02-16-2010 | On December 16, 2009, with the plant in Mode 1 at approximately 100 percent power, it was identified that one of the inputs to the secondary heat balance for steam temperature was indicating approximately 8 degrees F lower than the input for the opposite steam line temperature indication.
Based on heat balance calculations, this 8 degree F difference resulted in an indicated power of approximately 0.45 percent full power less than actual reactor thermal power. This 8 degree F difference resulted from a failed resistance temperature detector (RTD). The RTD failed due to the vibration of the main steam lines because the RTD was not long enough to ensure proper compression of the sensing element in the thermowell. A new RTD was installed, and this RTD will be replaced every two years until an RTD of appropriate length with better resistance to vibration is installed.
A review of historical plant computer data showed this temperature difference existed since April 2006, and resulted in the plant operating at a maximum 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average reactor power of 100.374 percent, which exceeded the maximum analyzed power level allowed by the Technical Specifications by 0.004 percent on one occasion. This issue is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as an operation prohibited by the Technical Specifications. |
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LER-2009-002, Vibration Induced Failure of Temperature Instrument Results in Operation above Licensed Power LimitDocket Number |
Event date: |
12-16-2009 |
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Report date: |
02-16-2010 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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3462009002R00 - NRC Website |
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Energy Industry Identification System (EllS) codes are identified in the text as [XX). All numerical values given in the discussion below are approximate, based on accuracy of the affected instruments and the averaging of historical computer data.
DESCRIPTION OF EVENT:
Applicable Technical Specifications:
Technical Specification (TS) Limiting Condition for Operation (LCO) 3.2.1 for Regulating Rod Insertion Limits requires that the regulating groups be within the physical insertion, sequence, and overlap limits specified in the Core Operating Limits Report (COLR) while in Modes 1 and 2. With regulating rod groups inserted in the restricted operation region, Surveillance Requirement 3.2.5.1 is required to be performed once per 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> if reactor thermal power is greater than 20 percent, and the regulating rod groups are required to be restored to within limits in 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> from discovery. The corresponding COLR Figures 2a and 2b for operation with 4 Reactor Coolant Pumps show a maximum 100.37 percent rated thermal power (including instrument error) as the top of the acceptable operation region.
TS LCO 3.2.3 for Axial Power Imbalance Operating Limits requires that the Axial Power Imbalance be within the limits specified in the COLR while in Mode 1 greater than 40 percent rated thermal power.
With the imbalance not within the specified limits, Surveillance Requirement 3.2.5.1 is required to be performed once per 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, and the Axial Power Imbalance is required to be reduced to within limits in 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The corresponding COLR Figures 4a, 4b, and 4c for operation with 4 Reactor Coolant Pumps show a maximum 100.37 percent rated thermal power (including instrument error) as the top of the permissible operating region.
Initial Plant Conditions:
On December 16, 2009, the Davis-Besse Nuclear Power Station (DBNPS) was operating in Mode 1 at approximately 100 percent power.
Event Description:
On December 16, 2009, the System Engineer for the Non-Nuclear Instrument System [IO] identified that one of the inputs to the secondary heat balance for the steam temperature at the inlet to the high pressure turbine was indicating 8 degrees Fahrenheit (F) lower than the input for the opposite steam line temperature indication. The value for plant computer point T476 for Steam Generator 2 indicated 583.7 degrees F compared to 591.8 for computer point T477 for Steam Generator 1. Alternate indications for the steam temperature at the outlet of the Steam Generators were consistent with the indications from computer point T477. Based on heat balance calculations, this 8 degree F difference resulted in a calculated/ indicated heat balance power of 0.45 percent reactor thermal power less than actual reactor thermal power.
A review of historical data from the plant computer showed that this difference has existed since the beginning of the previous operating cycle (April 2006). After replacement of both temperature elements providing steam temperature to the secondary heat balance, the temperature error was determined to be 5.5 to 6.0 degrees F instead of the initially-identified 8 degrees F. From the historical data review, which included actual operating conditions, the maximum one hour average reactor power was 100.475 percent, and the maximum 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average reactor power was 100.374 percent.
CAUSE OF EVENT:
In 2002, the two temperature elements (TESP15A and TESP15B) [10-TE] providing indication of the steam temperature at the inlet to the high pressure turbine were replaced with new Rosemount series 0078 Platinum Resistance Temperature Detectors (RTDs) along with matched transmitters to provide a greater accuracy than the previously installed RTDs. This replacement was done as part of the modification to install a Leading Edge Flow Meter and improve the accuracy of the plant power calorimetric measurement to allow an increase of 1.63 percent rated thermal power. The changes to the Operating License and Technical Specifications for this 1.63 percent rated thermal power increase were approved by the NRC on June 30, 2008 and plant power was increased accordingly on July 14, 2008.
