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"l$lf0C Telephone (412) 393-6000 Nuclear Group I
P O Dox 4 Shippingx4 PA 1W774%4 j
February 6, 1990 ND3MNO:2020 l
- - i Beaver Valley Power Station, Unit No. 2 Docket No. 50-412, License No. NPF-73 LER 90-001-00 J
i United States Nuclear Regulatory Commission Document Control Desk j
Washington, DC 20555 j
Gentlemen:
In-accordance
.with Appendix A,
Beaver Valle Technical Specifications,-the following Licensee Event Report-is ysubmitted:
LER 90-001-00, 10 CFR 50.73.a.2.iv, " Engineered Safet Features Actuation - Staam Generator-Blowdown Isolation".y
.j Very truly yours, W
T.
P. N onan General Manager l
Nuclear Operations j
Cj.
Attachment s
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February 6, 1990 ND3MNO 2020 Page two
'cc: Mr. William.T. Russell Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Road King of Prussia, PA 19406 C. A. Roteck, Ohio Edison Mr. Peter Tam, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, DC 20555 J.
Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector Dave Amerine Centerior Energy 6200 Oak Tree Blvd.
Independence, Ohio 44101 INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, GA 30339 G.
E. Muckle, Factory Mutual Engineering, Pittsburgh Mr. J.
N. Steinmetz, Operating Plant Projects Manager Mid Atlantic Area Westinghouse Electric Corporation Energy Systems Service Division Box 355 Pittsburgh, PA 15230 American Nuclear Insurers c/o Dottie Sherman, ANI Library The Exchange Suite 245 270 Farmington Avenue Farmington, CT 06032 Mr. Richard Janati Department of Environmental Resources P. O.
Box 2063 16th Floor, Fulton Building Harrisburg, PA 17120 Director, Safety Evaluation & Control Virginia Electric & Power Co.
P.O.
Box 26666 One James River Plaza Richmond, VA 23261
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.,,,,,,,,,,,,..,..,,,.,.,nei On 1/07 Unit
- 2 was in steady-state Power Operation (Operatin/90, g-Mode
- 1) at 85% reactor power.
At 1639 hours0.019 days <br />0.455 hours <br />0.00271 weeks <br />6.236395e-4 months <br />, a high radiation alarm was received on the Steam Generator Blowdown (SGBD)
Sample Radiation
- Monitor, 2SSR-RQIl00..
No equipment operation or activity was.in progress.
This.high alarm caused an isolation of the SGBD system.
This isolation is an Engineered Safety Features system actuation and reportable in accordance with 10CFR50.72 and 50.73.
- - The
cause
for this actuation was due to residual contaminated (crud) particles, remaining from a
prior SG tube leak, being swept into the SGBD Sample Radiation Monitor.
The SGBD Sample Radiation Monitor was purged and returned to service and the SG blowdown system was restored to normal system arrangement.
An Engineering evaluation has been performed to raise the setpoint on 2SSR-RQIl00.
There were no safety implications as a result of this event.
The radiation monitor actuated as designed to isolate the blowdown system in the event of any steam generator tube leakage.
The low level activity was only a momentary excursion due the residual activity in the piping.
This was less than 1 percent of the allowed limit for power operation.
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UCENSEE EVENT REPORT (LER) TEXT CONTINUATION Aernovto ous No a+oio.
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DESCRIPTION
On 1/07/90, Unit
- 2 was in steady-state Power Operation (Operating Mode
- 1) at 85% reactor power.
At 1639 hours0.019 days <br />0.455 hours <br />0.00271 weeks <br />6.236395e-4 months <br />, a high radiation alarm was-received on the Steam Generator Blowdown
=c (SGBD)
Sample Radiation
- Monitor, 2SSR-RQIl00.
No abnormal
- - equipment operation or activity was in progress.
This high.
alarm caused an isolation of the SGBD system.
The liquid in the SGBD-Sample Radiation Monitor which was isolated was analyzed.
