sea Turtle Annual Report BSEP 18-0052, Annual Radiological Environmental Operating Report - 20172018-05-10010 May 2018 Annual Radiological Environmental Operating Report - 2017 BSEP 18-0051, Annual Radioactive Effluent Release Report - 20172018-04-26026 April 2018 Annual Radioactive Effluent Release Report - 2017 BSEP 18-0045, Request for License Amendment: Technical Specification 3.8.3, Diesel Fuel Oil, One-Time Extension of Main Fuel Oil Storage Tank Completion Time2018-04-25025 April 2018 Request for License Amendment: Technical Specification 3.8.3, Diesel Fuel Oil, One-Time Extension of Main Fuel Oil Storage Tank Completion Time BSEP 18-0054, Response to Request for Additional Information Regarding Inservice Inspection Program Proposed Alternative ISI-09 in Accordance with 10 CFR 50.55a(z)(1) Regarding Reactor Pressure Vessel Circumferential.2018-04-24024 April 2018 Response to Request for Additional Information Regarding Inservice Inspection Program Proposed Alternative ISI-09 in Accordance with 10 CFR 50.55a(z)(1) Regarding Reactor Pressure Vessel Circumferential. BSEP 18-0048, Response to Request for Additional Information Regarding Inservice Inspection Program Proposed Alternative ISI-09 in Accordance with 10 CFR 50.55a(z)(1) Regarding Reactor Pressure Vessel Circumferential Shell Weld Examinations2018-04-11011 April 2018 Response to Request for Additional Information Regarding Inservice Inspection Program Proposed Alternative ISI-09 in Accordance with 10 CFR 50.55a(z)(1) Regarding Reactor Pressure Vessel Circumferential Shell Weld Examinations BSEP 18-0044, Application of Dissimilar Metal Weld Full Structural Overlay - Reactor Pressure Vessel Nozzles N4A and N4D2018-04-11011 April 2018 Application of Dissimilar Metal Weld Full Structural Overlay - Reactor Pressure Vessel Nozzles N4A and N4D BSEP 18-0046, Supplement to Response to Request for Additional Information SRXB-RAI-2 Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion2018-04-10010 April 2018 Supplement to Response to Request for Additional Information SRXB-RAI-2 Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion BSEP 18-0047, Supplement to Proposed Alternative in Accordance with 10 CFR 50.55a(z)(2) for End of Interval Leakage Test2018-04-0505 April 2018 Supplement to Proposed Alternative in Accordance with 10 CFR 50.55a(z)(2) for End of Interval Leakage Test BSEP 18-0041, Request for License Amendment to Revise the Technical Specifications to Relocate the Pressure-Temperature Limit Curves to a Pressure and Temperature Limits Report2018-04-0404 April 2018 Request for License Amendment to Revise the Technical Specifications to Relocate the Pressure-Temperature Limit Curves to a Pressure and Temperature Limits Report BSEP 18-0043, Application of Dissimilar Metal Weld Full Structural Overlay - Reactor Pressure Vessel Nozzles N4A and N4D2018-03-31031 March 2018 Application of Dissimilar Metal Weld Full Structural Overlay - Reactor Pressure Vessel Nozzles N4A and N4D BSEP 18-0035, Response to Request for Additional Information Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion2018-03-29029 March 2018 Response to Request for Additional Information Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion BSEP 18-0042, Cycle 22 Core Operating Limits Report (COLR)2018-03-27027 March 2018 Cycle 22 Core Operating Limits Report (COLR) BSEP 18-0040, Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1) for End of Interval Leakage Test2018-03-23023 March 2018 Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1) for End of Interval Leakage Test BSEP 18-0039, Proposed In-Service Inspection Alternative for Application of Dissimilar Metal Weld Full Structural Overlay - Nozzles N4A and N4D2018-03-19019 March 2018 Proposed In-Service Inspection Alternative for Application of Dissimilar Metal Weld Full Structural Overlay - Nozzles N4A and N4D BSEP 18-0034, Corrected Affidavit Relating to the Request for License Amendment Regarding Core Flow Operating Range Expansion2018-03-16016 March 2018 Corrected Affidavit Relating to the Request for License Amendment Regarding Core Flow Operating Range Expansion BSEP 18-0032, Additional Testing Information Relating to the Request for License Amendment Regarding Core Flow Operating Range Expansion2018-03-14014 March 2018 Additional Testing Information Relating to the Request for License Amendment Regarding Core Flow Operating Range Expansion