05000382/FIN-2018002-03
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Finding | |
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Title | Licensee-Identified Violation |
Description | This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. Violation: Technical Specification 3.6.3, Containment Isolation Valves, requires, in part, that when an isolation valve for containment penetrations associated with an open system are inoperable, the licensee must restore the inoperable valve(s) to operable status within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, isolate the affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or be in hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Contrary to the above, between December 8, 2017, and December 11, 2017, with containment isolation valves inoperable, the licensee did not restore the inoperable valves to operable status within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, isolate the affected penetrations within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or place the unit in hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The licensee restored the valves to operable status on December 20, 2017, exceeding the Technical Specification 3.6.3 allowed outage time by approximately 70 hours8.101852e-4 days <br />0.0194 hours <br />1.157407e-4 weeks <br />2.6635e-5 months <br />. Significance/Severity Level: The finding was of very low safety significance (Green) because the containment isolation valves were maintained closed during the period and did not represent an actual open pathway in the physical integrity of the reactor containment. Corrective Action Reference: CR-WF3-2018-00983 |
Site: | Waterford |
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Report | IR 05000382/2018002 Section 4OA3 |
Date counted | Jun 30, 2018 (2018Q2) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | F Ramirez C Speer C Henderson W Sifre C Smith E Uribe G Miller |
Violation of: | Technical Specification |
INPO aspect | |
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Finding - Waterford - IR 05000382/2018002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Waterford) @ 2018Q2
Self-Identified List (Waterford)
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