05000389/LER-2009-003

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LER-2009-003, RCP 2B2 Lower Seal Cavity Line Leak
Docket Number
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
3892009003R01 - NRC Website

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6)

Description of the Event

On July 8, 2009 during 100% power operation, control room operators noted a small increase in the St. Lucie Unit 2 reactor coolant system (RCS)[EIIS:AB] unidentified leakage rate. Operating crews started an RCS leakage investigation and confirmed the increasing trend. The unidentified leakage continued to rise to approximately 0.16 gpm by 0400 hrs on July 12, 2009. Reactor containment building (RCB) entries determined the RCS leak source as a cracked weld where the lower cavity seal Line I- 3/4"-RC-228 attaches to the 2B2 reactor coolant pump (RCP) seal cartridge. The reactor was down powered to 25% and manually tripped in accordance with plant procedures on 7/13/09.

Cause of the Event

The RCS leak source was identified as a cracked weld where lower cavity seal Line I- 3/4"-RC-228 attaches to the 2B2 RCP seal cartridge. The J- weld was cut from RCP seal housing and metallurgical failure analysis performed. The analysis concluded the failure mechanism was outside diameter (OD) initiated, low stress high cycle fatigue due to resonance vibration. The analysis did not identify any original welding or material deficiencies as contributors to the failure.

Analysis of the Event

This event is reportable under 10 CFR 50.73(a)(2)(ii)(A), as any event or condition resulting in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.

Analysis of Safety Significance The failure analyses that were performed concluded it was Line I-3/4-RC-228 resonance that magnified the vibration levels. The identified failure mechanism on the lower seal cavity line J- weld was outside diameter (OD) initiated, low stress high cycle fatigue.

The RCS leakage was discovered during daily RCS leakage rate calculations which identified the increased leakage prior to a significant degradation of the piping.

Experience has demonstrated that with this weld failure mechanism, there is ample time from the discovery of increased RCS leakage to allow a controlled shutdown to cold shutdown conditions without challenging the emergency core cooling system (ECCS) or small break loss-of-coolant accident analysis (SBLOCA).

Although stainless steel components are not susceptible to boric acid corrosion, the spray from the cracked weld deposited wet boric acid onto the external surfaces of numerous carbon and low alloy steel components, including pressure retaining bolting.

Inspection subsequent to cleaning of the affected areas revealed minor surface corrosion with no measurable material degradation or wastage. The inspection results were consistent with the expected corrosion rates provided in the industry guidelines for the specific leak parameters such as temperature and boric acid concentration.

Based on the above, the safety consequences of the event are low and there was no adverse impact on the health and safety of the public.

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6)

Corrective Actions

The corrective actions and supporting actions are entered into the site corrective action program. Any changes to the proposed actions will be managed under the corrective action program.

Action taken prior to restart:

1. Replaced the cracked seal housing.

2. Cut and capped the RCP seal lines that were susceptible to this failure mechanism, including seal injection on all four RCPs and the upper seal cavity lines on two of the RCPs as short term corrective action.

RCPs seal piping.

Long Term Corrective Action:

1. Seal injection via the chemical volume control system is being removed on all RCPs by cutting and capping the seal injection lines, thereby removing that portion of the vibration-vulnerable piping.� vibration-The remaining RCP vulnerable seal lines will be modified with flexible piping. This work will be completed by the end of the Spring 2011 Unit 2 refueling outage, SL2-19.

Similar Events There have been (3) three similar failure events at St. Lucie Unit 2 involving cracked RCP seal lines: 1) Inside diameter initiated low stress high cycle fatigue of the 2B1 RCP lower seal injection line socket weld; 2) outside diameter initiated low stress high cycle fatigue of the 2B2 RCP seal injection vendor J groove weld; 3) inside diameter initiated environmental assisted cracking under cyclic loading.

A search of the INPO Operating Experience database, Industry Owner Groups, and other Utilities identified multiple plant events involving RCP seal injection lines with cracked welds relating to vibration, environmental, water chemistry, and weld material. These failure mechanisms independently or collectively contributed to these types of events within the nuclear industry.

Failed Components

RCP 2B2 Lower Seal Cavity piping 34) inch schedule 160 304 SS piping J-weld at the seal housing.