The activity level of the liquid was found to be 4.99 E-7 microcuries per milliliter.
The high alarm setpoint is 1.53 E-5 microcuries per milliliter.
Operations personnel verified that the Condenser Air Ejector Radiation Monitor was indicating normal levels.
The SGBD Sample Radiation Monitor was purged and placed back in service.
The radiation monitor indications stabilized at pre-event values and the SGBD system was returned to service.
CAUSE OF THE EVENT
1 The
cause
for this event was residual contaminated (crud) particles, remaining from a prior SG tube leak, being swept into i
the SGBD Sample Radiation Monitor.
Total blowdown flow had been i
increased from its normal 220 gallons per minute to 280 gallons l
per minute for the previous three days to adjust Steam Generator Chemistry.
The increased flow was postulated to have caused i
some-residual crud particles to be released into the-system and to the-radiation monitor.
The residual activity deposited within the steam generator blowdown and blowdown sample system results in a relatively low level activity spike which is swept q
into the radiation moniter.
The design basis of the previous high alarm setpoint on the SGBD sample radiation monitor allows i
for the detection of primary-to-secondary leakage while limiting the secondary liquid concentration to less than 1.0E-5 j
microcuries per milliliter minimizing the buildup of steam generator blowdown demineralizer activity.
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CORRECTIVE ACTIONS
The following corrective actions have been taken as a result o this event:
1.
The SGBD Sample Radiation Monitor and the Auxiliary Steam Condensate effluent was directed to the Primary Auxiliary Building Sump until the analysis of the effluent was completed.
2.
The SGBD Sample Radiation Monitor was purged and returned to service.
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION' APPROVED OMB NO. MO.0@
EXPIRE $: $!3U88 F ACIL11Y hAmt (le.
DOCkki NUMDER (2)
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W *.D B aver Valley Power Station Unit 2 0 10 013 0F Ol4 O l Ol1 o l5 l0 j o lo l 411 l2 91 0 TEXT ty anore space is recured, ese am*reneRC Form Js5A as (171 3.-
The SGBD system was restored to normal system arrangement.
4.
An Engineering evaluation -has been performed to increase the setpoint for the High and Alert alarm setpoints for the SGBD Sample Radiation Monitor.
The ne*'
setpoints are less than 15% of the allowed limits fe' normal -Power Operation.
The new-setpoint is higaer than any previous observed crud induced spikes on this monitor.
These setpoints were approved for use on 1/19/90.
The setpoints were increased as follows:
Previous value New Value Alert 1.24 E-5 1.42 E-5 High 1.43 E-5 7.33 E-3 Setpoint values are microcuries per milliliter.
These setpoints are administrative limits which serve to minimize secondary contamination.
The Steam Generator Blowdown System has been constantly flushed during operation with clean secondary water at the rate of 200 to 300 gallons per minute since the Steam Generator Tube Leak event on 6/21/89 (reference:
LER 89-021).
The Llowdown Monitoring System has been flushed and purged on several occasions since then, however, due
.to the residual crud deposits within the systems, these actions were unsuccessful in - preventing an additional occurrence.
- - REPORTABILITY
- - This event was repporrted.as an Engineered Safety Features (ESP)
System Actuation, in accordance with 10CFR50.72.b.2.ii, at 1835 hour0.0212 days <br />0.51 hours <br />0.00303 weeks <br />6.982175e-4 months <br />s-on 1/07/90.
This written report is being-submitted in accordance with the requirements of 10CFR50.73.a.2.iv.
SAFETY IMPLICATIONS There were no. safety implications to the public as a result of this event because the radiation monitor actuated as designed to c
- - isolate.-the blowdown system in the-event of any steam generator tube leakage.
The low level activity was only a momentary excursion due to the residual activity in the piping.
The monitor's new alarm setpoint is less than 15% of the allowed limits for normal Power Operation (Reference: Beaver Valley Unit 2
UFSAR Table 15-0.8).
