05000412/LER-2011-002, Regarding Auxiliary Feedwater System Vent Line Weld Crack Results in Technical Specification Required Plant Shutdown and Valid Reactor Protection System/Engineered Safety Feature Actuation System Actuations

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Regarding Auxiliary Feedwater System Vent Line Weld Crack Results in Technical Specification Required Plant Shutdown and Valid Reactor Protection System/Engineered Safety Feature Actuation System Actuations
ML11159A162
Person / Time
Site: Beaver Valley
Issue date: 06/03/2011
From: Harden P
FirstEnergy Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-11-191 LER 11-002-00
Download: ML11159A162 (8)


LER-2011-002, Regarding Auxiliary Feedwater System Vent Line Weld Crack Results in Technical Specification Required Plant Shutdown and Valid Reactor Protection System/Engineered Safety Feature Actuation System Actuations
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(iv)(B), System Actuation

10 CFR 50.73(a)(2)(iv)(B)(1)

10 CFR 50.73(a)(2)(iv)(B)(2)

10 CFR 50.73(a)(2)(iv)(B)(6)
4122011002R00 - NRC Website

text

FENOC Beaver Valley Power Station P.O. Box 4 FirstEnergy Nuclear Operating Company Shippingport, PA 15077 Paul A. Harden 724-682-5234 Site Vice President Fax: 724-643-8069 June 3, 2011 L-1 1-191 10 CFR 50.73 ATTN: Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555-0001

SUBJECT:

Beaver Valley Power Station, Unit No. 2 Docket No. 50-412, License No. NPF-73 LER 2011-002-00 Enclosed is Licensee Event Report (LER) 2011-002-00, "Auxiliary Feedwater System Vent Line Weld Crack Results in Technical Specification Required Plant Shutdown and Valid Reactor Protection System / Engineered Safety Feature Actuation System Actuations." This event is being reported in accordance with 10 CFR 50.73(a)(2)(i)(A),

10 CFR 50.73(a)(2)(iv)(A), 10 CFR 50.73(a)(2)(v)(B), and 10 CFR 50.73(a)(2)(v)(D).

There are no regulatory commitments contained in this submittal. Any actions discussed in this document that represent intended or planned actions are described for the NRC's information, and are not regulatory commitments.

If there are any questions or if additional information is required, please contact Mr. Brian T. Tuite, Manager, Regulatory Compliance at 724-682-4284.

Sincere Paid! A. Harden Attachment c:

Mr. W. M. Dean, NRC Region I Administrator Mr. D. L. Werkheiser, NRC Senior Resident Inspector Ms. N. S. Morgan, NRR Project Manager INPO Records Center (via electronic image)

Mr. L. E. Ryan (BRPIDEP)

V.

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES 10/31/2013 (10-2010)

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Beaver Valley Power Station Unit Number 2 05000412 1 of 7
4. TITLE Auxiliary Feedwater System Vent Line Weld Crack Results in Technical Specification Required Plant Shutdown and Valid Reactor Protection System / Engineered Safety Feature Actuation System Actuations
5. EVENT DATE
6. LER NUMBER MONTH DAY YEAR YEAR I

SEQUENTIAL I

REV MONTH NUMBER NO.

IM I

04 09 2011 2011 002 00 106 03

9. OPERATING MODE 1
10. POWER LEVEL 14%

E2 L2 EJ 2

[_12

[_12 E] 2 EJ 2 L2 L2

11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 0.2201(b)

[] 20.2203(a)(3)(i)

F] 50.73(a)(2)(i)(C)

E] 50.73(a)(2)(vii) 0.2201(d)

Ei 20.2203(a)(3)(ii)

[] 50.73(a)(2)(ii)(A)

E] 50.73(a)(2)(viii)(A) 0.2203(a)(1)

[] 20.2203(a)(4)

[J 50.73(a)(2)(ii)(B)

Li 50.73(a)(2)(viii)(B)

0.2203(a)(2)(i)

Li 50.36(c)(1)(i)(A)

