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'%f Telephone (412) 393-6000 Nuclear Group P.O Box 4 Shippingport FA 15077MM i
February 251993
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ND3MNO:3417 1
i Beaver Valley Power Station, Unit No. 2 l
Docket No. 50-412, Licensee No. NPD-73 LER 93-001-00 l
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United States Nuclear Regulatory Commission l
Document Control Desk Washington, DC 20555 i
Gentlemen:
In accordance with Appendix A, Beaver Valley Technical Specifications, the following Licensee Event Report is submitted:
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i LER 93-001-00,10 CFR 50.73.a.2.ii.B, " Design Stress for the Auxiliary i
Feedwater System Exceeded Due to Water Hammer."
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j Freeland l
General Manager i
Nuclear Operations
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February 251993 ND3MNO:3417
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Mr. T. T. Martin, Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Road i
King of Prussia, PA 19406 Mr. G. E. Edison, BVPS Licensing Project Manager United States nuclear Regulatory Commission Washington, DC 20555 Larry Rossbach, Nuclear Regulatory Commission, BVPS Senior Resident Inspector l
J. A. Holtz, Ohio Edison 76 S. Main Street Akron, OH 44308 l
Larry Beck Centerior Energy 6200 Oak Tree Blvd.
Independence, OH 44101-4661 INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, GA 30339 t
G. E. Muckle, Factory Mutual Engineering 680 Anderson Drive #BLD10 Pittsburgh, PA 15220-2773 Mr. Richard Janati Department of Environmental Resources P.O. Box 2063 16th Floor, Fulton Building Harrisburg, PA 17120 Director, Safety Evaluation & Control Virginia Electric & Power Co.
P.O. Box 26666 One James River Plaza t
Richmond, VA 23261 E
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FOCILITV NAME (15 DOCKET IWUMBE R (24
' AGE 4 Beaver Valley Power Station Unit 2 o ;5 ; o g o ; o ; 4; 1l 2 ilorlOg4 TITLE to:
Design Stress Fcr The Auxiliary Feedwater System Exceeded Due To Water Harnmer EVENT DATE (5)
LER NUMBE R 16)
REPORT DATE 47p OTHER S ACtLtTitS INVOLVED 181 MONTH Day YE. AR YEAR MON T M DAY YEAR F ADuiv Nawts DOCw(T NUMBE RiSI g
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On 1/26/93 at 1720
- hours, the results of extensive engineering analysis of previous plant events identified that the stress on the Auxiliary Feedwater (AFW) piping to the "C" Steam Generator, for combined water hammer and seismic events, exceeded the design stress allowables.
It has been hypothesized that the "C" AFW line has been subjected to water hammer due to steam pocket formation (voiding) and steam bubble collapse.
There have been two events at Beaver Valley Power Station Unit 2 since it went operational in 1987 that have been attributed to water hammer.
The location of the inside containment AFW check valves (inside CV's) and piping layout have the potential to
cause
voiding (see Figure 1).
The inside CV's are located near the main feedwater lines causincJ the piping upstream to be at elevated temperatures.
The inside CV's are also at a
higher elevation
.a n the AFW supply tank minimum water level.
If the inside CV's leak rate is less than the outside CV's, the AFW piping will depressurize causing voiding upstream of the inside CV's due to elevated temperatures.
AFW automatic actuation with unthrottled flow to a
voided AFW line is the main concern for water hammer.
There were minimal safety implications as a result of this event.
The mechanical snubbers were replaced with new hydraulic snubbers with a higher load rating.
NQC F.,m 366 (649)
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Description of Event
On 1/26/93 at 1720
- hours, the results of extensive engineering analysis of previous plant events identified that the stress on the Auxiliary Feedwater (AFW) piping to the "C"
Steam Generator, for combined water hammer and seismic events, exceeded the design stress allowables.
It has been hypothesized that the "C" AFW line has been subjected to water hammer due to steam pocket formation (voiding) and
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steam bubble collapse.
There have been two events at Beaver Valley Power Station Unit 2
since it went operational in 1987 that could be attributed to water hammer.
In event No 1, identified in April 1989, mechanical snubbers 2FWE-PSSP-009 and 2FWE-PSSP-010 on the "C" AFW line were found mechanically frozen durincJ an ISI inspection.
The cause of i
event no.
I was unknown at that time and the snubbers were replaced with identical new snubbers.
Event No.