The previous alarm setpoint was less than 10% of the allowed limits for normal Power Operation.
This is an administrative limit chosen to control the contamination to the uncontrolled secondary plant systems in the event of a
'4 steam generator tube leak.
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PREVIOUS OCCURRENCES
There have been two previously reported events (Reference: LERs 89-024-00.and 89-026-00),
involving Engineered Safety Features (ESP)
Actuations resulting from steam generator blowdown system
~isolations, I
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| | | Reporting criterion |
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| 05000412/LER-1990-001, :on 900107,high Radiation Alarm Received on Steam Generator Blowdown (SGBD) Sample Radiation Monitor, Causing SGBD Sys Isolation.Caused by Crud Particles Swept Into Monitor.Monitor Purged & Returned to Svc |
- on 900107,high Radiation Alarm Received on Steam Generator Blowdown (SGBD) Sample Radiation Monitor, Causing SGBD Sys Isolation.Caused by Crud Particles Swept Into Monitor.Monitor Purged & Returned to Svc
| | | 05000412/LER-1990-002-02, :on 900217,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.Caused by Failure to Complete Tech Spec Required post-maint Test. Post-maint Test Procedure Revised |
- on 900217,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.Caused by Failure to Complete Tech Spec Required post-maint Test. Post-maint Test Procedure Revised
| | | 05000412/LER-1990-002-01, :on 900117,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.On 900119, Discovered That Channel Returned to Svc W/O Completing Required Time Response Testing on Transmitter |
- on 900117,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.On 900119, Discovered That Channel Returned to Svc W/O Completing Required Time Response Testing on Transmitter
| | | 05000334/LER-1990-002, :on 900114,120-volt Ac Inverter for Vital Bus 3 Experienced Blown Dc Input Fuse When Inverter Bypassed & Aligned to 480-volt Ac Emergency Power.Caused by Mgt Action. Administrative Guidance Issued |
- on 900114,120-volt Ac Inverter for Vital Bus 3 Experienced Blown Dc Input Fuse When Inverter Bypassed & Aligned to 480-volt Ac Emergency Power.Caused by Mgt Action. Administrative Guidance Issued
| | | 05000412/LER-1990-003-01, :on 900403,determined That Surveillance Test for Battery 3 Not Performed on Scheduled Date of 900329. Caused by Personnel Error.Inpo Human Performance Evaluation Sys Analysis Performed & Procedures Revised |
- on 900403,determined That Surveillance Test for Battery 3 Not Performed on Scheduled Date of 900329. Caused by Personnel Error.Inpo Human Performance Evaluation Sys Analysis Performed & Procedures Revised
| | | 05000334/LER-1990-003, :on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Lines Lacked Automatic,Remote Manual or Locked Shut Isolation Valve. Exemption Request from GDC 57 Initiated |
- on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Lines Lacked Automatic,Remote Manual or Locked Shut Isolation Valve. Exemption Request from GDC 57 Initiated
| | | 05000412/LER-1990-004, :on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Incorrect Assessment of Plant Configuration Prior to Breaker Closure. Safety Injection Sys Reset |
- on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Incorrect Assessment of Plant Configuration Prior to Breaker Closure. Safety Injection Sys Reset
| | | 05000412/LER-1990-004-01, :on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Personnel Closing Breaker Before Resetting Safety Injection Sys Signal.Signal Reset |