The Rosemount series 0078 RTD is a wire wound device with a resistance that changes as a function of temperature. The wire coil is encapsulated in a spring loaded sensor assembly, and the sensor is installed in a thermowell with the tip compressed against the end of the thermowell via a spring to provide an accurate measurement of the temperature along with a faster response time and better vibration resistance.
The RTD providing the erroneous indication (TESP15A) was removed from the system and sent for failure analysis, which determined that the temperature element had been damaged by vibration, resulting in the output shifting low. The Main Steam piping where the temperature element is installed is subject to constant vibration while the plant is in operation. The damage was caused by the piping vibration in conjunction with the incorrect length of the RTD. The RTD is approximately the same length as the thermowell in which it is installed. However, the RTD should be approximately 0.5 inches longer than the thermowell to ensure proper compression of the sensing element. Without the proper compression, additional movement of the RTD in the thermowell is likely, contributing to the vibration induced failure. The RTDs installed in 2002 were the same length as the originally installed RTDs, so the short RTD length appears to be a latent error from original plant construction. The original Rosemount 104AFP RTDs (installed prior to 2002) were less accurate than the new RTDs but appear to have been much more rugged, so the length of the thermowell and vibration did not adversely affect their operation.
ANALYSIS OF EVENT:
As discussed previously, actual plant operating conditions were reviewed from the plant computer and the heat balance power was recalculated based on the temperature input error to determine maximum power levels. The maximum one hour average reactor power was 100.475 percent and the maximum 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average reactor power was 100.374 percent, both occurring on August 16, 2008. Comparing the recalculated heat balance power to the COLR figures for Rod Insertion Limits and Axial Power Imbalance indicates the reactor was operated greater than the maximum power of the acceptable operation region for a total of 333 hours0.00385 days <br />0.0925 hours <br />5.505952e-4 weeks <br />1.267065e-4 months <br /> over the total 3769 hour0.0436 days <br />1.047 hours <br />0.00623 weeks <br />0.00143 months <br /> period from July 17, 2008 to December 21, 2008, based on the one hour average reactor power calculation. Based on the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average reactor power calculation, the reactor was operated greater than the maximum power of the acceptable region for one (1) 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> period on August 16, 2008.
ANALYSIS OF EVENT: (continued) Eight (8) hour periods were analyzed since these are equivalent to a shift. Under NRC Regulatory Issue Summary 2007-21, Revision 1, "Adherence to Licensed Power Limits," (dated February 9, 2009) and the referenced Nuclear Energy Institute (NEI) guidance, core thermal power average for a shift is not to exceed the licensed power level.
Prior to use of the Leading Edge Flow Meter, the maximum authorized steady-state reactor core power levels, per DBNPS Operating License Condition 2.C.(1) was 2772 Megawatts thermal (MWth). The maximum analyzed steady-state reactor core power levels, including uncertainties, was 102 percent of 2772 MWth, or 2828 MWth. With the change to the Operating License to allow use of the Leading Edge Flow Meter, while the maximum authorized steady-state reactor core power level was increased to 2817 megawatts thermal, the maximum analyzed steady state reactor core power level remained the same at 2828 MWth. For the time period of April 2006 to December 2009 when the temperature error existed, the maximum eight hour average reactor power exceeded the analyzed power level for only one eight hour time period and then by only 0.004 percent of rated thermal power; therefore, this issue had very low safety significance.
Reportability Discussion:
TS LCO 3.2.1 for Regulating Rod Insertion Limits requires that the regulating groups shall be within the physical insertion, sequence, and overlap limits specified in the COLR while in Modes 1 and 2. The corresponding COLR Figures 2a and 2b for operation with 4 Reactor Coolant Pumps show a maximum 100.37 percent rated thermal power (including instrument error) as the top of the acceptable operation region. TS LCO 3.2.3 for Axial Power Imbalance Operating Limits requires that the Axial Power Imbalance be within the limits specified in the COLR while in Modes 1 greater than 40 percent rated thermal power. The corresponding COLR Figures 4a, 4b, and 4c for operation with 4 Reactor Coolant Pumps show a maximum 100.37 percent rated thermal power (including instrument error) as the top of the permissible operating region. Because the plant operated at a maximum of 100.374 percent rated thermal power for an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> average, this was in excess of the 100.37 percent rated thermal power limit specified in the COLR, and represents a condition prohibited by TS LCO 3.2.1 and 3.2.3. Therefore, this issue is reportable per 10 CFR 50.73(a)(2)(i)(B) as operation or condition prohibited by the Technical Specifications.
