05000395/LER-2005-003

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LER-2005-003, PLANT TRIP AND ASSOCIATED FIRE IN S' CONDENSATE PUMP MOTOR
Docket Number
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
3952005003R01 - NRC Website

PLANT IDENTIFICATION

Westinghouse - Pressurized Water Reactor

EQUIPMENT IDENTIFICATION

XPP0042B, 'B' Condensate Pump XVB00614A-CO, 'A' Condensate Pump Discharge Valve

IDENTIFICATION OF EVENT

At approximately 1126 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.28443e-4 months <br /> on August 25, 2005, operators noticed 'B' Condensate (CO) pump had tripped. The 'A' CO pump was started. The 'A' CO pump discharge valve, XVB00614A-CO, did not respond as expected. Efforts to open the pump discharge valve, XVB00614A-CO, were unsuccessful and Deaerator (DA) level continued to drop. The operators were instructed to reduce power. During this time frame, smoke was reported issuing from 'B' CO pump motor. The Fire Brigade was dispatched to the scene.

Further attempts to open XVG00614A-CO were unsuccessful. Additional instructions were given to lower power further by 1% per minute in order to regain DA level. At 2.8 feet in the DA, the REACTOR TRIP order was given, but the reactor automatically tripped when Lo-Lo DA level caused the Feedwater Pumps (FWPs) and Feedwater Booster Pumps (FWBPs) to trip, thereby tripping the Main Turbine which tripped the Reactor per the P9 permissive (RX Power >50%). During this event, the fire reported in the 'B' CO pump motor was still not extinguished and a call for offsite assistance was made. At 1141, a NOTIFICATION OF UNUSUAL EVENT (NUE) was declared for a "FIRE IN THE PROTECTED AREA OR SWITCHYARD LASTING LONGER THAN 15 MINUTES". The fire was declared out at 1317 and the NUE was downgraded at 1327.

EVENT DATE

08/25/2005

REPORT DATE

October 24, 2005 Original submittal March 27, 2007 Revision 1

CONDITIONS PRIOR TO EVENT

Mode 1, 100% Power

DESCRIPTION OF EVENT

At approximately 1126 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.28443e-4 months <br /> on August 25, 2005, operators noticed 'B' Condensate (CO) pump had tripped. The Exhaust Hood Spray pumps were noticed to be running which would be expected due to low condensate pressure. The 'A' CO pump was started. The 'A' CO pump discharge valve, XVB00614A-CO, did not open as expected. Efforts to open the pump discharge valve, XVB00614A-CO, were unsuccessful. During this time Deaerator (DA) level was continuing to drop. The operators were instructed to reduce power. The Balance of Plant (BOP) operator was instructed to reduce load by manipulating the LOAD LIMITER one/half turn in the DECREASE direction, and the Nuclear Reactor Operator at the Controls (NROATC) was instructed to reduce power by borating 50 gallons.

During this time frame, smoke was reported issuing from 'B' CO pump motor. The Fire Brigade was dispatched to the scene.

DESCRIPTION OF EVENT (Continued) The BOP operator was instructed per procedure to reduce CO flow to the DA slightly by closing down on the DA Flow Control Valve in order to reduce CO delta-p enough to enable XVG00614A-CO to open. This proved unsuccessful. Further instructions were given to lower power further by 1% per minute in order to regain DA level. The decision was made to insert a MANUAL REACTOR TRIP if DA level approached 2.5 feet narrow range. At 2.8 feet, the REACTOR TRIP order was given, but the reactor tripped when LO-LO DA level caused the Feedwater Pumps (FWPs) and Feedwater Booster Pumps (FWBPs) to trip, thereby tripping the Main Turbine which tripped the Reactor per the P9 permissive (RX Power >50%).

The Control Room entered EOP-1.0, REACTOR TRIP/SAFETY INJECTION ACTUATION, and then EOP-1.1, REACTOR TRIP RECOVERY, to stabilize the plant. At 1139, a call for offsite assistance was made. At 1141, a NOTIFICATION OF UNUSUAL EVENT (NUE) was declared for a "FIRE IN THE PROTECTED AREA OR SWITCHYARD LASTING LONGER THAN 15 MINUTES". At 1253, a small flame was noted in the pump motor housing upon removal of an inspection cover. At no time had flames been seen external to the motor housing. At 1317, the fire was declared out with a re-flash watch stationed. The NUE was downgraded at 1327.

CAUSE OF EVENT

The cause of the trip of the 'B' Condensate Pump was determined to be a phase to ground short in the motor windings. A root cause evaluation is being performed to determine the root cause(s) of the failure of XVG00614A-CO to open.

The cause of the delayed opening of the condensate pump discharge valve was addressed by Root Cause Analysis Report RCA 05-3349. The root cause team used the Failure Modes analysis (FMA) to determine the cause. The analysis identified that the valve shafts and bearings were severely worn and galled which led to binding under high dP conditions. None of the three Condensate Pump discharge valves had ever been inspected for bearing wear since original installation. There are no vendor recommendations for periodic replacement or inspection.

ANALYSIS OF EVENT

When the 'A' CO Pump started and XVG00614A-CO failed to open, DA level decreased to the trip set point tripping all Feedwater Pumps and Feedwater Booster Pumps. This in turn tripped the Main Turbine, which tripped the Reactor per the P9 permissive (Rx Power >50%).

All plant equipment responded to the trip as designed.

Wear and galling were found on the valve shafts at the bearing locations and in both the upper and lower bearings in the valve body. The wear in these load bearing surfaces created a binding of the valve load bearing surfaces which could not be overcome under high dP conditions. Diagnostic testing of VCSNS air operated valves performed on all new components in RF16 showed a higher than expected opening load requirement. This, coupled with the as-found degraded valve internals, supports the conclusions developed by the root cause team.

A review of the vendor manual determined that neither preventive maintenance nor operation information was provided.

Discussions with the vendor indicated that no specific guidance is provided for these simple type valves.

CORRECTIVE ACTIONS

Condition Evaluation Report (CER) C-05-3349 was generated to document the event and perform a root cause evaluation to determine additional appropriate corrective actions for the failure of XVG00614A-CO to open. The discharge valve for the standby Condensate Pump was failed in the open position. During the Fall 2006 refueling outage XVG00614A-CO was disassembled and repaired.

CORRECTIVE ACTIONS (CONT'D) During RF16, all three Condensate Pump discharge valves were replaced or restored to original design.

Additional corrective actions, as determined through RCA 05-3349, include implementation of a periodic preventive maintenance inspection of the bearings and shafts. Additionally, an engineering review will be performed for other critical active butterfly valves to determine if they need to be included in the inspection program.

PRIOR OCCURRENCES

A similar event occurred in 1999, (CER 99-0007), where XVG00614A-CO took eight minutes to open. However, in that event, the plant did not trip.