- on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Personnel Closing Breaker Before Resetting Safety Injection Sys Signal.Signal Reset
| | | 05000334/LER-1990-004, :on 900124:discovered That Control Rod Positions Not Recorded on Operator Logs on 890425 When Control Rod Insertion Limit Monitor & Deviation Alarm Out of Svc.Cause Not Stated.Personnel Counseled |
- on 900124:discovered That Control Rod Positions Not Recorded on Operator Logs on 890425 When Control Rod Insertion Limit Monitor & Deviation Alarm Out of Svc.Cause Not Stated.Personnel Counseled
| | | 05000412/LER-1990-005-01, :on 900424,discovered That Three Valves in Quench Spray Chemical Addition Sys Had Spuriously Closed & Review Found That Two Had Closed on 900423.Caused by Error in Switch Calibr Procedures.Procedures Revised |
- on 900424,discovered That Three Valves in Quench Spray Chemical Addition Sys Had Spuriously Closed & Review Found That Two Had Closed on 900423.Caused by Error in Switch Calibr Procedures.Procedures Revised
| | | 05000412/LER-1990-005, :on 900209,defect Found in Casing of Limitorque Model HBC-1 Gear Operators,Causing Valve Motion to Cease Prematurely in Open Direction.Caused by Excess Matl on Housings.Also Reported Per Part 21 |
- on 900209,defect Found in Casing of Limitorque Model HBC-1 Gear Operators,Causing Valve Motion to Cease Prematurely in Open Direction.Caused by Excess Matl on Housings.Also Reported Per Part 21
| | | 05000412/LER-1990-006, :on 900605,containment Isolation Valves Exceeded Stroke Time Limit,Per Tech Spec 3.6.3.1.Caused by Deficient Surveillance Program.Surveillance Procedures Revised to Include Stroke Time Requirements |
- on 900605,containment Isolation Valves Exceeded Stroke Time Limit,Per Tech Spec 3.6.3.1.Caused by Deficient Surveillance Program.Surveillance Procedures Revised to Include Stroke Time Requirements
| | | 05000334/LER-1990-006, :on 900227,plant Operation in Excess of Licensing Basis.Caused by Failure of Computer to Synchronize File Addresses in Task 3D.Heat Balance Calculations Reverified Using Data from Plant Variable Computer |
- on 900227,plant Operation in Excess of Licensing Basis.Caused by Failure of Computer to Synchronize File Addresses in Task 3D.Heat Balance Calculations Reverified Using Data from Plant Variable Computer
| | | 05000412/LER-1990-007-01, :on 900622,refueling Cavity Drain Flanges Found to Be Installed During Operation.Caused by Deficiency in Transfer Canal Draining Procedure.Procedure Revised to Verify Removal of Flanges After Canal Drained |
- on 900622,refueling Cavity Drain Flanges Found to Be Installed During Operation.Caused by Deficiency in Transfer Canal Draining Procedure.Procedure Revised to Verify Removal of Flanges After Canal Drained
| | | 05000412/LER-1990-007, Responds to NRC Re Deviation 50-412/90-12-01 Noted in Insp Rept 50-412/90-12.Corrective Actions:Procedure OM 2.20-4.I Revised to Require Removal of Flanges Following Drain Operations & LER 90-007-00 Issued | Responds to NRC Re Deviation 50-412/90-12-01 Noted in Insp Rept 50-412/90-12.Corrective Actions:Procedure OM 2.20-4.I Revised to Require Removal of Flanges Following Drain Operations & LER 90-007-00 Issued | | | 05000334/LER-1990-008, :on 900401,RCS Letdown Isolation/Esf Actuation Occurred.Erratic Automatic Response of Condenser Steam Valve PCV-MS-106A Caused RCS Temp to Decrease Below Tech Spec Min. Operators Took Manual Control & Shut Valve |
- on 900401,RCS Letdown Isolation/Esf Actuation Occurred.Erratic Automatic Response of Condenser Steam Valve PCV-MS-106A Caused RCS Temp to Decrease Below Tech Spec Min. Operators Took Manual Control & Shut Valve