E] 50.73(a)(2)(iii)

Di 50.73(a)(2)(ix)(A)

>0.2203(a)(2)(ii)

[

50.36(c)(1)(ii)(A)

JE 50.73(a)(2)(iv)(A)

El 50.73(a)(2)(x)

0.2203(a)(2)(iii)

[

50.36(c)(2)

Li 50.73(a)(2)(v)(A)

E] 73.71(a)(4)

0.2203(a)(2)(iv)

[] 50.46(a)(3)(ii)

Z 50.73(a)(2)(v)(B)

Li 73.71(a)(5) 0.2203(a)(2)(v)

[

50.73(a)(2)(i)(A)

Li 50.73(a)(2)(v)(C)

El OTHER Specify in Abstract below 0.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D) or in reactor power). The control room operations staff communicated that the level in "A" SG was approaching the predetermined SG low-low level manual reactor trip criterion point of 25 percent. At 0357 hours0.00413 days <br />0.0992 hours <br />5.902778e-4 weeks <br />1.358385e-4 months <br />, "A" SG level reduced to 25 percent and a manual reactor trip was performed. The manual reactor trip was successfully completed without complications.

All controls rods were fully inserted in the reactor core and safety systems and equipment functioned as expected. The control room operations staff entered Emergency Operating Procedure E-0, "Reactor Trip or Safety Injection", as expected. The Reactor Coolant System (RCS) [AB] cooldown resulted in a shrink of level in the "A" SG to the Engineered Safety Feature Actuation Signal (ESFAS) setpoint. The steam driven AFW pump successfully automatically started on low-low SG level in the "A" SG due to the ESFAS start signal. As a result of the AFW automatic start of the steam driven AFW pump, AFW flow was injected into the "B" and "C" SGs. AFW flow injection to the "A" SG did not occur since the "A" SG feedwater injection header had been previously isolated at 0204 hours0.00236 days <br />0.0567 hours <br />3.373016e-4 weeks <br />7.7622e-5 months <br /> to repair the 2FWE-940 branch line crack. The reactor protection system (RPS) logic for an automatic reactor trip was also satisfied due to a low-low water level in "A" SG. However, the safety function of the automatic reactor trip was previously accomplished when the manual reactor trip was completed. At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br />, the control room operations staff transitioned from emergency operating procedure 20M-53A.1.E-0 (Reactor Trip or Safety Injection) to 20M-53A.1.ES-0.1 (Reactor Trip Response). The control room operations staff manually initiated main steam line isolation (SLI) utilizing the manual SLI pushbuttons in order to limit RCS cooldown per plant procedure 20M-53A.1.ES-0.1. The SLI actuation includes closure of all three main steam line isolation valves (MSIVs). The manual SLI initiation was expected should a reactor trip occur at the beginning of core life and had been pre-briefed as part of the plant shutdown preparations. The manual SLI was completed successfully with the required components actuating as expected. In addition, AFW flow was reduced to limit the RCS cooldown. The control room operations staff performed 20M-51.4.G, titled "Station Shutdown Establishing Mode 3 Conditions Following a Reactor Trip or SI", prior to returning to the normal shutdown procedure.

CAUSE OF EVENT

The most probable direct cause of the branch line crack was determined to be vibration induced high cycle fatigue failure of the vertical 0.75 inch pipe socket welded to the four inch "A" SG feedwater injection header line due to a less than adequate design in combination with a potential discontinuity in the socket weld toe.

The root cause of the branch line crack was determined to be less than adequate design guidance contained in the design process to prevent vibration induced high cycle fatigue failure of the pipe nipple associated with 2FWE-940. Various documents (i.e. Engineering Standards, Plant Installation Process Standards, and Weld Manual) did not contain

guidance for design or fabrication that was available through industry recommendation documents relative to free-end branch line design. This AFW line vent line was installed by a plant modification performed in 1993.

The direct cause of the manual reactor trip and automatic start of the steam driven AFW pump was determined to be that during a beginning of life (BOL) reactor shutdown, the control room operations staff was not able to maintain adequate steam generator level.