BSEP 18-0026, Additional Information Regarding Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1) for Reactor Pressure Vessel Nozzle-to-Vessel Weld Examination2018-03-0707 March 2018 Additional Information Regarding Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1) for Reactor Pressure Vessel Nozzle-to-Vessel Weld Examination BSEP 18-0014, Fifth 10-Year Inservice Testing Program Plan2018-02-19019 February 2018 Fifth 10-Year Inservice Testing Program Plan BSEP 18-0021, Response to Request for Additional Information Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion (CAC Nos. MF8864 and MF8865). Without Proprietary Enclosure2018-02-0505 February 2018 Response to Request for Additional Information Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion (CAC Nos. MF8864 and MF8865). Without Proprietary Enclosure BSEP 18-0017, Revision to Radiological Emergency Response Plan and Implementing Procedure2018-01-30030 January 2018 Revision to Radiological Emergency Response Plan and Implementing Procedure BSEP 18-0015, Inservice Inspection Program Proposed Alternative ISI-09 in Accordance with 10 CFR 50.55a(z)(1) Regarding Reactor Pressure Vessel Circumferential Shell Weld Examinations2018-01-23023 January 2018 Inservice Inspection Program Proposed Alternative ISI-09 in Accordance with 10 CFR 50.55a(z)(1) Regarding Reactor Pressure Vessel Circumferential Shell Weld Examinations BSEP 18-0013, Supplement to Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control2018-01-23023 January 2018 Supplement to Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control BSEP 18-0001, Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements2018-01-23023 January 2018 Application to Revise Technical Specifications to Adopt TSTF-551, Revise Secondary Containment Surveillance Requirements BSEP 18-0012, Application to Revise Technical Specifications to Adopt TSTF-208, Revision 0, Extension of Time to Reach Mode 2 in LCO 3.0.32018-01-23023 January 2018 Application to Revise Technical Specifications to Adopt TSTF-208, Revision 0, Extension of Time to Reach Mode 2 in LCO 3.0.3 BSEP 18-0009, 2017 Sea Turtle Annual Report2018-01-15015 January 2018 2017 Sea Turtle Annual Report BSEP 17-0098, Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components (Sscs) for Nuclear Power Reactors2018-01-10010 January 2018 Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components (Sscs) for Nuclear Power Reactors BSEP 17-0119, Snubber Program Plan for Fifth 10-Year Interval Inservice Testing Program2018-01-10010 January 2018 Snubber Program Plan for Fifth 10-Year Interval Inservice Testing Program BSEP 17-0115, Response to Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control2018-01-0404 January 2018 Response to Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control BSEP 17-0110, Seventh Six-Month Status Report in Response to June 6, 2013, Commission Order Modifying Licenses with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe Accident Conditions2017-12-20020 December 2017 Seventh Six-Month Status Report in Response to June 6, 2013, Commission Order Modifying Licenses with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe Accident Conditions BSEP 17-0121, Post-Examination Documentation and Comments for Operator Retake Initial Examination2017-12-14014 December 2017 Post-Examination Documentation and Comments for Operator Retake Initial Examination BSEP 17-0120, Withdrawal of Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel Generator Completion Times and Suspension..2017-12-12012 December 2017 Withdrawal of Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel Generator Completion Times and Suspension.. BSEP 17-0118, Supplement to Response to Request for Additional Information Regarding Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel..2017-12-0707 December 2017 Supplement to Response to Request for Additional Information Regarding Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel.. BSEP 17-0117, Response to Request for Additional Information (Probabilistic Risk Assessment and Human Performance Branches) Regarding Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1 AC Sources..2017-12-0606 December 2017 Response to Request for Additional Information (Probabilistic Risk Assessment and Human Performance Branches) Regarding Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1 AC Sources.. BSEP 17-0116, Response to