05000382/FIN-2018002-02
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Finding | |
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| Title | 10 CFR 50.59 Evaluation Associated with Emergency Feedwater Logic Modification |
| Description | The licensee changed the emergency feedwater logic, as described in the Updated Final Safety Analysis Report (UFSAR), Section 7.3.1.1.6, from flow control mode to level control mode during a safety injection actuation signal. To accomplish this change, the licensee had to modify the following logic system signals and setpoints: steam generator critical level, steam generator lo level, steam generator lo-lo level, safety injection actuation, control board manual control, and the steam generator lo-lo level annunciator. The NRC team questioned whether the emergency feedwater modification required additional information to determine if the 10 CFR 50.59 evaluation was adequate, or if NRC approval was needed for the change. Specifically, the NRC team questioned if the emergency feedwater logic change: used a method of evaluation other than what was described in the UFSAR (e.g. the use of the TRANFLOW program) or would result in a more than minimal increase in the likelihood of occurrence of a malfunction of a system important to safety. Specifically, because the emergency feedwater logic change introduced the potential to overcool the reactor, and substituted a previous automatic action for manual operator action, the NRC team questioned if the change and associated 50.59 evaluation addressed these concerns. Planned Closure Actions: The NRC and the licensee are working to gather more information related to the Final Safety Analysis Report-described methods for steam generator analyses and if the change resulted in a more-than-minimal increase in risk. Specifically, the licensee plans to provide an analysis that demonstrates the emergency feedwater logic change would not result in a more than minimal increase in the likelihood of an overcooling accident. Licensee Actions: The licensee has implemented a compensatory measure to take manual control of the emergency feedwater system during a safety injection signal such that an overcooling event will be prevented. Corrective Action References: CR-WF3-2017-06067, CR-WF3-2017-05882, CR-WF3-2017-05173 |
| Site: | Waterford |
|---|---|
| Report | IR 05000382/2018002 Section 1R17 |
| Date counted | Jun 30, 2018 (2018Q2) |
| Type: | URI: |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.17 |
| Inspectors (proximate) | F Ramirez C Speer C Henderson W Sifre C Smith E Uribe G Miller |
| INPO aspect | |
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Finding - Waterford - IR 05000382/2018002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Waterford) @ 2018Q2
Self-Identified List (Waterford)
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