2, identified in April 1992, t
j mechanical snubber 2FWE-PSSP-009 was found mechanically frozen and l
snubber 2FWE-PSSP-010 Pas found damaged during an ISI inspection on the l
l "C"
AFW line.
The cause for the snubber failure / damage was apparently i
due to excessive compressive or impact loading as a result of an unanticipated water hammer.
The mechanical snubbers were replaced with-new hydraulic snubbers with a higher load rating.
j i
l The location of the inside containment AFW check valves (inside CV's) l and piping layout have the potential to cause steam voiding (see Figure 1).
The inside CV's are located near the main feedwater lines causing l
the piping upstream to be at elevated temperatures (measured 268.3 degree F on top of pipe, 200 degrees F on bottom of pipe, approximately 2
feet upstream of the "C" AFW check valve).
The inside CV's are at a higher elevation than the AFW supply tank minimum water level.
If the I
inside CV's leak rate is less than the outside CV's, the AFW piping will depressurize causing voiding upstream of the inside CV's due to elevated temperatures.
The "C" AFW line has been depressurized.
Cause of Event
e The results of extensive engineering analysis of previous plant events identified that the stress on the Auxiliary Feedwater (AFW) piping to the "C"
Steam Generator, for combined water hammer and seismic events, exceeded the design stress allowables.
The AFW piping and pipe l
supports are classified as QA Category I, seismic, safety class II.
The piping is designed to the requirements of the ASME Boiler and j
Pressure Vessel
- Code, Section
- III, 1971 Edition including addenda through Wint^r 1972.
The supports are designed to the guidelines established 7
the 6th Edition of the AISC manual of Steel Construction.
The AFW piping and supports have been designed for
- thermal, pressure,
- deadload, and seismic conditions.
Anticipated or l
" designed" water hammer transients were not previously analytically i
considered.
It was previously assumed that the piping layout and j
components had been designed to preclude the development of postulated I
water hammer events.
In retrospect, there is the potential for l
unanticipated water hammer as a
result of unthrottled AFW flow from j
automatic AFW pump starts to a potentially voided "C" AFW line.
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Corrective Actions
i The following corrective actions have been or will be taken as a result of this event:
1.
Frequent monitoring of the AFW piping for evidence of elevated containment penetration temperatures, system pressures (temporary pressure gages t
installed), noise / water hammer.
2.
A Basis for Continued Operation (BCO) has been prepared to document operation in this condition.
This is based upon analysis to quantify loads resulting from a postulated water hammer event.
3.
The Station is pursuing a long term solution.
4.
The Station will perform ISI inspections of the
]
AFW piping and piping supports in containment following an unplanned AFW pump start that results in unthrottled AFW flow.
5.
The mechanical snubbers were replaced with new hydraulic snubbers with a higher load rating.
The new hydraulic snubbers are adequately sized to withstand a water hammer event.
Reportability
i This report is being submitted in accordance with 10CFR50.73.a.2.ii.B because this event resulted in operation outside the Unit 2 design basis.
Safety Implications d
The safety implications are minimal.
Engineering analysis has shown that in cases where the pipe stress levels under the-revised load combinations (to include water hammer) occurring simultaneously with a
seismic event exceeded original design code normal / upset allowables, an assessment of system operability was made to the design code faulted allowables.
The pipe stress
- levels, for combined water hammer and seismic
- events, are now within the design code faulted allowables.
In developing the BCO, it was determinen that the use of alternate code faulted allowables (i.e. Appendix F or later revisions of the ASME code) was not required due to the rigorous analysis performed to more adequately quantify the stress.
Previous Similar Events
There were no previously reported similar events.