CORRECTIVE ACTIONS:
Following discovery of this condition, reactor power was lowered to less than 99.5 percent on December 17, 2009, to account for the faulty RTD indication. A conservative value was manually input to the heat balance calculation to allow for the faulty RTD to be removed from the system for troubleshooting, and reactor power restored to 100 percent. The faulty RTD was replaced and the temperature transmitter calibrated on December 19, 2009. The other RTD (TESP15B) on the opposite steam side monitoring steam temperature at the inlet to the high pressure turbine was replaced on January 18, 2010.
These two RTDs will be replaced with RTDs of the appropriate length for the installed thermowells as well as with a type of RTD that is more resistant to vibration. As an interim measure, preventive maintenance activities will be revised to replace the 2 RTDs every 2 years until they are replaced with a more robust type.
PREVIOUS SIMILAR EVENTS
In 2004 a failure of TESP15B was identified, but no evaluation of the failure was performed. The RTD had been installed for 2 years at the time of the failure. The procedures in place at that time did not require a failure evaluation be performed for equipment designated as non-critical, such as these RTDs.
Current procedures require that the failure of critical or non-critical components be evaluated and an equipment apparent cause evaluation and failure mode analysis be performed.
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05000410/LER-2009-001 | Momentary Loss of Control Power to High Pressure Core Spray, Pump Due to Degraded Fuse Block Connection | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000266/LER-2009-001 | Component Coolina Water PumD Inoperable In Excess of Technical Specification Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2009-001 | Containment Overpressure Not Ensured in the Appendix R Analysis | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000250/LER-2009-001 | Procedure Inadequacy Causes Control Room Ventilation Isolation Technical Specification Noncompliance | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2009-001 | Common Mode Failure of Reactor Building Isolation Dampers | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000530/LER-2009-001 | Manual Reactor Trip Due to a Loss of Instrument Air to the Containment Building | | 05000457/LER-2009-001 | Reactor Trip on Over Temperature Delta Temperature due to a Signal Spike on One Channel With Another Channel Placed in the Tripped Condition for Surveillance Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000413/LER-2009-001 | Both Trains of Chemical and Volume Control, Auxiliary Feedwater and Containment Spray Systems were Inoperable due to a Component Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000412/LER-2009-001 | Equipment Operability for Steam Generator Tube Rupture Safety Analysis Not Met | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vi) | 05000461/LER-2009-001 | Safety Function Lost Due to Capacitor Failure on Circuit Card | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000382/LER-2009-001 | Waterford 3 Steam Electric Station 05000382 1 OF 3 | | 05000370/LER-2009-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2009-001 | Containment Air Cooler Fans Inoperable Due to Misapplication of Potter and Brumfield Rotary Relays | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2009-001 | Reactor Trip Due to High Pressurizer Pressure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2009-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000281/LER-2009-001 | Manual Reactor Trip Initiated to Replace a Rod Control Data Logging Card | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000261/LER-2009-001 | Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000220/LER-2009-001 | Failure to Implement Required Technical Specification Actions Associated with Failed Surveillance Test | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2009-001 | Unit 2 Main Feedwater Isolation Valves Stroke Time Potentially Affected by Temperature | 10 CFR 50.73(a)(2)(I)(B) | 05000321/LER-2009-001 | Pump Suction Swap for HPCI and RCIC Non-Conservative With Respect To Technical Specification Requirements | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2009-001 | Surveillance Test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2009-001 | III Duke Energy® BRUCE H HAMILTON Vice President McGuire Nuclear Station Duke Energy Corporation MGO1VP / 12700 Hagers Ferry Road Huntersville, NC 28078 704-875-5333 704-875-4809 fax bhhamilton@duke-energy.com June 24, 2009
U.S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, D.C. 20555
Subject: Duke Energy Carolinas, LLC
McGuire Nuclear Station, Units 1 and 2
Docket Nos. 50-369, 50-370
Licensee Event Report 369/2009-01, Revision 0
Problem Investigation Process (PIP) M-09-02216
Pursuant to 10 CFR 50.73 Sections (a) (1) and (d), attached
is Licensee Event Report 369/2009-01, Revision 0, regarding
the past inoperability of the Nuclear Service Water System
"A" Trains due to potential for strainer fouling.
This report is being submitted in accordance. with 10 CFR
50.73 (a) (2) (i)- (B), an Operation Prohibited by Technical
Specifications, and 10 CFR 50.73 (a) (2) (v) (B), any Event.
or Condition That Could Have Prevented Fulfillment of the
Safety Function.
