09-15-2005 | A valid automatic actuation of the reactor protection system was initiated by a main turbine trip that was caused by an invalid main generator lockout relay actuation. AA corroded disconnect position switch and concurrent ground on the balance of plant DC power distribution system adversely affected the main generator output breaker position monitoring circuit and caused the circuit to falsely sense that both main generator output breakers were open.A The corroded switch and ground were repaired and the unit was restarted.A Monitoring of the generator output breaker position monitoring circuit relays has been added to the operator rounds. Enhancements to the ground elimination processes, training and test equipment are planned. |
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Unit Conditions Prior to the Event Unit 1 was in Operational Condition (OPCON) 1 (Power Operation) at approximately 100% power. There were no structures, systems or components out of service that contributed to this event.
Description of the Event
On Monday July 18, 2005 Limerick Unit 1 was operating at 100% power. At 09:50 hours an automatic actuation of the reactor protection system (RPS) occurred as a result of a turbine (EIIS:TRB) trip. The operators entered the trip procedure for reactor pressure vessel (RPV) control (T-101) and stabilized reactor parameters. The operators verified that all control rods were fully inserted.
Reactor level initially decreased to a minimum of -3 inches and increased to a maximum of +34 inches then stabilized at +20 inches during level recovery. The +54 inch high-level turbine trip setpoint was not exceeded. Reactor pressure initially increased from 1035 to approximately 1154 psig, which is less than the lowest safety relief valve (SRV) setpoint of 1170 psig; no SRVs actuated. Reactor pressure then decreased to 910 psig and stabilized at 955 psig. The main steam bypass valves opened as designed to control pressure.
The reactor recirculation pumps (EIIS:AD) tripped on end-of-cycle recirculation pump trip (EOC-RPT) as designed due to a turbine trip at greater than 30 percent power. The redundant reactivity control system (RRCS) anticipated transient without scram (ATWS) trip actuated after the EOC-RPT trip when reactor pressure exceeded the trip setpoint of 1149 psig.
The post-scram investigation determined that generator lockout relay (EIIS:RLY) 386G-G101 had actuated. The 386G relay actuation was caused by an invalid actuation of the generator output breaker (EIIS:EL) position monitoring relays due to a DC ground. The 386G relay actuates if both Unit 1 generator output breakers (535 and 635) open. There were no relay targets present on any of the generator protection relays. This indicated an absence of a valid fault actuation signal to the generator lockout relays.
Immediately following the scram, I&C technicians were dispatched to monitor the temporary DC ground detection instrumentation that was installed to support in-progress DC ground troubleshooting.
There was no active troubleshooting in progress at the time of the scram. While observing instrumentation, the technicians noted a spike in ground current, which was concurrent with a main control room (MCR) alarm (EIIS:ALM) actuation. A degraded alarm horn (EIIS:IB) was replaced.
To support restart, the main generator protective relays were tested to ensure the actuation targets were functioning properly.
All relay targets operated as designed. Digital fault recorder (DFR) traces did not indicate any fault currents confirming that generator protection relays did not actuate on a valid fault condition.
The generator output breaker position monitoring circuit is comprised of two redundant channels (X and Y). Each channel monitors the position of both generator output breakers (535 and 635) and the generator disconnect (11 DISC). If both generator output breakers trip with the disconnect closed, the channel inputs a trip signal into the generator protective relay logic.
However, both channels must sense that both output breakers are tripped to actuate the 386G generator lockout relay.
Further investigation revealed corroded position switch (EIIS:33) contacts on the generator main disconnect (EIIS:FK). The investigation concluded that the X channel breaker position monitor circuit (relay 452X-1) was in a tripped condition prior to the scram due to the corroded disconnect position switch contacts. The investigation further concluded that the alarm horn ground combined with an existing ground to cause the 452Y-1 relay to change state and complete the generator lock-out logic.
The generator disconnects receive preventive maintenance.
However, no preventive maintenance is performed on the generator disconnect position switch that was corroded. Maintenance records could not be located on this switch.
A 4-hour NRC ENS notification was required by 10CFR50.72(b)(2)(iv)(B) for an actuation of RPS when the reactor was critical. An 8-hour NRC ENS notification was required by 10CFR50.72(b)(3)(iv)(A) for a valid actuation of RPS. The ENS notification (#41848) was completed on Monday July 18, 2005 at 11:15 EDT. This event involved an automatic actuation of RPS.