Request for Additional Information Regarding Request for Risk- Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of ..2017-12-0404 December 2017 Response to Request for Additional Information Regarding Request for Risk- Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of .. BSEP 17-0104, Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1) for Reactor Pressure Vessel Nozzle-to-Vessel Weld Examination2017-11-29029 November 2017 Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1) for Reactor Pressure Vessel Nozzle-to-Vessel Weld Examination BSEP 17-0111, Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources Operating, One-Time Extension of Emergency Diesel Generator Completion Times and Suspension of Surveillance Requirements2017-11-28028 November 2017 Request for Risk-Informed Exigent License Amendment - Technical Specification 3.8.1, AC Sources Operating, One-Time Extension of Emergency Diesel Generator Completion Times and Suspension of Surveillance Requirements BSEP 17-0109, Response to Request for Additional Information Regarding Request for Emergency License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel Generator Completion Times And.2017-11-24024 November 2017 Response to Request for Additional Information Regarding Request for Emergency License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel Generator Completion Times And. BSEP 17-0108, Request for Emergency License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel Generator Completion Times and Suspension of Surveillance Requirements2017-11-22022 November 2017 Request for Emergency License Amendment - Technical Specification 3.8.1, AC Sources - Operating, One-Time Extension of Emergency Diesel Generator Completion Times and Suspension of Surveillance Requirements BSEP 17-0017, Submittal of Request for License Amendment for Performance-Based Fire Protection Alternative for Thermal Insulation Material2017-11-15015 November 2017 Submittal of Request for License Amendment for Performance-Based Fire Protection Alternative for Thermal Insulation Material BSEP 17-0100, Fifth 10-Year Inservice Testing Interval2017-11-0202 November 2017 Fifth 10-Year Inservice Testing Interval BSEP 17-0089, Updates to Request for License Amendment Regarding Core Flow Operating Range Expansion2017-11-0101 November 2017 Updates to Request for License Amendment Regarding Core Flow Operating Range Expansion BSEP 17-0093, Response to Request for Additional Information Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion2017-11-0101 November 2017 Response to Request for Additional Information Regarding Request for License Amendment Regarding Core Flow Operating Range Expansion BSEP 17-0078, Request for License Amendment - DC Sources - Operating Surveillance Requirement (SR) 3.8.4.52017-10-0303 October 2017 Request for License Amendment - DC Sources - Operating Surveillance Requirement (SR) 3.8.4.5 BSEP 17-0076, Registration for Use of General License Spent Fuel Casks2017-09-0606 September 2017 Registration for Use of General License Spent Fuel Casks BSEP 17-0081, Revision to Radiological Emergency Response Plan Implementing Procedures2017-09-0505 September 2017 Revision to Radiological Emergency Response Plan Implementing Procedures BSEP 17-0039, Submittal of Response to Inspection Report 05000324/2015404 and 05000325/2015404, Dated March 30, 2015, Inspection of Interim Cyber Security Milestones 1-7 and Target Set Requirements2017-08-15015 August 2017 Submittal of Response to Inspection Report 05000324/2015404 and 05000325/2015404, Dated March 30, 2015, Inspection of Interim Cyber Security Milestones 1-7 and Target Set Requirements BSEP 17-0071, ISFSI - Registration for Use of General License Spent Fuel Casks2017-08-15015 August 2017 ISFSI - Registration for Use of General License Spent Fuel Casks BSEP 17-0064, Application of Dissimilar Metal Weld Full Structural Overlay on Reactor Pressure Vessel Nozzle N92017-07-10010 July 2017 Application of Dissimilar Metal Weld Full Structural Overlay on Reactor Pressure Vessel Nozzle N9 BSEP 17-0060, Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control.2017-06-29029 June 2017 Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control. 2019-01-17
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Text
SProgress Energy
- Benjamin C.Waldrep Brnsic NueasiPlnt Vice President Brunswick Nuclear Plant Progress Energy Carolinas, Inc.