NRC Fem 3e6A (6491
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PDETRATIONS: X-79 X-88 AUX. FEED PUMPS X-83 2FWE-P22 2FWE-P23A 2FWE-P238 NRC Form 3ASA (649)
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| | | Reporting criterion |
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| 05000412/LER-1993-001, :on 930126,identified That Stress on AFW Piping to C SG Exceeded Design Stress Due to Water Hammer.Station Will Perform ISI Insps of AFW Piping & Replace Mechanical Snubbers W/New Hydraulic Snubbers |
- on 930126,identified That Stress on AFW Piping to C SG Exceeded Design Stress Due to Water Hammer.Station Will Perform ISI Insps of AFW Piping & Replace Mechanical Snubbers W/New Hydraulic Snubbers
| | | 05000334/LER-1993-001-01, :on 930212,discovered That Inadvertent Main Steam Isolation Valve Closure Would Generate Pressure Transient Which Would Result in Increased Loading.Caused by Stresses Om Main Steam Piping.Exam Reviewed |
- on 930212,discovered That Inadvertent Main Steam Isolation Valve Closure Would Generate Pressure Transient Which Would Result in Increased Loading.Caused by Stresses Om Main Steam Piping.Exam Reviewed
| | | 05000412/LER-1993-002, :on 930130,bistaples for Loop a Channel II Ms Pressure in Tripped Condition for Transmitter Replacement. Caused by Comparator Card Power Supply Failure.Associated Valves Actuated to Design Positions |
- on 930130,bistaples for Loop a Channel II Ms Pressure in Tripped Condition for Transmitter Replacement. Caused by Comparator Card Power Supply Failure.Associated Valves Actuated to Design Positions
| | | 05000334/LER-1993-002-01, :on 930212,discovered Inadvertent Tripping & Automatic Starting of River Water Pumps.Caused by Personnel Error.Operators Were Immediately Counseled |
- on 930212,discovered Inadvertent Tripping & Automatic Starting of River Water Pumps.Caused by Personnel Error.Operators Were Immediately Counseled
| | | 05000412/LER-1993-003, :on 930205,steam Generator Blowdown Sys Isolated Due to High Level in Steam Generator Blowdown Tank. Caused by Discrepancies Between Actual & Indicated Tank Level.Temporary Operating Procedure Written |
- on 930205,steam Generator Blowdown Sys Isolated Due to High Level in Steam Generator Blowdown Tank. Caused by Discrepancies Between Actual & Indicated Tank Level.Temporary Operating Procedure Written
| | | 05000334/LER-1993-003-01, :on 930217,electrical Noise Spike Caused Spurious High Radiation Alarm on CR Radiation Monitor & Actuated CR Emergency Habitability Sys.Operating Procedure 1/2.44.4A Performed |
- on 930217,electrical Noise Spike Caused Spurious High Radiation Alarm on CR Radiation Monitor & Actuated CR Emergency Habitability Sys.Operating Procedure 1/2.44.4A Performed
| | | 05000334/LER-1993-004, :on 930218,condition Identified Which Could Have Prevented Fulfillment of Sys to Control Release of Radioactive Matl.Eops Revised to Diagnose Problems Based on Increasing VCT Level |
- on 930218,condition Identified Which Could Have Prevented Fulfillment of Sys to Control Release of Radioactive Matl.Eops Revised to Diagnose Problems Based on Increasing VCT Level
| | | 05000412/LER-1993-004-01, :on 930302,130-volt Ground on Dc Bus 2-1 Experienced,Resulting in SG Blowdown Isolation.Caused by Personnel Error.Esf Actuation Warning Placards Placed on Breaker 8-1 & Supervisors Counseled |
- on 930302,130-volt Ground on Dc Bus 2-1 Experienced,Resulting in SG Blowdown Isolation.Caused by Personnel Error.Esf Actuation Warning Placards Placed on Breaker 8-1 & Supervisors Counseled
| | | 05000334/LER-1993-005, :on 930302,identified Discrepancy in QA Categorization of Solenoid Valve.Caused by Inappropriate Replacement of Valve During Maint in 1986.Design Change Process Includes Administrative Guidance |
- on 930302,identified Discrepancy in QA Categorization of Solenoid Valve.Caused by Inappropriate Replacement of Valve During Maint in 1986.Design Change Process Includes Administrative Guidance
| | | 05000412/LER-1993-005-01, :on 930304,Westinghouse Notified Util Re Potential for Inadequate Core Cooling Flow During Hot Leg Recirculation.Caused by Inadequate Analysis of Failure of Lhsi Discharge Movs.Procedure Revised |
- on 930304,Westinghouse Notified Util Re Potential for Inadequate Core Cooling Flow During Hot Leg Recirculation.Caused by Inadequate Analysis of Failure of Lhsi Discharge Movs.Procedure Revised