Therefore, this LER is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(iv)(A).
Analysis of the Event
There were no actual safety consequences associated with this event. The potential safety consequences of this event were minimal. A turbine trip with bypass transient is categorized as an incident of moderate frequency per UFSAR section 15.2.3 Turbine Trip. The plant equipment performed as designed during the transient and the operators effectively stabilized reactor parameters.
The failure of the annunciator buzzer resulted in a low resistance positive ground on the DC distribution system (EIIS:EI) at the time of the event. A neutral ground was also present preceding the event. The resulting ground current caused a false actuation of a relay in the Y channel of the main generator output breaker position monitoring circuit. An additional pre-existing condition was a corroded disconnect position switch contact. This switch failure resulted in the X channel being in the tripped condition prior to the event. When the Y channel actuated the logic was completed for an actuation of the main generator lockout protective relay. This resulted in a main generator lockout, main turbine trip and subsequent reactor scram. A simplified computer model of the circuit was used to verify that the identified grounds had the potential to cause the invalid relay operation.
Cause of the Event
The event was caused by concurrent positive and neutral grounds and a corroded disconnect position switch that caused a false actuation of the main generator output breaker position monitoring circuit. A root cause of the event was lack of preventive maintenance on the disconnect position switch contact. An additional root cause was less than adequate station ground fault location capability.
Corrective Action Completed The corroded disconnect position switch was repaired.
The grounded annunciator horn was replaced.
Visual inspections of the generator output breaker position monitoring circuit auxiliary relays were added to the operator rounds.
The main generator output disconnect preventive maintenance activities have been revised to include an inspection of disconnect position switches.
Corrective Action Planned Recommended improvements to the ground fault location panel and troubleshooting tools will be presented to the station Plant Health Committee. The presentation to the committee will be complete by November 28, 2005.
Previous Similar Occurrences A Unit 2 scram was reported in LER 2-00-001 due to a troubleshooting activity on a balance-of-plant DC ground on a transformer alarm circuit.
Component data:
System: � IB � (Annunciator System) Component: � ANN (Annunciator) Manufacturer: � 170E (Edwards) Part#: � 343A-P1
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Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000362/LER-2005-001 | Emergency Diesel Generator (EDG) 3G003 Declared Inoperable Due to Loose Wiring Connection on Emergency Supply Fan | | 05000263/LER-2005-001 | | | 05000456/LER-2005-001 | Potential Technical Specification (TS) 3.9.4 Violation Due to Imprecise Original TS and TS Bases Wording | | 05000454/LER-2005-001 | Failed Technical Specification Ventilation Surveillance Requirements During Surveillance Requirement 3.0.3 Delay Period | | 05000282/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2005-001 | Plant in a Condition Prohibited by Technical Specifications due to Error Making Control Room Ventilation System Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000400/LER-2005-001 | Reactor Auxiliary Building Emergency Exhaust System Single Failure Vulnerability | | 05000395/LER-2005-001 | Emergency Diesel Generator Start and Load Due To A Loss Of Vital Bus | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2005-001 | RCS Pressure Boundary Leakage Due to Primary Water Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000305/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2005-001 | Reactor Coolant System Leakage Detection Instrumentation Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2005-002 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000255/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-002 | Missing Taper Pins on CCW Valve Cause Technical Specification Required Shutdown | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000370/LER-2005-002 | Ice Condenser Lower Inlet Door Failed Surveillance Testing | | 05000353/LER-2005-002 | High Pressure Coolant Injection System Inoperable due to a Degraded Control Power Fuse Clip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000263/LER-2005-002 | | | 05000454/LER-2005-002 | One of Two Trains of Hydrogen Recombiners Inoperable Longer Than Allowed by Technical Specifications Due to Inadequate Procedure | | 05000244/LER-2005-002 | Emergency Diesel Generator Start Resulting From Loss of Off-Site Power Circuit 751 | | 05000362/LER-2005-002 | Emergency Containment Cooling Inoperable for Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2005-002 | DTechnical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by Gas Intrusion from a Leaking Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000265/LER-2005-002 | Main Steam Relief Valve Actuator Degradation Due to Failure to Correct Vibration Levels Exceeding Equipment Design Capacities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000286/LER-2005-002 | • Entergy Nuclear Northeast Indian Point Energy Center 450 Broadway, GSB P.O. Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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