The RCS cooldown and SG shrink were greater than expected resulting in the control room operations staff initiating a manual reactor trip when narrow range level reduced to 25 percent in the "A" SG.

The root cause of the manual reactor trip and automatic start of the steam driven AFW pump was determined to be that the shutdown procedure guidance was not adequate for RCS temperature control and SG level control. The procedure for performing a controlled shutdown is the refueling outage shutdown procedure which was designed for end of life (EOL) conditions. Conditions at BOL are significantly different; however, the procedure had no guidance to address the difference in reactivity response from rod insertion or the expected SG level shrink. The station failed to recognize the need to develop procedure guidance for this scenario since controlled shutdowns at BOL are infrequent.

ANALYSIS OF EVENT

The AFW System automatically supplies feedwater to the SGs to remove decay heat from the RCS upon the loss of normal feedwater supply. The design basis of the AFW System is to supply water to the SG to remove decay heat and other residual heat by delivering at least the minimum required flow rate to the SGs. In addition, the AFW System must supply enough makeup water to replace the SG secondary inventory lost as the unit cools to Mode 4 conditions. Sufficient AFW flow must also be available to account for flow losses such as pump recirculation and line breaks. The limiting Design Basis Accidents (DBAs) for the AFW System are loss of normal feedwater and feedwater line break. With one feedwater injection header inoperable, an insufficient number of SGs are available to meet the feedline break analysis. This analysis assumes AFW flow will be provided to the two remaining intact feedwater lines. Should a feedline break occur on one of the operable feedwater headers with one feedwater injection header already inoperable, the plant could no longer meet its safety analysis.

The branch line crack on the AFW vent line resulted in the "A" SG feedwater injection line being declared inoperable and the subsequent isolation of injection line to repair the branch line crack. When the line was isolated from 0204 hours0.00236 days <br />0.0567 hours <br />3.373016e-4 weeks <br />7.7622e-5 months <br /> until shortly before the

feedwater injection header was restored to operable status at 1339 hours0.0155 days <br />0.372 hours <br />0.00221 weeks <br />5.094895e-4 months <br /> on April 10, 2011, this flow path was not available to supply AFW to the "A" SG. Following the discovery of the crack, the Technical Specification required actions were taken and a plant shutdown was initiated.

The safety significance associated with the BVPS-2 branch line crack on the piping associated with the AFW vent valve 2FWE-940 is considered to be very low. This is based on the delta core damage frequency and delta large early release frequency for the event during the limited period that the degraded condition existed.

The plant risk associated with the BVPS-2 manual reactor trip, the manual SLI, and automatic AFW actuation on April 10, 2011, due to a low water level condition in the "A" SG, while the plant was performing a Mode 1 to Mode 3 Technical Specification required shutdown is considered to be very low. This is based on the conditional core damage probability and conditional large early release probability for the event when considering the actual plant conditions that were present at the time of the event.

The branch line crack on the AFW vent line is reportable for the following reasons. The branch line crack resulted in the completion of a plant shutdown required by Technical Specification (TS), and is thus reportable per 10 CFR 50.73(a)(2)(i)(A). BVPS-2 completed a plant shutdown to Mode 3 in accordance with TS 3.7.5 Condition D at 0357 on April 10, 2011. The branch line crack also resulted in the common train "A" and "B" feedwater injection header to the "A" SG being inoperable, and is thus reportable per 10 CFR 50.73(a)(2)(v)(B) and 10 CFR 50.73(a)(2)(v)(D). With the common header inoperable and unavailable due to maintenance activities to repair the branch line crack, this configuration could have prevented the fulfillment of the safety function to remove residual heat (in the "A" SG) and to mitigate the consequences of an accident.

The manual reactor trip, the manual SLI, and the automatic start of the steam driven AFW pump is reportable per 10 CFR 50.73(a)(2)(iv)(A) as an event that was not part of a pre-planned sequence which resulted in the valid manual or automatic actuation of three systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B). The manual reactor trip was initiated due to the actual SG level on the "A" SG approaching the automatic trip setpoint.