| | | 05000412/LER-1990-008-01, :on 900702,reactor Trip Occurred,Resulting from Turbine/Generator Trip.Caused by Personnel Error Which Resulted in Protection Relay Actuation.Event Reviewed W/Personnel & Design Mod Being Reviewed |
- on 900702,reactor Trip Occurred,Resulting from Turbine/Generator Trip.Caused by Personnel Error Which Resulted in Protection Relay Actuation.Event Reviewed W/Personnel & Design Mod Being Reviewed
| | | 05000412/LER-1990-009-01, :on 900902,letdown Isolation on Loss of Containment Instrument Air Pressure Occurred.Caused by Deviation from Surveillance Procedure to Protect Plant Equipment from Unnecessary Stress |
- on 900902,letdown Isolation on Loss of Containment Instrument Air Pressure Occurred.Caused by Deviation from Surveillance Procedure to Protect Plant Equipment from Unnecessary Stress
| | | 05000412/LER-1990-010-01, :on 900904:letdown Isolation Occurred Due to Low Pressurizer Water Level.Caused by Interaction of Control Sys Dump Operation Combined W/Effects of Hydraulic Coupling of Rcs.Pressurizer Level Restored |
- on 900904:letdown Isolation Occurred Due to Low Pressurizer Water Level.Caused by Interaction of Control Sys Dump Operation Combined W/Effects of Hydraulic Coupling of Rcs.Pressurizer Level Restored
| | | 05000334/LER-1990-010, :on 900714,automatic Isolation of Reactor Coolant Letdown Sys Initiated When Transient/Cooldown Caused Pressurizer Level to Decrease Below Setpoint.Msiv Stroke Time Surveillance Tests Revised |
- on 900714,automatic Isolation of Reactor Coolant Letdown Sys Initiated When Transient/Cooldown Caused Pressurizer Level to Decrease Below Setpoint.Msiv Stroke Time Surveillance Tests Revised
| | | 05000334/LER-1990-011, :on 900719,ESF Actuation - Inadvertent Trip of Reactor Coolant Pump a Occurred During Maint Surveillance Procedure.Caused by Personnel Error.Procedures Revised |
- on 900719,ESF Actuation - Inadvertent Trip of Reactor Coolant Pump a Occurred During Maint Surveillance Procedure.Caused by Personnel Error.Procedures Revised
| | | 05000412/LER-1990-011, :on 900906,ESF Actuation & Containment Purge Occurred Due to High Radiation Signal.Caused by Electrical Disturbances Due to Lightning Strike.Damaged Instruments Replaced |
- on 900906,ESF Actuation & Containment Purge Occurred Due to High Radiation Signal.Caused by Electrical Disturbances Due to Lightning Strike.Damaged Instruments Replaced
| | | 05000412/LER-1990-012-01, :on 900913,ESF Actuation Involving Containment Purge Isolation Occurred.Caused by Communication Error by Personnel.Maint Surveillance Procedures for Control Room Radiation Monitors to Be Revised |
- on 900913,ESF Actuation Involving Containment Purge Isolation Occurred.Caused by Communication Error by Personnel.Maint Surveillance Procedures for Control Room Radiation Monitors to Be Revised
| | | 05000334/LER-1990-012, :on 900801,control Room Received 2 Battery Charger Failure Alarm.Caused by Failure of Battery Input Breaker a Phase Lug.Failed Input Breaker Replaced W/ Qualified,Equivalent Spare Breaker |
- on 900801,control Room Received 2 Battery Charger Failure Alarm.Caused by Failure of Battery Input Breaker a Phase Lug.Failed Input Breaker Replaced W/ Qualified,Equivalent Spare Breaker
| | | 05000334/LER-1990-013, :on 900815,control Room Emergency Breathing Air Pressurization Sys Actuated,Pressurizing Common Control Room Envelope.Caused by Erroneous Signal Spike.Monitor Output Signals Disabled |