This event is considered to be of no significance with
respect to the health and safety of the public. There are
no regulatory commitments contained in this LER.
If questions arise regarding this LER, contact Rick Abbott
at 980-875-4685.
Very truly yours,
Bruce H. Hamilton
Attachment
www.duke-energy.corn m U.S. Nuclear Regulatory Commission
Date
Page 2
CC: L. A. Reyes, Regional Administrator •U.S. Nuclear Regulatory Commission, Region.II
Sam Nunn Atlanta Federal Center
•61 Forsyth Street, SW, Suite 23T85
Atlanta, GA 30303
J. H. Thompson, Jr. (Addressee Only)
Senior Project Manager (McGuire)
U.S. Nuclear Regulatory Commission
Mail Stop 0-8G9A
Washington, DC 20555
J. B. Brady
Senior Resident Inspector
U.S. Nucle'ar Regulatory Commission-
McGuire Nuclear Station
B. 0. Hall, Section Chief
Radiation Protection Section
1645 Mall Service Center.
Raleigh, NC 27699
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104t EXPIRES: 08/31/2010
(9-2007) Estimated burden per response to comply with this mandatory collection request: 50 hours. Repoded
lessons learned are incorporated into the licensing process and fed back to industry. Send comments
regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information (See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or digits/characters for each block) sponsor, and a person is not required to respond to, the information collection. LICENSEE EVENT REPORT (LER) 1. FACILITY NAME 2. DOCKET NUMBER I 3. PAGE _McGuire Nuclear Station, . 0369 8 Unit 1 05000- OF 4. TITLE Nuclear Service Water System (NSWS)d
"A" Trains Past Inoperable when aligned
to the Standby Nuclear Service Water Pond due to'corrosion.
(SNSWP) | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000456/LER-2009-001 | Steam Generator Tube Exceeding Plugging Criteria Remained In Service During Previous Cycle | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000395/LER-2009-001 | Inadequate Procedure Results In EDG Not Obtaining Maximum Load Required By Technical Specification | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2009-002 | Reactor Coolant System Pressure Boundary Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000373/LER-2009-002 | Loss of Shutdown Cooling Due to Spurious Closure of the Shutdown Cooling Suction Isolation Valve | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000382/LER-2009-002 | Waterford 3 Steam Electric Station 05000382 10OF 4 | | 05000278/LER-2009-002 | Inoperable 'A' Wide Range Neutron Monitor Results in Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000287/LER-2009-002 | Unit 3 Trip Due to Generator Phase Differential Lockout | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2009-002 | | | 05000412/LER-2009-002 | Unacceptable Indications Identified During Reactor Vessel Head Inspection | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000354/LER-2009-002 | As Found Values for Safety Relief Valve Lift Setpoints Exceed Technical Specification Allowable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2009-002 | Vibration Induced Failure of Temperature Instrument Results in Operation above Licensed Power Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2009-002 | Failure to Complete Technical Specifications Required Action Within the Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2009-002 | Feedwater Isolation Initiates Auxiliary Feedwater System During Refueling Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000254/LER-2009-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 OF 5 | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000305/LER-2009-002 | Steam Exclusion Door Blocked Open During Maintenance Activities | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000250/LER-2009-002 | Turkey Point Unit 3 05000250 1 of 10 | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000220/LER-2009-002 | High Pressure Coolant Injection System Initiation Following a Manual Turbine Trip Due to High Turbine Bearing Vibrations | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2009-002 | Manual Scram On Low Water Level Caused By Turbine Trip From Hydraulic Fluid Leak | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2009-003 | Containment Spray Pump A Inoperable At Degraded Voltage Protection Setpoint | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000395/LER-2009-003 | ..Potential Loss of Residual Heat Removal System Safety Function In Mode 4 Due To An Unanalyzed Condition0 | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000389/LER-2009-003 | RCP 2B2 Lower Seal Cavity Line Leak | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000323/LER-2009-003 | Containment Sump Recirculation Valve Position Interlock Failure Due to Inadequate Testing | | 05000263/LER-2009-003 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000261/LER-2009-003 | Manual Reactor Trip Due to Failure of 'A' Steam Generator Level Module | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2009-003 | Reactor Recirculation Pump Failure Results in Manual Reactor Protection System Actuation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000361/LER-2009-003 | Pressurizer Auxiliary Spray Failed Inservice Test | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000457/LER-2009-003 | Drain Procedure for ECCS Suction Line Creates an Unanalyzed Condition Due to Inadequate Configuration Requirements | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000237/LER-2009-003 | Emergency Diesel Generator Oil Leak | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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