July 27, 2009 SERIAL: BSEP 09-0079 10 CFR 50.54(f)
U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001
Subject:
Brunswick Steam Electric Plant, Unit No. 2 Docket No. 50-324/License No. DPR-62 Post-Outage Supplemental Response to Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems"
References:
- 1. Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems,"
dated January 11, 2008 (ADAMS Accession Number ML072910759)
- 2. Letter from Benjamin C. Waldrep to the U.S. Nuclear Regulatory Commission (Serial: BSEP 08-0060), "Three-month Response to Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems" dated May 9, 2008 (ADAMS Accession Number ML081420026)
- 3. Letter from Benjamin C. Waldrep to the U.S. Nuclear Regulatory Commission (Serial: BSEP 08-0137), "Nine-month Response to Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems" dated October 10, 2008 (ADAMS Accession Number ML082950466)
Ladies and Gentlemen:
On January 11, 2008, the NRC issued Generic Letter (GL) 2008-01 (i.e., Reference 1) requesting that each licensee evaluate the licensing basis, design, testing, and corrective action programs for the Emergency Core Cooling Systems (ECCS), Decay Heat Removal (RHR) system, and Containment Spray system, to ensure that gas accumulation is maintained less than the amount that challenges operability of these systems, and that appropriate action will be taken when conditions adverse to quality are identified.
References 2 and 3 provided Carolina Power & Light Company's (CP&L), now doing business as Progress Energy Carolinas, Inc., responses to GL 2008-01 for the Brunswick Steam Electric Plant (BSEP), Units 1 and 2. In Reference 2, CP&L committed to P.O.Box 10429 Southport, NC 28461 T> 910.457.3698 i (7
Document Control Desk BSEP 09-0079 / Page 2 completing detailed walkdowns and any necessary ultrasonic examinations of inaccessible piping at locations potentially susceptible to gas accumulation for systems within the scope of GL 2008-01 and to submit a supplemental response to GL 2008-01, within 90 days following the completion of the 2009 Unit 2 refueling outage (i.e., B219R1), describing any changes to the nine-month response resulting from walkdowns and ultrasonic examination of inaccessible BSEP Unit 2 piping.
The enclosure to this letter provides CP&L's post-outage supplemental response to GL 2008-01 for BSEP Unit 2.
No new regulatory commitments are contained in this submittal. Please refer any questions regarding this submittal to Mr. Gene Atkinson, Supervisor -
Licensing/Regulatory Programs, at (910) 457-2056.
I declare, under penalty of perjury, that the foregoing is true and correct. Executed on July 27, 2009.
Sincerely, Benjamin C aldrep MAT/mat
Enclosure:
Post-Outage Supplemental Response to Generic Letter 2008-01 for BSEP Unit 2
Document Control Desk BSEP 09-0079 / Page 3 cc (with enclosure):
U. S. Nuclear Regulatory Commission, Region II ATTN- Mr. Luis A. Reyes, Regional Administrator Sam Nunn Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, GA. 30303-8931 U. S. Nuclear Regulatory Commission ATTN: Mr. Philip B. O'Bryan, NRC Senior Resident Inspector 8470 River Road Southport, NC 28461-8869 U. S. Nuclear Regulatory Commission (Electronic Copy Only)
ATTN: Mrs. Farideh E. Saba (Mail Stop OWFN 8G9A) 11555 Rockville Pike Rockville, MD 20852-2738 Chair - North Carolina Utilities Commission P.O. Box 29510 Raleigh, NC 27626-0510
BSEP 09-0079 Enclosure Page 1 of 3 Post-Outage Supplemental Response to Generic Letter 2008-01 for BSEP Unit 2 The 2009 Brunswick Steam Electric Plant (BSEP), Unit 2 refueling outage (i.e., B219R1) was completed on April 29, 2009. During this outage, as committed, Carolina Power & Light Company's (CP&L), now doing business as Progress Energy Carolinas, Inc., completed detailed walkdowns and necessary ultrasonic examinations of inaccessible piping at locations potentially susceptible to gas accumulation for systems within the scope of Generic Letter (GL) 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems," dated January 11, 2008. Based on completion of these activities, the following supplemental information to BSEP's nine-month response to GL 2008-01, dated October 10, 2008, is provided.