- on 900815,control Room Emergency Breathing Air Pressurization Sys Actuated,Pressurizing Common Control Room Envelope.Caused by Erroneous Signal Spike.Monitor Output Signals Disabled
| | | 05000412/LER-1990-013-01, :on 900915,ESF Actuation Containment Purge Isolation Occurred During Reactor Cavity Fill.Caused by Water Turbulence.Operators Verified Containment Purge Isolation Dampers Closed in Response to Alarm |
- on 900915,ESF Actuation Containment Purge Isolation Occurred During Reactor Cavity Fill.Caused by Water Turbulence.Operators Verified Containment Purge Isolation Dampers Closed in Response to Alarm
| | | 05000412/LER-1990-014-01, :on 900916,ESF Actuation - Containment Purge Isolation Occurred During Upper Internals Lift |
- on 900916,ESF Actuation - Containment Purge Isolation Occurred During Upper Internals Lift
| | | 05000334/LER-1990-014, :on 900831,ESF Actuation Steam Generator Blowdown Isolation Occurred.Caused by Failure of Steam Driven Auxiliary Feedwater Pump Discharge Pressure Switch. Pressure Switch Replaced |
- on 900831,ESF Actuation Steam Generator Blowdown Isolation Occurred.Caused by Failure of Steam Driven Auxiliary Feedwater Pump Discharge Pressure Switch. Pressure Switch Replaced
| | | 05000412/LER-1990-015, :on 900913,insp Discovered 25 Containment Liner Weld Test Channel Vent Plugs Missing |
- on 900913,insp Discovered 25 Containment Liner Weld Test Channel Vent Plugs Missing
| | | 05000334/LER-1990-015-01, :on 901006,ESF Actuation Resulted in Closure of Main Steam Trip Valve During Partial Stroke Testing of MSIVs |
- on 901006,ESF Actuation Resulted in Closure of Main Steam Trip Valve During Partial Stroke Testing of MSIVs
| | | 05000412/LER-1990-016, :on 900921,svc Water Sys Flow Found to Be Blocked Due to Buildup Corrosion Products |
- on 900921,svc Water Sys Flow Found to Be Blocked Due to Buildup Corrosion Products
| | | 05000334/LER-1990-016-01, :on 901024,ESF Actuation - Low Head Safety Injection Recirculation Valve Closed During Testing |
- on 901024,ESF Actuation - Low Head Safety Injection Recirculation Valve Closed During Testing
| | | 05000334/LER-1990-017-01, :on 901027,auxiliary Bldg Ventilation Relignment Occurred Due to Radiation Monitor Alarm |
- on 901027,auxiliary Bldg Ventilation Relignment Occurred Due to Radiation Monitor Alarm
| | | 05000412/LER-1990-017, :on 900927,during Recirculation Spray Pump Test,Pumps B,C & D Did Not Start After Containment Isolation Phase B Signal.Caused by Delay Timer Setpoint Drift.Timers Replaced |
- on 900927,during Recirculation Spray Pump Test,Pumps B,C & D Did Not Start After Containment Isolation Phase B Signal.Caused by Delay Timer Setpoint Drift.Timers Replaced
| | | 05000334/LER-1990-017, :on 901027,ESF Actuation - Radiation Monitor Alarm Caused Auxiliary Bldg Ventilation Realignment |
- on 901027,ESF Actuation - Radiation Monitor Alarm Caused Auxiliary Bldg Ventilation Realignment
| | | 05000412/LER-1990-018, :on 901026,ESF Actuation - Inadvertent Diesel Start Occurred & Deficiency Discovered in D/G Ventilation Fan Circuit |
- on 901026,ESF Actuation - Inadvertent Diesel Start Occurred & Deficiency Discovered in D/G Ventilation Fan Circuit
| | | 05000334/LER-1990-018-01, :on 901211,ESF Actuation - Automatic Start of Standby River Water Pump Occurred During Performance of Surveillance Test.Caused by Operator Error.Pump Shut Down & Operator Counseled |
- on 901211,ESF Actuation - Automatic Start of Standby River Water Pump Occurred During Performance of Surveillance Test.Caused by Operator Error.Pump Shut Down & Operator Counseled