Therefore, this RPS manual actuation (Manual Reactor trip) is reportable per 10 CFR 50.73(a)(2)(iv)(B)(1). The manual SLI was initiated per plant procedure 20M-53A.1.ES-0.1 (Reactor Trip Response) due to the continued cooldown of the RCS following the manual reactor trip. Therefore, this manual SLI actuation, which includes closure of multiple MSIVs, is reportable per 10 CFR 50.73(a)(2)(iv)(B)(2). The AFW automatic start of the steam driven AFW pump was initiated due to the actual SG level on "A" SG reaching the automatic start setpoint following the manual reactor trip. Therefore, this automatic actuation is reportable per 50.73(a)(2)(iv)(B)(6).

This event was previously reported as pursuant to 10 CFR 50.72(b)(2)(i), 10 CFR 50.72(b)(2)(iv)(B), 10 CFR 50.72(b)(3)(ii)(A), and 10 CFR 50.72(b)(3)(iv)(A) at 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br /> on April 10, 2011 (Event Notification 46744). However upon further review, the initial reportability of this event under 10 CFR 50.72(b)(3)(ii)(A) is retracted since the credited inside containment boundary (the steam generator closed system located inside containment) remained intact and operable during this event. The containment function or integrity was thus maintained during this event and therefore, this event did not result in serious degradation of a principal safety barrier. In addition, EN 46744 should have reported the manual SLI actuation under 10 CFR 50.72(b)(3)(iv)(A) as a valid system actuation. A loss of safety function should have also been reported under 10 CFR 50.72(b)(3)(v)(B) & (D) when the "A" feedwater injection header was declared inoperable and isolated for repair. This issue has been entered into the Corrective Action Program.

CORRECTIVE ACTIONS

Applicable to the AFW vent line branch line crack:

1. The cracked pipe nipple was replaced to the original configuration and the "A" SG feedwater injection header was returned to operable status on April 10, 2011 at 1339 hours0.0155 days <br />0.372 hours <br />0.00221 weeks <br />5.094895e-4 months <br />. For the repair, the weld size and profile was increased (i.e. two to one leg length). This action should reduce stresses at the weld toe which should reduce the likelihood of a fatigue-type failure at this location.
2. Pipe supports are being designed to inhibit vibration on all three feedwater injection line vent lines.
3. Liquid penetrant testing of the branch line pipe-to-cupolet socket weld on the vent valves at the similar locations on the feedwater injection lines to the "B" and "C" Steam Generators will be performed.
4. A review against the Architectural Engineer (AE) vent/drain guidance document will be performed on select vents/drains located on systems as defined in the Extent of Cause Strategy.
5. Design guidance will be incorporated into engineering standards to address system induced vibration on free end branch connections.

Applicable to the manual reactor trip and AFW pump automatic start:

1. Develop procedure guidance for plant shutdown applicable to all times (beginning, middle, and end) of core life.
2. BVPS-1 and BVPS-2 procedures governing plant startup and shutdown evolutions will be reviewed for content and appropriate guidance for expected initial conditions.
3. Additional simulator training on low power operation will be performed for BVPS-1 and BVPS-2 licensed operators as part of the continuing training program.

Completion of the above and other corrective actions are being tracked through the BVPS corrective action program.

PREVIOUS SIMILAR EVENTS

A review of previous BVPS LERs for approximately the previous five years determined that there were two LERs that involved similar events.

1. BVPS-1 LER 2010-002-01, "270 Degree Circumferential Flaw Found on Residual Heat Removal System Drain Valve Socket Weld."

Cause

Vibration induced fatigue, due to less than adequate design considerations

2. BVPS-2 LER 2008-001-00, "Unplanned Actuation of the Auxiliary Feedwater System During Plant Startup."

Cause

Unfamiliar with SG water level control during low power operation. Operations Management Team failed to ensure the startup crew was staged for success in operating the plant in a low power configuration.

CR 11-92597/11-92603