A. Evaluation Results
- 1. Design Basis Documents There have been no changes in the BSEP design basis documents related to gas accumulation since the nine-month response. Plant drawings have been updated to reflect the addition of the new vent valves discussed below.
The nine-month response stated that BSEP would, as an enhancement, develop a calculation that provides an analytical basis for void acceptance criteria for systems within the scope of GL 2008-01. This calculation has been completed and acceptable void volumes have been established for specific locations that were identified to be potentially susceptible to gas accumulation, based on the gas void acceptance criteria described in the nine-month response.
- 2. Confirmatory Walkdowns As noted in BSEP's three-month response to GL 2008-01, dated May 9, 2008, walkdowns of BSEP Unit 2 piping systems, in a number of inaccessible areas of the plant, were scheduled to be completed during the Spring 2009 Unit 2 refueling outage (i.e., B219R1). These inspections of the normally inaccessible piping were completed, as scheduled, and the piping was confirmed to be routed as shown on plant isometric drawings. No Ultrasonic Test (UT) inspections or slope measurements were taken on discharge piping downstream of normally closed injection valves because the configuration downstream of the injection valves is an open flow path to the Reactor Coolant System. As such, there is no opportunity for pressure wave reflection from a downstream surface.
The GL 2008-01 subject systems were drained to support the installation of new vent valves and/or for other scheduled maintenance. Following these maintenance evolutions, post fill and vent UT inspections were performed on the systems at
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BSEP 09-0079 Enclosure Page 2 of 3 potentially susceptible locations to confirm the effectiveness of the new vent valves and fill and vent procedure revisions. In each of the subject systems, UT inspections were performed on both suction and discharge piping. Only very minor voiding was identified and all voids were found to be significantly less than the acceptable void volumes determined in the acceptance criteria calculation. Suction side voids were removed by dynamic venting and were verified to be removed by UT inspections.
- 3. Venzt Valves Beyond those planned for the outage, no additional vent valves or modifications to existing vent valves were required as a result of the walkdowns performed during B219R1.
- 4. Procedures No new procedure revisions were identified as a result of the walkdowns performed during B219R1.
B. Description of Necessary Additional Corrective Actions
- 1. Additional Corrective Actions No new corrective actions were identified as a result of the walkdowns performed during B219R1.
- 2. Corrective Action Updates New vent valves were installed at the locations specified in the nine-month response, with the exception of the HPCI injection line downstream of check valve 2-E4 I-V159 and the Core Spray torus suction lines. Since the nine-month response was submitted, further analysis of the piping downstream of 2-E41-V 159 determined that this location is not susceptible to adverse pressure transients since there is no opportunity for pressure wave reflection from a downstream surface in the flow stream. Installation of the Core Spray torus suction line vents was not required because: (1) these lines are not subjected to any active source of gas intrusion, and as such there is no potential for gas introduction while the system is in its normal standby condition and (2) dynamic venting has been proven to be effective at eliminating small residual voids (i.e., significantly smaller than the acceptable void volumes at the respective locations) that remain following initial filling and venting of these lines.
I' BSEP 09-0079 Enclosure Page 3 of 3 Except for the vent valve changes identified above, all previously identified BSEP Unit 2 corrective actions associated with this GL, with due dates prior to startup from B219R1, have been completed.
C. Conclusion BSEP has completed the evaluation of the previously inaccessible portions of the applicable systems at BSEP Unit 2 that perform the functions described in the GL and has concluded that these systems are operable, as defined in the BSEP Technical Specifications, and are in conformance with the BSEP licensing basis and compliance with all applicable regulations, including 10 CFR 50 Appendix B, Criteria III, V, XI, XVI, and XVII.