| | | 05000334/LER-1990-019-01, :on 901226,MSIV Closed During Partial Stroke Testing,Isolating Steam from SG B.Caused by tar-like Matl Accumulation on Valve Test Limit Switch.Switch Replaced & Design Changed to Modify MSIV Test Circuit |
- on 901226,MSIV Closed During Partial Stroke Testing,Isolating Steam from SG B.Caused by tar-like Matl Accumulation on Valve Test Limit Switch.Switch Replaced & Design Changed to Modify MSIV Test Circuit
| | | 05000412/LER-1990-019, :on 901105,fault Occurred on 138-kV Bus,Causing Loss of Power to Train a Normal & Emergency 4 Kv Buses. Caused by Adverse Weather Conditions.Air Bottles Isolated & Signal Reset |
- on 901105,fault Occurred on 138-kV Bus,Causing Loss of Power to Train a Normal & Emergency 4 Kv Buses. Caused by Adverse Weather Conditions.Air Bottles Isolated & Signal Reset
| | | 05000412/LER-1990-020, :on 901112,inadvertent Reactor Trip Occurred During RTD Verification Test |
- on 901112,inadvertent Reactor Trip Occurred During RTD Verification Test
| | | 05000334/LER-1990-020-01, :on 901217,review of Plant Logs Determined That Memory Allocation Error Occurred in Computer Operation. Caused by Dynamic Memory Allocation Problem.Plant Parameters Remained within Required Thermal Limits |
- on 901217,review of Plant Logs Determined That Memory Allocation Error Occurred in Computer Operation. Caused by Dynamic Memory Allocation Problem.Plant Parameters Remained within Required Thermal Limits
| | | 05000412/LER-1990-021, :on 901113,ESF Actuation & Feedwater Isolation Occurred During MSIV Stroke Testing.Caused by Operator Error.Feedwater Isolation Signal Reset & Isolation Valves Reopened |
- on 901113,ESF Actuation & Feedwater Isolation Occurred During MSIV Stroke Testing.Caused by Operator Error.Feedwater Isolation Signal Reset & Isolation Valves Reopened
| | | 05000412/LER-1990-022, :on 901019,discovered Inadequate Electrical Isolation Between Control & Protection Circuits |
- on 901019,discovered Inadequate Electrical Isolation Between Control & Protection Circuits
| | | 05000412/LER-1990-023, :on 901114,ESF Actuation & Feedwater Isolation Occurred in Response to Opening Condenser Steam Dump Valve. Caused by Operation of Steam Dump Sys in Steam Pressure Control Mode.Signal Reset |
- on 901114,ESF Actuation & Feedwater Isolation Occurred in Response to Opening Condenser Steam Dump Valve. Caused by Operation of Steam Dump Sys in Steam Pressure Control Mode.Signal Reset
| | | 05000412/LER-1990-024, :on 901112,discovered That Boric Acid Storage Tank Sample Exceeded 7-day Surveillance Required by Ts. Caused by Abnormal Evolution.Personnel Counseled |
- on 901112,discovered That Boric Acid Storage Tank Sample Exceeded 7-day Surveillance Required by Ts. Caused by Abnormal Evolution.Personnel Counseled
| | | 05000412/LER-1990-025, :on 901201,intake Structure Instrument Air Compressor Failed to Automatically Start on Low Air Pressure During Power Operation.Caused by Failed Pressure Switch.New Pressure Switch Calibr & Installed |
- on 901201,intake Structure Instrument Air Compressor Failed to Automatically Start on Low Air Pressure During Power Operation.Caused by Failed Pressure Switch.New Pressure Switch Calibr & Installed
| | | 05000412/LER-1990-026, :on 901202,loss of Flow Alarm Received on Containment Airborne Radiation Monitor Skid.Monitor Inlet Isolation Valve Found Shut Due to Isolation Valve Limit Switch Being Out of Adjustment |
- on 901202,loss of Flow Alarm Received on Containment Airborne Radiation Monitor Skid.Monitor Inlet Isolation Valve Found Shut Due to Isolation Valve Limit Switch Being Out of Adjustment
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