| | | 05000412/LER-1993-006, :on 930312,an Automatic Realignment of Contiguous Area Ventilation from Unfiltered to Filtered Exhaust Occurred Due to High Sensitivity of DG Controls. DG Procedure Will Be Revised |
- on 930312,an Automatic Realignment of Contiguous Area Ventilation from Unfiltered to Filtered Exhaust Occurred Due to High Sensitivity of DG Controls. DG Procedure Will Be Revised
| | | 05000334/LER-1993-006-01, :on 930415,two Operators Entered Posted Area W/O Radiation Monitoring Device & Entered Locked High Radiation Area & Left Barrier Open.Caused by Personnel Error in Judgement.Operators Counseled |
- on 930415,two Operators Entered Posted Area W/O Radiation Monitoring Device & Entered Locked High Radiation Area & Left Barrier Open.Caused by Personnel Error in Judgement.Operators Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000334/LER-1993-007-01, :on 930423,discoverd That Original Piping Did Not Conform to Design Code Requirement.Caused by Design Deficiency.Headers Fitted W/Code Approved End Caps & Tested & Now Conform to Design Requirements |
- on 930423,discoverd That Original Piping Did Not Conform to Design Code Requirement.Caused by Design Deficiency.Headers Fitted W/Code Approved End Caps & Tested & Now Conform to Design Requirements
| | | 05000412/LER-1993-007, :on 930405,identified Deficiency in Testing of Reactor Trip Breaker Manual Shunt Trip Circuitry.Caused by Deficient Procedure.All Licensed Operators Will Receive Training on ATWS as Part of Retraining |
- on 930405,identified Deficiency in Testing of Reactor Trip Breaker Manual Shunt Trip Circuitry.Caused by Deficient Procedure.All Licensed Operators Will Receive Training on ATWS as Part of Retraining
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000334/LER-1993-008, :on 930423,leakage Detected Through Two Check Valves in Chlorine Injection Line.Caused by Failure to Include Valves in ASME Section XI Testing Program.Check Valves Added to ASME Testing Program |
- on 930423,leakage Detected Through Two Check Valves in Chlorine Injection Line.Caused by Failure to Include Valves in ASME Section XI Testing Program.Check Valves Added to ASME Testing Program
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000334/LER-1993-009, :on 930607,high Radiation Area Barrier Was Unlocked Due to Personnel Error.Comprehensive Confirmation Survey Performed,Personnel Interviewed & Task Force Formed |
- on 930607,high Radiation Area Barrier Was Unlocked Due to Personnel Error.Comprehensive Confirmation Survey Performed,Personnel Interviewed & Task Force Formed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | | 05000412/LER-1993-009-01, :on 930902,failure to Calibr Radiation Monitor Velocity Probes Identified.Caused by Personnel Error.Maint Planning & Scheduling Sys Updated to Include Calibrations of Involved Velocity Probes |
- on 930902,failure to Calibr Radiation Monitor Velocity Probes Identified.Caused by Personnel Error.Maint Planning & Scheduling Sys Updated to Include Calibrations of Involved Velocity Probes
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000334/LER-1993-010, :on 930614,determined That TS Surveillance on SI Accumulator Samples Missed Due to Draining & Refilling Accumulators Several Times During Outage.Accumulators a & C Immediately Sampled |
- on 930614,determined That TS Surveillance on SI Accumulator Samples Missed Due to Draining & Refilling Accumulators Several Times During Outage.Accumulators a & C Immediately Sampled
| 10 CFR 50.73(a)(2)(x) | | 05000412/LER-1993-010-01, :on 931004,identified Deteriorated Electrical Insulation in Rc Loop RTD Due to Inadequate Installation of Thermal Insulation on RCS Piping Where RTDs Penetrate. Replaced RTDs |
- on 931004,identified Deteriorated Electrical Insulation in Rc Loop RTD Due to Inadequate Installation of Thermal Insulation on RCS Piping Where RTDs Penetrate. Replaced RTDs
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000334/LER-1993-011, :on 930619,ESF Actuation Letdown Isolation Occurred While Synchronizing Main Unit Generator.Caused by Cooldown of RCS Due to Steam Demand.Plant Stabilized within Three Minutes & Pressurizer Level Restored |
- on 930619,ESF Actuation Letdown Isolation Occurred While Synchronizing Main Unit Generator.Caused by Cooldown of RCS Due to Steam Demand.Plant Stabilized within Three Minutes & Pressurizer Level Restored
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | | 05000412/LER-1993-011-01, :on 931006,containment Closure Deficiency During Refueling Occurred.Caused by Incomplete Installation of Temporary Seal on Spare Penetration Through Primary Containment Bldg.Control Room Notified |
- on 931006,containment Closure Deficiency During Refueling Occurred.Caused by Incomplete Installation of Temporary Seal on Spare Penetration Through Primary Containment Bldg.Control Room Notified
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000334/LER-1993-012, :on 930702,discovered That Hydrogen Analyzer Inoperable During Quarterly Performance of Calibration Procedure.Test Personnel Contributed to Cause of Event.Test & Calibration Procedures Will Be Revised |
- on 930702,discovered That Hydrogen Analyzer Inoperable During Quarterly Performance of Calibration Procedure.Test Personnel Contributed to Cause of Event.Test & Calibration Procedures Will Be Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000412/LER-1993-012-01, :on 931106,EDG Sequencer Circuit Deficiencies Occurred Due to Misoperation of Digital Solid State Timer Associated W/Load Sequencer Circuitry.Functionally Tested & Returned EDG to Svc on 931116 |
- on 931106,EDG Sequencer Circuit Deficiencies Occurred Due to Misoperation of Digital Solid State Timer Associated W/Load Sequencer Circuitry.Functionally Tested & Returned EDG to Svc on 931116
| 10 CFR 50.73(a)(2)(x) | | 05000334/LER-1993-013, :on 931012,unit 1 RT Occurred & Required Shutdown Due to Loss of Offsite Power in Units 1 & 2. Caused by Personnel Error.Performed Detailed Root Cause Analysis |
- on 931012,unit 1 RT Occurred & Required Shutdown Due to Loss of Offsite Power in Units 1 & 2. Caused by Personnel Error.Performed Detailed Root Cause Analysis
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000412/LER-1993-013-01, :on 931109,identified Error in Original Test Analysis Resulted in Failure to Plug to Degraded Tube.Caused by Personnel Error.Degraded Tube Plugged During Fourth Refueling Outage |
- on 931109,identified Error in Original Test Analysis Resulted in Failure to Plug to Degraded Tube.Caused by Personnel Error.Degraded Tube Plugged During Fourth Refueling Outage
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000334/LER-1993-014, :on 931021,identified That Surveillance Test Conducted on 930731 Stroked Valve to Closed Position Resulting in Missed Surveillance.Caused by Personnel Error. Involved Individual Received Written Reprimand |
- on 931021,identified That Surveillance Test Conducted on 930731 Stroked Valve to Closed Position Resulting in Missed Surveillance.Caused by Personnel Error. Involved Individual Received Written Reprimand
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000412/LER-1993-014-01, :on 931129,required Plant Shutdown Occurred Due to Inoperable Sdafp.Caused by Improper Reassembly of 2MSS*S0V105A & Stem Failure on 2MSS*S0V105D.Steam Supply Valve Reinstalled & Solenoid Tightened |
- on 931129,required Plant Shutdown Occurred Due to Inoperable Sdafp.Caused by Improper Reassembly of 2MSS*S0V105A & Stem Failure on 2MSS*S0V105D.Steam Supply Valve Reinstalled & Solenoid Tightened
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) | | 05000334/LER-1993-015, :on 931101,recognized That TS Violation Occurred When Power Restored to Loop Isolation Valves for Isolated Rcl Due to Inadequate Work Organization & Planning. Caution Tags Posted on 480 Volt Ac Breakers |
- on 931101,recognized That TS Violation Occurred When Power Restored to Loop Isolation Valves for Isolated Rcl Due to Inadequate Work Organization & Planning. Caution Tags Posted on 480 Volt Ac Breakers
| | | 05000412/LER-1993-015, :on 931205,identified That Oxygen Analyzers Inlet Header Insolation Valve 2GWS-306 Closed,Causing Oxygen Analyzer to Be Inoperable.Subj Valve Returned to Normal Open Position |
- on 931205,identified That Oxygen Analyzers Inlet Header Insolation Valve 2GWS-306 Closed,Causing Oxygen Analyzer to Be Inoperable.Subj Valve Returned to Normal Open Position
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000412/LER-1993-016, :on 931209,inadvertent Deactivation of Signal from Two Containment Isolation Valves Occurred.Caused by Personnel Error.Temporary Mod 2-94-001 Implemented on 931210,restoring Power to Auxiliary Relays |
- on 931209,inadvertent Deactivation of Signal from Two Containment Isolation Valves Occurred.Caused by Personnel Error.Temporary Mod 2-94-001 Implemented on 931210,restoring Power to Auxiliary Relays
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